ML16154A792

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Insp Repts 50-269/95-06,50-270/95-06 & 50-287/95-06 on 950326-0429.Violations Noted.Major Areas Inspected:Plant Operations,Maint & Surveillance Testing
ML16154A792
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 05/24/1995
From: Crlenjak R, Harmon P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML16154A790 List:
References
50-269-95-06, 50-269-95-6, 50-270-95-06, 50-270-95-6, 50-287-95-06, 50-287-95-6, NUDOCS 9505310076
Download: ML16154A792 (15)


See also: IR 05000269/1995006

Text

REGU'

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report Nos.:

50-269/95-06, 50-270/95-06 and 50-287/95-06

Licensee:

Duke Power Company

422 South Church Street

Charlotte, NC 28242-0001

Docket Nos.:

50-269, 50-270 and 50-287

License Nos.:

DPR-38, DPR-47 and DPR-55

Facility Name:

Oconee Units 1, 2 and 3

Inspection Conducted:

March 26 - April 29, 1995

Inspector:

(e-i-Cv

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P. E. Harmon, Senioi'Resident Inspector

Date Signed

W. K. Poertner, Resident Inspector

L. A. Keller, Resident Inspector

P. G. Humphrey, Resident Inspector

R. E. Carroll, Project Engineer

Approved by:

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R. V. Crlenjak, Chief

Date Signed

Reactor Projects Branch 3

SUMMARY

Scope:

This routine, resident inspection was conducted in the areas of

plant operations, maintenance and surveillance testing, onsite

engineering, plant support, and inspection of open items.

Inspections were performed during normal and backshift hours and

on weekends.

Results:

A violation was identified in the area of plant operations

concerning inadequate corrective actions for controlling Keowee

operating limits (paragraph 2.d).

Knowledgeable of a

probabilistic risk assessment study, operations personnel took

conservative action to preclude a high risk maintenance situation

(paragraph 2.f).

Unit 2 tripped from 100 percent power due to a

disturbance on the system grid (paragraph 2.c).

Previously

identified problems with slow rod drop times resulted in a

shutdown of Unit 1 (paragraph 2.e).

ENCLOSURE 2

9505310076 950524

PDR ADOCK 05000269

G

PDR

2

In general, maintenance activities were accomplished in an

acceptable manner with appropriate procedure use and adherence.

One instance was observed where maintenance personnel were not

using procedures appropriately (paragraph 3.a.(2)).

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

B. Peele, Station Manager

  • E. Burchfield, Regulatory Compliance Manager
  • D. Coyle, Systems Engineering Manager
  • J. Davis, Engineering Manager

T. Coutu, Operations Support Manager

W. Foster, Safety Assurance Manager

J. Hampton, Vice President, Oconee Site

D. Hubbard, Maintenance Superintendent

C. Little, Electrical Systems/Equipment Manager

  • J. Smith, Regulatory Compliance
  • G. Rothenberger, Operations Superintendent

R. Sweigart, Work Control Superintendent

Other licensee employees contacted included technicians, operators,

mechanics, security force members, and staff engineers.

  • Attended exit interview.

2.

Plant Operations (71707)

a.

General

The inspectors reviewed plant operations throughout the reporting

period to verify conformance with regulatory requirements,

Technical Specifications (TS), and administrative controls.

Control room logs, shift turnover records, temporary modification

logs, and equipment removal and restoration records were reviewed

routinely. Discussions were conducted with plant operations,

maintenance, chemistry, health physics, instrument & electrical

(I&E), and engineering personnel.

Activities within the control rooms were monitored on an almost

daily basis.

Inspections were conducted on day and night shifts,

during weekdays and on weekends.

Inspectors attended some shift

changes to evaluate shift turnover performance. Actions observed

were conducted as required by the licensee's Administrative

Procedures. The complement of licensed personnel on each shift

inspected met or exceeded the requirements of TS. Operators were

responsive to plant annunciator alarms and were cognizant of plant

conditions.

Plant tours were taken throughout the reporting period on a

routine basis. During the plant tours, ongoing activities,

housekeeping, security, equipment status, and radiation control

practices were observed.

.2

b.

Plant Status

Unit 1 operated at or near full power until April 27, 1995, when

the Unit was taken off-line for control rod drive testing. The

Unit remained shutdown the remainder of the reporting period for a

control rod drive mechanism refurbishment outage.

Unit 2 operated at or near full power until April 8, 1995, when an

observed loss of efficiency was attributed to a ruptured steam

extraction expansion joint in the main condenser. The Unit

continued operation with reduced secondary output until a fault on

the transmission grid resulted in a generator lockout and

subsequent reactor trip on April 14, 1995.

The unit was restarted

on April 16, 1995.

On April 21, 1995, Unit 2 began experiencing

problems with tube leaks in the main condenser. The unit

continued to operate throughout the remainder of the reporting

period while coping with power reductions for condenser water box

outages as necessary for on-going condenser tube repair/plugging

activities.

Unit 3 operated at or near full power throughout the inspection

period.

c.

Unit 2 Reactor Trip

The Unit 2 reactor tripped at 9:59 a.m., on April 14, 1995.

The

reactor trip was attributed to a main generator lockout that

occurred as a result of a fault on the electrical grid system.

The following is a sequence of the event:

(1) A fault on the 100KV electrical transmission system occurred

when a tree fell across the Pickens Black 100KV line.

(2) A failed trip coil in the Pickens Black 100KV supply breaker

prevented the breaker from opening and isolation of the

fault. This resulted in system disturbances upstream of the

100KV lines and into the 230KV portion of the system grid.

(3) The fault was detected by the Oconee Unit 2 main generator

Loss of Field protective relays, which tripped the generator

off-line prior to the fault being cleared by the Central and

North Greenville substation breakers located between the

failed 100KV breaker and the Oconee generating units. The

circuit timer was set at 0.8 seconds for the generator trip

signal.

The licensee indicated that a modification would be

proposed to change the generator trip signal timer to 30

seconds when the signal does not involve a loss of voltage.

The increased time delay will allow time for generator

recovery without damage to the generator and will serve to

avoid unnecessary unit trips.

3

All 3 Oconee units were operating at the time of the Unit 2 trip.

Units 1 and 2 were tied to the 230KV grid which was supplying the

faulted 100KV system. Unit 3 was connected to the 525KV system

and was less affected by the fault. Unit 2 experienced the most

effect from the fault since it was operating with its generator

voltage regulator in automatic and attempted to follow the grid

load. This resulted in the generator lockout followed by a

reactor trip. Unit 1 had previously experienced problems with

operating the voltage regulator in the automatic mode and had

switched control to manual prior to the event.

The inspectors were in the control room immediately following the

reactor trip and observed operator responses. The unit trip was

well controlled by the control room operators.

Control rod drop times were recorded on the events recorder at the

time of the reactor trip and 12 rods required more than 1.40

seconds to drop into the core. One of the 12 rods (Group 2, Rod

6) had a drop time of 1.842 seconds, which is greater than the

1.66 seconds allowed by Technical Specification (TS) Section

4.7.1.

Based on previous experience, the type A control rod drive

mechanisms that exceed 1.40 seconds appear to significantly

increase in drop times during the operating cycle. (Note: Units 1

and 2 have the type A control rod drive mechanisms).

Unit 2 was

restarted (critical) at 3:47 p.m., on April 15, 1995, with the

inoperable rod as allowed by TS 3.5.2.

The inspectors reviewed the licensee's trip report and attended

the Plant Operating Review Committee meeting for evaluating the

trip and authorization for restart.

d.

Inadequate Control of Keowee Load Limits

The licensee reported by Licensee Event Report (LER) 269/93-01

that under certain conditions the emergency power supplied by the

Keowee Hydro Station to the Oconee Station could be lost. If an

emergency start was initiated while a Keowee unit was generating

to the system grid at high load, the Keowee unit could trip or

load reject on overspeed. To prevent this problem, Procedure

OP/0/A/2000/041, Keowee-Mode of Operation, was revised on January

15, 1993, to administratively limit the maximum output to 60 MW

for a Keowee unit generating to the system grid.

On June 2, 1993, based on the results from load rejection tests

and on revised calculation OSC-6003, "Keowee Operating Limits to

Prevent Overspeed Due to Load Rejection", the licensee's Keowee

Station Manager issued a memorandum to the Keowee Operators that

raised the maximum permissible output of the Keowee unit gener

ating to the grid, from 66 to 75 MW. Although calculations were

performed to verify maximum load limits, the controlling

procedure, OP/0/A/2000/041 was not revised. As a result, the

Keowee units were operated for a period of time in excess of the

4

official limit. The failure to revise this procedure was

identified as Violation 50-269,270,287/93-20-03: Failure to Follow

Procedures at Keowee.

The 75 MW limit was later found to be in error by NRC reviewers

and revised to 69 MW maximum. To ensure the 69 MW limit would not

be exceeded due to the expected unit swing, an operational limit

of 64 MW was imposed by procedure.

On March 15, 1995, the licensee revised calculation OSC-6003 to

change the maximum operating limit for a Keowee Hydro Unit

generating to the grid from 69 to 68 MW. Upon revising this

calculation, the responsible engineer called Keowee Hydro

Operations and advised them of the analysis results which changed

the administrative operating limit from 64 to 63 MW. The Keowee

operator agreed that the unit would be run at 63 MW or less until

the procedure was changed (procedure limit was 64 MW).

The

procedure was changed on March 20, 1995.

The resident staff

reviewed the Keowee Operating Log for the period of March 15 - 20,

1995, and noted that on March 16 & 17, 1995, a Keowee Hydro Unit

was operated at 64 MW. The inspectors concluded that attempting

to change a Keowee operating limit based on a phone conversation

between a system engineer and a Keowee operator was both

inappropriate and ineffective, in that it did not include the

proper chain of command and did not achieve the desired result.

The inspectors determined that this was similar to Violation

93-20-03 in that the operating limit was inappropriately changed

(the first time by memo, the second time by phone).

The licensee

has initiated a Duke-wide study of Engineering to Operations

communication and whether it should be additionally formalized.

The inspectors.agree that more careful, formal communications are

needed. However, both the engineer involved and the Keowee

operators treated this issue as a Keowee issue rather than an

Oconee issue. As a result, the Oconee shift supervisor was not

contacted concerning the new limits. Keowee operations and chain

of command has officially been integrated into Oconee Operations,

but this incident indicates further efforts are needed. This

matter is identified as Violation 50-269,270,287/95-06-01:

Inadequate Corrective Action for Control of Keowee Operating

Limits.

e.

Unit 1 Shutdown

On April 27, 1995, Unit I was taken off-line to perform control

rod drive trip time testing. Testing revealed that 5 control rods

had trip times which exceeded the TS limit of 1.66 seconds.

The Unit had been operating with a conditional control rod

operability determination based on a statistical analysis which

determined that rod drop times would not exceed the Technical

Specification limit of 1.66 seconds. The conditional operability

statement expired on April 21, 1995. On March 30, 1995, the

5

licensee's Plant Operating Review Committee had reviewed this item

and determined that the Unit 1 control rods would be considered

operable for the remainder of the cycle. This decision was based

on the unit starting the cycle with no inoperable control rods,

and statistical analysis that showed that 1 rod may become

inoperable due to slow drop times at the 95/95 confidence level

during the cycle.

On April 14, 1995, Unit 2 tripped from 100 percent power. Review

of the rod drop times identified that 1 control rod's drop time

was greater than the Technical Specification limit of 1.66 seconds

and that 11 control rods exceeded 1.4 seconds, the value that the

licensee has established for replacing rod drives during a

refueling outage (see paragraph 2.c).

Based on the rod drop data

obtained during the Unit 2 reactor trip, the licensee decided to

re-evaluate the operability of the Unit 1 control rods.

This

decision was based on the knowledge that Unit 1 had been operating

longer than Unit 2 and that a greater number of control rod drive

mechanisms (CRDMs) had been refurbished during the Unit 2

refueling outage.

As a result of the re-evaluation, the licensee decided to take

Unit I off-line on April 27, 1995, and perform rod drop time

testing to confirm operability of the Unit 1 control rods.

The

testing identified five control rods with drop times greater than

the Technical Specification limit of 1.66 seconds and four control

rods with drop times greater than 1.5 seconds, but less than 1.66

seconds. After reviewing the Unit 1 rod drop data, the licensee

commenced a reactor cooldown to cold shutdown to allow

refurbishment of the slow CRDMs. At the end of the inspection

period the Unit was in cold shutdown with the loops dropped. The

licensee plans to refurbish nine CRDMs during the outage. The

inspectors will follow the licensee's repair efforts during the

next monthly inspection period.

f.

Control of Scheduled Work

The inspectors noted that the operations shift manager had

rejected work.orders (WO) on March 30, 1995, for concurrence of

work scheduled for the following Monday (April 3, 1995).

One work

order was for lubrication of the Unit #1 turbine driven emergency

feedwater pump (WO 9501518-01, PM Lube: Ul TDEFWP And Turbine) and

two others (WO 95026645-01, PM: 16 CYL Diesel Engine, and WO 95026646-01, PM: 12 Cyl Diesel Engine) involved preventive

maintenance that required taking the standby shutdown facility

(SSF) diesel generator out of service.

The SSF generator is the

power supply for the auxiliary service water pumps.

Although simultaneous removal of the equipment was allowed by TS,

the shift manager's decision was based on his awareness of a

Probabilistic Risk Assessment (PRA) that concluded the proposed

configuration would put the plant in a high risk situation by the

II

6

elimination of two sources of emergency feedwater to the Unit 1

steam generators at the same time. The shift manager's decision

was conservative since the PRA program had not been implemented at

that time.

Within the areas reviewed, one violation was identified.

3.

Maintenance and Surveillance Testing (62703 and 61726)

a.

Maintenance activities were observed and/or reviewed during the

reporting period to verify that work was performed by qualified

personnel and that approved procedures adequately described work

that was not within the skill of the craft. Activities,

procedures, and work orders (WO) were examined to verify that

proper authorization and clearance to begin work were given,

cleanliness was maintained, exposure was controlled, equipment was

properly returned to service, and limiting conditions for

operation were met.

Maintenance activities observed or reviewed in whole or in part

are as follows:

(1) Calibrate Reactor Protection System (RPS) Feedwater Pump

(FDWP) Discharge Pressure Switches, Work Order 95005657

The inspectors witnessed calibration of the Unit 2 RPS FDWP

Discharge Pressure Switches. The activity was performed in

accordance with IP/0/A/0305/009, RPS Channel A Main

Feedwater Pumps and Main Turbine Trips Calibration. The

calibration was on an increased schedule, biweekly, due to

drifts in the setpoints associated with the Static-O-Ring

pressure switches.

The unit pressure switches were replaced with a different

model of the Static-0-Ring switch. However, the new

switches have not performed well and the licensee is

evaluating their replacement.

The inspector determined the calibration activity was

performed to acceptable standards.

(2) Perform Preventive Maintenance On Condenser Circulating

Water (CCW) Pump Motor IC, Work Order 95027249

On April 17, 1995, the inspectors observed activities during

the performance of preventive maintenance on the IC CCW

pump. The work instructions involved implementation of

maintenance procedures MP/O/A/1840/040, Pumps-Motors

Miscellaneous Components, and MP/O/B/1300/037, Motor-CCW

Lubrication and Inspection. In addition, electrical tag

outs OPS-95-0693-1, 1C CCW Pump Breaker, and OPS-95-0693-6,

7

1C CCW Pump Motor Heater Breaker, were reviewed as part of

the work package.

The inspectors noted that the completed steps in procedure

MP/0/B/1300/037, had not been initialed. The procedure was

required to be in use and the steps were to be initialed as

they were accomplished. The inspectors questioned the

craftsmen and were informed that the missed initials were an

oversight. As a result, the completed steps were then

initialed by the craftsmen.

The licensee performed an investigation of the event and

took appropriate corrective actions, which included

counselling the individuals involved.

In addition,

expectations for verbatim procedure compliance were stressed

in maintenance team meetings. -The inspectors consider the

corrective actions to be appropriate for the circumstances.

The CCW pump motors are not presently classified as safety

related, but the licensee has committed to a future upgrade

of the pump motors to a safety-related classification and to

perform maintenance activities per safety-related

procedures.

(3) 3C Low Pressure Injection (LPI) Pump Vent Line Replacement,

Work Order 95030288

Due to minor leaks in the weld area, the vent line for the

3C LPI Pump was replaced. The inspectors verified that the

replacement flexible hose (stainless steel), welding rods,

and work procedures were of the appropriate Quality

Assurance classification. The inspectors concluded that

procedural compliance for this activity was good. All

activities observed were satisfactory.

(4) Replace Capacitor Coupled Voltage Transformers (CCVTs) on

230KV Red Bus, Work Order 94062794

The CCVTs were replaced on the 230KV switchyard red bus per

NSM-52950. The inspectors verified that appropriate

precautions were taken to prevent an inadvertent red bus

lockout. The inspectors verified that procedures were in

place and were being followed. All activities observed were

satisfactory.

(5) Repair Seat Leak on Low Pressure Service Water (LPSW) Valve

304, Work Order 95031118

The inspectors reviewed the work request and observed work

activities in progress associated with this corrective

maintenance activity. The activity consisted of replacing

the old globe valve installed in the system with a new globe

8

valve. The inspectors verified that procedures were in

place and were being followed. The inspectors noted that

the maintenance activity was well coordinated between

operations and maintenance personnel and that the valve

replacement was accomplished in an efficient and expedient

manner. No discrepancies were noted.

b.

The inspectors observed surveillance activities to ensure they

were conducted with approved procedures and in accordance with

site directives. The inspectors reviewed surveillance

performance, as well as system alignments and restorations. The

inspectors assessed the licensee's disposition of any

discrepancies which were identified during the surveillance.

Surveillance activities observed or reviewed in whole or in part

are as follows:

(1) Unit 3 Control Rod Movement, PT/3/A/600/15

The inspector witnessed the monthly performance test of the

Unit 3 control rods.

All equipment operated as expected.

Operator communication and procedural compliance were good.

(2) Control of Control Rod Drive Trip Time Testing,

PT/O/A/0300/01

The inspectors monitored this surveillance activity

conducted on April 27, 1995, during the Unit 1 shutdown to

perform control rod drive trip time testing. The test was

performed when reactor power was below 2 percent with all

control rods fully withdrawn. The test consisted of

manually tripping the control rods and determining rod drop

times using the operator aid computer and the events

recorder. The inspectors monitored the test in progress and

reviewed the test results.

The test identified that five

control rods exceeded the Technical Specification required

trip time of 1.66 seconds or less.

The slowest rod dropped

in 2.084 seconds as recorded on the events recorder. Based

on the test results, the licensee initiated a reactor

cooldown to cold shutdown to commence a control rod drive

mechanism refurbishment outage.

Within the areas reviewed, licensee activities were satisfactory.

4.

Onsite Engineering (37551 and 40500)

During the inspection period, the inspectors assessed the effectiveness

of the onsite design and engineering processes by reviewing engineering

evaluations, operability determinations, modification packages and other

areas involving the Engineering Department.

  • I

9

a.

Oconee Emergency Power Upgrade Project

Keowee Hydro Station was designed, constructed, and maintained -to

hydroelectric standards. The hydro station was not originally

under the Nuclear Generation Department management and

documentation and programmatic controls have not been consistent

with nuclear industry standards. Over the years several events

and internal/external assessments resulted in a growing list of

commitment items. These included the May 15, 1992, Self-Initiated

Technical Audit (SITA), October 1992 Loss of Offsite Power Event,

Electrical Distribution System Functional Inspection, and the

Design Basis Document (DBD) review program. In order to manage

the list of commitment items, the licensee initiated the Oconee

Emergency Power Upgrade Project. On September 29, 1994, the

licensee presented their plans for this project to NRC Region II

management.

The upgrade project provides for the engineering analyses,

procedure upgrades, maintenance program development, and

configuration documentation/upgrade for the Keowee Hydro Station

and the Emergency Power Path of Oconee Nuclear Station. The

licensee stated that this project will fully incorporate Keowee

into the Oconee nuclear maintenance program and satisfy all open

commitment items. The project is scheduled for completion no

later than January 1996.

b.

Review of SITA Items

During the inspection period, the inspectors confirmed that all

NRC open items related to Oconee emergency power were addressed by

the Emergency Power Upgrade Project. Additionally, the inspectors

reviewed the status of the May 15, 1992, SITA. The inspectors

noted that there were 86 SITA items (findings, followups, and

document discrepancies) that required a written response with

proposed corrective action to Duke's Quality Verification group in

Charlotte. Thirty of these SITA items remained to be completed by

Oconee. The inspectors reviewed the 30 open SITA items to

determine if they were being appropriately dispositioned. The

inspectors verified that all 30 open items were included in either

the Emergency Power Upgrade Program or the Problem Investigation

Process. A detailed review of several of the SITA items was

conducted to determine the adequacy of the licensee's response.

The results of this review were as follows:

(1) SITA item 3.1.4-1, "The Keowee Station has not been Analyzed

for Flooding" (Emergency Power Upgrade Project Item #26)

The SITA auditors identified a finding where the Keowee

units could be incapacitated due to internal flooding. The

source of flooding was listed as a break in the service

water line, a fire hose or the drinking water system. The

recommended corrective action from the audit team was to

10

assess the effect of flooding on the Keowee units. Oconee's

response to this finding was that no flood analysis for the

Keowee units was necessary. The basis for this position was

that, according to the Oconee licensing basis, the flood

does not occur simultaneously with nor subsequent to any

other accident condition. Therefore if internal flooding

rendered both Keowee units inoperable, the appropriate

Technical Specification would be entered. The inspectors

confirmed that the Oconee licensing basis does not postulate

any mechanical passive failures coincident with, or

subsequent to, a loss of offsite power (LOOP).

The

inspectors concluded that the licensee's position on this

item was acceptable.

(2) SITA item 3.8-1, "Problems Associated with the Integrated

Systems Analysis (ISA) Report 81-04" (Emergency power

upgrade project Item #30)

This finding was due to perceived problems.associated with

ISA Report 81-04. This report assessed the ability of the

station to perform ten basic shutdown functions following a

seismic event. The finding stated that basic assumptions in

this report that certain initiating events were outside the

licensing basis were incorrect. The Oconee site response

was that this ISA Report does not represent a licensing or

design basis document. Accordingly, the inspectors verified

that ISA Report 81-04 was not intended to be used as a

reference by licensee personnel.

Within the areas reviewed, licensee activities were satisfactory.

5.

Plant Support (71750 and 40500)

a.

Fire Protection

During the course of normal tours, the inspectors routinely

examined facets of the licensee's fire protection plan. The

inspectors reviewed transient fire loads, flammable materials

storage, housekeeping, control of hazardous chemicals, ignition

source/fire risk reduction efforts, and fire barriers.

b.

Physical Protection

During this inspection, the inspectors toured the protected area

and noted that the perimeter fence was intact and not compromised

by erosion or disrepair. Isolation zones were maintained and were

clear of objects which could shield or conceal an individual.

The inspectors observed that personnel and packages entering the

protected area were searched either by special purpose detectors

or by a physical patdown for firearms, explosives, and contraband.

The processing and escorting of visitors was observed.

11

c.

Radiological Protection Program

Radiation protection control activities were observed to verify

that these activities were in conformance with the facility

policies and procedures, and in compliance with regulatory

requirements. These observations included:

-

Entry to and exit from contaminated areas, including stepoff

pad conditions and disposal of contaminated clothing

-

Area postings and controls

-

Work activity within radiation, high radiation, and

contaminated areas

-

Radiation Control Area (RCA) exiting practices

-

Proper wearing of personnel monitoring equipment, protective

clothing, and respirator equipment

d.

Licensee Self-Assessment

On April 19, 1995, the inspectors attended the licensee's

Corrective Action Continuous Improvement Team (CACIT) meeting. The

meeting addressed the program status and implementation of

corrective actions, performance goals, trend reviews, and

effectiveness. Site senior management participated in the meeting

and informed the committee that the number of overdue items were

expected to be reduced to zero within the near future.

On April 20, 1995, the inspectors attended a Plant Operations

Review Committee (PORC) meeting. The principal topic of the

meeting was the slow rod drop times during the April 14, 1995,

Unit 2 trip, and the implications for Unit 1. As discussed in

paragraph 2.e above, the licensee decided to shut down Unit 1 in

order to measure the control rod drop times.

The inspectors

concluded that the PORC encouraged an open discussion of the

issues involved, with a proper focus on safety.

Within the areas reviewed, licensee activities were satisfactory.

6.

Inspection of Open Items (92901, 92902 and 92903)

The following open items were reviewed using licensee reports,

inspection record review, and discussions with licensee personnel, as

appropriate:

a.

(Closed) Unresolved Item 50-270/95-03-03, Valve Configuration

This issue involved a mispositioned Unit 2 valve in the CCW system

(2CCW-110) that was discovered on March 23, 1995. The valve had

been closed for a hydrostatic leak test and was not reopened at

12

the completion of the test on November 4, 1994.

The licensee had

relied on a system realignment to return the valve to the required

open position.

However, the system realignment had been performed

prior to completion of the hydrostatic test and the valve was not

returned to its open position. This event was described as

similar to an event discovered on August 15, 1994, when the

licensee had found comparable valves misaligned in the CCW System

on Units 1 and 3. The licensee had relied on a system realignment

after a hydrostatic test to restore the valves to their required

position. Again, the system had already been realigned prior to

completion of the testing activities.

Corrective actions taken by the licensee as a result of the valve

configuration problems identified on August 15, 1994, were

implemented on March 14, 1995. This included change 26 to

MP/0/A/1720/010, System/Component Hydrostatic Test Controlling

Procedure, to require a listing of each component to ensure proper

system realignment after completion of hydrostatic testing. Since

the licensee identified the second occurrence and it was prior to

implementation of actions designed to prevent recurrence of the

previous event, associated corrective actions were determined by

the inspectors to be acceptable. This item is closed.

b.

(Closed) Unresolved Item 269,270,287/94-16-03, Engineered

Safeguards Wiring Discrepancies

This item involved a design deficiency associated with the

Engineered Safeguards cabinets. During post-modification testing

conducted on Unit 1 during a scheduled refueling outage, the

licensee identified that the manual control relays inside the

engineered safeguards (ES) unit control modules were connected to

the instrument ground system. The electrical circuit for manual

control after an ES actuation are dependent on the instrument

ground system, through the station ground system and the KRA

regulated power panelboard neutral conductor, to the 120 volt

vital power inverters neutral conductor. The instrument ground

system, station ground system, and regulated power supply system

are not considered safety-related. The electrical circuit relied

on a common electrical cable in several locations to maintain an

electrical circuit for manual control of ES components following

an ES actuation.

The licensee modified the Unit 1 circuitry during the refueling

outage and performed an operability evaluation on the Unit 2 and 3

ES systems. The operability evaluation determined that the ES

systems were operable based on the fact that the grounding systems

were passive and no credible single failure could be postulated

for any design basis events. The inspectors verified that the

Unit 2 and 3 ES systems were subsequently modified to correct the

design deficiency. Unit 2 was corrected by Minor Modification

6710 and Unit 3 was corrected by Minor Modification 6711. Based

on these actions, this item is closed.

7.

Exit Interview

13

The inspection scope and findings were summarized on May 8, 1995, with

those persons indicated in paragraph 1 above. The inspectors described

the areas inspected and discussed in detail the inspection findings.

The licensee did not identify as proprietary any of the material

provided to or reviewed by the inspectors during this inspection.

Item Number

Status

Description and Reference

Violation 269,270,

Open

Inadequate Corrective Action

287/95-06-01

for Control of Keowee Operating

Limits (paragraph 2.d).

Unresolved Item

Closed

Valve Configuration (paragraph

270/95-03-03

6.a).

Unresolved Item

Closed

Engineered Safeguards Wiring

269,270,287/94-16-03

Discrepancies (paragraph 6.b).

0II

0