ML16154A761

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Insp Repts 50-269/94-38,50-270/94-38 & 50-287/94-38 on 941127-1231.Violations Noted.Major Areas Inspected:Plant Operations,Surveillance Testing,Maint Activities,Onsite Engineering & Technical Assistance
ML16154A761
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 01/25/1995
From: Crlenjak R, Harmon P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML16154A760 List:
References
50-269-94-38, 50-270-94-38, 50-287-94-38, NUDOCS 9502030122
Download: ML16154A761 (15)


See also: IR 05000269/1994038

Text

Epk REGo

UNITED STATES

.o

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report Nos.:

50-269/94-38, 50-270/94-38 and 50-287/94-38

Licensee:

Duke Power Company

422 South Church Street

Charlotte, NC

28242-0001

Docket Nos.: 50-269, 50-270 and 50-287

License Nos.: DPR-38, DPR-47 and DPR-55

Facility Name:

Oconee Units 1, 2 and 3

Inspection Conducted: November 27 - December 31, 1994

Inspector:

>1(siv.t4-t"

,)'s 1'/5

P. E. Harmon, Senior Pogidei

Inspector

Date Signed

W. K. Poertner, Resident Inspector

L. A. Keller, Resident Inspector

P. G. Hum rey, Resident Inspector

Approved by:

R.'V. Crlenj , Chief, Brdnch 3

ate

igned

Division of Reactor Projects

SUMMARY

Scope:

This routine, resident inspection was conducted in the areas of

plant operations, surveillance testing, maintenance activities,

onsite engineering and technical assistance.

Results:

One violation was identified for failure to follow procedures when

transferring operation of the Keowee Hydro Unit from Remote to

Local, paragraph 2.e.

The licensee's practices for performing on-line maintenance

revealed that while no formal assessment is performed, on-line

maintenance involving taking multiple components out-of-service is

not routine at Oconee, paragraph 6.

A reactor trip of Unit 2 from 100 percent power occurred on

December 8,.1994. The cause of the trip was a loss of power to

the Integrated Control System (ICS) due to a loose lug on the

power supply breaker. The unit was returned to power the

following day, paragraph 2.c.

ENCLOSURE 2

9502030122 950125

PDR ADOCK 05000269

0-

PDR

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

  • B. Peele, Station Manager
  • E. Burchfield, Regulatory Compliance Manager
  • D. Coyle, Systems Engineering Manager

J. Davis, Engineering Manager

T. Coutu, Operations Support Manager

  • W. Foster, Safety Assurance Manager
  • J. Hampton, Vice President, Oconee Site

0. Hubbard, Superintendent, Instrument and Electrical (I&E)

C. Little, Electrical Systems/Equipment Manager

  • J Smith, Regulatory Compliance
  • G. Rothenberger, Operations Superintendent

R. Sweigart, Work Control Superintendent

Other licensee employees contacted included technicians, operators,

mechanics, security force members, and staff engineers.

  • Attended exit interview.

2.

Plant Operations (71707)

  • a.

General

The inspectors reviewed plant operations throughout the reporting

period to verify conformance with regulatory requirements,

Technical Specifications (TS), and administrative controls.

Control room logs, shift turnover records, temporary modification

log, and equipment removal and restoration records were reviewed

routinely. Discussions were conducted with plant operations,

maintenance, chemistry,,health physics, instrument & electrical

(I&E), and engineering personnel.

Activities within the control rooms were monitored on an almost

daily basis.

Inspections were conducted on day and night shifts,

during weekdays and on weekends.

Inspectors attended some shift

changes to evaluate shift turnover performance. Actions observed

were conducted as required by the licensee's Administrative

Procedures. The complement of licensed personnel on each shift

inspected met or exceeded the requirements of TS. Operators were

responsive to plant annunciator alarmsand were cognizant of plant

conditions..

Plant tours were taken throughout the reporting period on A

routine basis.

During the plant tours, ongoing activities,

housekeeping, security, equipment status, and radiation control

practices were observed.

2

b.

Plant Status

Unit 1 essentially operated at 100 percent power the entire

reporting.period.

Unit 2 experienced a reactor trip on December 8, 1994, due to a

loss of control power to the ICS. The unit was restarted and was

back on line December 9, 1994, and operated at essentially 100

percent power for the remainder of the reporting period.

Unit 3 essentially operated at 100 percent power the entire

reporting period.

C.

Unit 2 Reactor Trip

Responding to the Unit 2 reactor trip which occurred on December

8, 1994, at 2:24 p.m., the- inspectors monitored control room

operations during trip recovery. The trip resulted from a loss of

power to the ICS which was caused by a breaker tripping in the

circuit. A loose connection on the load side of the breaker

terminal was determined to have caused the breaker to trip. The

loss of power to the ICS generated a false "high steam generator

level" signal which tripped the main feedwater pumps. Loss of

both feedwater pumps in turn generated a signal that tripped the

reactor. All systems responded appropriately and the reactor was

shut down without adverse conditions noted.

As the loose lug could not be tightened, and the affected breaker

(number 25 on the 2KI load center) could not be removed without

de-energizing the entire load center, the breaker's outputs were

swapped to an installed spare breaker (number 26).

Oconee has not

developed load lists for power supply breakers, so the

consequences of de-energizing the entire 2KI load center could not

be determined. The plant was restarted the following day and the

turbine generator was on-line at 1:57 p.m.

The inspectors witnessed the operator's response to the reactor

trip and reviewed the licensee's post trip report. The operators

responded in a very professional manner and conducted the post

trip actions in a very calm, organized fashion. The post trip

review placed particular emphasis on the turbine by-pass valves'

response to the trip. This was prompted by past problems when

these valves repositioned to a random setting and failed to

maintain proper steam generator inventory. Since that time, the

licensee modified the control system, and the post trip review

confirmed that the valves operated properly. The inspector

determined that a thorough post trip review had been conducted,

and that the operators had performed well in their response to the

trip.

3

d.

Unit 2 Control Room Instrumentation

The inspector noted that a total of 51 Unit 2 control instruments

(including computer indications and alarms) were out-of-service or

were not indicating correctly prior to the Unit 2 refueling outage

which began on October 6, 1994. Since the outage has been

completed, the inspectors have been monitoring the status of

control room instrumentation. On December 30, 1994, a total of 37

instruments and computer points were listed as out-of-service or

not indicating properly.

Based on the significant number of instruments with noted

problems, it appears that more emphasis is needed to maintain

control room instrumentation and assure that the operators have

sufficient indications for operating the plant. At the end of the

inspection period, the licensee had formed a task force to

aggressively pursue restoration of out-of-service control room

instruments. The inspectors will monitor the results of this

team's efforts in future inspection reports.

e.

Keowee Unit 1 Loss of Excitation

On December 11, 1994, Keowee Unit 1 tripped while connected to the

grid at no-load conditions. The unit had been operability tested

from the Oconee control room and the Local/Remote switch had been

placed in Remote to perform the operability test. The dispatcher

requested that control of the Keowee unit be transferred back to

Keowee as soon as possible because of lake level letdown

requirements. To accomplish this, Procedure OP/O/A/1106/019,

Keowee Hydro at Oconee, requires shutting down the hydro unit

prior to transferring control of the unit to Keowee. Recalling

past hydro practices where the transfer was done with the unit on

line, the Keowee operator, with concurrence from the Oconee

control room, attempted to transfer control from Oconee to Keowee

by depressing the Manual to Auto Control Transfer push button and

taking the Local/Remote switch from Remote to Local.

When the Keowee operator attempted to transfer control of the

Keowee unit from Remote to Local, the generator output breaker

opened, the generator field breaker and field supply breakers

opened and the voltage regulator transferred to manual.

The

Keowee Unit 1 turbine continued to operate, so the Keowee operator

secured the Keowee unit by pressing the stop button.

Subsequent to securing the unit, the Keowee operator smelled

smoke.

Investigating, the operator found the closing coil on the

generator field breaker smoking and racked out the breaker to

deenergize the closing coil.

The generator field breaker closing

coil was replaced with a spare closing coil and the breaker was

returned to service. The subsequent operability testing was

satisfactory.

4

The loss of excitation resulted from momentary dropouts of the

master run relays with the unit at speed-no-load conditions. The

transfer could have possibly been accomplished if the Keowee unit

had been loaded prior to the transfer from remote to local.

The

coil failure resulted from concurrent close and trip signals being

applied to the generator field breaker and the breaker mechanism

operating to the trip free condition prior to the closing coil

being deenergized, resulting in the coil overheating.

The failure to operate the Keowee hydro station in accordance with

approved procedures is identified as Violation 50-269,270,287/94

38-01:

Failure to Follow Keowee Transfer Procedures.

f.

Reactor Building Spray Inoperability Due to Inadequate Procedure

On December 27, 1994, the licensee performed a review of the

abnormal procedure for loss of low pressure injection. For a

postulated loss of coolant accident in which a single failure

disables 1 of the 2 reactor building emergency sump lines, the

abnormal procedure directs the operators to secure both reactor

building spray pumps. The licensee determined that this condition

was beyond the design basis assumptions contained in the maximum

hypothetical accident safety evaluation report. The licensee

declared both trains of reactor building spray inoperable on all

three units and entered TS 3.0 at 4:45 p.m. TS 3.0 requires that

the unit be placed in a hot shutdown condition within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

To correct the procedural inadequacy the licensee initiated a

procedure change to require that one train of reactor building

spray be maintained operable assuming a postulated single failure

of a reactor building emergency sump line. The procedure changes

were completed and TS 3.0 was exited at 10:25 p.m. on December 27,

1994. The licensee was reviewing this item further to determine

if the reactor building spray systems were actually inoperable as

a result of the procedural inadequacy. The inspectors considered

the licensee's action with regard to declaring the reactor

building spray systems inoperable appropriately conservative and

reviewed the proposed procedure changes. The inspectors will

continue to review this item further.

Within the areas reviewed, one Violation was identified.

3.

Maintenance and Surveillance Testing (62703 and 61726)

a.

Maintenance activities were observed and/or reviewed during the

reporting period to verify that work was performed by qualified

personnel and that approved procedures adequately described work

that was not within the skill of the craft. Activities,

procedures and work orders (WO) were examined to verify that

5

proper authorization and clearance to begin work were given,

cleanliness was maintained, exposure was controlled, equipment was

properly returned to service, and limiting conditions for

operation were met. The following maintenance activities were

observed or reviewed in whole or part:

(1) Reactor Protection System (RPS) Channel 'D'

Main Feedwater

Pumps and Main Turbine Trips Calibration, IP/0/A/0305/012

The inspector reviewed activities in progress during the

calibration of pressure switch 2PS-419 on December 27, 1994.

The work effort was being performed in accordance with

calibration procedure IP/O/A/0305/012. RPS Channel 'D,' had

been removed from service as specified in IP/O/A/0305/015,

Nuclear Instrumentation RPS Removal From and Return to

Service for Channels A,B,C and D for the switch calibration.

The activity had been authorized per Work Order 94093207,

Task 01.

The inspector determined that the activity was performed to

acceptable standards, and no discrepancies were noted.

(2) Work Order 94093081, Task 01, Check/Calibrate Emergency

Feedwater Pressure Switches

The inspectors observed activities in progress to calibrate

the Unit 1 emergency feedwater pressure switches using

procedure IP/O/A/0275/005I, Motor Driven Emergency Feedwater

Pump Safety-Related Instrumentation Calibration and System

Functional Check. The work activity was verified performed

in accordance with the procedure and no maintenance

discrepancies were noted during the performance of the work

activity. Numerous pressure switches did not meet the

calibration tolerance band stipulated in the procedure.

This issue is discussed further in paragraph 4.

b.

The inspectors observed surveillance activities to ensure they

were conducted with approved procedures and in accordance with

site directives. The inspectors reviewed surveillance

performance, as well as system alignments and restorations. The

inspectors assessed the licensee's disposition of any

discrepancies which were identified during the surveillance. The

following surveillance activities were observed or reviewed:

(1) Stroke Test of 3BS-1, IP/0/A/3001/016

Valve 3BS-1 is the 3A Reactor Building Spray Pump's

discharge isolation valve. On October 16, 1994, Valve 3BS-1

exceeded the performance stroke testing requirements by one

second. As discussed in Inspection Report 94-32, the

6

Slicensee's evaluation concluded that maintenance performed

during January 1994 altered the baseline for this valve and

that this accounted for the slower stroke time. The

licensee has instituted a weekly stroke test of Valve 3BS-1

to verify that the stroke time is not degrading. On

November 30, 1994, the inspector observed one of these

weekly stroke tests. The stroke time was 13.96 seconds,

which was consistent with the previous stroke times. All

activities observed were satisfactory.

(2) Standby Shutdown Facility (SSF) Instrument Surveillance,

PT/O/A/600/20

This monthly surveillance verifies that the SSF control room

instrumentation is operable and that it agrees with the

corresponding instrumentation in the main control rooms.

The inspector observed the surveillance check of the SSF

Unit 1 RCS temperature instruments on December 19, 1994.

During this check, the operators experienced-great

difficulty in getting all six RCS temperature gauges to go

to mid scale as required. Eventually, the operators were

able to complete the step as required. The inspector

confirmed that operators properly filled out a test

deficiency form for this problem. All activities observed

were satisfactory.

(3) Keowee Hydro Operation, PT/O/A/620/09

On December 21, 1994, the inspector observed the performance

of the monthly Keowee hydro test. Both hydro units started

and supplied the Main Feeder Buses as required. All

parameters were verified by the inspector to be within

specifications. All activities observed were satisfactory.

(4) Reactor Protection System Control Rod Drive Breaker Trip and

Timing Test, IP/O/A/305/14

Procedure IP/O/A/305/14 implements the requirements of

Technical Specification (TS) 4.1.1, Table 4.1-1, Instrument

Surveillance Requirements. This surveillance requires a

monthly test of the control rod drive trip breakers. The

inspectors monitored the performance of the procedure and

verified that the acceptance criteria were met. No

deficiencies were noted.

(5) High Pressure Service Water Pump and Power Supply,

PT/0/A/250/05

Procedure PT/O/A/250/05 implements the requirements of TS 4.1.2, Table 4.1-2, Minimum Equipment Test Frequency. This

surveillance requires a monthly functional test of the High

Pressure Service Water pumps and power supplies. The

7

inspectors reviewed the completed performance test conducted

on December 31, 1994. No discrepancies were noted.

No violations or deviations were identified.

4.

Onsite Engineering (71707)

During the inspection period, the inspectors assessed the effectiveness

of the onsite design and engineering processes by reviewing engineering

evaluations, operability determinations, modification packages and other

areas involving the Engineering Department.

On December 7, 1994, during the performance of a routine calibration of

the Unit 1 RPS feedwater pressure switches, four of the eight pressure

switches were found out of calibration. These pressure switches, which

are set at 770 psig, provide an anticipatory reactor trip signal on a

loss of main feedwater. The as found setpoints for the out of

calibration instruments ranged from 735 psig to 750 psig. These values

exceeded the 15.5 psig maximum setpoint drift assumed in the uncertainty

calculation assumptions. The pressure switches in question are Static

0-Ring model 9N6-W5-U8-C1A-JJTTNQ pressure switches. They had been

installed during the previous refueling outage. These new pressure

switches had also been installed in the emergency feedwater (EFW)

initiation circuitry.

Based on the data obtained from the Unit 1 RPS switches, the licensee

initiated a program to calibrate all the Static-0-Ring EFW and RPS

pressure switches on all three units. The calibration of the switches

was completed on December 14, 1994.

Five of the six EFW pressure

switches on Unit 1 were out of calibration. Eleven of the fourteen

total feedwater pressure switches on Unit 2 were found out of

calibration and twelve of the fourteen pressure switches on Unit 3 were

found out of calibration.

The pressure switches were reset to the proper setpoint and a

conditional operability evaluation was performed for all three units.

The conditional operability evaluation concluded that the pressure

switches could be considered operable if the calibration frequency was

increased to weekly for Unit 3 and every two weeks for Units 1 and 2.

Having reviewed the conditional operability determination and the

calibration data collected since the problem was first identified, the

inspectors concur with the licensee's conditional operability

evaluation.

The licensee was still reviewing this issue at the end of the inspection

period, but had already determined that portions of the Unit 1 and Unit

3 initiation circuitry were inoperable due to the excessive instrument

calibration drift. The inspectors will continue to review this item in

the future via the Licensee Event Report required to be submitted to the

NRC per 10 CFR 50.73.

8

Within the areas reviewed, licensee activities were satisfactory and no

violations or deviations were identified.

5.

Cold Weather Preparations (71714)

The inspector reviewed the licensee's program to protect equipment and

systems against extreme cold weather conditions. The program is

outlined in Enclosure 5.12, Cold Weather Checklist of Operations

Procedure, OP/1/A/1102/20, Shift Turnover, and is initiated via a

computer alarm when the outside temperature reaches a low of 35 degrees

F. The procedure checklist specifies various preventive measures to be

implemented such as building doors closed, dampers closed, heaters

turned on and operating properly, outside equipment cooling water at

rated flows, trench covers in place, heat tracing operating properly and

building heating systems in service.

In addition, alarm 1SA9B3, Reactor Building Ventilation Purge Inlet Temp

Low, annunciates when the outside temperature reaches a low temperature

of 40 degrees F. The response requires that various heater alarms be

reviewed for malfunctions and steam supplies be readied for use per

procedure OP/0/A/1106/22, Auxiliary Steam System.

The cold weather program was based on an evaluation of equipment where

freeze protection was required and a compiled list of areas that have

experienced problems with freezing. The inspector witnessed

implementation of the procedure on December 1, 1994, when the outside

temperature dropped to 35 degrees F. No discrepancies were identified

during the inspector's review of the completed checklist, and the

program was considered to be adequate.

6.

Evaluation of On-Line Maintenance (TI 2515/126)

The objective of this inspection was to evaluate the impact on safety of

the licensee's practices regarding the removal of equipment from service

for on-line scheduled maintenance. The licensee indicated that it was

their policy to limit the scope of maintenance activities being

conducted simultaneously, and the scope of maintenance activities

conducted on-line that could be accomplished during an outage. However,

the licensee had no formalized process or procedures for assessing the

risk associated with.taking multiple components out of service at the

same time for maintenance, or for doing maintenance on-line rather than

during an outage. The inspector noted that the only formal mechanism

for restricting maintenance activities were the requirements of TS. The

inspector conducted a review of the maintenance history from January

1993 until December 1994 to determine the amount and frequency of

maintenance performed during power operation. The inspector noted that

it was rare for there to be multiple entries into Limiting Conditions

for Operations (LCOs) for maintenance or testing. However, several

specific examples when this occurred included:

9

On January 12, 1993, the 3B Reactor Building Cooling Unit (RBCU),

3A Low Pressure Injection (LPI) pump, and Keowee Unit I were all

out of service at the same time.

On March 8, 1993, the Unit 1 Turbine Driven Emergency Feedwater

(TDEFW) pump and lB LPI train were both taken out of service for

maintenance/testing simultaneously.

On May 19, 1993, the IC Low Pressure Service Water pump,

containment isolation valve 1RC-7, and switchyard battery charger

SY-2 were taken out of service at the same time.

-

On October 4, 1993, the SSF, Unit 1 Emergency Condenser

Circulating Water (ECCW), and the Unit 1 TDEFW pump were all taken

out of service simultaneously.

Additionally, the inspector noted that following the most recent Unit 2

refueling outage the licensee entered the LCO for the Unit 2 RBCUs on

three separate occasions to perform maintenance on cooler outlet valves

(under the LCO for 9 days over a 15 day period). This maintenance was

originally slated for completion during the outage, but was purposely

deferred to on-line maintenance in order to prevent extending the outage

duration.

The inspector concluded that in general the licensee limits on-line

maintenance. However, there were no requirements, other than TS, to

limit either the scope or frequency of maintenance conducted while at

power. Additionally, there was no formal mechanism to assess the

potential risks of conducting multiple maintenance/testing activities at

the same time. The licensee indicated that as part of their planned

implementation of the Maintenance Rule, they were preparing a matrix

that would administratively prohibit certain combinations of maintenance

activities based on insights gained from Probabilistic Risk Assessment

(PRA).

The inspectors noted that the licensee did perform a PRA as part

of their planning for an extended outage of the Keowee overhead path.

This outage activity, which lasted 14 days while all three Oconee units

were on-line, consisted of reblocking the Keowee main transformer. The

PRA concluded that the attendant work should be performed during periods

of Oconee unit "innages."

No violations or deviations were identified.

7.

Inspection of Open Items (92902 and 92903)

The following open items were reviewed using licensee reports,

inspection record review, and discussions with licensee personnel, as

appropriate:

a.

(Closed) Unresolved Item 50-269,270,287/90-30-02: Clarification

of TS 3.4.1.

10

As a result of this item the licensee submitted a TS change

request to clarify the operability requirements of the emergency

feedwater automatic initiation circuitry. This change was

approved and incorporated into the TS by amendment 207 for Units 1

and 2, and amendment 204 for Unit 3. Based on the TS change, this

item is closed.

b.

(Closed) Unresolved Item 50-269,270,287/94-36-01: Failure To Meet

SSF Activation Time Requirement

This.URI was identified concerning the ability of Oconee operators

to place the SSF into operation within 10 minutes. The licensee

had determined that the SSF must be activated within 10 minutes of

the onset of an SSF required event in order to prevent Reactor

Coolant Pump (RCP) seal damage/failure and/or loss of natural

circulation due to steam void formation.

On July 27, 1994, the licensee performed a drill that was written

with the intent of showing how plant personnel and equipment were

prepared to cope with mitigation of an Appendix "R" type event.

The drill scenario included a requirement to activate the SSF.

The SSF activation time for this drill was approximately 28

minutes. During this drill, it took approximately 8 minutes for

the personnel to acknowledge the need to activate the SSF, and 20

additional minutes before the SSF was in service. The licensee

indicated that this drill failure was an isolated instance and did

not indicate that the SSF could not be activated within 10

minutes. The licensee based this on the "numerous successful

testing of the 10 minute criterion" previously performed. The

inspector noted that the only previous documented test for SSF

activation was conducted on December 13, 1987. This was a single

unit scenario in which the total elapsed time was 9 minutes, 26

seconds.

The inspector observed a training exercise during the previous

inspection period and noted that the exercise did not account for

the time required for the necessary valve manipulations (valves

were not actually stroked during the drill, rather the valves were

assumed to go instantly open or closed). Additionally, the

inspector noted that completing the procedure as written within

ten minutes was extremely challenging. The inspector noted that

the necessary valve manipulations would add approximately one

minute to the activation time, and that this apparently had not

been accounted for in previous drills/tests. Due to the lack of

documentation, it was impossible to determine if factoring in the

valve stroke times into the previous tests would have resulted in

test failures.

The licensee agreed that valve stroke times should be included in

any future drill/test used to verify that the SSF could be placed

into operation within 10 minutes. The licensee concluded that

11

valve stroke times would add 56 seconds to the Unit 1 activation

time, 75 seconds to Unit 2, and 58 seconds to Unit 3.

On December 7, 1994, the inspectors observed a special drill which

was conducted to verify that the SSF could be placed in service

within 10 minutes with valve stroke times included. The

licensee's scenario for this drill assumed all Turbine Building

components were simultaneously destroyed by a fire. This required

full activation of the SSF in order to provide Reactor Coolant

Makeup and Auxiliary Service Water to all three Oconee units. The

results of the drill were as follows:

Unit 1:

9:46

Unit 2:

10:48

Unit 3:

10:00 (times in minutes:seconds)

A conference call was held between the licensee and NRC (Region II

and NRR) to discuss issues associated with the recent drill

failures. During the call the licensee maintained that the recent

drill failures indicated the need for additional operator training

and procedural enhancements, but did not indicate that the SSF was

inoperable. The licensee subsequently conducted additional

operator training and revised the SSF activation procedure. The

licensee then performed another three unit drill scenario on

December 20, 1994, similar to the one conducted on December 7,

1994. The results of the drill were as follows:

Unit 1:

6:17

Unit 2:

6:05

Unit 3:

6:18

(times in minutes:seconds)

The licensee indicated that they would continue to perform

periodic drills in order to test all shift personnel.

The

inspectors will continue to follow the licensee's drills. Based

on the last drill, the inspectors concluded that the licensee's

training and procedures had improved sufficiently to provide

reasonable assurance that the SSF could be manned within 10

minutes. The inspectors concluded that the failure to factor in

valve stroke times in drills conducted prior to December 7, 1994,

constituted a weakness in the licensee's test program for the SSF.

8.

Review of Licensee Event Reports (92700)

The below listed Licensee Event Reports (LER) were reviewed to determine

if the information provided met NRC requirements. The determination

included: adequacy of description, compliance with Technical

Specification and regulatory requirements, corrective actions taken,

existence of potential generic problems, reporting requirements

satisfied, and the relative safety significance of each event. The

following LERs were closed:

12

a.

(Closed) LER 269/92-09:

Unit 1 RCP Seal Leakage Exceeds 4 1/2

Gallons

The licensee made an evaluation on July 22, 1992, that the SSF

Make-up Pump (MUP) was inoperable when Unit 1 was shut down on May

24, 1992, due to a capacity restraint that was exceeded when 1A2

RCP seal leakage exceeded 4.5 gpm. During the unit shutdown, the

RCP seals were inspected. It was discovered that obsolete (black)

seals had been installed in each of the RCPs and this was the

source of the excess leakage observed from the 1A2 RCP seal.

The

obsolete seals were replaced with the proper seals (tan) and the

unit was returned to service on June 9, 1992. In addition, the

obsolete seals were removed from inventory and maintenance

procedure, MP/A/A/1310/004A, Seals RCP - Westinghouse Controlled

Leakage - Removal, Inspection, and Installation was revised to

specify the correct seals to be installed.

On December 14, 1994, the inspector reviewed the referenced

procedure change (change 22) and both the supply and seal return

flows for the Unit 1 RCPs. The corrective actions taken by the

licensee were determined to be acceptable. Accordingly, this LER

is considered closed.

b.

(Closed) LER 270/93-01:

U2 Trip/KI Loss/Loss of Main Feedwater

During a shutdown of Unit 2 for a refueling outage on April 4,

1993, alarm "MS Pressure Mismatch" annunciated. The reactor

temperature was at 536 degrees F and the turbine bypass valves

were closed. At that time, control room indicators began to

fluctuate and the operating feedwater pump tripped. The reactor

operator manually tripped the reactor.

During the event, the operators found that the 2A turbine bypass

valves were tripped to manual and throttled. The partially open

2A bypass valves had been responsible for the erratic indications

observed. The operator took manual control and closed both the 2A

and 2B bypass valves to control steam line pressure and reactor

cooldown.

The opening of the 2A bypass valves was determined to have been

caused by a momentary loss of the 2KI inverter power prior to

rapid transfer to the backup power supply. The loss of the 2KI

power was a result of a blown fuse. It was further learned that

when the 2KI was re-powered from the backup source, the Static

Analog Memory (SAM) module allowed the bypass valves to reset at a

random position. A similar event occurred in Unit 3 on August 10,

1994, following a loss of the "3KI" inverter. Again, the SAM

module allowed the turbine bypass valves to reset at random

positions. However, the 1994 event resulted in a dryout of the 3B

Once Through Steam Generator and the licensee had to enter the

Emergency Operating Procedures to recover the plant. Violation

269,270,287/94-23-94 was issued because of the licensee's failure

13

to take the necessary actions to correct the bypass valve problem

in a timely manner.

The licensee determined the inverters (i.e., KI, KU, and KX) to be

aged and no longer reliable. As.a result, the inverters on Units

1 & 2 have been replaced and those for Unit 3 have been procured

and scheduled for replacement during the next refueling outage.

The SAM modules were finally replaced after the August 10, 1994

event with modules which reset the turbine bypass valves back to

the closed position after a power loss.

Based on the licensee's evaluations and corrective actions, this

LER is closed.

c.

(Closed) LER 270-92-04: Loss of Off-site Power and Unit Trip Due

To Management Deficiency, Less Than Adequate Corrective Action

Program

On October 19, Oconee Unit 2 experienced a Loss of Off-site Power

event, a generator load rejection, and a Unit 2 trip from 100

percent power. A battery charger had been placed in service

without a connected battery. This produced excessive voltage

swings which caused a series of switchyard breaker failure relays

to actuate, locking out both the red and yellow buses in the 230

KV switchyard. These relays had previously been identified by the

licensee as susceptible to spurious operation due to excessive

voltages in 1980, but were not modified as recommended by the

manufacturer (Westinghouse). Lockout of the switchyard caused a

Unit 2 trip, a temporary loss of power, and startup of the

emergency power source (a Keowee emergency generator).

During recovery, the Keowee operator reset the emergency start

signal, which tripped the emergency generator and resulted in a

second loss of power on Oconee Unit 2.

Extensive corrective actions proposed in this event report have

been completed with the exception of an upgrade in the emergency

lighting at Keowee, which is currently scheduled for November

1995. The proposed corrective actions have been reviewed and

found acceptable.

This item is considered closed.

9.

Exit Interview

The inspection scope and findings were summarized on January 5, 1995,

with those persons indicated in paragraph 1 above. The inspectors

described the areas inspected and discussed in detail the inspection

findings in the summary and listed below. The licensee did not identify

14

as proprietary any of the material provided to or reviewed by the

inspectors during this inspection.

Item Number

Description/Reference Paragraph

50-269,270,287/94-38-01

VIOLATION: Failure to Follow Keowee

Transfer Procedure (paragraph 2e).