ML16161A810

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Discusses Insp Repts 50-269/87-02,50-270/87-02 & 50-287/87-02 on 870126-30 & Forwards Notice of Violation. Civil Penalty Will Not Be Proposed Due to Unusually Prompt & Extensive Corrective Actions Initiated
ML16161A810
Person / Time
Site: Oconee  
Issue date: 05/05/1987
From: Grace J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To: Tucker H
DUKE POWER CO.
Shared Package
ML16161A811 List:
References
EA-87-043, EA-87-43, NUDOCS 8705190272
Download: ML16161A810 (3)


See also: IR 05000269/1987002

Text

MAY0 5 1987

Docket Nos. 50-269, 50-270, 50-287

License Nos. DPR-38, DPR-47, DPR-55

EA 87-43

Duke Power Company

V/ATTN:

Mr. H. B. Tucker, Vice President

Nuclear Production Department

422 South Church Street

Charlotte, NC

28242

Gentlemen:

SUBJECT:

NOTICE OF VIOLATION

(INSPECTION REPORT NOS.

0-269/87-02 50-270/87-02 AND 50-287/87-02)

This refers to the Nuclear Regulatory Commission (NRC) inspection conducted

on January 26-30, 1987 at the Oconee Station. As a result of this inspection, a

failure to comply with NRC regulatory requirements was identified. The report

documenting this inspection was sent to you with a letter dated February 19, 1987.

NRC concerns relative to the inspection findings were discussed by L. A. Reyes,

Director, Division of Reactor Projects, NRC, Region II, with R. B. Priory, Vice

President, Design Engineering, in an Enforcement Conference held on March 6, 1987.

A summary of this Enforcement Conference was sent to you by a letter dated

March 25, 1987.

The violation described in the enclosed Notice of Violation involved a failure

to provide the alternate shutdown capability with the required independence of

cabling for reactor coolant letdown valves. The licensee took prompt corrective

action to remedy any potential problems which may have occurred in the event

of a fire, which included closing the appropriate valves and de-energizing the

power supply to the motor operators for the valves involved. The cause of the

violation was the use of improper assumptions when preparing Appendix R fire

protection analyses. We are also concerned with your fire hazards analysis

which did not recognize a condition that could have affected the ability to

maintain reactor coolant inventory. While not a violation, the fire hazards

analysis did not consider circuit failure modes which could cause spurious

operation of valve operator motors for the decay heat removal suction isola

tion valves. It was fortuitous that an after-the-fact analysis indicated

that simultaneous opening of the valves, which provide a high to low pressure

system interface, would not take place during a fire.

In accordance with the "General Statement of Policy and Procedure for NRC

Enforcement Actions," 10 CFR Part 2, Appendix C (1987) (Enforcement Policy),

the violation described in the enclosed Notice has been classified at a

Severity Level III.

Normally, a civil penalty is proposed for a Severity

Level III violation. However, after consultation with the Director, Office

of Enforcement, and the Deputy Executive Director for Regional Operations, I

have decided that a civil penalty will not be proposed in this case because

unusually prompt and extensive corrective actions were initiated to prevent

recurrence, and because your prior performance in the area of fire protection

has been good.

8705190272 870505

PDR

ADOCK 05000269DR

I

Duke Power Company

-

2 -

MAY 0 5 1987

You are required to respond to this letter and should follow the instructions

specified in the enclosed Notice when preparing your response. In your

response, you should document the specific actions taken and any additional

actions you plan to prevent recurrence. After reviewing your response to this

Notice, including your proposed corrective actions, the NRC will determine

whether further NRC enforcement action is necessary to ensure compliance with

NRC regulatory requirements.

In accordance with Section 2.790 of the NRC's "Rules of Practice," Part 2,

Title 10, Code of Federal Regulations, a copy of this letter and its enclosure

will be placed in the NRC Public-Document Room.

The responses directed.by this letter and its enclosure are not subject to the

clearance procedures of the Office of Management and Budget as required by the

Paperwork Reduction Act of 1980, Pub. L. No.96-511.

Sincerely,

ORIGINAL SIGNED BY

A.F. Gibson

J. Nelson Grace

Regional Administrator

.

Enclosure:

Notice of Violation

Ic w/encl:

M. S. Tuckman, Station Manager

05/01/87

14:36

NRC-M&M-MNBB

NO.032

002

.

, ,Duke

Power Company

- 3 -

MAY 0 5 1987

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