ML16161A758

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Insp Repts 50-269/86-20,50-270/86-20 & 50-287/86-20 on 860610-0707.Noncompliance & Deviation Noted:Failure to Follow Procedure in Documentation & Failure of Seismic Instrumentation to Conform to Fsar,Respectively
ML16161A758
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 08/01/1986
From: Bryant J, Peebles T, Sasser M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML16161A756 List:
References
50-269-86-20, 50-270-86-20, 50-287-86-20, NUDOCS 8608120198
Download: ML16161A758 (10)


See also: IR 05000269/1986020

Text

  • 10F

EU 9

UNITED STATES

o

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

AUG 0 1 1986

Report Nos.:

50-269/86-20, 50-270/86-20, and 50-287/86-20

Licensee:

Duke Power Company

422 South Church Street

Charlotte, N.C. 28242

Facility Name:

Oconee Nuclear Station

Docket Nos.:

50-269, 50-270, 50-287

License Nos.:

DPR-38, DPR-47, and DPR-55

Inspection Conducted: Ju e 10 - July 7, 1986

Inspectors:

4

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/

/4

J. C. Bryant Senio

esid

Inspector

ate Sgned

M

ser,

esi

t Ins

re

Approved by:

T. Pebbles, Section Chief

Da e Signed

Division of Reactor Projects

SUMMARY

Scope:

This routine,

announced inspection involved inspection on-site in the

areas of operations, surveillance, station modifications, followup of events, and

safeguards.

Results:

Of the 5 areas inspected, one item of noncompliance was found in one

area; Failure to follow procedure in documentation.

One deviation was found in

one area; Failure of seismic instrumentation to conform to FSAR.

~0o269c

pDR

DC

5 PDR

REPORT DETAILS

1.

Licensee Employees Contacted

  • M.S. Tuckman, Station Manager

R.L. Sweigart, Operations Superintendent

T.S. Barr, Technical Services Superintendent

C.L. Harlin, Compliance Engineer

  • D.S. Compton. Assistant Compliance Engineer

Other

licensee employees contacted included technicians, operators,

mechanics, security force members, and staff engineers.

Resident Inspectors

  • J.C. Bryant
  • M.K. Sasser
  • Attended exit interview.

2.

Exit Interview

.

The inspection scope and findings were summarized on July 9, 1986 with those

persons indicated in paragraph 1 above.

The licensee did not identify as proprietary any of the materials provided

to or reviewed by the inspectors during this inspection.

3.

Licensee Action on Previous Enforcement Matters

This area was not inspected during the report period.

4.

Inspector Followup Items and Unresolved Items

(Closed)

IFI

270/85-20-03:

Review of Temporary Modifications.

The

inspectors have reviewed revised station directives and their implementation

to ensure periodic reviews of temporary modifications and have found the

actions taken to be satisfactory.

(Closed)

UNR 269/86-18-03:

Discrepancies in Seismic Equipment as

Installed. The inspectors have determined this to be a deviation from the

Final Safety Analysis Report (FSAR).

See Deviation 269/86-20-01,

para

graph 9.

(Closed) UNR 269/86-18-04:

Failure to Independently Verify Valve Lineup.

The inspectors have determined this to be a violation of station procedures.

See violation 269/86-20-02, paragraph 13.

2

(Closed)

IFI 269,270,287/DRP 85-01:

Station Battery Operation, Mainten

ance,

and Inspection.

Unresolved item,

UNR

269,

270,287/85-10-01,

was

issued by the residents after inspection of the areas covered by this

inspector followup item. This IFI is considered closed.

5. Unresolved Items

Unresolved items are matters about which more information is required to

determine whether they

are acceptable or

may

involve violations or

deviations. One unresolved item was identified during the course of this

inspection and is discussed in paragraph 11.

6.

Plant Operations

The inspectors reviewed plant operations throughout the reporting period to

verify conformance with regulatory requirements,

technical specifications

(TS),

and administrative controls.

Control room logs, shift turnover

records,

and equipment removal

and restoration records were reviewed

routinely. Interviews were conducted with plant operations, maintenance,

chemistry, health physics and performance personnel.

Activities within the control rooms were monitored on an almost daily basis.

Inspections were conducted on day and on night shifts, during week days and

on weekends.

Some inspections were made during shift change in order to

evaluate shift turnover performance.

Actions observed were conducted as

required by Operations Management Procedure 2-1. The complement of licensed

personnel

on each shift inspected met or exceeded the requirements of TS.

Operators were responsive to plant annunciator alarms and were cognizant of

plant conditions.

Plant tours were taken throughout the reporting period on a routine basis.

The areas toured included the following:

Turbine Building

Auxiliary Building

Units 1,2, and 3 Control Battery Rooms

Units 1,2, and 3 Electrical Equipment Rooms

Units 1,2, and 3 Cable Spreading Rooms

Station Yard Zone within the Protected Area

Standby Shutdown Facility

Keowee Hydro Station

During the

plant tours, ongoing activities, housekeeping, security,

equipment status, and radiation control practices were observed.

Unit 1 began the report period at 100% power.

On June 24 the unit

experienced an asymmetric rod run back to 50% power.

The run back was

caused by a blown fuse which resulted in loss of the Group 2 out limit

light. The fuse was replaced and the unit returned to 100% power the same

day. The reactor operated at 100% power during the remainder of the report

period.

4I3

Unit 2 operated at 100% power throughout the report period.

Unit 3 operated at essentially 100% power throughout the report period.

7.

Surveillance Testing

The surveillance tests listed below were reviewed and/or witnessed by the

inspectors to verify procedural and performance adequacy.

The completed tests reviewed were examined for necessary test prerequisites,

instructions, acceptance criteria, technical content, authorization to begin

work, data collection, independent verification where required, handling of

deficiencies noted, and review of completed work.

The tests witnessed, in whole or in part, were inspected to determine that

approved procedures were available, test equipment was calibrated,

prerequisites were met, tests were conducted according to procedure, test

results were acceptable and systems restoration was completed.

A number of surveillances were reviewed during the inspection of biofouling

of heat exchangers (see paragraph 12).

Surveillances reviewed:

PT/0/A/600/20 SSF Instrument Surveillance

Surveillances witnessed in whole or part:

PT/2/A/600/13 Motor Driven Emergency Feedwater Pump

Performance Test

PT/O/A/0150/31 Hydrogen Analyzer Panel Post Maintenance

Leak Rate Test

PT/0/A/253/6A RB Hydrogen Sampling System Annual Check, Unit 3,

Train A

No violations or deviations were identified.

8.

Resident Inspector Safeguards Inspection

In the course of the monthly activities, the Resident Inspectors included a

review of the licensee's physical security program.

The performance of

various shifts of the security force was observed in the conduct of daily

activities which included; protected and vital areas access controls,

searching of personnel, packages and vehicles, badge issuance and retrieval,

escorting of visitors, patrols and compensatory posts.

In addition, the

Resident Inspectors, observed protected area lighting, protected and vital

4

areas barrier integrity and verified interfaces between the security

organization and operations or maintenance.

Specifically, the resident

inspectors:

Reviewed the

licensee's

security plan, discussing the

licensee's transition to an upgraded security system; visited the secondary

and central alarm stations; witnessed activities associated with a spent

fuel shipment; witnessed stress firing with shotguns and pistols; and

witnessed training in small unit tactics.

The licensee is voluntarily upgrading security locks on several access areas

after having found some doors unlocked.

Security officers have increased

patrols in the interim.

Followup of this action will be listed as an

inspector followup item; IFI-50-269,270,287/86-20-01, Security Access Doors.

No violations or deviations were identified.

9.

Oconee Seismic Instrumentation

During previous report periods (see reports 86-10, 86-18) the inspectors

conducted an inspection of the seismic instrumentation installed at the

site. Results of the inspection indicated a significant discrepancy between

the instrumentation installed at the site and that described by the FSAR.

As restated from report 86-18, the discrepancy is as follows:

The FSAR states that peak recording accelerometers are installed in six

locations within the unit 1 reactor building.

Only one of these

accelerometers

is currently

operable,

the

other

five

became

deteriorated beyond use and may have been removed in 1979. Calibrations

and checks of these instruments by the I&E Department were discontinued

at that time. Nuclear Station Modification (NSM) 1110 was initiated to

complete a design review and replacement for the accelerometers;

however,

the NSM was cancelled subsequent to its original issue in

1980.

The above finding was listed as an unresolved item,

UNR 269/86-18-03,

Discrepancies in the Installation of Seismic Recording Equipment.

Based on

further review the inspectors have determined this to be a deviation from

FSAR commitments, and, as such, are closing the unresolved item and issuing

a deviation; DEV 269/86-20-02,

Discrepancies Between

FSAR

and Installed

Seismic Instrumentation.

10.

Unusual Event -

Seismic Activity

An Unusual Event was declared at the Oconee Station on June 11 at 12:15 p.m.

due to a seismic event.

All three units were operating at 100% power.

While the event was felt at the station, no alarms were recorded at the

Oconee site. Seismic readings were recorded by the more sensitive Jocassee

Hydro Plant instrumentation located approximately 12 miles from the Oconee

site. The Jocassee instruments recorded two quakes.

The first quake,

at

5

12:12 p.m., registered 2.47 on the Ricter scale with a duration of 120

seconds. The second registered 1.54 on the Ricter scale with a duration of

45 seconds occurring at 12:24 p.m. Subsequent inspection of plant equip

ment, as required by plant Abnormal Operating Procedures revealed no damage

or detrimental effects. The state and county were notified. The unusual

event was terminated at 1:43 p.m.

11.

Seismic Inoperability of Keowee Batteries

On June 10, at approximately 3 p.m., NRC-Safety System Functional Inspection

(SSFI) team members touring the Keowee hydro station, noted a deficiency in

the installation of the batteries relative to current drawings.

Excess

clearance (greater than 1/4 inch) between the battery end cells and the end

cell horizontal supports (stringers) was found. This condition was noted

for 15 of 16 end cells, with as much as 3 to 4 inches of space in some

locations. The Keowee batteries are safety related, with a separate battery

for each Keowee unit, and are required for generator "field flashing" in the

event of loss of AC power. The Keowee hydro units are the class 1E onsite

emergency power source for the Oconee Nuclear Station.

During an internal NRC meeting later that day, in which SSFI team findings

were being summarized

for later presentation

to the licensee, this

particular finding was noted as a possible concern relative to operability

of the batteries.

The excessive clearance invalidates the seismic

qualification of the

racks, requiring the batteries to be declared

inoperable. When the resident inspectors became aware of the deficiency at

7:00 p.m.

on June 10,

they immediately notified the station maintenance

superintendent and the operations shift supervisor that the batteries were

technically inoperable,

which placed the plant in a 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> limiting

condition for operation (LCO).

The maintenance superintendent called in

engineers and the residents kept in touch with progress.

At 10:30 p.m. on

June 10, the residents were informed by the station I&E Engineer that work

was complete and the Keowee batteries were operable. He also described the

work that had been done and the residents agreed that corrective action

taken met requirements. Subsequent inspection verified that the work had

been performed as described. An inspection into the station modification

which installed these batteries indicated that they had been installed in

August 1985.

Inspection of Operations SRO and

RO logs found no entry concerning the

inoperability of the Keowee batteries during the period following the

initial discussion with the NRC residents at 7:00 p.m., June 10. There were

no log entries concerning licensee corrective actions on the battery racks.

On June 13 the resident was informed by Compliance that the licensee was

continuing his analysis to determine if an NRC notification by red phone was

appropriate. Apparently,

since the item was found by

NRC,

operations

personnel had not considered it a required report.

The resident expressed

concern that the licensee's Operations personnel failed to appropriately

consider and address the battery operability question at the time the

problem was identified, as evidenced in part by there being no log entries

concerning the problem.

6

At 4:40 p.m. on June 13 the licensee initiated a red phone call to the NRC.

The inoperability of both Keowee hydro station batteries was reported under

the requirements of 10 CFR 50.72 (b) (1) Non-emergency events -

One hour

reports, section (ii)

(B),

operating in-a condition that is outside the

design basis of the plant. In addition, a licensee event report (LER) will

be submitted under the appropriate section of 50.73.

The residents, during their review of the battery installation process,

found the following:

a. The batteries were installed under NSM 52466 with battery #1 being

completed August 17,1985 and battery #2 completed on August 25,1986.

b. The installation was

performed by the

Duke Transmission Services

(Greenville, S.C.)

and the Duke CMD organizations in conjunction with

the Oconee Project Services staff.

Transmission Services normally

works on fossil and hydro projects only. Keowee station is hydro.

c. Documents reviewed by the residents were the following:

KM 320-15

Battery & Rack Instruction Manual (Gould)

KM 320-11

EQ For Class 1E Pb-Acid Keowee Batteries

KS 320-02

DPC Specification for Keowee Hydro Station

125vDC Class 1E Batteries

NSM 52466

Station Modification Package for Keowee

Hydro Station Batteries

TN/1&2/A/52466/00/AL1

Implementation Procedure for

Keowee

Battery

&

Storage

Rack

Replacement

d.

The implementing procedure was reviewed to determine the level of

detail required in complying with drawings and manuals. The procedure

was found to adequately reference the Gould manuals and included

drawings showing details for exact rack specifications.

Procedural

signoffs were also noted to have been completed by both the personnel

installing the racks and the QA inspector following the job.

Per the

procedure, there

was

QA

involvement throughout the entire rack

fabrication and installation.

7

Based on the above, the initial conclusion was that the installing and QA

personnel did not actually install the racks per the drawing.

However, on

July 2, additional information was received indicating this not to be the

case. A more accurate assessment of the -sequence is as follows:

a. The initial vendor drawing (Gould 400304-D) did not include the note

requiring 1/4 inch or less clearance between the end cell and stringer

or that this space be filled by appropriate filler material.

b.

The licensee's installation procedures were followed and completed in

August 1985 to install the battery racks per the vendor drawing.

c.

The

licensee's Design Engineering staff questioned the

vendor

concerning clearances on the battery racks, finding that the drawing

was

in error,

and should have contained the notes relative to

clearances and the use of filler material when required.

The drawing

was subsequently revised to include these notes on September 5, 1985.

d.

The revised drawing was received at the Oconee station; however,

the

change apparently was not noted by cognizant personnel and no action

was taken to correct the battery rack installation.

10

CFR

50,

Appendix B, Criterion VI,

Document Control,

requires that

measures assure that changes to documents are distributed to and used at the

location where the prescribed activity is performed.

Since the corrected

drawing was issued on September 5, 1985,

nine months elapsed prior to the

NRC finding on June 10, 1986. It appears that ample time had elapsed to

correct the battery rack deficiency since the drawing had been distributed

to the site, but had not been used, there is an apparent noncompliance with

the

regulation.

However, pending issuance

of

Headquarters

Report

Nos. 50-269/86-16, 50-270/86-16,

and 50-287/86-16 this item will be listed

as

an unresolved item, UNR 269,270,287/86-20-03;

discrepancies

in

document/design control.

No violations or deviations were identified.

12.

Biofouling of Heat Exchangers (TI 2515/77-02.02)

In response to Temporary Instruction 2515/77, the inspectors examined the

practices and procedures in effect at Oconee to identify fouling,

particularly biofouling, of the open cycle cooling water systems.

A Duke Power Company response of May 22, 1981 to IE Bulletin 81-03 included

the following statement, "....evidence of clams has not been detected in any

Oconee systems except for the Amertap system,

and no evidence of clam

fouling has been detected whatsoever. As a precaution, however, maintenance

procedures

and performance criteria are currently being reviewed

and

evaluated for inclusion in a formal monitoring program to provide early

8

detection of clam infestation of service water systems. Detection of clams

may consist of differential pressure readings across an equipment item,

examination of strainers and drainage discharge lines, and visual inspection

of inlet heat exchanger heads and piping supply lines. Supply and discharge

line flow rates to a piece of equipment may also be monitored. The criteria

for the acceptable, minimum flow rate in

a specific line are currently

being evaluated.

Flow monitoring will consist of either existing flow

meters or manually operated, sonic flow meters."

To determine how the above commitment was being carried out, the 'inspectors

held discussions with cognizant personnel, examined equipment, and reviewed

the following procedures:

PT/1/A/251/1

Low Pressure Service Water (LPSW) Pump Performance

Test (quarterly and after major maintenance)

PT/O/A/230/15 High Pressure Injection Motor Cooler Flow Rate Test

(weekly)

PT/O/A/203/08 LPI System ES Test (Refueling - test also verifies

LPSW flow)

PT/O/A/160/03 R.B. Cooling System ES and Performance Test

(Refueling)

PT/O/A/250/24 Fire Protection System Three Year Flow Test

CP/O/B/4002/12 Monitoring Program for Asiatic Clams (quarterly)

LPSW flow through the various equipment is instrumented locally or in the

control room,

but instrumentation is used to control or determine adequacy

of flow rather than to determine degradation of flow.

LPSW flow through

individual systems is measured and recorded during the tests, and an

acceptable range

is given.

During the LPSW pump performance test,

acceptable, alert, and required action ranges are given, but none of the

procedures currently in use specify comparing with design parameters.

However, procedures for measuring, recording and comparison of cooling water

flows with design specifications are in preparation for decay heat removal

and reactor building cooling units. These are scheduled to be implemented

in June and August of 1986.

Operator training and procedures are geared toward response to inadequate

cooling rather than to detect degradation of flow.

On the most recent

refueling outage, a DHR heat exchanger was opened and cleaned because heat

transfer appeared to be degraded even though cooling water flow was normal.

Degradation of heat transfer was determined to be due to sludge and not to

clams.

A total of 18 drains in the LPSW, HPSW, condensate coolers, and recirculated

cooling water heat exchangers are flushed quarterly with flush water passing

through a wire mesh.

Residue is searched for clams and shell particles.

The Amertap ball collection basket is searched weekly for clam shells.

Six

fire hydrants and four fire hose stations are flushed quarterly at full flow

for one minute. The flow is screened and the screen inspected for clams.

9

Whenever any work is done involving opening of the lake water portion of

components, valves or piping,

the interior is visually inspected by

environmental personnel for clams. Also, maintenance is required to notify

environmental personnel if any clams are observed. A visual examination of

condenser water boxes for clams is performed on unit shutdowns.

The licensee appears'to be meeting the commitments made in response to

Bulletin 81-03.

No violations or deviations were identified.

13.

Documentation of Independent Verification

On

May 23,

1986,

Unit 1 was being taken to cold shutdown according to

Procedure OP/1/A/1102/10, Controlling Procedure for Unit Shutdown. At 4:43

to 4:44 a.m.,

Enclosure 4.3,

250 F/350 PSI Conditions to Cold Shutdown,

steps 4, 5 and 6 were performed.

These steps dealt with initiating high

pressure injection flow to the pressurizer auxiliary spray line.

These

steps required independent verification of action.

At about 7:00 a.m., a Regional Inspector, who was observing shift turnover,

noted that steps 4, 5, and 6 of Enclosure 4.3 had not been signed off as

independently verified even though subsequent steps of the procedure had

been completed.

The resident inspectors subsequently reviewed the shift incident report and

talked to personnel involved. It was determined that, due to many jobs in

progress, shift personnel had decided to send only one operator to the field

for valve lineup while verification of flow was determined by control room

personnel.

Control

room personnel later stated that they had made the

verification but failed to sign off the data sheet.

The inspectors consider that the verification was made but was

not

documented. Failure to sign off the procedure is a violation, (Violation

269/86-20-04, Failure to Document Actions).