ML17055E429
| ML17055E429 | |
| Person / Time | |
|---|---|
| Site: | Nine Mile Point |
| Issue date: | 01/09/1989 |
| From: | Kane W NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | Burkhardt L NIAGARA MOHAWK POWER CORP. |
| Shared Package | |
| ML17055E430 | List: |
| References | |
| NUDOCS 8901130153 | |
| Download: ML17055E429 (8) | |
See also: IR 05000410/1988021
Text
AC CELE RATED
DlSTKBUTION
DEMONSTRATION
SYSTEM
REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:8901130153
DOC.DATE: 89/01/06
NOTARIZED: NO
DOCKET
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FACIL:50-410 Nine Mile Point Nuclear Station, Unit 2, Niagara
Moha
05000410
AUTH.NAME
AUTHOR AFF1LIATION
KANE,W.F.
Region 1, Ofc of the Director
RECIP.NAME
RECIPIENT AFFILIATION
BURKHARDT,L.
Niagara
Mohawk Power Corp.
R
SUBJECT:
Forwards Safety Insp Rept 50-410/88-21
on .881203-21.
Violations noted.
DISTRIBUTION CODE:
IE01D
COPIES
RECEIVED:LTR
-ENCL
SIZE:
TITLE: General
(50 Dkt)-Insp Rept/Notice of Violation Response
NOTES:
RECIPIENT
ID CODE/NAME
PD1-1
BENEDICT,R
INTERNAL: ACRS
AEOD/DEIIB
NRR SHANKMAN,S
NRR/DLPQ/PEB ll
NRR/DOEA DIR ll
NRR/DREP/RPB
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EXTERNAL: LPDR
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ID CODE/NAME
HAUGHEY,M
DEDRO
NRR/DEST DIR
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NUDOCS-ABSTRACT
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4
h
Docket No. 50-410
Niagara
Mohawk Power Corporation
ATTN:
Mr. Lawrence Burkhardt, III
Executive Vice President - Nuclear
301 Plainfield Road
Syracuse,
13212
Gentlemen:
Subject:
Inspection
Report
No. 50-410/88-21
This letter transmits
the results of the special
safety inspection
conducted
by Mr. W. Cook and Mr.
R.
Laura of this office on December
3,
1988 thru
December
21,
1988 at Nine Mile Point Unit
2, Scriba,
A summary of
the findings was presented
to Mr. J. Willis and other members of your staff at
the conclusion of the inspection.
This inspection
was conducted
to review the circumstances
which 'led to the
discovery,
by your staff, that the
Division
. 1 Automatic Depressurization
System
(ADS) logic circuitry for Unit 2 was found to be inoperable
due to
a wiring
error since initial fuel load on November 2,
1986.
ADS is an
Emergency
Core Cooling System
(ECCS) designed
to mitigate the
consequences
of an accident
by automatically reducing reactor pressure, if
necessary,
to the discharge
head of the
Low Pressure
Core Injection and Spray
Systems.
Operation of the unit in Modes 1,2 and
3 (Power Operations,
Startup
and Hot Shutdown) with Division I ADS inoperable
is an apparent violation of
Technical Specification 3.3.3.
We intend to schedule
an enforcement
conference
to discuss this matter
and
will contact you to arrange
a mutually agreeable
time and date.
At the
conference
you should
be prepared
to discuss
the causes
of and corrective
action for this event,
as well as the safety significance of the
configuration.
You should also
be prepared
to discuss
why the operational,
star tup and periodic surviellance testing failed to properly detect this
deficiency,
and action you have taken to ensure that there
are
no other
similar wiring problems.
+~g
OFFICIAL RECORD
COPY
IR NMP2 88-21 - 0001.0.0
01/05/89
89011='0153
85'0106
ADOCK 05000410
Q
RDC
Niagara
Mohawk Power Corporation
-2-
We appreciate
your cooperation.
Sincerely,
William F.
Kane, Director
Division of Reactor Projects
Enclosures:
1)
NRC Region
1 Special
Inspection
Report
Number 50-410/88-21
2)
Attachment
1
ADS Wiring Problem Chronology
Summary
cc w/encl:
Connor
& Wetterhahn
Gary Wilson, Senior Attorney
C.
Mangan,
Senior Vice President
J. Willis, General
Superintendent
K. Dahlberg,
Station Superintendent,
Unit
1
R. Abbott, Station Superintendent,
Unit 2
R. Randall, Unit
1 Superintendent
of Operations
R. Smith, Unit 2 Superintendent
of Operations
J.
Perry, Director,
Nine Mile One Restart
Task Force
D. Palmer, Acting Manager Quality Assurance
C.
Beckham,
Manager Nuclear Quality Assurance
Operations
W. Hansen,
Manager
Corporate Quality Assurance
Troy B. Conner, Jr.,
Esquire
Director,
Power Division
Department of Public Service,
State of New York
James
F. Warden,
New York Consumer
Protection
Branch
New York State,
Department of Law
Public Document
Room (PDR)
Local Public Document
Room ( LPDR)
Nuclear Safety Information Center
(NSIC)
NRC Resident
Inspector
State of New York
OFFICIAL RECORD
COPY
IR NMP2 88-21 - 0002.0. 0
01/03/89
Niagara
Mohawk Power Corporation
bcc w/encl:
Region
I Docket
Room (with concurrences)
Management Assistant,
DRMA (w/o encls)
J.
Johnson,
Section Chief,
M. Haughey,
Licensing Project Manager,
Unit
1 and
2
State
Liaison Officer (SLO)
M. Johnson,
EDO, Regional
I Coordinator
P. Koltay, SRI,
IP3
W. Schmidt,
SRI, Fitzpatrick
D. Holody, Enforcement Director,
Region I
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PIL5
pg JAN 1989
RI: DRP
Bapn njee/rhl
1/3/89
RI:DRP
Johnson
1/Q /89
R~
W
'nger
1/g /89
1/V /89
OFFICIAL RECORD
COPY
IR NMP2 88-21 - 0002.1.0
01/03/89