ML16342B545
| ML16342B545 | |
| Person / Time | |
|---|---|
| Site: | Diablo Canyon |
| Issue date: | 03/23/1989 |
| From: | Johnston K, Mendonca M, Narbut P, Obrien J NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V) |
| To: | |
| Shared Package | |
| ML16341F094 | List: |
| References | |
| 50-275-89-05, 50-275-89-5, 50-323-89-05, 50-323-89-5, GL-88-14, IEB-88-010, IEB-88-10, NUDOCS 8904170086 | |
| Download: ML16342B545 (56) | |
See also: IR 05000275/1989005
Text
U.
S.
NUCLEAR REGULATORY COMMISSION
REGION V
Report Nos:
50-275/89-05
and 50-323/89-05
Docket Nos:
50-275
and 50-323
License
Nos:
DPR-80 and
Licensee:
Pacific Gas
and Electric Company
77 Beale Street,
Room 1451
,San
Fr anci sco,
Cal ifornia 94106
Facility Name:
Inspection at:
Diab1 o Canyon
Units
1 and
2
Diablo Canyon Site,
San Luis Obispo County, California
Inspection
Conducted:
-January
22 through March 4,
1989
c/~~'~ Jcl l c
J.
P. O'rien,
Reactor Project Insp ctor
/
K.
E. Johnston,
Resident
Inspector
(.-..4 (
P.
P.
Narbut, Senior Resident
Inspector
9 8< 3 /z p
Date Signed
~lz-9+sg
Date Signed
p/z aPZ"P
Date Signed
Approved by:
M.
M. Mendonca,
Chief,
Reactor
Projects
Section
1
Date Signed
Summary:
Ins ection from Januar
22 throu
h March 4
1989
Re ort Nos.
50-275/89-05
and
~i
Areas
Ins ected:
The inspection
included routine inspections
of plant
operations,
maintenance
and surveillance activities, follow-up of onsite
events,
open items,
and licensee
event reports
(LERs),.as well as selected
independent
inspection activities.
Inspection
Procedures
30702,
30703,
37700,
40500,
61726,
62700,
62702,
62703,
71707,
71710,
90712,
92700,
92701,
92702,
and
93702 were
used
as guidance
during this inspection.
Results of Ins ection:
Three'pparent
violations were identified.
The
violations involved the fai lure to follow licensee
procedures
for a design
change to the Auxiliary Feedwater
turbine driven pump overspeed trip device,
omission of backwater
from the floor drains of the diesel
fuel
oil transfer vaults,
and the failure to take prompt corrective action
upon
discovery of the missing dies'el fuel transfer vault drain check valves.
gpp4 i7QOBb
ADO
pgg
6
Areas of Stren th
In response
to the main feedwater
pump transient of February
23, 1989,
both operations
and plant staff responded
thoughtfully and quickly.
The
operators
acted quickly in identifying the apparent
cause
and thoughtfully
in the recovery.
Plant staff acted quickly in assembling all the facts
and personnel
involved, enacted
prudent compensatory
actions,
and
initiated comprehensive
corrective action.
On February 14 a guality Control inspectoV discovered that the packing
gland retainer
studs
on Unit'
ASW pump discharge crosstie
valve FCV-495
'ad
sheared
and the retainer
was rotating with the shaft.
This is
notable since it was not an inspection point, the
room was dark, the
valve was not readily accessible,
and the sheared
studs. were not readily
apparent.
Areas of Weakness
Confi uration Control: This inspection identified a number of examples
of
inadequate
design configuration control.
The examples
cover various aspects
of the maintenance
of plant design
such
as the plant understanding
and
implementation of the. design basis,
the authorization of design
changes,
the
control of maintenance
on equipment
such that design qualification is
preserved,
and the design integrity of original plant construction.
Examples of an inadequate
understanding
of the design basis
were the
removal
from service of an
AFW turbine steam supply valve when it was
required for the operability of the
pump (Section
3b) and the lack of a
definition of emergency
diesel
generator
OC, power supply operability
requirements
(Section 12b).
The two examples of making design
changes
without the appropriate
review
both involved maintenance
engineers
authorizing design
changes
to the
turbine driven pump overspeed trip device.
In one instance
a washer
was
machined to fit the valve actuator
stem when on further review it was
determined that it was the stem which had the wrong dimensions.
This was
the subject of a notice of violation.
The second
example involved the
rotation of the spring mounting bracket
by 90 degrees
to increase
spring
tension (Section 4h).
Examples of inadequate
controls in the maintenance
process for hardware
required to maintain seismic qualification were identified.
The
inspectors
identified an example of a missing bracket
on an
AFW motor
thermocouple
conduit (Section 8).
Two other examples,
both licensee
identified, loose bolting of control
room ventilation system seismic
'upports
(Section 4a)
and missing seismic bracing
on the Unit 2 reactor
cavity sump wide level channels
(Section 4c) were identified.
-3-
The example of design configuration weakness
in the area of original
construction integrity involved the discovery that backwater
had not been installed in the diesel
fuel transfer
pump vaults
and this
discrepancy
was not discovered
because
the 'check valves
were not part of
the surveillance
and preventive
maintenance
program (Section 6b).
Valve Ali nments
The inspectors
continued to find examples of weak valve
alignment practices.
An injection of a large "bubble" of air into the
condensate
system could have
been avoided
had the auxiliary operator
had
adequate
valve and system alignment instructions
(Section 4g).
Also
identified in this report period
was
a lack of control of system drain caps
and plugs (Section 8).
Poor Work Orders
Mork orders associated
with the corrective maintenance
of
the
AFW overspeed trip mechanism exhibited weaknesses
of a type which have
been previously identified.
In this case the work order lacked detail
and
provided drawings of the device diff'erent than that installed (Section 4h).
The work order for the installation of temporary instrumentation to accomplish
the Auxiliary Saltwater performance test lacked specificity.
As a result,
the
instrumentation
was not adequate
to perform the test initially (Section 7a).
Untimel
Action
A lack of timely action i n identifying and resolving problems
was
a central
issue
discussed
in the licensee's
SALP report for 1988.
This report describes
additional
examples
of untimely action which deserve
management
attention.
Specifically, this report describes
an apparent violation due to untimely
corrective action
upon discovering missing backflow check valves in the diesel
fuel oil transfer vaults (paragraph
6b).
A second
example involved the
fai lure to assure
the use of a proper drawing for an
AFM over speed trip device
problem in November l988 leading to the use of the wrong drawing again in
February
1989 (paragraph
4h).
A third example
was
a failure to act for 5 days
on an
OSRG concern
r egarding diesel
generator operability
due to particulate
contamination
(paragraph
4e).
A fourth example involved slowness
to act due
to inadequate
gA overview on
a Part
21 report for motor operated
valves
(paragraph 4f).
DETAILS
Persons
Cohtacted
J.
D.
D.
B.
"L'. F.
"B..W.
"J.
M.
"C.
L.
"K.
C.
R.
G.
"T. A.
"D. A.
T. J.
Yl.
G.
J.
V.
- T
L
"M. J.
"J.
A.
"M.
E.
- G.
C.
S.
R.
R.
P.
M.
R.
J.
E.
D.
R.
Townsend,
Plant Manager
Miklush, Assistant Plant Manager,
Maintenance
Services
Womack, Assistant Plant Manager,
Operations
Services
Giffin, Assistant Plant Manager, Technical-Services
Gisclon, Assistant Plant Manager for Support Services
Eldridge, equality Control
Manager
Doss, -Onsite Safety
Review Group
Todaro, Security Supervisor
Bennett,
Maintenance
Manager
Taggert, Director guality Support
Martin, Training Manager
Crockett,
Instrumentation
and Control Maintenance
Manager
Boots, Chemistry and Radiation Protection
Manager
Grebel,
Regulatory
Compliance
Supervisor
Angus,
Work Planning
Manager
Shoulders,
Onsite Project Engineering
Group Manager
Leppke,
Engineering
Manager
Sarkis'ian,
News Services
Fridley, Operations
Manager
Powers,
Radiation Protection
Manager
Tresler,
Project Engineer
Holden, Supervisor/Operations
and Engineering Training
Clifton, Supervisor/Technical
and Maintenance Training
The inspectors
interviewed several
other licensee
employees
including ..
shift foremen
(SFM), reactor
and auxiliary operators,
maintenance
personnel,
plant technicians
and engineers,
quality assurance
personnel
and general
construction/startup
personnel.
"Denotes
those attending the exit interview.
0 erational
Status of Diablo Can on Units 1 and
2
Both Units
1 and
2 were at 100 percent
power for the duration of the
reporting period except for periodic turbine valve testing.
No reactor
trips or significant events
occurred.
An NRC team inspection
was conducted
from January
12 to February
3.
The
team raised
a number of questions
concerning the design basis of the
Auxiliary Saltwater
and Component Cooling Water
systems.
In response,
the licensee
made required
10 CFR 50.72 reports
and took compensatory
measures
which in some
cases
are
more restrictive than current Technical
Specification requirements.
These
concerns
are covered in detail in
Inspection
Report 50-275/89-01.
Other significant events
include the valid failure of Diesel Generator
l-l to start
due the the failure of two air start motors (section 4b)
and
2
the failure of the Unit 2 turbine drive Auxiliary Feedwater
pump
overspeed trip to actuate
(Section 4h).
In addition, during the reporting period
a team inspection
reviewed the
installation of the Accident Mitigation System Actuation Circuitry
Modification and
on February
16, Commissioner
Kenneth Carr visited the site.
3.
0 erati onal Safet
Ver ificati on
71707
General
During the inspection period,
the inspectors
observed
and examined
activities to verify the operational
safety of the licensee's
facility.
The observations
and examinations
of those activities
were conducted
on
a daily, weekly or monthly basis.,
On
a daily basis,
the inspectors
observed
control
room activities to
verify compliance with selected
Limiting Conditions for Operations
(LCOs) as prescribed
in the facility Technical Specifications
(TS).
Logs, instrumentation,
recorder traces,
and other operational
records
were examined to obtain information on plant conditions,
and
trends
were reviewed for compliance with regulatory requirements.
Shift turnovers
were observed
on
a sample basis to verify that all
pertinent information of plant status
was relayed.
During each
week, the inspectors
toured the accessible
areas
of the facility to
observe
the following:
(a)
General plant and equipment conditions.
(b)
Fire hazards
and fire fighting equipment.
(c)
Radiation protection controls.
(d)
Conduct of selected activities for compliance with the
licensee's
administrative controls
and approved
procedures.
(e)
Interiors of electrical
and control panels.
(f)
Implementation of selected
portions of the licensee's
physical
security plan.
(g)
Plant housekeeping
and cleanliness.
(h)
Engineered
safety feature
equipment alignment
and conditions.
(i)
Storage of pressurized
gas bottles.
The inspectors
talked with .operators
in the control
room,
and other
plant personnel.
The discussions
centered
on pertinent topics of
general
plant conditions,
procedures,
security, training,
and other
aspects
of the involved work activities.
b.
Unit 2 Turbine Driven Auxiliar
Pum
Ino erable With One
Steam
Su
1
Out Of Service
Technical Specification 3.7. 1.2 requires'that
three
pumps
and associated
flow paths shall
be
OPERABLE with the
one
steam turbine-driven auxiliary feedwater
pump
capable of being supplied
from an
OPERABLE steam supply system.
On
January
17, the main steam line 2-2 steam supply to turbine driven
AFW pump 2-1,
FCV-2-37 was closed with power removed without
declaring
AFW pump 2-1 inoperable.
Concurrently,
motor driven pump
was declared
inoperable with is discharge isolation valve (FW-2-190)
shut for maintenance
of LCV-2-115, its supply to steam generator
2 3 ~
Following questions'by
the resident inspector,
the licensee
on
February
3, 1989,
determined that, with FCV-.2-37 closed,
the
turbine steam
supply system could not have performed
a design
function as described
in Chapter
15 of the licensee's
Final Safety
Analysis Report
(FSAR).
The licensee
further determined that
pump 2-1 should
have
been declared
The licensee
issued
an
LER (2-89-01)
on this subject
on February
24,
1989.
This issue will be discussed
in more detail in Inspection
Report 50-275/89-13..
Plant Tour
The project inspector
conducted
a tour of the facility buildings
on
March 1, 1989,,with the senior resident
inspector
(SRI).
This was
done to assess
the licensee's
housekeeping activities,
and the
was able to point out recent
areas
of,improvements.
No equipment of
housekeeping
deficiencies
(not previously identified by the
licensee),
were identified.
E
No violations or deviations
were identified.
4.
Onsite
Event Follow-u
(93702
Seismic
Su
ort Unbolted
Unit 1
On January
25, 1989,
a control
room ventilation seismic support
was
found unbolted.
This item is discussed
in NRC team inspection
report 50-275/89-01.
Diesel Generator l-l Failure to Start
On February 1, 1989, at 1:05 p.m.
PST the Unit 1 Diesel
Generator
l-l failed to start during periodic monthly testing.
For the testing performed only two of four air start motors are
energized.
Both were subsequently
found to have failed due to gear
retaining capscrew's
in the air start motors.
Subsequent
testing
with the remaining two air, start motors
was successful
in that the
diesel started.
In an emergency
actuation all four air motors would
have
been actuated
and therefore
the diesel
would have started.
The licensee
prepared
a special
report to the
NRC "Special
Report
89-01,
Diesel Generator l-l'Failure to Start" dated
March 3,
1989
which provides further details.
The inspectors
f'ollowed-up licensee actions.
Actions included:
Test starts of all remaining diesels
and observation of the air
start motors.
Repair of the
damaged air start motors
on DG1-1.
Initiation of metallagraphic
examinations
of failed parts.
Network inquiry to determine if other plants
had similar
problems (the results
were negative).
Inquiry to the diesel
and air start motor manufacturers
to
determine failure histories
and possible
causes.
Investigation of Diablo Canyon maintenance
history and adequacy
of maintenance
procedures
for the air start motors.
At the
end of the inspection period the licensee
had not totally
resolved the cause of failure of the two air start motors.
One air
motor had
been judged to fail because
the air pressure
downstream of
the air pressure
regulator
had drifted up to 190 psig, contrary to
the vendors recently offered recommendation
of air pressure
not
greater
than
160 psig.
This was apparently
due to a leaking
regulator which was replaced
subsequently.
The second failed air
motor had proper air pressure
and,
per the vendors would not have
been overloaded
as it attempted to start the diesel, i.e. the diesel
is designed
to start
on
a single air motor.
The licensee's
theories
on failure postulate that the torque
on the
gear retaining capscrews
may not have
been sufficient resulting in
insufficient friction in the tapered shaft connection
between the
tapered
gear
and the tapered shaft.
The licensee
plans additional investigative actions
as stated in
their special
report.
The inspectors will follow-up licensee
actions
through the nonconformance
report on the subject.
Seismic Bracin
Not Installed
Unit 2
On February 3, 1989,
I8C technicians
discovered
a seismic brace not
installed
on a instrumentation
rack containing the reactor cavity
sump level wide range channels
942 and 943.
The licensee
prepared
nonconformance
report
DC 2-89-TI-N016.
In additiop,
on March 3,
1989, the licensee
issued
LER 2-88-25-00 regarding this event.
The
inspectors
wi11 follow-up the licensee's
LER in a future report.
Boron In'ection Tank
BIT
B
ass
Flow
On February
3, 1989, the licensee
discovered,
during planned
surveillance testing, that the BIT bypass
flow (for reactor
coolant
-'
pump seal injection flow) was in excess of technical specification
requirements.
The as-found valve was 45.3
gpm vs technical
specification limits of 40 gpm.
The licensee
prepared
a
nonconformance
report
(NCR DC2 89-TI-N019) on 'the subject.
The
inspectors will follow-up through the
NCR process.
e.
Diesel Generator
1-2
Da
Tank Fuel
Hi h Particulate
On February 8, 1989, licensee
management
became
aware of a problem
with particulates
in a diesel fuel oil day tank.
A sample of the
diesel
generator
(D/6) 1-2 day tank fuel, taken
on January
20, 1989,
was found to have
a particulate concentration of 11.5 mg/L.
The
sample
was taken in accordance
with procedure
STP H-lOB, Revision 4,
"Diesel
Fuel Oil Analysis,"
which states
in its acceptance
criteria
for the
D/G day tank:
"When the particulate
contaminant
concentration
of a day tank reaches
10 mg/L, the fuel in the tank
must be cleaned
up using filtration or replaced to avoid plugging
fuel filters."
D/G 1-2 day tank was
sampled
a second
time on
January
31 and was found to have
a particulate concentration of 12.5
mg/L.
An action request
was then initiated to have the day tank
drained
and refi'lied from the main storage
tank.
On February 8, 1989,
the Unit 1 shift foreman (SFN),'subsequent
to
his review of the fuel change
work order,
declared
DG 1-2
The basis for his decision
was Technical Specification (TS) 4.8. l. 1.3.d which states
in part:
"The diesel
fuel storage
and transfer
system shall
be
demonstrated
OPERABLE...at least
once every 31 days
by
obtaining
a sample of fuel oil...and verifying that total
particulate
contamination is less than
10 mg/liter...."
. In addition, the Onsite Safety
Review Group
(OSRG)
had identified
this
TS concern in their review of the action request
on February 3,
1989.
At that time, they referred this concern to the Regulatory
Compliance
group.
On February 8, 1989,
a review had not be.
completed.
This issue raised
two concerns:
(1) the adequacy
of the day tank
acceptance
criteria in STP N-10B and (2) the lack of a timely review
of a Technical Specification concern.
Ade uac
of the
Da
Tank Particulate
Acce tance Criteria:
The day tank particulate
sampling
and acceptance
criteria were added
to
STP M-10B on October 21,
1988,
as part of corrective actions
taken following the day tank biofouling events in May 1988 (refer to
LER 1-88-14).
Historically, the licensee
has complied with TS 4.8. 1. 1.3 by sampling the main storage. tanks,
has only sampled for
water in the
day tanks (in accordance
with TS 4.8. 1, 1.2a),
and
have
considered
the day tanks part of the
D/G as
opposed to the diesel
fuel oil transfer
system.
Based
on the above,
the judgement that 10 mg/L is
a conservative
limit, and
an earlier Justification for Continued Operation
(JCO)
for. high particulate
due to biofouling, the Chemistry Department did
not consider there to be
an operability
concern in their initial
reviews.
However, it seems intuitive that if 10 mg/liter is an acceptance
limit for the storage
tanks,
the limit should
be applicable to the
day tanks since the fuel oil passes
through particulate filters when
coming from the storage
tanks.
In addition, the basis for measuring
just the storage
tanks
appears
to be -that since they supply the 'day
tanks,
there
should
be
no difference in particulate
between
the two.
Also, the earlier
JCO contained
compensatory
measures
which were not
reinitiated when high -particulate
was again discovered.
Finally,
the
FSAR, in section 9.5.4.2, lists the diesel
fuel oil day tanks
as
part of the
D/G fuel oil system.
The inspector
discussed
these
concerns with licensee
management.
While the
TS does
not appear to 'be directly applicable to the
D/G
day tanks,
the licensee
did not have
any documented
technical
basis
for an acceptance
criteria of greater
than
10 mg/L for the day
tanks.
.The lack of including
a strict acceptance
criteria in STP
M-10B was
an error by the Plant Staff Review Committee
(PSRC)
and
indicates
a lack of thorough review.
Following the above discussions,
the licensee
established
an
admini strative
day tank particulate operability limit of 10 mg/L.
The licensee
also initiated a study of the. effects of particulate in
the day tanks
on the fuel filters to determine if. a higher
particulate limit would be more appropriate.
In a separate
occurrence
on February
24,
1989, the licensee
found
a
particulate concentration
of 12 mg/L in D/G day tank 2-2.
The
D/G
was declared
and
a two hour
TS action
was entered
since
a
Safety Injection pump
on
a redundant train was cleared.
Operations
was able to expeditiously return the SI
pump .service
since
maintenance activities
had not yet begun.
Two subsequent
samples
showed particulate to be below 10 mg/L.
Timel
Review of Technical
S ecification Concern:
Al,though it was insightful of the OSRG'o identify day tank high
particulate
as
a potential
TS concern,
the operability review was
not performed in a timely manner since, at the time of their
discovery
on February 3, 1989, the
D/G was in a condition for which
its operability
was in question.
The
TS should
have
been resolved
in, an expeditious
manner.
After this issue
was brought to the attention of plant management
during
a routine weekly exit meeting, it was reviewed in by'he
reviewing the
NCR.
It was determined that the problem resolution
process
had not been adequately
followed.
Licensee
management
considered
that the reviewer
should- have initiated a new Action
Request
(AR) to track the resolution of a "new" problem (problem one
was high fuel oil particulate,
problem two was the potential
TS
concern).
Reinitiating the
AR process
would have required the
.reviewer to reconsider
TS applicability within the
TS action limits.
As corrective action,
the licensee
intends to revise their problem
reporting procedure
to move clearly state .the urgency
needed to
address
operability concerns.
At the end of the reporting period,
the licensee
had determined that
the particulate consisted
mostly of iron oxide and carbon
parti,culate.
A contractor
had been hired to review the particulate
results to determine its origin.
The inspector will continue to
follow the licensee's
actions.
I
Limitor ue Tor ue Switch
Part
21
Re ort
On November 3, 1988,
Limitorque Corporation issued
report concerning torque switches in three valve motor operators.
On February
9, 1989,
the licensee initiated a nonconformance
report
(NCR DC0-89-EM-N011).
The licensee
made
an initial determination that while some of'heir
safety related valves
may be susceptible
to the described failure,
the failures would not,prevent
any of these
valves
from performing
a
design function.
The licensee
intends to perform required
modifications in the next refueling outages.
A secondary
concern
has
been the timeliness of the licensee's
actions.
Preliminari ly it appears
that the,guality Assurance
Department
received
two letters
from Limitorque on the
same
day and
mistook them for the
same letter.
It was not until the Electrical
Maintenance
Department,
which knew separately
of the issue,
questioned
the whereabouts
of the letter that
a review was
initiated.
The inspectors will follow-up licensee
actions with respect to the
issues
of Limitorque operator operability
and the confusion
upon
receipt of the
10 CFR Part 21 notification during routine review of
the
NCR.
Air In 'ected Into The Unit 2 Condensate
S stem
On February ll, 1989 at 9:41 p.m.
a volume of air was injected into
the Unit 2 condensate
system
and traveled through the feedwater
and
system.
This caused
a minor feedwater
flow, condensate
flow, and hotwell level transient.
The licensee
has
had chronic problems with internal
leakage of many
condensate
polisher
system valves.
Because of these valve-leaks,
operators
have
been required to manipulate
manual
valves
beyond what
is called out in procedures.
On February ll, while transferring
a
resin
bed back to a condensate, polisher,
the operator did not open
a
valve which would normally be open but was closed to isolate the
leakage of other valves.
The valve would have allowed water to fill
the polisher prior to its return -to service.
With the fill water
isolated,
the polisher did not completely fillwith water
and when
it was placed
on recirculation through the in service polishers it
allowed air to enter the condensate
system.
The following night in prepqration for the
same evolution on
a
different polisher,
the Shift Foreman
issued
a "formal
communications
sheet"
which added
steps
to the procedure.
The
following day (a. Monday)
an "on-the-spot-change"
(OTSC) was written
to the procedure to establish
interim steps until the leaky valves
are repaired.
The repairs
are scheduled for the next outage.
The chronic problems with the valves
and the lack of adequate
procedures
are just a few indicators of the
need for additional
attention to the condensate
polisher syst'm.
The inspector
discussed
these
weaknesses
with the Operations
Manager
who concurred
that additional attention
was
needed
in the area.
A guality
Evaluation
was initiated to track the root cause of the described
event
and to propose corrective actions.
The operations
manager
stated that one corrective action 'will be to issue
an operations
policy statement
which requires
an,OTSC to a procedure if the
instructions
are
inadequate
to cope with long term equipment,
problems.
In addition,
the Operations
Department is working on
upgrading the control computer at the Condensate
Polisher watch
and
adding
a computer terminal
so that those at the station
can initiate
Action Requests.
The inspector will follow the licensee's
progress
in these
areas
in the course of routine inspection.
Failure of the Auxiliar
Pum
Overs
eed Tri
Actuatin
Device and the Overs
eed Tri
Sto
Valve
FCV 152
On February
12,
1989, at 10:45 p.m.
PST, the licensee
discovered
that the overspeed trip device for the turbine driven auxiliary
(AFW) pump 2-1 was inoperable.
The
pump was declared
and
a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> action statement
was entered
in accordance
with technical specifications.
The discovery of the inoperable
device
was
made
inadvertently during training of auxiliary operators.
The trainees
are being taught
how to trip and relatch the device.
Upon manual
tripping, the overspeed
device did not cause
the overspeed
stop
valve
(FCV 152) to go shut.
This was
a cold test,
steam
had not
been admitted to the line.
The cause of the failure to actuate,
including a discussion .of
inadequate
maintenance
for the overspeed trip valves, is included in
Inspection
Report 50-275/89-13.
Described
below are additional
weaknesses,
identified by the inspector,
that did not have
a direct
effect on the operability of the valve,'ut which indicate the
need
for management
attention.
Poor Work Orders
Corrective maintenance
work order
(WO C0049505),
issued to
investigate
and repair
FCV 152,
was lacking in detail
and provided
the craft with a drawing of an, overspeed trip device different than
that installed.
Work orders
lacking in detail (e.g.,
in this case
"investigate," "disassemble,"
and "lubricate
and dust
as required")
can lead to improperly performed work.
This has
been the subject of
a previous inspection report (50-275/88-32
paragraph
5a).
The licensee
response
has
been, limited to addressing
the specific
items addressed
by the inspector
and
has not embarked
on a general
program of work order improvement.
The examples identified to date
have not resulted in improperly performed maintenance.
Poor Oesi
n Confi uration Controls
Some of the actions
taken
by the licensee that were examined in this
incident
show that licensee
personnel still lack. sensitivity to the
proper process
for making design
changes.
Although the examples
appear to be technically satisfactory
they demonstrate
that the
wrong organizations
are making design decisions.
~Exam les
o
A split brass
washer
used
as
a stem bushing for
FCV 152 was
replaced during the maintenance
work on
FCV 152
on February
14,
1989.
The replacement
part (Schutte
and Koerting PN-765012)
did not fit and
was modified to a larger inside diameter
by
verbal direction of a maintenance
engineer.
Maintenance
engineers
do not have design authority per licensee
procedures.
The maintenance
engineer
considered
the authorization to be
a
duplication of the part installed but had
no knowledge
as to
whether the part supplied
from the warehouse
was misordered.
The problem and the maintenance
engineers
resolution were
recorded
on action request
A-0140624.
However, through
discussion
the inspector
concluded that the maintenance
engineer
and the lead
gC inspector involved were not conscious
of the fact that the part obtained might not be adequate.
On
February
23,
1989,
the inspector
requested
maintenance
engineering to contact the vendor to resolve whether the part
was adequate
and whether part ordering information was faulted.
Neither
gC nor maintenance
had raised the question.
On March 1, 1989,
maintenance
personnel
stated that the vendor
had
been contacted
on February
28,
1989,
and
had stated that
the split washer received
was the proper part and of the proper
dimension.
The vendor stated that the valve actuator
stem,
which contains
a step to accept
the split washer did not appear
to be
a standard part -based
on the dimensions
provided by PG8E.
PG8E further determined
through research
of maintenance
history
that the valve bonnet assembly
had
been
loaned to Portland
General Electric, Trojan, in 1976
and returned in May 1977
and
10
has
been installed ever since.
PG8E committed to contact
Trojan and resolve the ambiguities of parts for FCV 152.
The modification of the split brass
washer authorized
by the
maintenance
engineer with out the appropriate
design
review is
an apparent violation of 10 CFR 50 Appendix
B Criterion III
which states
"Design Changes
including field changes
shall
be
subject to design control measures
commensurate
with those-
applied to the original design...."
(Enforcement
Item
50-323/89-05-01)
A second
example of'poor configuration control
and possibly
an
unauthorized
design
change
involved the configuration of the
overspeed trip device for the auxiliary feedwater
pump 2-1.
In November of '1988,
the mechanism first failed to trip during
testing.
Subsequent
maintenance
was performed
as
documented
on Work Order
WO C0045447.
However when mechanical
checkout
showed the mechanism still would not work, mechanics
rotated the spring mounting bracket
90 degrees
to increase
the
spring tension
as recorded
in the handwritten
comments
on the
work order entered
by the craft.
Further investigation
by the inspector
showed that the change
(to rotate the bracket
90 degrees)
was discussed
with a
maintenance
engin'eer
who in turn discussed it with the vendor
who approved
the change verbally.,
None--of these
conversations
were recorded
on
a telephone
record
and such verbal
approval
does
not follow the licensee
requirements
for a design
change.
In the opinion of the licensee's
maintenance
engineer
the
change did not constitute
a design
change
and was
an acceptable
means of adjusting spring tension.
Even if the change
was not viewed as
a design
change
there
were
no actions
taken to record the position of the spring mounting
bracket in an instruction for future maintenance,
i.e.,
no
assurance
of future configuration control
was provided.
The work performed i n November 1988, contained
a s'eparate
example of lax configuration control.
That is, the drawing
issued with Work Order
WO C0045447 for the overspeed trip
mechanism did not represent
the mechanism installed in that
parts
were physically different and part orientation
and
actuation directions
were different.
The drawing provided was
Terry Corporation drawing 800269E dated
March 30,
1982.
In
this earlier case
the work order recognized
the drawing problem
and
had
a line item 8 (on Activity 3) for mechanical
engineering
to submit
a field change to the drawing to reflect
field conditions.
I
However at the close of work, the. maintenance
engineer "N/A'd"
the step with a note that the plant system engineer
was to
"review documents
and update
as necessary".
This was not done
and
as
a result in February
1989,
when the overspeed trip
11
mechanism
again did not operate,
the corrective work order
(WO
C0049505)
wa's issued with the wrong drawing again.
Although
the wrong drawing did not apparently contribute to improper
maintenance,
the formality of recognizing
and handling of
changes
was poor.
Subsequent
to questions
raised
by the inspector the licensee
obtained
an applicable
drawing from the vendor. (Terry
Corporation drawing
B 12556 dated
June
14,
1968)
and
has
included
an action to incorporate
the drawing in a detailed
maintenance
procedure.
The issue of maintenance
personnel
authorizing design
changes,
contrary to
PG8E procedures
restricting design
change authorization
to design engineering
personnel,
has
been the subject of previous
inspection reports
and violations.
Specifically inspection report
50-275/87-08 involved the manufacture
of an auxiliary feedwa'ter
pump
oil slinger ring with a material different than the drawing and
.
report 50-323/86-30 dealt with the omission of nece'ssary
washers
from pipe snubbers
by verbal
maintenance
engineer
authorization.
The similar design authorization
issues
raised in this report
may
arguably not be clear cut design
changes
but do demonstrate
that
plant quality control, maintenance,
and system engineering
are not
sensitive to design authorization
issues.
The lack of sensitivity of plant personnel
to potential
de'sign
changes
was discussed
with plant management.
Plant management
committed to include corrective action to prevent recurrence
in
their nonconformance
report and in the
LER being prepared
on the
overspeed trip mechanism.
Unit 1 Auxiliar Saltwater Crosstie
Valve Ino erable
On February
14,
1989,
a guality Control inspector
discovered that
the packing gland retainer
studs
on Unit 1
ASW pump discharge
crosstie
valve FCV-495 had sheared
and the retainer
was rotating
with the shaft.
He reported it to.operations
and
FCV-495 was
declared
entering the plant into a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />
TS action
statement.
Maintenance
mechanics
found that packing gland retainer
had frozen
to the shaft
due to excessive
rust.
Therefore,
the carbon steel
retainer
studs',
which were also badly oxidized, broke'hen
the valve
rotated.
The mechanics
were able to remove the retainer
from the
shaft
on February 16th.
After cleaning the shaft
and the retainer
of rust,
they were reassembled
with new stainless
steel
studs.
The licensee
has initiated
NCR DCI-89-MM-N018 on this issue.
The
inspectors will follow this
NCR during routine inspection with
emphasis
on
how the licensee
addresses
the use of carbon steel
components
in the highly corrosive,
saltwater
atmosphere
of the
intake area.
12
Unit 2 Main Feedwater
Pum
On February
23, 1989, at 6:34 a.m.,
the Unit 2 main feedwater
(MFW)
pump 2-1 experienced
a control transient'in
which the high pressure
and low pressure
MFW pump gover'nor went to full open.
The control
transient,was
due to a loss of power to the
MFW pump 2-1 speed
probes.
At 6:41 a.m.
the transient
was terminated
when power was
r'estored
to the speed
probes.
During the transient
MFW pump 2-1
increased
flow to above
10 million pounds per hour (MPPH)'hile pump
2-2 automatically
reduced to approximately 4.5
MPPH resulting in
slightly less
than
100X total flow to the steam generators,
which in
turn lowered
levels..
Pump discharge
pressure
remained relatively constant during the event.
The loss of power to the speed
probes resulted
when its breaker.was
opened.
The breaker
was
opened to -perform maintenance
on the
2-1 lube'oil strainer,
which it also supplies.
Electrical drawing
of the breaker,
PJ 21-2-13, which is on
a panel that supplies mostly
turbine plant house
loads
such
as lighting, did not indicate it
~
supplied the
MFW pump 2-1 control
speed
probes.
Operations
and the
clearance
coordinator,
unaware that
PJ 21-2-13 supplied the speed
probes,
wrote and issued
a clearance
to open the breaker.
As. a result of the transient,
the licensee initiated an event
investigation.
Some of the immediate acti'ons
included
a moratorium
on the clearing of lighting panel
breakers
since drawings are
apparently
incomplete.
The licensee
also initiated an investigation
of why
MFW pump 2-1 did not trip on overspeed.
Preliminary it was
determined,
using the pump'curve.-and
conservative
pump differential
pressure
and flow valves, that the turbine was at least
100
rpm
below its 6380
rpm trip setpoint.
In the nonconformance
report the licensee
addressed
the adequacy of
lighting panel
drawings to describe
equipment they supplied.. It was
determined that this "fed from" information is available for
electrical
panels other than lighting panels.
Action was initiated
to revise this information for lighting panels'n
addition, the
,licensee initiated an evaluation of all equipment
whose failure
would cause
a
MFW pump trip.
As an example,
the redundant
speed
probes
are
powered
from the
same
power supply.
Had they been
powered
by redundant breakers,
the
MFW pump would have
remained
stable.
The inspector
found that the licensee
took prompt andithorough
action in evaluating this transient
an'd
showed the proper attention
to an indicator of a balance of plant problems.
Nonconformin
Circuit Breaker to
ASW
S stem'nit Crosstie Valve
In their review of NRC Bulletin No. 88-10;
"Nonconforming
Molded-Case Circuit Breakers,"
which documents
the misrepresentation
of refurbished ci rcuit breakers
as
new equipment,
the licensee
identified circuit breaker
as traceable
to,a supplier of
"refurbished" circuit breakers.
The class
1 breaker supplies
the
0
13
motor operator for valve FCV-601; the Unit 1 to Unit 2
ASW system
crosstie
valve.
The licensee
completed,
on February
24,
1989,
a Justification For
Continued Operations
(JCO) including a Safety Evaluation
and
a 10 CFR 50. 59 evaluation.
The licensee
based
continued operations until
the October Unit 1. refueling outage
on the following factors;
Installation and routine testing of the breaker since its
installation in March 1988.
This included magnetic trip
characteristics
testing.
All results
were satisfactory.
0
The licensee
did not take credit for the operation of the valve
in the
FSAR.
It would be opened,
in accordance
with procedure,
with the complete
loss 'of ASW to one Unit.
The inspector
reviewed the
JCO and found it acceptable.
1.
Diesel
Fuel Oil Transfer Vault Backflow Check Valves
On February
24,
1989, the. licensee
took compensatory
actions in
accordance
with a justification for continued operation for missing
diesel
fuel oil pump
room (vault) check valves.
The room floor
drains
were to-have
been protected with backflow check valves.
This
item is discussed
in detail in 'paragraph
6b.
m.
Auxiliar
Saltwater
Pum
'Overcurrent Tri
Breakers
On February
27,
1989,
the licensee
made
a 10 CFR 50'2 four hour
non-emergency
report based
on the licensee's
technical
review group
decision that the plant had operated
in a degraded
condition in that
the
pump circuit breakers
had not been set to higher values
when
larger
pump impellers were installed.
This issue
was identified by the
NRC team inspection
conducted
in
February
1989 and it discussed
in. detail in inspection report
50-275/89-01.
One Violation and
no deviations
were identified.
5.
Maintenance
62703)
The inspectors
observed .portions. of, and reviewed records
on, selected
maintenance activities to assure
compliance with approved procedures,
technical specifications,
and appropriate
industry codes
and standards.
Furthermore,
the inspectors verified maintenance activities were
performed
by qualified personnel,
in accordance
with fire protection
and
housekeeping
controls,
and replacement
parts
were appropriately
certified.
The inspectors
observed
and reviewed portions of the the following
maintenance activities which are described
elsewhere
in the report;
a)
Corrective Maintenance
performed
on
AFW pump 2-1 turbine stop valve
FCV-152 (Section 4h).
b)
Corrective Maintenance
performed
on Unit 1
ASW train cross-tie
valve
FCV-495 (Section 4i).
c)
Diesel
Generator air-start motors (Section 4b).
The violation related to item a) is described
in the referenced
section.
No additional violations or deviations
were identified.
6.
Maintenance
Team Ins ection Follow-u
62700
62702
92702
92701.
a.
Failure to
U date
0 en Item 1-88-15-01
Closed
~Findin:
The maintenance
team identified four instances
where
modifications were
made to the facility compressed air system
as
described
in the
FSAR without subsequent
revision of the
FSAR.
These
include:
(1)
Addition of air compressors
and their operational
interfaces
with plant permanent
equipment,
interlocks,
and alarms.
(2)
Procedure
changes
and operation with dewpoint greater
than
minus 48 degrees
F.
(3)
Use of 5 micron filters in lieu of 3 micron filters -in
compressor
configurations.
(4)'nability of main steam isolation valves to remain
open for all
but main steam rupture events,
Licensee Corrective Actions:
In response
to these findings, the
licensee
committed to do the fol'lowing:
(1)
Incorporate all items into the
FSAR Update,
Revision 4,
submitted
on September
22,
1988;
(2)
Revise Nuclear Plant Administrative Procedure
(NPAP) C-1
"Nuclear Power Plant Modification Program,"
NEMP 3.6
ON, and
NPG Procedure
4.4, "Final Safety Analysis Report Update
Change
Request,"
to clarify requirements
on temporary design
changes.
In addition,
a commitment
was
made to write a procedure
for the
annual
FASR update revision.
(3)
Include
a review of the
FSAR update
as part of the
configuration management
program.
Review:
The inspector
reviewed the licensee's
commitments
and
found, they adequately
addressed
the team's
finding.
In addition,
the inspector
reviewed the status of the licensee's
implementation
and found:
(1)
The revisions
were
made to the
FSAR as stated.
In addition,
the inspector
reviewed Operating
Procedure
AP K-1: I and found
that revisions
had been
made to provide guidance
on actions to
be taken resulting from high dewpoint, including a detailed
walkdown check list.
(2)
The revisions
were
made to procedures
NPAP C-1 and
NEMP 3.6
ON,
as stated.
In addition
NPG procedures
4.4 and 4.8 were issued
in November,
1988, to describe
the process
of requesting
and
implementing revisions to the 'FSAR.
(3)
See section
6g describing the review of Configuration
Management
Program
commitments.
Based
on the above review,
Open Item 50-275/88-15-01 is closed.
b.
Testin
of Check Valves
Used in Accident Miti ation and Plant
Shutdown
Com onents
0 en Item 50-275/88-15-02
Closed)
~Findin:
The team found that the licensee
had failed to establish
a
test program that would assure that check valves
necessary
for
accident mitigation and/or
shutdown of the plant would perform
satisfactorily
in service.
Licensee
Corrective Actions:
The licensee
committed to:
(1)
Create test procedures
for the deficienc'ies identified in the
(2)
Complete
a review of the maintenance
and testing of the
instrument air system,
in accordance
with Generic Letter 88-14
and other check valves in accordance
with SOER 86-03;
and
(3)
Review the adequacy
and timeliness of the incorporation of
operating
experience
into licensee plant programs.
In addition,
the licensee
committed to have
a task force led by
Engineering,
in conjunction with the Configuration Management
Program,
to review the surveillance test program.
Review:
The inspector
reviewed the licensee's
commitments
and found
that they acceptably
addressed
the finding.
The adequacy of the
licensee's
response
to Generic Letter 88-14 will be addressed
in a
separate
inspection.
One example in the Notice of Violation was the lack of a testing or
maintenance
on diesel
engine fuel oil vault floor drain backflow
In the response
to the Notice of Violation the
licensee
committed that by December
31,
1988,
a program would be
established
to test the check valves.
On December
22,
1988, in the process
of creating test procedures
to
test the backwater
the maintenance
manager
found
grease
traps
and not backwater
were installed.
On
January
19,
1989,
a senior maintenance
engineer initiated an
evaluation to determine if backwater
check valves were necessary
and
to either replace
the grease
traps with check valves or revise the
FSAR.
On January
27,
1989,
the onsite project engineering
group
(OPEG) performed
a walkdown which confirm that grease
traps
were
installed.
OPEG requested
corporate
engineering
to review the
backflow check valves.
Corporate
Engineering
had not completed
their review on February
21,
1989,
when the inspector, initiated his
review.
On February 24, 1989, the inspectors
questioned if the licensee
was
operating in an unreviewed condition, since the installed equipment
did not meet the
FSAR description.
The licensee
subsequently
determined that the backflow check valve were required to prevent
flooding from the
5'2 heater drip pump pit drain which, is headered
down stream.
Had the drain line been blocked downstream of the
and
had the k2 heater drip pump room flooded (either "due to
the failure of its associated
piping or the circulating water to the
condenser
expansion joint) both diesel
fuel transfer vaults would
have flooded creating
the possibility of a
common
mode failure.
The
lack of blackflow check valves installed in the diesel
fuel transfer
pump vault drains is
an apparent violation (50-275/89-05-01).
Enforcement will be the subject of separate
correspondence.
The licensee
performed
a
10 CFR 50.59 evaluation
and took
compensatory
measures.
These
included blocking the 82 heater drip
pump pit drain and monitoring the
room for flooding, verifying the
operability of the
room water level indicators,
inspecting
the fuel
oil transfer vaults for debris,
and verifving the drain line was
fr'ee of obstructions. 'n addition the licensee
made
a report to the
NRC in accordance
with 10
CRF 50.72.
The inspector
found these
actions to be acceptable,
The inspector interviewed the senior maintenance
enqineer
and the
OPEG civil engineer
involved to determine
why it had taken
two
months
and s'ubsequent
NRC questioning
to resolve the backwater
check
valve issue.
They noted that the analysis
contained in the
which addressed
the maintenance
team's
findings indicated that the
chance of flooding the diesel
fuel oil transfer
pump vaults
was
"a
highly unlikely event".
In addition, the
rooms were equipped with
high water level annunciators.
However, the licensee
should
have
recognized
the
need f'r compensatory
measures.
The lack of prompt
corrective action is an apparent violation (Enforcement
Item
50-275/89-05-03).
Enforcement will be the subject of separate
correspondence.
At the
end of the inspection period,
the licensee
was implementing
the compensatory
measures
prior to resolution which could include
the installation of a check valve in the floor drain.
The licensee
also initiated
a
new
NCR to address
the timeliness of corrective
actions
and the installation of grease
traps
instead of check
valves.
The licensee
determined that in 1978,
when the vaults
had
been relocated
to facilitate construction of the turbine butresses,
drains with check valves
were not reinstalled.
The inspector will
further review the root cause
and corrective actions
in fnllowup
inspection activity.
17
c.
Lack of ASME Section
XI Test Pro
ram for 10% Atmos heric Steam
Dum
Valves
0 en Item 50-275/88-15-03
Closed
~pindin:
The team found that no testing
was performed to
demonstrate
the ability of the lOX Atmospheric
Steam
Dump Valves to
operate
using only its backup air supply.
Licensee Corrective Actions:
The licensee
committed to develop
procedures
to demonstrate
the operational
readiness
of the
10K steam
dump valves to withstand the loss of the normal air supply and the
backup nitrogen supply.
Additionally, the licensee reiterated their
commitment to review air and nitrogen supply system
whose fai lure could compromise
the ability to mitigate transients
as
discussed
in Section
6b.
Review:
The inspector
reviewed the licensee's
commitments
and
found that they acceptably
addressed
the team's findings.
Open Item
50-275/88-15-03
is closed..
d.
Failure to Assure that Conditions Adverse to
ualit
were
Prom tl
Identified and Corrected
0 en Items 50-275/88-15-04
and
50-323/88-14-01
Closed)
~Findin:
The team found
a number of problems,
resulting in water
intrusion to the plant compressed
air system,
were not adequately
identified, investigated
and corrected
using the plants
administrative
procedures
for problem resolution.
Licensee Corrective Actions:
The licensee
committed to:
(1)
Revise Administrative procedure
C-12 to require that quality
evaluations
and non-conformance
reports
be written to
document'nd
resolve non-safety related
problems significant enough to
warrant root cause
determination.
(2) 'ave
PG8E General
Construction
(GC) switch to the plant problem
reporting system.
(3)
Train
GC personnel
on plant problem reporting procedures
to
assure
that problems identified by
GC personnel will be
- properly reported
and evaluated.
The licensee identified five other immediate corrective actions
taken which implemented training of personnel
to stress
the
need for
adequate
resolution of non-safety related significant problems.
Review:
The inspector
found the licensee's
commitments
acceptably
address
the team's
findings.
Open Items 50-275/88-15-04
.and
50-323/88-14-01
are closed.
Inade
uate Auxiliar
Pum
Inservice Testin
Criteria
0 en
Item 50-275/88-15-05
Closed)
~Findin:
The team
found that the licensee
specified
low
differential pressure
action criteria for the turbine driven
(AFM) pumps
was
lower than the
ASNE code Section
XI requirement of 90K of reference.
The licensee
had used the
Technical Specification acceptance
criteria instead of the more
conservative
ASNE code requirement.
Licensee
Corrective Actions:
In response
to these findings, the
licensee
did the following:
(1)
Revised the acceptance
criteria to meet the more conservative
requirements
of ASNE Section XI.
(2)
Reviewed previous test data
and found that the
ASME Section
XI
requirements
had not been violated.
(3)
The
AFM pump test procedures
were revised to discuss
the
different acceptance
criteria.
(4)
A review of other
pump test acceptance
criteria was performed.
(5)
The'icensee
committed to develop
a procedure for the
establishment
of alert and action acceptance
criteria for
pumps.
(6)
The licensee
committed that the configuration management
program would include review of the Technical Specifications
to
assure
cohsistency with applicable
requirements
of the
code.
Review:
The inspector
found the licensee's
commitments
and
corrective actions
acceptably.
address
the teams findings.
This item
i s c 1 osed.
Inade uate
Pro
ram for Review of Inservice Test Procedure
Chan
es
0 en Item 50-275/88-15-06
Closed
~Findin:
The team
found that changes
to inservice testing
acceptance
criteria (contained in Volume
9 of the plant manual)
were
not being approved
by the power plant engineer
and reported to the
Plant Staff Review Committee
(PSRC)
as committed in
PSRC minutes
dated
August 29,
1979,
and that
no documented
program existed
defining the requirements
for review and approval of changes
to
Volume 9.
Licensee Corrective Action:
The licensee
committed that by October
31,
1988,
an administrative
procedure
to control
changes
to Volume 9
of the plant manual
would be developed.
Review:
The inspector
found that the licensee's
corrective actions
acceptably
addressed
the teams findings.
This item is closed.
19
,h.
Corrective Action Commitments in Res
onse to Notices of Violation to
e
m
emente
b t e
on i uration
Mana ement
ro ram
NP
In response
to. the Hotices of Violations discussed
in the previous
paragraphs,
the licensee
made .the following commitments
which are to
be implemented
by the Configuration Management
Program
(CNP):
(I)
A review of the adequacy of the surveillance test
program by a
task force led by Engineering with membership
from the plant
system engineering
group.
(2)
A review will be conducted
to assure
consistency
among
operational,
design,
and regulatory documents,
including the
FSAR update
(3)
A review of the Technical Specifications
to assure
consistency
with applicable
requi'rements
of the
ASME code.
At the time of this inspection,
these
commitments
had not been
implemented
and were scheduled for long term completion.
The
residents
and regional
sta f will continue to follow the licensee's
implementation of the
CNP including the listed commitments.
Trainin
Re uirements Definition Follow-u
(0 en Item
50-323 88-1 -02.
C osed
Durino the maintenance
team inspection it was identified that there
was
no clear definition of the minimum traininq requirements
(content
and timeliness) for various staff engineering
positions
specific to the
DCPP organizational
structure.
The inspector
reviewed the licensee's
response
to the inspection report
(PGSE
letter Ho. DCL-88-236).
The response
only addressed
the training
'eouirements
as it pertained
to the systems
engineers
and found that
for these
individuals the training requirements
were defined
and
reasonable
goals
and schedules
for training were developed.
The
inspector
interviewed the Assistant Plant Manager/Technical
Services,
the Operations
and Engineering Training supervisor
and
various training staff members.
The inspector further reviewed the
.applicable
procedures
and schedules
for the Technical Staff Training
program.
The Inspector verified that
a similar training effort
conducted for the systems
engineers
was completed or is planned for
the Chemistry Department,
Maintenance
Department,
Onsite Safety
Review, guality Control, Radiation Protection,
and Regulatory
,Compliance
groups.
Also evident
was voluntary participation
by
engineers
from Emeroency
Planning, Material Services,
Planning
and,
Scheduling
and equality Assurance.
This item is closed.
Two violations
and
no deviations
were identified.
7.
Survei1 lance
(61726)
By direct observation
and record review of selected
surveillance testing,
the inspectors
assured
compliance with TS -requirements
and plant
20
procedures.
The inspectors verified that test .equipment
was calibrated,
and acceptance
criteria were met or appropriately dispositioned.
a.
Auxiliar Saltwater
S stem Performance
Test
As a commitment
made in response
to the. Safety System Functional
Inspection
(SSFI)
team findings, the licensee
conducted
an Auxiliary
Saltwater
(ASW) system performance test.
As discussed
in inspection
report 50-275/88-01,
the team questioned
the ability of one
ASW pump
to fill both heat exchangers
and felt there
was the potential for
the heat exchangers
running without ASW flow through all tubes
resulting in reduced
heat
removal capability.
In response
to this
finding, the licensee
committed at the team's= exit meeting, to
perform a system test to determine flow characteristics
of the
ASW
system.
The licensee's
test procedure
(TP TB-8903) was designed
to obtain
flow, pressure,
differential pressure,
and temperature
measurements
of'arious parameters
while altering system configuration.
The
tested configurations
included
one pump/one
heat exchanger,
two
pumps/one
heat. exchanger,
one pump/two heat exchangers,
and
one
pump/one
heat exchanger
through the train crosstie
valve.
When the licensee first attempted to perform the test
on February
17,
1989,
two problems
were encountered.
The first problem was that
no procedures
allowed the operation of two pumps through
one heat
exchanger.
This required
an "on-the-spot-change"
to the test
procedure.
The second
problem was the adequacy of the temporary
instrumentation installed.
Plant engineering
had specified tygon
hose to be used
as
a level indicator on the inlet and outlet water
boxes of each heat exchanger.
The instrumentation
was installed by
the Instrumentation
and Controls (I&C) department.
Thin translucent
tubing was
used
and,
as
a result,
strong capillary action in the
tubing combined with air entrainment
resulted
in bubbles which
affected the readings.
Additionally, tubing slope
was not specified
in the instructions
and
as
a result the installed tubing had high
and low spots,
creating air pockets
and collecting crud
respectively,
again affecting readings.
As
a result of these
problems,
the test
was postponed shortly after its start.
On February
22, 1989, the licensee
attempted
and completed the test,
having provided specific instrumentation instructions for IBC.
The
inspector
observed portions of the test.
At the
end of the report period the licensee
was in the process
of
reviewing the data
and extrapolating it to various expected
operations
conditions (e.g.,
low tide).
Preliminary findings
indicate that in all configurations the heat exchangers
run full
with adequate
flow to meet design basis criteria.
It was noted to plant management that the first test attempt
was not
the first time temporary
instrumentation
was not adequately
specified in instructions resulting in erroneous
readings.
Since
the loss of
RHR event in April 1987, which was aggravated
by a
. 21
poorly installed instrumentation
system,
there
have
been several
similar examples
such
as the temporary instrumentation
used
on the
Unit 2 steam generator.
In the exit meeting,
the licensee
committed
to review its policy of installing temporary instrumentation.
This
will be followed up by the inspector during routine inspection.
Other Surveillance
Testin
In addition to the above the inspectors
examined portions of
'surveillance testing
as described
in other
sections
of this report.
Specifically:
Diesel'Generator=Testing
(4b); Diesel
Fuel Oil
Testing (4e); Auxiliary Feedwater
Overspeed Trip Test (4h); and
Pump 1-2 Inservice Testing (8) were examined.
No violations or deviations
were identified.
8.
En ineerin
Safet
Feature Verification
71707
Unit 1 Auxiliar
S stem
On January
24,
1989, the inspector performed
a w'alkdown of the Unit 1
Auxiliary'eedwater
(AFW) system.'he
inspector verified breakers
and
valves were in their appropriate positions,
appropriate
valves
were
sealed,
hanger
supports
and instrumentation
were properly installed,
and
assessed
overall
system condition.
Additionally, the inspector
observed
portions of a
AF'W pump 1-2 inservice test.
The inspector
made the
following observations:
1)
The seismic support for AFW pump 1-3 motor bearing thermocouple
conduit was missing its bracket
and
was therefore
2)
There
was
a loose support bracket attached
to
AFW pump 1-3
recirculation'line
downstream of its throttle valve.
The purpose of
the bracket
was not apparent
to the inspector.
3)
In a
number of instances
the inspector
found that drain lines
on the
AF'W system
were missing
caps
as indicated
on plant drawings.
4)
The inspector
noted
a periodic high pitched sharp rattle
on
AFW pump
l-l turbine
steam supply check valve 1-5167.
These findings were discussed
with the
AFW system engineer.
Resolution
of these
items is as follows:
1)
The system
engineer initiated
a seismic evaluation
by the Onsite
Project Engineering
Group
(OPEG).
OPEG determined that the conduit
was seismic class
one,
however the instrumentation
was class
two.
The reason for
installing
.class
one conduit was to limit the
possibility for seismic interaction by maintaining seismic
qualification of all components.
It was determined that even in the
as found configuration', there were
no seis'mic interaction concerns
and neighboring equipment
would not have
been effected.-
However,.to those'or king on the pump, the conduit should
have
been
treated
as seismic class
one.
A number of recent
examples
indicate
22
there is further need for the licensee to more explicitly address
seismic configuration in work packages.
Specific corrective actions
were identified in
LER 2-88-25,
"Seismic Bracing Hissing
From
Instrument
Panel
Due to Inadequate
Configuration Control" which will
be reviewed
by the inspector in a future inspection.
2)
The system engineer,
after
some searching,
was able to identify the
bracket
as
an old recirculation throttle valve locking device which
has
had it's function superseded
by the current valve sealing
program.
OPEG inspected
the device
and found it did not affect
seismic qualifications.
A work package
was generated
to remove the
device.
3)
As a result of recent events,
including the steaming of the
AFM pump
2-1, described
in detai
1 in Inspection
Report 50-275/89-13,
the
licensee
has
undertaken
a program to more carefully control drain
caps.
The operations
manager
committed to revise all system. valve
alignment procedures,
as part of the two year
review cycle, to
include plugs
and caps.
In addition, all clearances
are to include
the installation
and removal of plugs
and caps.
The inspector" will
follow this program in later inspections.
4)
The noisy check valve had been previously identified by the licensee
and will be replaced
during the next refueling outage with a
=
different model.
No violations or deviations
were identified.
9.
Radi ol o ical Protecti on
71707
The inspectors periodically observed radiological protection practices
to
determine whether the licensee's
program
was being implemented in
conformance with facility policies
and procedures
and in compliance with
regulatory requirements.
The inspectors'erified
that health physics
supervisors
and professionals
conducted
frequent plant tours to observe
activities in progress
and were generally
aware of significant plant
activities, particularly those related to radiological conditions and/or
challenges.
ALARA consideration
was found to be an integral part of each
RMP (Radiation Work Permit).
It was noted that
some
RWPs were
somewhat
ambiguous
as toprotective
equipment
requirements
(such
as clothing, dosimetry
and respirators).
The ambiguity was discussed
with the Radiation Protection
Manager.
The
RP Manager reviewed the matter
and responded
that the
RWPs are computer
generated
and the ambiguity had resulted
from a software
inadequacy.
He
noted that all the information required to make the appropriate
selection
of protective
equipment
was contained
on the
RMPs and that there
had been
no history of plant personnel
using inappropriate protective equipment.
However
he concurred that the
RMPs could be clearer'nd initiated actions
to have
them revised.
The inspectors will review the improvements
when
the
RMPs are revised.
No violations or deviations
were identified.
23
10.
Ph sical Securit
(71707)
Security activities were observed for conformance with regulatory
requirements,
implementation of the site security plan,
and
administrative procedures
including vehicle and personnel
access
screening,'ersonnel
badging, site security force manning,
compensatory
measures,
and protected
and vital area integrity.
Exterior lighting was
checked during backshift inspections.
No violations or deviations
were identified.
11.
Licensee
Event
Re ort,Follow-u
92700
a.
Status of LERs
t
The
LERs identified below were also closed out after review and
follow-up inspections
were performed
by the inspectors
to verify
selected
licensee
corrective actions:
Unit 1:
88-13 (Revisions
0 and 1), 87-29
, 88-28
Unit 2:
88-07
, 88-24 (Revisions
0 and 1)
See following write-ups
b.
Autostart of Dies'el Generator
2-1 due to Inadvertent. Removal of
Vital Bus
Fuse Block Durin
LER 2-88-07-LO (Closed
On June
30,
1988, plant electricians
performing preventive
maintenance
on a component cooling water
pump breaker inadvertently
pulled
a wrong fuse block which supplies portions of the vital 4KV
bus
G voltage potential
sensing circuit.
The sensed
loss of bus
potential
caused
bus
G to strip and initiate a transfer to startup
power.
The
LER was reviewed for event description,
root cause,
corrective
actions
taken,
generic applicability, and timeliness'f reporting.
Corrective actions
were verified completed
by review of site
documentation
and action request
system.
This
LER is closed.
c.
LER 1-87-29'-LO
Closed
This
LER dealt with ESF time response
testing.
The remaining issue
dealt with the fact that the licensee
does
not measure
slave relay
actuation
times
as part of the
ESF actuation
time test.
The licensee's
rationale
and compensatory
actions which are
described
in the
LER were discussed
in a conference call between
the
resident
inspector
and
NRR on June
9,
1989.
The,licensee's
actions
were found to be appropriate.
Therefore this
LER is considered
closed.
No violations or deviations
were identified.
12.
0 en Item Follow-u
92703
92702
a.
Auxiliar
Control Board Annunciators
Res
onse
Procedures
Follow-u
Item 50-275/88-03-04
Closed
In-.inspection report 50/275/88-03,
dated March 28, 1988, it was
identified that the Auxiliary Con'trol Board Annunciators
response
procedures
were not formally controlled
and that operators
were
authorized to make pen and ink changes without'urther approvals.
The licensee
committed to formalize the procedures
at that time.
On February
10, 1989, the licensee
issued
a complete set of Plant
Staff Review Committee reviewed
and approved annunciators
response
procedures
for the Auxiliary Control Board.
The inspectors will
review the adequacy of these
procedures
during routine inspection.
This item is closed.
b.
Redundanc
of Diesel
Generator
Air Start Trains
0 en Item
50-275/88-17-01
Closed
On February 6, 1989, the plant engineering
manager
informed the
resident. inspector that the "normal" diesel
generator
(D/G)
DC power
supply must be operable
and selected for control at the local panel
for the D/6 to be operable.
The licensee
made these findings in
response
to a June
1988 question of the operability of a D/G with
one air start train inoperable
or otherwise
unable to start the
D/G
within its required start, time.
This conclusion
was based
on the following:
The emergency
backup vital
AC power system is required to
'erform
its specified design function given
.a single failure.
If a component is declared
and
a
TS action statement
entered
the component is considered
to be the single failure.
Each of the. three
D/Gs has "normal" and "backup"
DC power
supply,
each of which actuates
two of four air start solenoids.
Therefore
each of the three
DC buses
supply
a D/G's "normal"
and another
D/G's "backup" power.
There is
a
DC power select switch on each
D/G local control
panel to select either
"normal" or "backup" power'for D/G
control, including the generator field flash.
Two possible
scenarios
where the single fai lure of a
DC bus results
in two D/Gs not supplying vital power are
as follows:
If any D/G has its select switch in the "backup" position and
that
DC bus fails, that
D/G will not.start, a'nd the D/G, which.
has its "normal" supply from the failed
DC bus will not have
a
generator field flash.
25
With all select
switches in "normal", if a "normal" supply to
one
D/G is out of service
and its "backup" power
DC bus fails,
that D/G would fail to start
and the
D/G which has "normal"
power supplied
by the out of service
DC bus would start but not
flash.
This appears
to be another
case
where the understanding
of, the
design basis
was not implemented in plant procedures.
What
compounds
the problem in this case is that it appears
the licensee
had
a number of opportunities to review their design, failed to
do'o,
and thus failed to resolve the fundamental
question of why there
are two start trains for'he D/G.
Opportunities
included
a January
1988 gA Audit finding report and
a June
1988
NCR.
This item is unresolved
pending
a review to determine if the
licensee
should
have identified D/G
DC and airstart train
oper ability requi rements eajlier, if the licensee
has
ever operated
with an undeclared
D/G, and if corrective actions
are
taken in a timely manner
(Unresolved
Item 50-275/89-05-02).
No Violations or, Deviations
were identified.
13.
Desi
n Chan
es
and Modification Pro
rams
37700)
The purpose of this inspection
was to evaluate
the effectiveness
of the
licensee's
program for implementing plant modifications
and for effecting
changes
in the design of Diablo Canyon Units 1 and 2,
and to determine
that'such plant modifications
and changes
in design are in conformance
with the requirements
of the technical specification
(TS) and
To this end,
the processes
for initiating, approving,
processing,
and documenting
design
change
and
new design;
and the mechanics
of
installing/constructing,
inspecting,
accepting,
testing
and placing in
service modifications
and
new systems
were to be examined in detail
and
normally are verified on a annual
sampling of the design
and plant
modification packages.
The inspector
reviewed the last two team inspection reports,
additional
project and resident inspection reports
and recent
changes
to the
facilities procedures
in this area.
The inspector
concluded that
adequate
co'verage of the inspection
requirements
has already
been
performed.
Future inspection effort is planned to follow-up on the
findings of the above mentioned inspections.
No violations or deviations
were identified.
14.
Exit (30703)
On March 10,
1989,
an exit meeting
was conducted with the licensee's
representatives
identified in paragraph
1.
The inspectors
summarized
the
scope and'findings of the inspection
as described
in this report.