ML16342A339

From kanterella
Jump to navigation Jump to search
Insp Repts 50-275/93-29 & 50-323/93-29 on 930929-1103.No Violations Noted.Major Areas Inspected:Maint & Surveillance activities,follow-up of Onsite Events,Open Items & LERs & Selected Independent Insp Activities
ML16342A339
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 11/24/1993
From: Johnson P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML16342A340 List:
References
50-275-93-29, 50-323-93-29, NUDOCS 9312160010
Download: ML16342A339 (28)


See also: IR 05000275/1993029

Text

U.S.

NUCLEAR .REGULATORY COHHISSION

REGION

V

I

a

Report Nos:

Docket Nos:

License

Nos:

Licensee:

Facility Name:,

Inspection at:

Inspection

Conducted:

Inspectors:

50-275/93-29

and 50-323/93-29

50-275

and 50-323

DPR-80 and

DPR-82

Pacific

Gas

and Electric Company

Nuclear

Power Generation,

B14A

77 Scale Street,

Room 1451

P. 0.

Box 770000

San Francisco,

California 94177

Diabl o Canyon

Uni ts

1 and

2

Diablo Canyon Site,

San Luis Obispo County, California

September

29 through

November 3,

1993

H. Hiller, Senior Resident

Inspector

H. Tschi ltz, Resident

inspector

D. Corporandy,

Project Inspector

(October 4-8,

1993)

D. Kirsch, Technical Advisor, Division of Reactor

Safety

and Projects,

Region

V

(September

29 October

1,

1993)

F. Huey,

Enforcement Officer, Region

V

(October 21-22,

1993)

Approved by:

P.

H. Johnson,

C ref

Reactor Projects

Section

1

h-~%-~S

Date Signed

~Summar:

I

Ins ection

on

Se tember

29 throu

h November

3

1993

Re ort Nos.

50-275 93-29

~d

Areas

Ins ected:

Routine,

announced

resident inspection of plant operations;

maintenance

and surveillance activities; follow-up of onsite events,

open

items,

and licensee

event reports

(LERs);

and selected

independent

inspection

activities.

Inspection

Procedures

40500,

61726,

62703,

71707,

90712,

92701,

and

93702 were used

as guidance

during this inspection.

Safet

Issues

Hang ement

S stem

SIHS

Items:

None

9312260010

932124

PDR

ADOCK 05000275

8

PDR

Results:

General

Conclusions

on Stren ths

and Weaknesses:

The licensee

cnntinued operation with no events,

no significant equipment

failures,

and

no significant personnel

errors

(Paragraph

2) .

Si nificant Safet

Matters:

None

Summar

of Violations:

A non-cited violation was identified for several

cases

of minor'procedural

non-compliance

(Paragraph

4).

ll

I

!

DETAILS

I

Persons

Contacted

Pacific

Gas

and Electric

Com an

G. H. Rueger,

Senior Vice President

and General

Manager,

Nuclear

Power Generation

Business. Unit

J.

D. Townsend,

Vice President

and Plant Manager,

Diablo

Canyon Operations

W. H. Fujimoto, Vice President,

Nuclear Technical

Services

~

  • M. J. Angus,

Manager,

Nuclear Engineering Services

  • R. P.

Powers,

Manager,

Nuclear guality Services

  • J. A. Sexton,

Manager,

Nuclear Regulatory Services

  • J. S, Bard, Director, Mechanical

Haintenance

D. H. Behnke,

Senior Engineer,

Regulatory

Compliance

G. H. Burgess,

Director,

Systems

Engineering

  • M. G. Crockett,

Manager,

Technical

and Support Services

S.

R. Fridley, Director, Operations

  • R. D. Glynn, Senior guality Assurance

Supervisor

  • T. L. Grebel,

Supervisor,

Regulatory

Compliance

B.

W. Giffin, Manager,

Haintenance

Services

C.

R. Groff, Director, Plant'Engineering

  • J. R. Hinds, Director, Nuclear Safety Engineering
  • K. A. Hubbard,

Engineer,

Regulatory

Compliance

T. H. HcKnight, Senior Engineer, guality Control

  • J. E. Holden, Acting Direztor, Operations

Services

  • S. R. Ortore, Director, 'Electrical Maintenance

J.

H. Rappa,

General

Foreman, Electrical Haintenance

P.

G. Sarafian,

Senior Engineer,

Nuclear guality Services

R. A. Savard,

Director, Technical

Services

  • J. A. Shoulders,

Director, Onsite Nuclear Engineering Services

D. A. Taggart, Director, Onsite guality Assurance

R.

C. Washington,

Acting Director, Instrumentation

and

Controls

  • Denotes those attending the exit interview;

The inspectors

interviewed other licensee

employees

including shift

supervisors,

shift foremen, reactor

and auxiliary operators,

maintenance

personnel,

plant technicians

and engineers,

and quality assurance

personnel.

2.

0 erational

Status of Diablo Can

on Units

1 and

2

During this inspection period, Unit

1 operated at

100 percent

power

except for a reduction to 50 percent

power on October

15,

1993, for

approximately twenty-nine hours,

to perform cleaning of the circulating

water

pump 1-2 forebay.

Unit 2 operated at

100% power for the entire report period.

I

N

3.

0 erational

Safet

Verification

71707

a.

General

During the inspection period,

the inspectors

o6served

and examined

activities to verify the operational

safety of the licensee's

facility.

The observations

and examinations of those activities

were conducted

on

a daily, weekly, or monthly basis.

On a daily basis,

the inspectors

observed control

room activities to

verify compliance with selected

Limiting Conditions for Operation

(LCOs)

as prescribed in the facility Technical Specifications

(TS).

Logs, instrumentation,

recorder traces,

and other operational

records

were examined, to, obtain information on plant conditions

and

to evaluate

trends.

This operational

information was then evaluated

to-determine

whether regulatory requirements

were satisfied.

Shift

turnovers

were observed

on a sampling basis to verify that all

pertinent information on plant status

was relayed to the oncoming

crew.

During each

week, the inspectors

toured accessible

areas of

the facility to observe

the following:

(I)

General plant and equipment conditions

(2)

Fire hazards

and fire fighting equipment

(3)

Conduct of selected activities for compliance with the

licensee's

administrative controls

and approved

procedures

(4)

Interiors of electrical

and control panels

(5)

Plant housekeeping

and cleanliness

(6)

Engineered safety features

equipment alignment

and conditions

(7)

Storage of pressurized

gas bottles

The inspectors

talked with control

room operators

and other plant

personnel.

The discussions

centered

on pertizent topics of general

plant conditions,

procedures,

security, training, and-other

aspects

of the work activities.

b.

Radiolo ical Protection

The inspectors periodically observed radiological protection

practices

to determine whether the licensee's

program was being

implemented in conformance with facility policies

and procedures

and

in compliance with regulatory requirements.

The inspectors verified

that health physics supervisors

and professionals

conducted

frequent

plant tours to observe activities in progress

and were aware of

significant plant activities, particularly those related to radio-

logical conditions and/or challeriges.

ALARA considerations

were

found to be

an integral part of each

RWP (Radiation

Work Permit).

~

~

c ~

No

Ph sical Securit

Security activities were ob'served for conformance with regulatory

requirements;

the site security plan,

and administrative

procedures,

including vehicle

and personnel

access

screening,

personnel

badging,

site security force manning,

compensatory

measures,

and protected

and vital area integrity.

Exterior lighting was checked during

backshift inspections.

violations or deviations

were identified.

4. 'inor Failures to

Com

1

With Procedures

93702

During-. this inspection report period,

several

minor examples

occurred

which involved the licensee's

failure to comply with their procedures.

Although each of these

cases

was of low safety significance,

the number

of examples

indicated-a

lack. of attention-to-detail

in procedure

implementation.

These

cases

are described briefly below.

'I

a.

Im ro er Performance of Diesel

Generator. Surveillance

Testin

On November

1,

1993, during the performance of routine surveillance

test

STP M-9A, Revision 25, "Diesel Engine Generator

Routine

Surveillance," for emergency

diesel

generator

(EDG) l-l, a licensed

operator mistakenly went to the wrong 4-KV switchgear

room and

actuated

a relay which inadvertently started

EDG 1-3.

The purpose

of surveillance test

was to verify that

a start-up

bus under-voltage

relay output sent

an auto-start

signal to the

EDG 1-1 supplying

4 KV

Bus "H".

When

STP H-9A directed the operator to actuate

the start-

up transformer relay toggle switch for EDG 1-1, the licensed

operator incorrectly went to bus "F" associated

with

EDG 1-3.

Control

room operators

immediately recognized that the incorrect

EDG

had

been started.

EDG 1-3 was run for 5 minutes

and secured without

loading in accordance

with licensee

procedures.

The licensee

reported the occurrence

in a four-hour, non-emergency

report to the

NRC, after classifying it as

a condition that 'resulted in the

actuation of an engineered

safety feature

(ESF).

The inspectors

will review the licensee corrective actions associated

with the

event after issuance

of the licensee

event report.

b.

Exhaust

Fan

104

Auxiliar Salt Water

Pum

Vault Ventilation Fan

Im ro er Lifted Lead Record

On October

21,

1993,

an

NRC inspector

observed portions of the

replacement

of auxiliary salt water

(ASW) pump 2-1 room ventilation

exhaust

fan E-104 due to motor bearing degradation.

Fan E-104's

safety function is to provide ventilation. cooling for the

ASW pump.

During the review of the work package

and the observation of the

restoration

and associated

retest of the fan motor, the inspector

noted that the E-104 fan motor did not start

as expected

when

ASW

pump 2-1 was started.

The inspector

noted that the fan motor controller fuse

had been

e

removed

and the load side-of the circuit grounded in accordance

with

the licensee's

standard electrical safety work practices

by the

electrician

who initially prepared for the fan replacement.

However,

the removal of the fan controller fuse

was not recorded

on

the lifted circuit and tag control status

sheet

and the cauti.on -tag

identifying that the fuse was. removed

was

hung

on the interior of

the electrical

panel.

Therefore,

the caution tag was not visible to.

the personnel

performing the restoration without opening the panel.

Additionally; the annotation for the caution tag

on the lifted

circuit and tag control status

sheet did not clearly indicate that

the fuse

was removed.

Consequently,

during the electrical

restoration for post-maintenance

testing the controller fuse

was not

re-installed.

The failure to log the fuse removal

on the lifted

circuit and tag control status

sheet

was

a violation of the

requirements

of licensee

procedure

AP C-4S3 Revision 4, "Control of

Lifted Circuitry, Process

Tubing and Jumpers

During Maintenance

Leads

and Circuits"..

Surveillance

Test Ste

's Performed

Out of Se uence

On September

30,

1993,

the

NRC inspectors

observed

the performance

of surveillance

test

STP I-16A28, Revision 8, "Actuation Logic Test

of Protection

System Logic", and portions of STP I-16Al, Revision

11,

"Removal

from Service of the

SSPS for Actuating Logic Testing

During Modes

1, 2, 3, or 4," for Unit 2.

-The inspectors

noted that

the instrumentation

and controls

(I&C) personnel

were familiar with

both the procedure

and the equipment.

During the surveillance

the

18C personnel

understood

and anticipated

the results of their-

actions

and kept the control

room operator

informed .of the

performance of steps

which initiated annunciator

alarms.

However,

the

NRC inspectors identified two minor concerns listed below.

~

STP I-16A1 requires

the reactor trip bypass circuit breakers

to

be racked into the test position and closed.

Contrary to

operations

procedure

OP A-3: IV Revision

10, "Control

Rod System

Manual Operation of Reactor Trip and

Bypass

Breakers,"

the

licensed

operator

attempted

to close the train

B reactor trip

bypass breaker'ithout first re-installing the associated

DC

control'power fuses.

After the initial unsuccessful

attempt to

close the trip breaker the operator re-installed the

DC control

power fuses

and closed the trip bypass

breaker.

Although the

operator

had reviewed the procedure prior to performing the

required actions,

he did not accomplish the procedure

steps in

the specified

sequence.

~

At two points in STP I-16A2B, the

NRC inspector noted that the

IKC technician operating

the equipment

was performing the test

steps faster than the

I&C technician reading the procedure

could read

and record the results

and i'nitial for the

completion of the step.

In one instance,

this resulted in the

testing of a function wi.th the function test switch in the

incorrect position.

In the second instance,

this resulted in

the

ISC mechanic performing a step prior to the procedure

reader

being able to ascertain if the actions

taken were in the

4

procedure.

In each of these

instances,

the improper operation

of equipment

and the potential for the improper operation of

equipment

was introduced

by not reading

and understanding .the

procedural

step prior to operating plant equipment.

The

inspectors

discussed

these

concerns

with Haintenance,

Operations,

and guality Assurance

management.

Licensee

management

has di scussed

these attention-to-detai

1 concerns

with supervision

and technician staff,

and

has

scheduled

further discussions

with supervisors

and technicians

in this

area.

d.

Surveillance

Procedure

Ste

s Performed

Out of Se

uence to Neet

Intent of Procedure

On October

13,

1993,

the

NRC inspector

observed. surveillance

procedure

STP V-3H8, Revision 8, "Exercising FCV-430 and

FCV-431

CCW

System

Heat Exchanger Isolation Outlet Valves," which tested

the

stroke times of valves

FCV-430 and FCV-431.

The operators

noted

that, for the heat exchanger

valve line-up in service in Unit 2, if

the procedure

steps

were followed as written, the valves would be

stroked

once prior to obtaining the stroke times;

This would

precondition the valves, contrary to the prohibiti on of

preconditioning stated in the procedure.

When'he

NRC inspector

questioned

the implementation of steps

out of order,

the licensee

issued

AR A0431906 to review the circumstances

of the event.

The

licensee

determined that the operators

understood

the intent of the

procedure

and that all the steps

were performed.

However, if the

steps

had

been performed in the order written, the intent of the

procedure

would not have

been

met for the Unit 2 initial test

conditions.

A more appropriate

approach

would have

been to change

the procedure

before implementation to address all the possible

initial test conditions.

In response

to these

and other examples of incorrect implementation of

procedures

which were identified by the licensee,

operations

management

issued

a memorandum,

and briefed all operations

crew members

on the need

for attention-to-detail

and procedural

compliance.

The memorandum

and

discussions

with shift members

reviewed lessons

learned

from improper

procedure

implementation.

The maintenance

organization

has identified

the need for consistency

in expectations

regarding procedure

compliance,

and is continuing emphasis

in this area.

Human performance

expertise

has

been applied in both the maintenance

and operations

organizations.

Each of these

occurrences

of failure to follow procedures

was of very low

safety significance.

However, the programmatic aspects

of lack of

compliance with procedures

indicate

a potential

problem.

These

examples

of a failure to follow plant procedure

requirements

are

a violation of

TS 6.8. 1.

Since the violations,

even in aggregate,

are of low safety

significance,

and since the criteria of Section VII.B.2 of the

enforcement policy were satisfied,

this violation is not cited (50-

275/93-29-01,

closed).

One non-cited violation was identified.

Maintenance

62703

During the inspection period,

the inspectors

observed portions of, and

reviewed records

on selected

maintenance activities to assure

compliance

with approved

procedures,

Technical Specifications,

And appropriate

industry codes

and standards.

Furthermore,

the inspectors verified that

maintenance activities were performed

by qualified personnel,

in

accordance

with fire protection

and housekeeping

controls,

and that

replacement

parts

were appropriately certified.

The inspectors

observed portions of the following maintenance activities:

Dates

Performed

Replacement

and retest of ASW pump 2-1

ventilation exhaust

fan E-104

(Wprk order:C0119279)

Replacement

and retest of

Diesel Generator

2-1

125

VDC

undervoltage

relay

(Work order: C0119171)

Main annunciator

spare wire

identi ficati on

(Unit 1)

(Work order: C0118304)

Scaffolding installation in

125

VDC switchgear

room 1-3 to

support pre-outage

inverter replacement

(Work Order:C0117487)

October

21

1993

October

18,

1993

September

29,

1993

October 4,

1993

October

12,

1993 and

October

19,

1993

No violations or deviations

were identified.

Block Wall Modifications in 4 KV

Switchgear areas,

Units

1 and

2

On September. 29,

1993,

an inspector

observed

ongoing work in the Unit

1

cable spreading

room on the annunciator panels.

The annunciator

panel

doors

on both sides .of the cabinets

were removed for modification and

spare

cables

were hanging out of the cabinets

and secured

to overhead

supports.

The inspector

expressed

concerns

to licensee

management

over

work on an operating

system in preparation for the next outage.

The

ongoing work involved spare wiring identification, relocation

and

removal.

The circuits were energized,

since the main annunciator

could

not be removed

from service while the work was being performed.

The

licensee

did not restrict access

into areas

adjacent to the open

energized

panels until after the inspector raised

concerns

over the

access

into the area.

In response

to these

concerns,

the licensee

placed

boundary tape at the entrance

points for the work areas

associated

with

open panels.

The inspectors will continue to closely monitor the control

of the work area

and the extent of the work being performed

as part of

routine inspection activities.

tl

~ ~

6.

Survei 1 1 ance

61726

The inspectors

reviewed

a sampling of Technical Specifications

(TS)

surveillance tests

and verified that:

(1)'a technically adequate

pro'cedure existed for performance of the surveillance tests;

(2)

the

surveillance tests

had

been performed at the frequency specified in the

TS and in accordance

with the

TS surveillance

requirements;

and

(3) test

results satisfied

acceptance

criteria or were properly disposi tioned.

The inspectors

observed portions of the following surveillance tests

on

the dates

shown:

d

Dates

Performed

STP I-16A2B

STP I-16A1

STP V-3P5

Actuation Logic Test of Protection

System Logic, including Protection

,Master Relays

and Reactor Trip-

Breakers

Removal

From Service of the

SSPS for

Actuation Logic Testing

Exercising

and Timing of Valves

-LCV-106,107,108

and

109 Auxiliary

Feedwater

Pump Discharge

September

30,

1993

September

30,

1993

October 7,

1993

STP M-9A

STP-3H8

Diesel

Generator

Routine Surveillance

October

18,

1993

Exercising

FCV-430 and FCV-431,

October

13,

1993

CCM Heat Exchanger Outlet Isolation

Valves

7.

One non-cited violation was identified, which is discussed

in Paragraph

4

above.

Review of ualit

Hotline

HL

Pro

ram

40500

As of. October

22,

1993, .the following statistics

were noted with regard

to the Quality Hotline files initiated by the. licensee

during the last

four years:.

Number of NSC concerns

submitted:

Number of anonymous

concerns:

Number using

QHL Hotline Recording Machine:

Average length of time to close file (weeks

Longest period file was

open

weeks

. Number of concerns

substantiated:

Number of fi.les remaining open:

'990

1991

1992

1993

4

4

7

5

2

2

5

5

1

2

5

3

66

34

37+

18+

145

100

56+

, 36+

2

1

3

2

0

0

3

1

The inspector

reviewed the licensee's

procedures

and training covering

the

QHL program

and each of the

QHL files noted above, identifying the

following observations:

~ ~

iP

Licensee

procedure

OM3. ID3,

equal ity Hotl ine,

impl ements

the

licensee's

guality Hotline program.

The licensee's

program is

significantly different from others in Region V,. in that,

the

program is structured

to place high emphasis

on users of the program

remaicing completely anonymous.

Although this 'approach

appears

to

have merit in that potential

users of the program

may feel

more

comfortable,

the inspector noted several

concerns

that may warrant

additional

consideration:

~

Specific details of the employee's

concerns

may not be clearly

understood

and 'documented.

The employee is not provided with a clearly documented

resolution of his concerns.

Failure to provide

a formal

closure letter may detract

from employee confidence in the

formality and thoroughness

of the

gHL program.

A formal

closure letter appears

to be especially important for concerns

that are determined

to be unsubstantiated.

Failure to do so

may result in a chilling effect of the employee

and/or result

in his pursuing his concerns

elsewhere.

The licensee

may miss valuable opportunities for employee

feedback

on the

gHL process.

Licensee

procedure

OH3.ID3 provides

no requirements

for security of

gHL files or how employee confidentiality is to be maintained in

instances

where the employee's

name is known. 'he inspector noted

that the

gHL log and

some of the

gHL files (August 21,

1991 log

entry,

and files 91-02 and 90-03) contain the employee's identity,

yet these

documents

are not secure.

The inspector also noted that

the licensee's

gHL phone recording machine

was not secure.

The

gHL log identified a July 5,

1991,

concern

about unqualified

members of the fire brigade for which no gHL file was initiated.

Licensee

procedure

OH3.ID3 does not provide specific requirements

for how files are to be closed or who is authorized to close out

gHL'iles.

Few of the files included clear documentation

as to how each

of the employee's

concerns

had

been resolved.

The time required to close

some files seems

excessive

(e.g.,

145

weeks) .

Although the inspector did not evaluate

the reasons

for

files remaining

open for extended periods,

the lack of specific

requirements

for periodic review and management

oversight of file

status

may result in unwarranted

delays in resolving significant

employee

concerns.

Safety concern training provided to licensee

and contractor

supervisory personnel

does not specifically emphasize

the

supervisor's

personal

culpability for NRC enforcement

action under

10 CFR 50.5.

Consi,dering

some of the significant problems other

licensees

have experienced

involving allegations of discrimination

associated

with raising safety concerns

(especially involving

contractor personnel),

additional

emphasis

may be warranted.

~

~

~

~

As of October

22,

1993,

the licensee

has not performed

any

.independent

audits of the

gHL program.

In light of the relatively-

small

number of employee

concerns

documented

in the licensee's

gHL

program, it may be prudent

and informative to perform

a random

survey of licensee

and contractor

personnel

in drder to establish

employee

knowledge of and confidence in the

gHL program.

No violations or deviations

were identified.

8.

Licensee

Event

Re ort

LER

Followu

90712

a.

The inspector

performed

an in-office review of the following LERs

associated

with operating events.

Based

on the information provided

in the report, the inspectors

concluded that the licensee

had met

the reporting requirements,

had identified root causes,

and had

taken appropriate corrective actions.

The following LERs are

closed:

LER NUMBER

Unit 1:

DESCRIPTION

91-021,

Revision

0 'Failure of Motor Pinion Keys in Limitorque

SHB-3-80 Motor Operators

Due to Inadequate

Design of Material

92-003,

Revision

0

SG Tube Rupture Analysis Deficiency Due to

Inadequate

Communications with NSSS Supplier

92-006,

Revi si on

1

92-009,

Revision

1

92-012,

Revision

1

92-018,

Revision

1

Diesel

Fuel Oil Transfer

System Degradation

Due

to General

Corrosion

Dose Limits Potentially Exceeded

from Chemical

and Volume Control

System Valve Diaphragm

Leakage

Due to Thermally Induced Degradation

Entry into Technical Specification 3.0.3

Due to

Auxiliar'y Building Ventilation System

Inoperability Resulting from a Single Failure

Manual Reactor Trip to Prevent Inadvertent

Criticality from Inadvertent

Cooldown

Due to

Abnormal Operation of Governor Valves92-020,

Revision

1

Control

Room Temperature

Limit Potentially

Exceeded

During Design Basis Accident Conditions92-021,

Revision

1

Techni cal

Speci ficati on 6.2. 2 Overtime

Restriction Violations Due to Inadequate

Overtime Control

Program

92-022,

Revision

1

Indications

on Hain Feedwater

Piping Near the

SG

Nozzles

Due- to Thermal Fatigue

~

E

~

-10-

92-025,

Revision

1

Lack of Redundant

Over-Current Protection for a

Class II Electrical Penetration

Circuit Due to.

Personnel

Error

92-027,

Revision

0

Containment Ventilation Isdlation Technical Specification 3.3.2 Not Met Due to Personnel

Error

92-029,

Revision

1

Fuel Handling Building Activities in

Noncompliance with Technical Specification 3.9, 12 Due.to Personnel

Error

92-030,

Revision

0

93-003, Revision

0

93-003, Revision

1

93-004,

Revision

0

Technical Specification 3.7.3. 1 Not Het When

Valves

Were Not Sealed

Open. or Periodically

Verified to be

Open

Due to Personnel

Error-

Low Temperature

Overpressure

Setpoint Analysis

Nonconservatism

Due to Hiscommunication

Low Temperature

Overpressure

Setpoint Analysis

Nonconservatism

Due to Miscommunication

Non-Conservative

Penalty

Used for the Heat Flux

Hot Channel

Factor Multiplier Due to Vendor

Oversight

93-007,

Revision

0

Technical Specification 6.8.4.e

Not Met Due to

Inadequate

Review of Licensing Requirements93-008, .Revision

0

Block Valves Installed

on the Inlet/Discharge

Side of Overpressure

Protection

Devices

Due to

Vendor Design Deficiency

Unit 2:

90-011, Revision

0

92-002,

Revision.

1

92-002,

Revision

2

Technical Specification 3.6.1.3

and 3.0.4 Not

Het for Unit 2 Containment Air Lock Due to

Programmatic Deficiency

Technical Specification 3.3.2 Action Requirement

Not Het When

a Steam

Flow Channel

was Calibrated

Using an Incorrect Data Sheet

Due to Personnel

Error

Technical

Speci fication 3.3.2 Action Requirement

Not Met When

a Steam

Flow Channel

was Calibrated

Using an Incorrect Data Sheet

Due to Personnel

Error

93-001, Revision

0

Turbine

and Reactor Trip During Surveillance

Testing

Due to Unknown Cause

93-001,

Revision

1

Turbine and Reactor Trip During Surveillance

Testing

Due to Unknown Cause

~ I

~

~

~

-11-

93-002,

Revision

1

Entry into Technical Specification 3.0.3

Due to

Auxi 1 iary .Building Ventilation System

Inoperability Caused

by Inadequate

Work

Instructions93-004,

Revision

1

Technical Specification 3.9. lg Not Net When Fuel

Handling Building Ventilation System

Was

Inoperable

During Fuel

Movement

Due to

Programmatic

Deficiency

93-005,

Revision

0

Valve Disc Separated

From Its Disc Nut as

a

Result of a Hanufacturing Error

93-006,

Revision

0

Anchor-Darling Check Valve Bonnet

Dowel Pins Not

in Compliance With Design Requirements

Due

to'anufacturing

Error

b.

The inspectors

reviewed the following LER by on-site review based

on

the details contained therein:

Closed

LER 50-275 92-04 Revision

0

"Low Vacuum Turbine Tri

and

Subse

uent Reactor Tri

Due to a Pro rammatic Deficienc "

. i

This

LER concerned

an Unit

1 turbine trip and subsequent

reactor

trip which occurred

on April 25,

1992,

due to low condenser

vacuum.

The low condenser

vacuum and subsequent trip were attributed .to

a

number of causes

including a faulty condenser

vacuum

pump suction

line check valve, personnel

errors encountered

when placing the

condenser

vacuum

pump in service,

and inadequate

procedural

instructions.

The inspectors

reviewed the licensee's

root cause

assessment

and proposed corrective actions which included:

~

Inspection of the condenser

vacuum

pump suction line check

valve for both units,

as well as repair, if necessary.

~

Preparation

and distribution of an Operations

Incident Summary

of this event in order to sensitize

operations

personnel

to the

type of personnel

error which contributed to this event.

~

Review of all emergency

and abnormal

operating procedures

to

identify situations

where operators

might be dispatched

to

perform equipment operations

without normal, procedure

issuance

(For such cases,

the licensee

decided to post local

instructions).

Revision of Operating

Procedure C-8:III, "Shutdown and Clearing

of a Hain Feedwater

Pump," to add precautions

and limitations

for possible

vacuum transients

when removing the

pump from

service.

The inspectors

found the licensee's

assessment

of root cause

and

proposed corrective actions to be acceptable.

The inspectors

verified that the licensee

had taken steps

to complete its proposed

12

correcti ve acti ons.

Thi s

LER i s cl osed.

No 'violati ons or devi ati ons were identi fied.

9.

Fo11owu

of 0 en

Items

9270l

a.

Closed

0 en Item 50-275 93-22-04:

Ade uac

of Flow to Cool'he

Reactor

Core in the Event

RHR Valve 8703 Fails to 0 en in the Hot

Le

Recirculation

Mode

This item was concerned

with the adequacy of flow to cool the

reactor core in the event of a single failure of resi dual heat

removal

(RHR) Valve 8703 to open during the hot leg recirculation

mode following a loss-of-coolant-accident.

The inspectors

interviewed cognizant licensee

personnel

and reviewed licensee

and

Westinghouse

documents.

The purpose of the hot leg recirculation

mode is to prevent excessive

boron precipftation onto the fuel rods.

If Valve 8703 -failed to open,

the

RHR pump discharge

would not have

a flow path to the hot legs.

In this event,

the safety injection

(SI)

pumps would provide the only flow to the hot legs.

Licensee

calculations

demonstrated

that the flow through the hot legs with

one safety injection pump running was adequate

to satisfy

Westinghouse

estimates

of required flow to prevent

boron

precipitation.

The licensee

had revised its emergency operating

procedures

to realign the

RHR pump discharge

flow to inject through

the cold legs in the event that valve 8703 failed to open during the

hot leg recirculation

mode.

The inspector

concluded that the

licensee

and Westinghouse

evaluations of core flow wi th the SI

pumps

injecting into the hot legs concurrent with the

RHR pumps injecting

'into the cold legs demonstrated

reasonable

assurance

of adequate

core cooling.

This followup item is closed.

No"violations or deviations

were identified.

An exit meeting

was conducted

on. November

10,

1993, with the licensee

representatives

identified in paragraph I.

The inspectors

summarized

the

scope

and findings of the inspection

as described

in this report.

The licensee

did not,identify as proprietary any of the materials

reviewed

by or discussed

with the inspectors

during this inspection.

~

~