ML17056B578

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Insp Repts 50-220/91-23 & 50-410/91-23 on 911006-1109. Violations Noted.Major Areas Inspected:Plant Operations, Radiological Controls,Maint,Surveillance,Security & Safety Assessment & Quality Verification Activities
ML17056B578
Person / Time
Site: Nine Mile Point  
Issue date: 12/02/1991
From: Haverkamp D
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML17056B576 List:
References
50-220-91-23, 50-410-91-23, NUDOCS 9112260023
Download: ML17056B578 (34)


See also: IR 05000220/1991023

Text

Report Nos.:

Docket Nos.:

License Nos.:

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

91-23; 91-23

50-220; 50-410

DPR-63; NPF-69

Licensee:

Niagara Mohawk Power Corporation

301 Plainfield Road

Syracuse,

New York

13212

Facility:

Location:

Dates:

Nine Mile Point, Units

1 and 2

Scriba, New York

October 6 through November 9, 1991

Inspectors:

W. L. Schmidt, Senior Resident Inspector

R. A. Laura, Resident Inspector

R. R. Temps, Resident Inspector

R. J. Summers, Project Engineer

Approved by:

Donald R. Haverkamp, Chief

Reactor Projects Section 1B

Division of Reactor Projects

Date

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d

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f

plant

operations,

radiological

controls,

maintenance,

surveillance,

security,

and

safety

assessment/quality

verification activities.

~Riltg See Executive Summary.

p~gpg g Pi i

PDR

ADOCK 0500

ARV

Nine Mile Point Vnits 1 and 2

NRC Region I Inspection Report Nos. 50-220/91-23 & 50-410/91-23

October 6 - November 9, 1991

Plant

erati

NMPC continued to operate both units safely. Good operator performance was indicated in their

response at both units to challenging events, such as the leaking feedwater heater at Unit 1 and

the loss of condenser

vacuum at Unit 2.

However, inattention to detail by operators at both

units caused notable operational problems.

Unit 1 was required to be taken sub-critical during

a startup because an operator failed to complete a startup prerequisite step properly, and.at Unit

2 a loss of condenser

vacuum was caused by operators who did not perform or verify proper

performance of a preventive maintenance activity.

R

i I

ical

nr

Radiological control activities at both units generally were observed to have been conducted

properly during the period.

However, the inspector identified a violation (410/91-23-01) of

station frisking requirements at Unit 2. Specifically, several individuals failed to complete the

required two-minute frisk with a hand-held frisker before leaving a radiologically controlled

ai'ea.

Maintenance

The maintenance activities observed indicated continued good performance in this area.

5

~

The surveillance activities observed during the period indicated continued good performance.

Inspector review of NMPC's actions to address

a previously unresolved item on the installation

and use of temporary

gauges

on the core spray systems

at Unit

1 was upgraded

from an

unresolved

item to a violation (220/91-23-02);

the NRC determined

that NMPC did not

adequately review and approve the procedure for installation and use of the gauges

so as to

assure the continued operability of the core spray system.

ecurit

Observations of security activities and tours of the plant indicated continued good performance

in this area.

Executive Summary (Continued)

f t

A

nt/

u li

V riTi ti n

Routine review of several

licensee event reports indicated that in-depth reviews were being

completed and that corrective actions were taken commensurate with the safety significance of

the issues.

An unresolved item was opened (410/91-23-03), pending further NRC assessment

ofthe appropriateness ofNMPC's actions followinginspector identification ofa cable separation

issue on a reactor core isolation cooling system valve.

Based on the Unit 1 violation discussed

above and on continued deficiencies identified with

temporary

modifications,

there

continues

to be

a problem

with the

general

employee

understanding of plant configuration changes and how they should be controlled, including the

use of required safety reviews when such configuration changes potentially affect equipment or

system operability.

As a result of a Rosemount transmitter failure, the licensee has initiated a root cause analysis.

The licensee has agreed to provide the results to the NRC when complete.

11

TABLE

F

NTK

1.0

SUMMARYOF FACILITYACTIVITIES

1.1

Niagara Mohawk Power Corporation Activities ...........

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NRC Activities

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2.0

PLANTOPERATIONS.............................

2.1

Routine Plant Operations Review - Unit 1

2.2

Routine Plant Operations Review - Unit 2

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3.0

RADIOLOGICALAND CHEMISTRY CONTROLS ..................

5

3.1

Routine Observations - Unit 1 and Unit 2 ....................

5

4.0

MAINTENANCE .... ~..................................

6

4.1

Routine Observation of Maintenance Activities .................

6

5.0

SURVEILLANCE

5.1

Routine Observation of Surveillance Activities - Unit 1

5.2

(Closed) Unresolved Item 91-20-01

Inadequate

Controls During Core

Spray Testing - Unit 1

e

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6.0

EMERGENCY PREPAREDNESS ............................

10

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~6.1

Declaration of an Unusual Event at Unit 2 ...................

10

7.0

SECURITY AND SAFEGUARDS ............................

10

8.0

SAFETY ASSESSMENT AND QUALITYVERIFICATION...........

8.1

Routine Review of Licensee Event Reports (LERs) and Special Reports

8.2

Reactor Core Isolation Cooling Cable Separation - Unit2.........

8.3

Temporary Modifications Implementation Weaknesses

- Unit 2

8.4

Safety Review and Audit Board (SRAB) Meeting of October 23 and 24

11

11

11

12

13

9.0

MANAGEMENTMEETINGS...............................

13

  • The NRC inspection manual procedure or temporary instruction that was used as inspection

guidance is listed for each applicable report section.)

111

DETAILS

1.0

SVMMARYOF FACILITYACTIVITIF8

11

i

Mh

kP

r

ratinA

ii't

the beginning of the period, the Niagara Mohawk Power Corporation (NMPC) maintained

Unit 1 in cold shutdown following the September 26, 1991 automatic reactor scram caused by

a failed generator

current transformer.

Plant startup commenced

on October

10 following

replacement of the current transformer.

After reaching rated pressure,

operators identified that

second stage feedwater heater valves had been mispositioned during pre-startup valve lineups.

The unit was taken sub-critical to resolve the issue.

Once the mispositioned valve issue was

resolved, the unit startup was recommenced.

The unit achieved fullpower on October 15 and

operated

there until October

16, when one of the three high pressure

feedwater

heaters

developed a tube leak.

The affected heater string was isolated and reactor power was lowered

to within the known capacity of the remaining heaters

strings (approximately 80%).

NMPC

performed a safety evaluation and conducted a special test which determined that the maximum

power level achievable with only two heater strings was approximately 94%. The unit operated

at that power level through the end of the period.

NMPC operated Unit 2 at fullpower throughout the report period except for October 23, when

operators reduced power to 54% to prevent a low condenser vacuum scram.

Vacuum was being

lost, because an operator error during the performance ofa preventative maintenance procedure

on the condenser air removal pumps caused the air ejectors to be isolated.

Shortly following

unisolation of the air ejectors and recovery ofvacuum, an Unusual Event was declared because

of a hydrogen gas release into the turbine building. The release, from a broken generator sight

glass, was identified and isolated by an operator.

The Unusual Event was terminated, following

ventilation and sampling of the turbine building, and the unit was returned to 100% power,

where it operated for the remainder of the period.

1.2

N~R

An electrical distribution system functional inspection (EDSFI) was conducted at Unit 1 from

October 9 through 25.

The findings of this team inspection willbe documented in inspection

report 50-220/91-81.

Resident inspectors conducted inspection activities during normal, backshift and weekend hours

over this period.

There were ten hours of backshift (evening shift) and

14 hours1.62037e-4 days <br />0.00389 hours <br />2.314815e-5 weeks <br />5.327e-6 months <br /> of deep

backshift (weekend, holiday, and midnight shift) inspection during this period.

2.0

PLANT OPERATIONS

2.1

R

in

Pl nt

n Rviw-

ni

1

The inspector assessed

that routine plant operations generally were performed properly. During

the inspection period the inspectors

observed control room activities including operator shift

turnovers, shift crew briefings, panel manipulations,

and response to alarms.

The number of

lit annunciators remained low and operator response to alarming annunciators

was observed to

be proper.

Routine safety and auxiliary system operations generally were conducted in accordance

with

approved operating procedures

and administrative guidelines, except for the mispositioning of

the

second

stage

feedwater

heater

low load

valves

discussed

below.

The

inspectors

independently verified safety system operability by review of operator logs, system markups,

control panel walkdowns and component

status

verifications in the field.

Operator

logs

contained a sufficient level of detail.

Specifically, the mispositioned second

stage feed water

valve and the leaking feedwater heater were both properly logged. Two markups were reviewed

and were found to provide satisfactory isolation for personnel and equipment protection.

The

inspector performed a control room panel and in-plant component alignment verification for the

core spray and liquid poison systems and no discrepancies

were identified.

erat r In tenti n

De il Re

1

in V 1v

fP iin

NMPC management took conservative actions, during plant startup, when operators identified

that second

stage feedwater heater valves had been mispositioned due to inattention to detail.

Specifically, a control room operator observed a mismatch between reactor power and reactor

pressure

and identified by control room indication that the heater light load pressure control

valves 8-31 and 8-36, were open vice shut, as required by a prerequisite

step in the startup

procedure (OP-43). The valves were subsequently shut and operations management directed that

the reactor be taken sub-critical while a reverification of the OP-43 prerequisites

was made.

This review revealed no other discrepancies

and reactor startup was recommenced.

Inspector review determined that the chief shift operator (CSO), a licensed reactor operator, who

signed offthe prerequisite step off, failed to read and perform the entire step.

The CSO closed

the valve but did not ensure that the valve controller was in manual.

Placing the controllers in

manual was in the body of the procedural step, but the sign-off sheet only reflected that the

valves were shut.

This allowed the valves to open automatically during the startup process.

NMPC investigation of this event yielded the same results as the inspector's review. Operations

management

discussed this event with all members of the operations staff emphasizing the need

for attention to detail.

The step in OP-43 was revised to improve the human factors aspect of

the sign-off. The operations manager counseled the CSO involved in the event.

The inspector

concluded that, although the event was caused by operator inattention to detail, the discrepancy

was identified by an operator which was indicative of careful attention to plant operation, and

operations management took prompt and effective corrective actions.

0

2.1.2

F

w

r H

r

R

r

On October 16, an attentive control room reactor operator noticed a step change in feedwater

flow with no power change in progress.

Investigation determined that the number 135 high

pressure feedwater heater had developed a tube leak. The steam and feedwater sides of the heat

exchanger were isolated.

The inoperability of the heater rendered its respective heater string

unavailable, thus leaving two heater strings in service.

Reactor power was lowered to 80%, the

previously set limitfor two feedwater heater strings.

NMPC performed a safety evaluation and

wrote a special

test procedure,

which allowed increasing

reactor power to determine

the

maximum achievable level with the two heater strings in operation.

The inspector reviewed

these documents and found them to be comprehensive

and to reflect a good safety perspective.

Reactor power was slowly increased to approximately 94% power before reaching the operating

limitations of the two feedwater heater strings.

The inspector determined that the tube rupture

was identified by an attentive operator at the panels.

Further, site management performed a safe

and cautious increase of power with the two remaining heater strings in service.

2.2

Routine Plant

in Rview-

ni 2

During the inspection period, the inspector observed

that control room operations generally

reflected a safety conscious approach to operations.

Turnovers in the control room were

properly conducted with good exchange ofinformation between station shift supervisors (SSS),

the assistant

SSS (ASSS), and the shift crews.

Shift briefings were generally well attended by

operations and other departmental personnel, and were conducted in a professional atmosphere.

Operations management

presence at turnover shift briefings was noted on numerous occasions.

Panel

manipulations

and alarm

response,

and routine safety

system

and auxiliary system

operations were conducted in accordance with approved operating procedures and administrative

guidelines.

The inspectors

independently verified safety system operability by review of operator logs,

system

markups, control panel walkdowns, and component

status verifications in the field.

Discussions were held with operators and technicians in the field to assess their familiaritywith

current system status and personnel response to events during the inspection period.

2.2.1

R utinePl ntT

r

Throughout the inspection period, the inspector conducted

routine tours of the plant.

The

inspector identified three concerns during these plant tours, as described below:

On October 8, the inspector identified a cable separation concern which was brought to

the attention of Unit 2 management

on October 9. The concern was with the separation

of the limit switch cabling for the reactor

core isolation cooling (RCIC) system

condensate

storage tank suction valve and non-divisional wiring for a space heater.

This

concern is discussed in section 8.2.

The inspector identified four air-operated valves in RHR pump room 'B'hich had air

leaks in their air regulators.

The condition was identified to the control room operators

and investigated

by operation personnel.

Work requests

were issued

and the leaks

repaired.

Two floor drains in the diesel generator building were noted to be taped over and

identified to the control room personnel.

NMPC uncovered the floor drains and wrote

DER 2-91-Q-1243 to track the issue.

This issue is discussed

further in section 8.3.

2.2.2

Partial Loss of Condenser Vacuum

On October 23, a non-licensed operator did not properly followand control room operators did

not provide proper oversight of a preventive maintenance

procedure,

which led to a loss of

condenser

vacuum and nearly resulted in an automatic reactor scram.

Specifically, a non-

licensed operator performing N2-PM-BM1, "Periodic Operation of the Condenser AirRemoval

Pumps," lined up the "B" condenser air removal pump, 2ARC-P1B, in preparation for running

the pump.

Although the operator had the procedure in the field, he failed to perform and sign

offseveral key steps which required repositioning ofcontrol room panel switches.

As a result,

when pump 2ARC-P1B was started from the control room, an interlock caused

the steam air

ejector isolation valve, 2ARC-AOV104, to close thus causing

condenser

vacuum to start

lowering. Had the missed procedural steps been performed, the interlock would not have been

activated.

Control room operators noticed the decreasing

vacuum and took immediate actions

to reduce reactor power to about 54% (from 100%).

Valve 2ARC-AOV104 could not be

reopened

from the control room, so'operators

were dispatched

to the field. While they had

difficulties, operators eventually reopened the valve locally allowing the air ejectors to restore

proper condenser vacuum before an automatic plant trip on low vacuum could occur.

The inspectors

determined

that the operators

responded

properly to the decreasing

vacuum.

However, as noted by NMPC and inspector followup to this event, the failure of the operator

to follow the procedural

steps

and the control room operator

starting

the pump without

understanding

the consequences

of his actions were deficiencies.

Further, NMPC determined

that it would have been more appropriate to have a licensed operator perform this procedure.

The following actions were implemented by operations

management

in response

to this and

previous recent personnel errors:

The non-licensed

operator was disciplined for failing to implement the procedure

as

written.

All operations personnel were directed to read the site administrative procedure (AP)

governing procedural

usage

and to sign a statement

acknowledging

they read

and

understood the AP. Also, this incident and the rules ofprocedure usage were reviewed

with all operators at shift briefings by operations department managers.

To increase supervisory oversight, the ASSS's duty station was moved out of the SSS

office into the control room floor area and his job duties were redefined to provide

greater oversight and control of operations related activities, and better interface with

other work groups.

The inspectors determined that the actions taken were appropriate.

However, the error in this

case is an additional example of recent attention-to-detail and procedural adherence problems at

the site, indicating that continued attention by NMPC management

is warranted.

2.2.3

nc ntrolled Relea

f

H

r

n

h T r in

B il in

On October 23, operators properly responded

to a hydrogen leak in the turbine building by

declaring an Unusual Event and by taking actions to isolate the leak and monitor for explosive

mixtures of hydrogen.

Shortly after the event described in section 2.2.2 above,

a diligent

operator, investigating a hissing sound, identified a shattered

main generator liquid detector

(sight glass) leaking hydrogen gas into the turbine building. The operator isolated the leak and

notified the control room.

An Unusual Event was declared due to the uncontrolled release of

flammable gas. At about the time the sight glass was isolated, a control room alarm (indicative

of a 25% explosive mixture of hydrogen in air) monitoring an area of the turbine building

momentarily alarmed.

Sustained alarms were not received nor were concentrations greater than

25% explosive mixture detected during manual sampling in the turbine building.

NMPC technicians

sampled

the turbine building for hydrogen pockets,

and plant managers

evaluated methods for ventilating the building. While this was going on, all activities that had

potential for igniting hydrogen pockets were suspended.

Unit2 generator hydrogen pressure fell

from a nominal 70 psig to 30 psig indicating that an estimated

10,000 standard cubic feet of

hydrogen was released.

No explosive pockets were found and the roof vents were opened to

allow ventilation of the building.

The Unusual Event was exited following the sampling and

ventilation of the turbine building.

NMPC investigation revealed that the root cause for the sight glass shattering was that it was

the wrong thickness

glass,

0.1 inches versus

the required 0.24 inch thick glass.

NMPC

determined that a work request (WR) was issued before initialunit startup in 1986 to replace the

sight glass, which was broken, but the WR was later voided.

Operations personnel interviewed

remembered

the broken sight glass being repaired, however, no documentation exists for this

action.

The inspector assessed

that this incident was not indicative of a current maintenance

program weakness.

3.0

RADIOLOGICALAND CHEMISTRY CONTROLS

3.1

ine

erv

n -

ni

nl 2

During plant tours the inspector observed proper radiological postings and generally good use

of radiological practices at both units.

However, during plant tours at Unit 2 the inspector

identified deficiencies in frisking practices,

discussed

below, and continued problems with

temporary modifications by chemistry personnel to sample water systems,

discussed in section

8.3.

3.1.1 Fil r

Mee R

i

1

i IP

n

R

uirem n -

ni 2

On November 6, the inspector observed that individuals exiting a radiologically controHed area

were not properly performing the whole body frisk required prior to entering the unrestricted

(clean) area of the plant.

Specifically, personnel leaving the auxiliary boiler room at Unit 2

performed whole body frisks (hand held frisker) in significantly less time than the minimum two-

minute frisk required by the radiological posting at the step-off-pad.

After observing one

person,

which he believed

had not completed

the required two-minute frisk, the inspector

reviewed the security logs for the appropriate door to determine ifthe individual could have

properly frisked. The inspector reviewed the security logs and confirmed by the computer time

logs that the individual observed and other personnel could not have completed the frisk in the

required two minutes.

In the 30-minute time period around the inspector's field observation,

the security log indicated that eight of nine individuals failed to properly perform the frisk in

accordance with posted requirements.

This was a violation of the site s Administrative Procedure 3.3.3, Radiation Worker Conduct,

section 6.2.6 which requires in part that radiation workers follow proper radiological work

practices,

which includes observing radiological postings and step-off-pad requirements

(50-

410/91-23-01).

The inspector determined that this finding was not indicative of a programmatic

breakdown on the part of the radiation protection department,

as proper radiological controls

were in place.

This was indicative of a failure on the part of individuals to comply with a site

administrative requirement.

Whileoflow safety significance, this violation was cited due to past

NRC-identified instances of poor radiation work practices

at Unit 2 ( failure to adhere to

radiological postings while working on a control rod drive hydraulic control unit and failure of

an individual to perform a frisk when leaving a radiologically controlled area) and due to recent

problems at Unit 2 with personnel inattention to routine administrative requirements

(such as

failure to follow the markup procedure

controls

and other examples of poor procedural

adherence).

4.0

MAINTENANCE

4.1

R

ine

bservati

n fM in

n n

A

vi

'he

inspector observed and reviewed selected portions ofpreventive and corrective maintenance

to verify adherence

to regulations,

use of administrative

and

maintenance

procedures,

conformance with codes and standards,

proper QA/QC involvement, and proper equipment

alignment and retest.

The following activities were observed:

WR 197131, Investigate and repair the number 11 reactor water cleanup pump vibration

inside the bearing end ofthe motor. The inspector observed a portion ofthe maintenance

in progress

and reviewed the associated

work package.

The work in progress

sheet,

work request,

radiation work permit request,

and troubleshooting plan were reviewed

with no discrepancies

identified.

The electrical maintenance

technicians identified that

the vibration was due to a cap screw that loosened and fell out between the end bell and

shield inside the motor.

The cap

screw

was replaced.

The inspector

found the

technicians were experienced

and competent.

4.1.2

gni~2

The inspector observed troubleshooting and repair activities associated with the Division

I emergency

diesel generator

(EDG).

On October

10, the machine

was declared

inoperable as a result ofit failing to achieve its required output frequency within the TS

required time.

This testing was being conducted at an increased

frequency because of

previous failures to achieve rated frequency in the required time. Initialtroubleshooting

efforts narrowed the problem down to the fuel rack mechanism which was not operating

quickly enough during the EDG start sequence.

The air cylinder which operates the fuel

rack assembly was replaced, but under retest the EDG still failed to come up to rated

frequency in the required time.

Subsequent

troubleshooting

determined

that an air-

operated relay, that allows operating air to the air cylinder, was sticking, thus causing

the delay in the startup sequence of the EDG. Following replacement of the relay, the

inspector observed the maintenance department retest of the EDG. Review of traces in

the control room showed satisfactory results.

The EDG was then satisfactorily retested

by an operations surveillance procedure, N2-OSP-EGS-M001, and the EDG was declared

operable.

The inspectors determined that the corrective and testing actions were proper

and timely.

5.0

SURVEILLANCE

5.1

R utine

ervation of Surveill n

A tivi i

-

nit 1

The inspector

observed

and reviewed

portions of completed

surveillance

tests

to assess

performance in accordance

with approved procedures

and Limiting Conditions of Operation,

removal and restoration of equipment, and deficiency review and resolution.

'

5.1.1

nit 1

Nl-ST-Q8, Liquidpoison pump and check valve operability test. The inspector observed

the performance of N1-ST-Q8 for subsystem

11.

The subsystem failed the test due to

lower than required flow at rated pressure,

was immediately declared inoperable and a

seven-day

limiting condition

for operation

was

entered

per

TS 3.1.2.b.

A

deficiency/event report was generated

to troubleshoot the problem and the number 12

subsystem

tested immediately to demonstrate operability per TS surveillance 4.1.2.c.

NMPC investigation determined the ultrasonic flow measuring device used during N1-

ST-Q8 for subsystem

11 was yielding inaccurate data.

The surveillance was run again

per N1-ST-Q8T which determined flow by measuring the rate of water level change in

the test tank with a calibrated measuring stick. Satisfactory results were obtained using

this method and the number

11 liquid poison subsystem

was declared operable.

The

inspector determined that the operations staff properly implemented the TS requirements

and took the appropriate corrective actions to resolve the test methodology deficiency.

5.1.2

gni~2

Quarterly surveillance test of the Division IIIemergency diesel generator (EDG) fuel oil

transfer pumps.

The test was run in accordance

with procedure N2-OSP-EGF-0001,

Revision 3, Diesel Generator Fuel Oil Transfer Pump and Valve Operability Test.

The

inspector determined that the procedure was being used in the field and that it was being

followed with appropriate

signoffs made.

Good coordination

was

noted

between

operations personnel, who ran the test and recorded pump flow and differential pressure

data, and instrumentation and control (1&C) technicians, who obtained pump vibration

data per procedure N2-IMP-GENE-28.0. The inspector verified that all gauges and test

equipment used were in calibration.

The inspector assessed

this activity to be properly

performed.

'I

Calibration of air-start system pressure

gauges on the Division IIEDG.

The inspector

determined that this activity was properly conducted.

5.2

I

~nit

1

nre

lved I

m

1-2 -

1

n

l Drin

r

During the previous inspection report period the inspector identified three concerns with the

process that NMPC used to install test gauges to the bottom of pressure control valves (PCV)

in the core spray system.

Specifically, gauges were installed on the PCVs which control the

cooling water supplies to the core spray pump and core spray topping pump.

The maintenance

department installed the gauges, using a special maintenance instruction (SMI), so that setpoint

data could be obtained and adjustment made to the PCVs, ifrequired, while the system was run

during a normal quarterly surveillance

test Nl-ST-Q1A and B, Rev. 00.

However,

the

installation of the gauges and test methodology of the PCVs was never added to the surveillance

and was performed instead by a special maintenance instruction which was not an approved test

procedure.

The inspector reviewed the dispositions ofthe three deviation/event reports that were

written to address

the three concerns associated

with this matter.

The first concern

was that installation of the test gauges

was not adequately

reviewed or

evaluated by an appropriate level of plant management

and thus was an unauthorized change to

the facility. The inspector determined that the gauges were not installed and removed within an

approved

station procedure or some other acceptable

administrative control process,

and no

safety review was performed before the gauges were installed into the core spray system.

The

Unit 1 plant manager agreed with the inspector's determination and stated that the installation

of the test gauges and test methodology should have been incorporated into the surveillance test.

Specifically, AP 2.0, "Procedure Use and Control" step 3.2 states that surveillance procedures

willbe implemented to ensure the orderly, safe and efficient testing of safety related equipment

with sufficient administrative controls to provide equipment configuration control, assessment

of plant impact, and personnel

and equipment protection. If a procedure

change

had been

completed,

an evaluation would have been required to determine the safety significance of the

installation.

The second concern was that, as a result of the failure to adequately review and evaluate the

facility change, NMPC had not determined its effect upon the operability of the core spray

system when the plug from the test fittingin the bottom ofthe PCVs was removed to install and

remove the test gauges.

Specifically, the inspector questioned NMPC management

regarding

the operability of the core spray system, and whether the operation of the PCV was degraded

during that time had a core spray initiation occurred.

NMPC reviewed

this concern by

calculation S14-81-F026.

This calculation, performed by site and corporate engineering,

was

detailed and concluded that the core spray pump motor cooler flow and the core spray topping

pump bearing box cooler flow would have been adequate with the .25 inch orifice left when the

plug was removed from the test fittingon the bottom of the PCVs. The inspector reviewed this

calculation and found the overall conclusions to be acceptable.

Some minor deficiencies were

identified, apparently due to miscommunication between site engineering, corporate engineering

and the vendor, and were discussed with engineering.

Engineering stated that a change would

be issued to the package to make the necessary

minor corrections.

The third concern was that no markup (isolation) was used when the test gauges were installed

in the PCVs.

NMPC initial review of this issue concluded that no requirements

existed to

prepare

and issue a markup to support the surveillance test of the core spray system.

The

inspector took exception to this disposition because the gauges were installed and utilized under

the SMI, not the surveillance

test.

The disposition did not clearly address

the inspector's

concern.

This was discussed with the general supervisor of operations support who agreed and

re-evaluated the disposition.

Operations management determined that it was prudent to provide

the operations planning group with additional guidance on decision making related to markups.

Specifically, when a breach is made to a system that is radioactive or that could experience

pressure,

then a markup should be issued for personnel and equipment protection.

This final

resolution addressed

the inspector's concerns.

0

10

In summary, the inspector determined that NMPC had not properly reviewed and evaluated the

installation of these test gauges,

and as a result, the effect on the operability of the system was

not reviewed until after it was questioned by the inspector.

The installations of the test gauges

and testing of the PCVs were changes

to the facility and to facility procedures

that were not

adequately reviewed and evaluated

as required generally by 10 CFR 50.59 and specifically by

NMPC AP 2.0, which is considered a violation (210/91-23-02).

The actual safety significance

ofthis violation was low because the core spray system would have performed its safety function

ifcalled upon, as verified by review of the calculation package and disposition to DER 1-91-0-

11-23. The installation and removal of the gauges in the PCVs without the use of a markup was

a poor practice.

These

observations

reflected poorly on the operations

and maintenance

departments.

During review of this issue, the inspector attempted to obtain a safety evaluation, which NMPC

management

stated existed for a similar condition which arose on the containment spray system.

The inspector subsequently determined that a safety evaluation had not been performed.

Based

on followup discussions,

the inspector concluded that the operations managers

and regulatory

compliance supervisor failed to verify the validity of information from their subordinates prior

to discussions

with the inspector when they told the inspector about the evaluation.

The

providing of this erroneous

information appeared

to be inadvertent

and did not affect the

inspector's findings and NRC staff actions, as all aspects of this surveillance testing issue were

reviewed.

The need to provide complete information was discussed with the Unit 1 and Unit

2 plant managers.

Both managers

agreed with the concern and stated

that their intent was

always to provide complete and accurate information.

The inspector had no further questions

regarding this concern.

6.0

EMERGENCY PREPAREDNESS

6.1

Declaration of an

nu

al Event at

nit 2

As discussed in section 2.2.3 above, an Unusual event was declared on October 23. This event

was appropriately classified and handled by the control room operators and the site management.

7.0

SECURITY AND SAFEGUARDS

During the period, the inspectors conducted plant tours and observed security guards performing

their duties, and no deficiencies were noted. Further, the inspectors conducted a perimeter fence

walkdown and noted no deficiencies.

11

8.0

SAFETY ASSESSM<24T AND QUALITYVERIHCATION

8.1

Routine Review of Licensee Even

R

ERs

and

ial Re

8.1.1

iinit 1

The following LER was reviewed and found satisfactory:

LER 91-12,

Reactor scram caused by main generator trip due to a failed current transformer.

The licensee root cause investigation determined that the failure was a short in the

current transformer windings caused by high localized ambient temperature in the

area.

The failed current transformer and two others on the phase two neutral side

were replaced.

Licensee

testing

and evaluation

determined

that immediate

replacement

of other current

transformers

was

not required.

Long term

corrective

actions

include

the

development

of a

periodic

thermographic

surveillance ofcurrent transformer in operations to identify degrading conditions.

The inspector

determined

that the root cause

and

corrective

actions

were

appropriate.

8.1.2

+nit 2

~

~

~

The following LER was reviewed and found satisfactory:

LER 91-20,

High pressure core spray (HPCS) system inoperable due to a failed instrument.

This LER documented

the failure of HPCS level transmitter 21SC*LT10D, a

Rosemount manufactured transmitter.

Problems with the transmitter was detected

during performance ofTS required 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> channel check surveillances on ECCS

actuation instrumentation.

Subsequent

troubleshooting identified the transmitter

was

defective.

The failed unit was

sent

to the vendor for specification

determination of the failure mode, however, preliminary indications are that the

transmitter suffered from a loss offilloil which is a generic problem encountered

throughout the industry with specific models of Rosemount

transmitters.

The

inspector

determined

that NMPC's program

for identifying and

replacing

detectors which suffer from this syndrome was adequate

and that the corrective

actions taken were appropriate.

NMPC has sent the affected transmitter to the

manufacturer for root cause determination.

Licensee management

has agreed to

provide NRC with the results of this evaluation when it is complete.

8.2

React r

re I

I '

lin

I

tin-

ni 2

As discussed

in section 2.2.1, the inspector identified a concern regarding the separation of

RCIC valve cabling from non-divisional power cabling. Specifically, on October 9 the inspector

identified to NMPC what appeared

to be inadequate separation between a Division I cable for

valve

2ICS*MOV129

and

non-divisional

cables.

Although

identified

on

that

date,

deviation/event report (DER) 2-91-Q-1301, describing this concern, was not issued until October

15 at which time RCIC was declared inoperable pending resolution and correction of the cable

separation

concern.

Inspector review of site procedure NMP2-SPEC-EO61A,

Appendix I,

12

indicated that a ten-inch separation

was required in this case, however, the cables were found

to be eight inches apart.

To correct this, the procedure allowed installation of a protective wrap

(Siltemp) for cases when ten-inch separation

cannot be achieved.

The inspector verified that

Siltemp was applied to the non-divisional power cables

as resolution to this problem.

This

action corrected the technical deficiency.

However, at the end of this inspection period, the

inspector was continuing the NRC review of some specific aspects of the NMPC followup to the

original concern, including why it took a week to initiate the DER and what effect the deficiency

had on the operability of the RCIC.

The inspector was still reviewing the safety significance

of this issue with respect to operability of the system and was concerned with the time it took

for the DER to be processed

and corrective actions taken.

This is an unresolved item (410/91-

23-03), pending further NRC review of the NMPC followup actions.

8.3

Tem

ra

Modifiicati n Im lemen

i n W

kn

-

ni 2

During plant tours the inspector identified two temporary modification issues, which had not

been previously identified by NMPC in their efforts to review temporary modification controls

at Unit 2.

Specifically:

Temporary Modification 89-78 initiated the addition oftubing and a temporary sampling

valve to facilitate sampling of the service water system by chemistry personnel.

The

inspector identified the following concerns to plant management:

The temporary

sampling

valve,

designated

2SWP*V1097

was

not

added

to the

appropriate SW piping and instrumentation diagram (P&ID) until eighteen months after

implementation of the TM. Further, the addition of this valve and its operation was not

reflected on the SW operating procedure valve lineup section (N2-OP-11) nor was it

called out for by valve number in the chemistry sampling procedure N2-CSP-SV.

Valve 2SWP*V912A,'pstream of valve 2SWP*V1097, required to be open while

sampling, was routinely opened and left in the open position without the knowledge of

operations personnel and contrary to its required closed position as specified in N2-OP-

11.

NMPC initiated actions to remove the TM after identification of these discrepancies,

because it was no longer needed.

NMPC also initiated action to perform a review of all

TMs to ensure that any repositionings or additions ofvalves by TMs were recognized in

prints and/or in procedures.

A DER was initiated to document the finding for corrective

actions and remained open at the end of the report period.

The inspector identified that several floor drains were taped in the diesel generator and

control building.

NMPC personnel

had

toured

this area

previously looking for

unauthorized TMs, but had not identified this issue.

Initial NMPC review considered

that the condition was not in accordance with the temporary modification procedure, AP 6.1, since the two floor drains did not have documentation supporting their being taped

over.

13

Each of these issues was of minor safety significance, and has been corrected.

However, they

do indicate that continued NMPC management attention is needed in response to the temporary

modifications concerns and inspection findings discussed in Inspection Report 91-17.

8.4

fe Rviw

A

i

r

RAB M

'n

f

r2

24

The inspector attended the SRAB meeting conducted October 23 and 24 and verified the SRAB

composition met the TS requirements.

Committee reports and audit activity reports were clearly

presented

and provided good assessment

of performance in the areas reviewed.

Open items

listed in the committee reports and audits were aggressively discussed at the meeting to ensure

proper identification of root causes

and the adequacy of proposed corrective actions. Further,

SRAB findings appeared

consistent with NRC assessment

and inspection findings, especially in

the area of human performance problems.

9.0

MANAGE<'ENTMEETINGS

At periodic intervals and at the conclusion of the inspection, meetings were held with senior

station management

to discuss the scope and findings of this inspection.

Based on the NRC

Region Ireview of this report and discussions held with Niagara Mohawk representatives, itwas

determined that this report does not contain safeguards or proprietary information.