ML16154A621

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Insp Repts 50-269/94-16,50-270/94-16 & 50-287/94-16 on 940501-0604.Violation Noted.Major Areas Inspected:Plant Operations,Surveillance Testing,Maint Activities & Engineering & Technical Assistance
ML16154A621
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 06/16/1994
From: Harmon P, Sinkule M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML16154A618 List:
References
50-269-94-16, 50-270-94-16, 50-287-94-16, NUDOCS 9406290237
Download: ML16154A621 (17)


See also: IR 05000269/1994016

Text

A

REGU

UNITED STATES

o

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report Nos.:

50-269/94-16, 50-270/94-16 and 50-287/94-16

Licensee:

Duke Power Company

422 South Church Street

Charlotte, NC 28242-0001

Docket Nos.:

50-269, 50-270, and 50-287

License Nos.: DPR-38, DPR-47, and DPR-55

Facility Name:

Oconee Units 1, 2, and 3

Inspection Conducted: May 1 - June 4, 1994

.r

.Harmon,

Senior R

dent Inspector

D Ate ignd

W. K. Poertner, Resident Inspector

L. A. Keller, Resident Inspector

P. 'G.

Humphrey, Resident Inspector

Approved by:

t

-

c?

6

/

,

M. V. Sinkule, Chief,

Date Signed

Reactor Projects Branch 3

SUMMARY

Scope:

This routine, resident inspection was conducted in the areas of

plant operations, surveillance testing, maintenance activities,

and engineering and technical assistance.

Results:

An apparent violation (with two examples) was identified

involving the failure to follow refueling procedures (paragraph

2.c).

Additionally, a violation occurred when a control room operator

inadvertently diluted the Unit 3 Reactor Coolant System (paragraph

2.d).

The licensee discovered a potential single failure vulnerability

in the Engineered Safeguards (ES) System involving a loss of

manual control of certain ES equipment from the control room

following a failure of a common grounding wire. The Licensee

completed an operability evaluation for this configuration which

is being reviewed by the NRC. This issue was identified as an

Unresolved Item (paragraph 4.b).

The inspectors noted that the reactor coolant pump seal injection

flow path and the normal makeup flow path were isolated during the

9406290237 940616

PDR ADOCK 05000269

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PDR

2

performance of a High Pressure Injection pump run-out test. These

flow paths would normally be open during an accident and could

result in different pump run-out flows than that produced during

the test. This item was identified as an Inspector Followup Item

(paragraph 3.b.(3)).

Inconsistencies between the Final Safety Analysis Report, the

Emergency Operating Procedures, the Design Basis Document, and

various calculations were noted regarding the minimum Reactor

Building sump level required for adequate Reactor Building Spray

pump net positive suction head (paragraph 4).

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

  • B. Peele, Station Manager
  • S. Benesole, Regulatory Compliance Manager

D. Coyle, Systems Engineering Manager

J. Davis, Engineering Manager

T. Coutu, Operations Support Manager

  • B. Dolan, Safety AssuranceManager

W. Foster, Superintendent, Mechanical Maintenance

  • J. Hampton, Vice President, Oconee Site

D. Hubbard, Component Engineering Manager

C. Little-, Superintendent, Instrument and Electrical (I&E)

S. Perry, Regulatory Compliance

  • G. Rothenberger, Operations Superintendent

R. Sweigart, Work Control Superintendent

Other licensee employees contactedincluded technicians, operators,

mechanics, security force members, and staff engineers.

  • Attended exit interview.

.2.

Plant Operations (71707)

a.

General

The inspectors reviewed plant operations throughout the reporting

period to verify conformance with regulatory requirements,

Technical Specifications (TS), and administrative controls.

Control room logs, shift turnover records, temporary modification

log, and equipment removal and restoration records were reviewed

routinely. Discussions were conducted with plant operations,

maintenance, chemistry, health physics, instrument & electrical

(I&E), and engineering personnel.

Activities within the control rooms were monitored on an almost

daily basis.

Inspections were conducted on day and night shifts,

during weekdays and on weekends.

Inspectors attended some shift

changes to evaluate shift turnover performance.

Actions observed

were conducted as required by the licensee's Administrative

Procedures. The complement of licensed personnel on each shift

inspected met or exceeded the requirements of TS. Operators were

responsive to plant annunciator alarms and were cognizant of plant

conditions.

Plant tours were taken throughout the reporting period on a

routine basis. During the plant tours, ongoing activities,

housekeeping, security, equipment status, and radiation control

practices were observed.

2

b.

Plant Status

Unit 1 was in a scheduled refueling outage throughout the

inspection period.

Units 2 & 3 operated at or near 100 percent power throughout the

inspection period.

c.

Unit 1 Refueling Activities

The licensee commenced Unit 1 refueling activities on May 25,

1994. Refueling activities were controlled by procedure

OP/1/A/1502/07, Refueling Procedure. Step 1A of Enclosure 5.2,

Refueling Verification Form, required Fuel Assembly 585 located in

Spent Fuel Pool location C62 to be inserted in core location N14.

Fuel Assembly 585 was the first fuel assembly to be inserted into

the reactor vessel for core reload.

During a routine review of

refueling activities the inspectors determined that Fuel Assembly

585 was located in core location 013 with the fuel assembly still

grappled to the fuel handling mast. Discussions with the

refueling Senior Reactor Operator (SRO) determined that Fuel

Assembly 585 was located in core location 013 per an intrastation

letter from Nuclear.Engineering. The letter identified

intermediate core locations for Fuel Assemblies

585,587,58F,5RV,5RL,57G, and 5T9.

The purpose of the alternate

fuel moves was to obtain data on source counts at the different

locations to determine if regenerative source rods were needed to

bring the new Gamma-Metric Nuclear instruments on scale. The

inspectors questioned the acceptability of positioning fuel

assemblies in intermediate locations without approved procedural

guidance. Based on the inspectors' concerns the licensee

suspended fuel handling activities until alternate fuel handling

steps were generated in Enclosure 5.2A of OP/1/A/1502/07 to

reflect the fuel handling activities requested by the intrastation

letter.

(Note: only fuel assemblies 585 and 587 underwent

positioning in intermediate locations.)

OP/1/A/1502/07, Refueling Procedure, Step 4.2, Procedure, Note 2

states:

If it becomes necessary to alter the planned refueling

sequence, a note should be placed in Enclosure 5.2 (Refueling

Verification Form) where the departure occurs. The alternate

moves shall then be documented in enclosure 5.2A (Alternate Core

Loading Verification Form).

The failure to meet the requirements

of OP/1/A/1502/07 with respect to documenting the alternate fuel

movement activities associated with Fuel Assembly 585 is

identified as Apparent Violation 269/94-16-01:

Failure to Follow

Refueling Procedures.

On May 26, 1994, at approximately 4:10 p.m., the licensee

determined that the fuel assembly located in core location M4 was

not the correct fuel assembly required by the refueling procedure.

The licensee identified the problem during the performance of step

3

70 of enclosure 5.2, Refueling Verification Form. Step 70

required Fuel Assembly 75L located in Spent Fuel Pool location K1

to be placed in core location N9. When the Spent Fuel Pool bridge

operators went to location KI to retrieve Fuel Assembly 75L, the

location was empty.

Subsequent investigation by the licensee

determined that Spent Fuel Pool location Li contained a fuel

assembly. This location should have been empty per the refueling

procedure. Step 38 of enclosure 5.2, Refueling Verification Form

required Fuel Assembly 75V located in Spent Fuel Pool location Li

to be placed in core location M4. The-licensee then verified that

core location M4 contained Fuel Assembly 75L. Fuel Assembly 75L

was placed into core location N9 as required by the refueling

procedure and Fuel Assembly 75V was then placed in core location

M4. The failure to meet the requirements of procedure

OP/1/A/1502/07, Enclosure 5.2, step 38 is identified as another

example of Apparent Violation 269/94-16-01:

Failure to Follow

Refueling Procedures.

The licensee was cited three times in the past four years for

failure to maintain configuration control of fuel assemblies in

the Spent Fuel Pool and the Reactor Vessel during core offload and

reload activities. The last citation occurred on December 31,

1992, when Fuel Assembly 4MU was placed in core location M13

instead of Fuel Assembly 5R4 as required by the refueling

procedure.

The most recent examples demonstrate a continued

weakness in the licensee's program for fuel handling, as well as a

continued lack of attention to detail on the part of the fuel

handling staff.

d.

Inadvertent Dilution Of Unit 3 Reactor Coolant System

At approximately 11:00 p.m., on May 23, 1994, the Chemistry

Department requested the Unit 3 Balance Of Plant (BOP) reactor

operator to de-lithiate the reactor coolant system (RCS) for 10

minutes.

De-lithiation of the RCS via demineralizers in the

letdown portion of the High Pressure Injection (HPI) system is a

routine process for RCS pH control. The BOP operator discussed

using the 38 Deborating Demineralizer for this process, as the

Control Room Turnover Sheet designated using this boron saturated

demineralizer for de-lithiation. The appropriate procedure for

this process was OP/3/A/1103/04, Soluble Poison Concentration

Control, Enclosure 3.17, Operation of 3B Deborating Demineralizer

to De-lithiate Unit 3. The BOP operator inadvertently utilized

Enclosure 3.16, Operation of 3A Deborating Demineralizer to De

Lithiate Unit 3", which routed letdown flow through the non-boron

saturated 3A Deborating Demineralizer, for 10 minutes. At 11:30

p.m., the control room operators noted the control rods were

inserting and discovered the use of the wrong Enclosure. Feed and

bleed via the 3A Bleed Holdup Tank (BHUT) was initiated

immediately to restore previous RCS boron concentration. As a

result of the dilution, the Integrated Control System (ICS)

automatically inserted the control rods from 93.5% to 87.5% on

4

Group 7 (23.2 % on group 7 was the rod insertion limit).

The

total deboration of the RCS was 6 ppm, from 1071 to 1065 ppm.

Utilization of Enclosure 3.16 (Demineralizer 3A) and 3.17

(Demineralizer 3B) is procedurally controlled by initial condition

verification.

Initial Condition Step 1.1 of Enclosure 3.16 to

OP/3/A/1103/04 requires verification that:

"Operations notified

by Chemist that de-lithiation is required with the use of 3A

Deborating Demineralizer." The BOP operator mistakenly

initialed/verified this step and utilized Enclosure 3.16. The

chemist had in fact requested the 3B Deborating Demineralizer,

which was consistent with the Control Room Turnover Sheet. This

matter is identified as Violation 287/94-16-02:

Failure to Follow

Procedure Results in Inadvertent Dilution.of the RCS.

e.

Mid-loop/Reduced Inventory Activities

During the Unit 1 End Of Cycle 15 Refueling Outage, the licensee

reduced RCS inventory and reached the mid-loop operations level on

May 3, 1994, at 9:24 p.m. This was done for the purpose of

removing the steam generator manway covers and installation of

steam generator nozzle dams. The inspectors reviewed the

licensee's program prior to the reduction of RCS inventory and

verified that the requirements were met while operating at the

OP/3/A/1103/11, Draining And Nitrogen Purging Of RC System,

reducedlinventoryr leel As dspecifid inOperations Procedure

5nclosure 3.6, Requirements For Reducing RXV Level To < 50" on LT

5. This procedure stipulated the sequence and steps required for

reduction of RCS inventory and mid-loop operation. It further

specified the precautions and limitations to be adhered to while

in mid-loop.

Step 1 of Enclosure 3.6 specifically addressed the ability to

establish containment closure. The licensee implemented a

Shutdown Protection Plan for the outage which required the

containment to be closed except as necessary to bring materials

and tools in and out of the Reactor Building. It further required

that penetrations be closed except for those with temporary cables

installed for necessary outage activities (e.g., steam generator

tube testing, maintenance, etc.).

In both instances when

containment integrity was not maintained, a plan for quick closure

was addressed.

The requirement for two independent trains of RCS le vel monitoring

was met when operating at reduced inventory. It was accomplished

by the use of one permanently installed instrument (LT-5) and two

temporarily installed ultrasonic instruments for the outage.

Level indications were displayed in the control room on the LT-5

indicator, the Inadequate Core Cooling Monitor, and on the

Operations Aid Computer.

5

The inspector verified that two trains of core exit thermocouples

were available/utilized while at reduced inventory and that two

sources of inventory makeup and cooling were either in use or

available for operation., In addition, the inspector verified that

contingency plans existed to re-power vital busses from available

alternate electrical power supplies in the event of a loss of the

primary source.

During the time that Unit 1 was in a reduced inventory status, the

licensee implemented and maintained the requirements specified for

the condition. The unit exited the mid-loop operating regime on

May 4, 1994, at 6:05 p.m. The unit was in mid-loop operations for

20 hours2.314815e-4 days <br />0.00556 hours <br />3.306878e-5 weeks <br />7.61e-6 months <br /> and 41 minutes. The program was well implemented and the

operation at reduced inventory was accomplished without incident.

f.

Missing Unit 1.Steam Generator Plug

On May 5, 1994, the licensee identified that the rolled tube plug

installed in Steam Generator IB lower tubesheet row 130, tube 89,

was missing. The missing plug was identified during a video scan

of the lower tubesheet. The missing plug was an inconel 600 plug

that was installed during the Unit 1 End of Cycle (EOC) 11

refueling outage in January 1989. The plug was inspected with a

Motorized Rotating Pancake Coil (MRPC) eddy current probe during

the last Unit 1 refueling outage (EOC 14) in December 1992, and no

degradation was observed. The licensee verified by review of a

video tape made of the installation of a nearby rolled plug (row

131, tube 88) that the plug was in place as of December 1992.

The

licensee verified that no other plugs were missing and initiated

plans to search for the missing plug and retrieve it. The plan

included inspecting the 1B steam generator lower bowl drain line,

the Reactor Vessel and the fuel assemblies during core off-load.

On May 10, 1994, during core off-load activities the licensee

identified two pieces of metal on the bottom of Fuel Assembly 57M

located in core location K7. The fuel assembly was transferred to

the Spent Fuel Pool and the pieces of metal were removed from the

fuel assembly and stored in the Spent Fuel Pool.

Video inspection

of the pieces showed that they were definitely part of a tube plug

and that the total length approximated an intact plug. The pieces

were removed from the pool and shipped to Babcock & Wilcox (B&W)

for review and failure analysis.

Licensee activities associated with steam generator inspections

were reviewed by,Region based specialists during the weeks of May

16 and May 23, and licensee activities were found to be

acceptable. These activities are documented in NRC Inspection

Report 269,270,287/94-17. As of the end of this inspection

period, the licensee had not identified the failure mechanism that

resulted in the plug failure.

6

Within the areas reviewed one violation and one apparent violation were

identified. The violation involved an inadvertent dilution of the Unit

3 RCS. The apparent violation involved two examples of failure to

follow refueling procedures.

3.

Maintenance and Surveillance Testing (62703 & 61726)

a.

Maintenance activities were observed and/or reviewed during the

reporting period to verify that.work was performed by qualified

personnel and that approved procedures adequately described work

that was not within the skill of the craft. Activities,

procedures, and work orders (WO) were examined to verify that:

proper authorization and clearance to begin work was given;

cleanliness was maintained; exposure was controlled; equipment was

properly returned to service; and limiting conditions for

operation were met.

Maintenance activities observed or reviewed in whole or in part:

(1) Work Order Task, 94000681-01, Perform OE-5803, Modify ICS

BTU Limit Circuit (Minor Modification).

On May 4, 1994, the inspector reviewed activities in

progress on Unit 1 during the implementation of the minor

modification to simplify the BTU Limits Circuitry that feeds

the Integrated Control System (ICS).

The modification was

to simplify the ICS BTU circuitry by removing the Reactor

Coolant flow and Feedwater temperature inputs to the BTU

limit calculation. The new calculation for BTU limits would

be based on the T-hot and Once Through Steam Generator

(OTSG) outlet pressure inputs only.

The primary purpose of the BTU Limits Circuitry is to alert

the operator of potential BTU limit conditions and assure

rapid runback of feedwater flow following a reactor trip.

The technical basis for the modification was documented in

B & W Document, 12-1175342-00 which determined that only the

T-hot and the OTSG outlet pressure inputs were needed.

The inspector reviewed the licensee's safety evaluation

which determined the modification met acceptable criteria

for implementation. In addition, the work efforts were

reviewed and it was concluded that the activity was

performed per the work instructions and properly documented.

(2) Work Order 94018639-01, Investigate and Repair 3FDW-107.

During the performance of a quarterly stroke test

(PT/3/A/0150/22A), 3FDW-107 did not give a full open

indication. This valve is the Unit 3 "B" steam generator

sample isolation valve, located inside containment. This

normally closed valve is a motor operated containment

7

isolation valve that receives an Engineered Safeguards close

signal. A containment entry was made to investigate the

apparent failure to fully open. The investigation revealed

a problem with mechanical binding within the valve.. Given

the recent problems at Oconee with Limitorque valve torque

switches (see IFI 94-11-02), the inspector observed the

troubleshooting efforts to verify that the problem was not

related to the torque switch. The valve was subsequently

closed and its feeder breaker left tagged in the open

position. The licensee indicated that the valve would be

repaired at the next available outage.

(3) Work Order 94012651-01, Repair ES Analog Channel B Jack.

The inspector reviewed the work order and monitored work in

progress during the implementation of this work activity.

The activity was performed per the work instructions and

properly documented on the work order.

(4) Work Order 94040400-01, Implement Minor Mod OE-6668.

The inspector reviewed the work package and monitored work

in progress during the implementation of this work activity.

Minor Modification OE-6668 was implemented to connect the

neutral side of the Engineered Safeguards (ES) unit control

module latch permissive relays (K1 and K2) to AC neutral

instead of instrument ground as previously configured. This

modification was implemented to correct a problem identified

during component ES testing (see paragraph 4.b).

The work

activities observed were performed in accordance with

approved procedures and properly documented in the work

package.

b.

Surveillance activities were conducted with approved procedures

and in accordance with site directives. The inspectors reviewed

surveillance performance as well as system alignments and

restorations. The inspector assessed the licensee's disposition

of discrepancies which were identified during the surveillance.

Surveillance activities observed or reviewed in whole or in part:

(1) Work Order Task 93081903-01, Perform Test On CT-1 Relays.

On May 12, 1994, the inspector reviewed performance testing

of the CT-i relays that are utilized in the electrical power

,transfer to the startup busses upon loss of the normal

feeder busses. The testing was part of the Unit 1 refueling

outage scheduled activities to be performed while the

reactor was defueled. Some minor discrepancies were noted

in the step signoff sequence in that more than one step in

the instructions had been performed prior to the craftsmen

8

signing for the work completion. After the inspector

identified the discrepancy, immediate corrections were made.

(2) Turbine Driven Emergency Feedwater (TDEFW) Pump Cooling

Water Supply Valve Test (PT/3/A/0150/22L).

This quarterly test verifies cooling water supply to TDEFW

pump cooling jackets and oil coolers. The inspector

observed portions of the test conducted on the Unit 3 TDEFW

pump on May 12, 1994.. The test revealed that the stroke

times for 3LPSW-138 (cooling water supply to pump jacket),

and 3HPSW-184 (cooling water supply to pump oil cooler) were

not within the acceptance criteria (1-2 seconds for both

valves). The stroke time observed during this test was 4

seconds for both valves. 3LPSW-138 and 3HPSW-184 are

pneumatically operated valves that are designed to fail open

following a loss of power or loss of instrument air. These

valves are normally closed and are designed to open

automatically following a pump start. As a result of the

slow stroke times, the licensee declared these valves

inoperable per their Inservice Test (IST) program. The

switch that manually controls both valves was subsequently

placed in the bypass position. This failed open both

valves; thereby, establishing continuous cooling water flow

through the pump jacket and oil cooler. The licensee stated

that this arrangement resulted in the TDEFW pump being

operable, despite the valves being inoperable, since the

valves were in their "fail safe" position.

The inspector noted that the licensee did not perform a

10 CFR 50.59 or other formal engineering evaluation for this

abnormal lineup. However, OP/0/A/1102/06, Removal and

Restoration of Station Equipment, was used to remove the

control switch from its normal position. This

required/resulted in an evaluation of the impact on plant

equipment by two licensed individuals, one of which held a

senior reactor operator license. The inspector questioned

whether continuous flow of relatively cool water through the

idle pump and oil cooler might result in increased moisture

in the oil.

Oil samples taken on May 16, revealed that

moisture levels had not increased. The licensee

subsequently performed numerous stroke tests of these valves

to determine if the stroke times were degrading. The.valves

consistently stroked at 2.5 seconds. On May 26, after

changing the stroke time acceptance criteria to 1-4 seconds

the licensee declared the valves operable and restored them

to their normal (closed) status. The inspector concluded

that there was no impact on TDEFW pump operability, nor a

design basis issue associated with extending the stroke time

acceptance criteria.

9

(3) High Pressure Injection (HPI) Pump Run-Out Test

(TT/1/A/251/41).

This temporary test procedure was conducted to verify that

the flow resistance in the HPI system piping was sufficient

to prevent the HPI pumps from reaching a pump run-out

condition when the injection valves were completely open and

RCS pressure was at 0 psig. The normal pump run-out flow

value is 525 gpm, but the licensee has received concurrence

from the pump vendor that flow rates up to 585 gpm are

acceptable if Net Positive Suction Head (NPSH) available is

greater than 30 feet of head. The licensee takes credit for

throttling HPI flow within ten minutes following an accident

to ensure HPI flows are balanced.

The test consisted of running each HPI pump individually and

measuring injection flow and minimum recirculation flow with

the respective HPI valve fully open. Pump vibration data

was monitored throughout the test and if vibration levels

exceeded 0.75 in/sec the pump was to be immediately secured.

The A, B, and C HPI pumps developed approximately 545 gpm,

562.5 gpm and 562 gpm respectively with the injection valves

fully open. Vibration levels remained below 0.75 in/sec.

The inspector noted that the reactor coolant pump seal

injection flow path and the normal makeup flowpath were

isolated during the performance of the test. These

flowpaths would normally be open during an accident and

would decrease system resistance in the A injection header

and would affect the pump run-out flows for the A and B HPI

pumps. This item was discussed with the accountable

engineer and he stated that the test was for data

acquisition and that the possible affect on delivered flow

would be reviewed by Design Engineering. The inspectors

plan to review this item further after the licensee

evaluation is completed. This is identified as Inspector

Followup Item 269/94-16-04: HPI Pump Run-out Flow Testing.

The inspectors reviewed the test procedure and witnessed the

entire testing sequence for all three HPI pumps. The

licensee plans to perform this special test on both Units 2

and 3 during the next scheduled refueling outages.

(4) SSF Service Water Test with ASWP, HVAC Pump, and DESWP

Running Simultaneously (TT/O/A/600/12).

The purpose of this temporary test procedure was to

demonstrate and document the ability of the Safe Shutdown

Facility (SSF) service water piping to provide adequate

suction pressure and flow while the SSF auxiliary service

water pump (ASWP), SSF HVAC pump, and diesel engine service

water pump were running simultaneously. The test was

conducted with the Unit 2 Condenser Circulating Water (CCW)

system in service and supplying suction to the SSF service

water systems. Under SSF conditions the Unit 2 CCW system

would not be operating. Discussions with the system

engineer determined that plans were being established to

reperform this test during the next Unit 2 refueling outage

when the CCW system could be secured so that actual system

conditions could be verified.

The procedure established a minimum suction pressure of 5

psig for the ASWP and the DESWP, and 2 psig for the HVAC

pump. The minimum suction pressure observed during the test

was 21.8 psig. The inspectors reviewed the test procedure

and witnessed the performance of the entire test.

(5) Turbine Stop Valve Movement (PT/O/A/290/04).

This is a monthly test to verify the proper operation of the

Main Steam Stop Valves (MSSVs) and Intercept Valves. The

inspector observed the test for Unit 3 conducted on May 19,

1994.

No discrepancies were noted.

No violations or deviations were identified. One IFI was identified

regarding the system lineup during a HPI pump run-out test.

4.

Onsite Engineering (37551)

During the inspection period, the inspectors assessed the effectiveness

of the onsite design and engineering processes by reviewing engineering

evaluations, operability determinations, modification packages and other

areas involving the Engineering Department.

a.

Design Basis Documentation Issues Associated With Reactor Building

Spray.

On Mayp17, 1994, the inspector observed the Reactor Building Spray

(RBS) pump test (PT/3/A/0204/O7) for Unit 3.. As part of this

activity the inspector reviewed various design basis documents to

evaluate how well this test verified that the RBS system performed

its design basis functions. The inspector noted that Section

6.1.3 of the Oconee Final Safety Analysis Report (FSAR) stated, in

part, that the NPSH available to the Low Pressure Injection and

RBS pumps during the post-LOCA recirculation phase has been

calculated based on three feet of level remaining in the BWST at

time of switchover, and water level in the Reactor Building of 6.5

feet above basement level.

It further indicated that based on the

6.5 foot water level, there would be 19.8 feet of NPSH available

to the RBS pumps (only slightly greater than the pump

manufacturers required NPSH of 17.0 feet)..

the inspector noted that this conflicted with step 14.0 of section

CP-601 of the Emergency Operating Procedure (EOP) which instructed

the operators to swap RBS suction to the Reactor Building

Emergency Sump when BWST level was less than 6 feet, and RB level

was greater than 3.5 feet. The licensee's Design Basis

Specification for the Reactor Building Spray System (OSS-0254.00

00-1034) also stated that the minimum reactor building level

setpoint was 3.5 feet.

When questioned about the apparent discrepancy between the FSAR

and the EOP, the licensee stated that the information in Section

6.1 of the FSAR was inaccurate, and that it would be corrected

during the next update to the FSAR.

In responding to the inspector's questions regarding the basis for

the EOP's guidance for swapover (BWST level < 6 ft, and RB level >

3.5 ft), the licensee provided OSC-2820, Emergency Procedure

Guideline Setpoints, which indicated that a reactor building level

of at least 3.75 feet was necessary to ensure adequate RBS pump

NPSH. This was different from both the EOP & DBD (3.5 ft) and the

FSAR (6.5 ft).

In fact, revision 3 to OSC-2820, dated July 17,

1989, specifically changed the setpoint for swapover from 3.5 to

3.75 feet. Both the licensee and the inspector were unclear as to

what the actual requirement was for minimum sump level to ensure

adequate NPSH for the RBS pumps, or if the EOP guidance was

adequate. Shortly thereafter, the licensee concluded that the

current EOP guidance was acceptable due to the fact that an

injection of BWST water into the RB which reduces BWST level below

6 feet, assuming an initial level of at least 46 feet (TS

requirement), would ensure at least 5 feet of RB water level.

Based on independent calculations, the inspector agreed with this

assessment for immediate EOP acceptability. However, the

inspector was concerned that a revision to the licensee's

procedure for EOP setpoints which specifically changed a setpoint

was not incorporated into the EOP, and that this was not realized

by the licensee until questioned by the NRC approximately 5 years

later.

Given the many conflicting references, the inspector concluded

that there were shortcomings in the licensee's program for

maintaining their design basis documentation for the RBS system.

The licensee should determine the actual minimum RB water level

necessary to ensure adequate NPSH for the RBS pumps, and adjust

their documentation accordingly.

b.

Engineered Safeguards (ES) Wiring Discrepancies

On May 20, 1994, during the performance of ES functional testing

on valves 1PR-8 and 1PR-10 the licensee found that with an ES

signal present, manual control of the valves could not be achieved

using the manual pushbutton on the RZ module located on the

vertical board in the control room. The ES testing of 1PR-8 and

1PR-10 was being conducted as part of a post modification test

requirement for minor modification OE-6338. The licensee reviewed

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all wiring changes performed per the minor modification and

determined that the inability to take manual control from the RZ

module under ES conditions was not related to the implementation

of the minor modification. A troubleshooting work order was

initiated to identify and correct the problem.

Subsequent investigation by the licensee determined that the

manual control relays inside the ES cabinets' unit control modules

were connected to the instrument ground system and that the

electrical circuit for manual control after an ES actuation relied

on the instrument ground system, through the station ground

system, through the regulated power panelboard 1KRA neutral

conductor, to the 120 volt vital power inverters' neutral

conductor. The Unit 1 vital inverters and manual bypass switches

had been replaced earlier in the current outage per modification

NSM-ON-12881. This modification had replaced the single pole

bypass switch with a double pole bypass switch. The double pole

design switches both the hot wire and the neutral wire between the

vital inverter and the regulated power supply, whereas the old

single pole switch only switched the hot wires and a common

neutral was maintained between the vital inverters and the

regulated power supply. With the vital inverters in service

following the vital inverter modification, the electrical circuit

for manual control following an ES signal was defeated. The

licensee plans to modify the Unit 1 Engineered Safeguards

electrical circuitry to correct this deficiency prior to

completion of the Unit 1 refueling outage. The licensee planned

to connect the manual control relays to the vital 120 VAC neutral

wire to ensure that an electrical circuit could be achieved.

The licensee performed an operability evaluation on the present

Unit 2 and 3 Engineered Safeguards systems. The Unit 2 and 3

systems still contained single pole bypass switches and relied on

a common neutral wire, instrument ground system, and station

ground system to establish an electrical circuit. The instrument

ground system, station ground system, and regulated power supply

system were not considered safety-related and the electrical

circuit relied on a common electrical cable in several locations

to maintain an electrical circuit for manual control of ES

components following an ES actuation.

The licensee determined that the Unit 2 and Unit 3 ES systems were

operable based on the fact that the grounding system was a passive

system and no credible single failure could be postulated for any

design basis events.. The licensee's operability evaluation was

13

still under NRC review at the end of the inspection period and is

identified as Unresolved Item 269,270,287/94-16-03: Engineered

Safeguards Wiring Discrepancies.

No violations or deviations were identified. One Unresolved Item

regarding Engineered Safeguards neutral and ground wiring arrangements

was identified.

5.

Plant Support (71750)

The inspectors assessed selected activities of licensee programs to

ensure conformance with facility policies and regulatory requirements.

During the inspection period, the following areas were reviewed:

a.

Combustible Material In The Reactor Buildings

The inspectors toured the Unit 1 reactor building on May 5, 1994,

during the refueling outage. At this time, less than 100 bundles

of fuel had been removed from the reactor core. The inspectors

noted that large amounts of non-flame retardant plastic had been

used to cover equipment and other plant items for protection

during containment decontamination and had remained after

decontamination was completed. In addition, it was noted that

rolls of the plastic material were stored in the building and

there was no apparent control over the location or amount allowed.

A violation (VIO 287/93-31-03) was issued by the NRC for use of

non-fire retardant plastic in the Unit 2 penetration room in

December 15, 1993. The use of this material in the unit 3 Reactor

Building was questioned during the previous Unit 3 refueling

outage and the inspectors learned that fire loading in the Reactor

Building was not addressed in the site directives. As a result,

Oconee Nuclear Site Directive 3.2.7, Control Of Combustible

Materials, was revised. Step 12.7 of the revised directive

addressed specific areas of the Reactor Building necessary for

cables and equipment important for decay heat removal and required

that the Reactor Building Coordinator or designee monitor and

control the use of combustibles in those areas through periodic

inspections.

Although the directive did not limit the use of combustible

materials in the Reactor Building, or require an evaluation for

the use of this material, the licensee agreed that the amount

appeared excessive and the fire loading was reduced to a much

lower level.

b.

Maintenance Chemicals With Wintergreen Odor

The inspector detected the smell of wintergreen during a tour of

the turbine building on May 12, 1994. Wintergreen odor is

utilized in the Carbon Dioxide and Halon fire protection systems

at Oconee to alert personnel in those areas of an actuation of the

14

system. After the inspector exited the area and notified the

control room of the odor, he learned that plant maintenance

utilized a chemical with this odor to assist in loosening bolts.

The inspector questioned the use of this chemical for maintenance

activities given that the licensee plant systems training course

emphasized the specific use of wintergreen in the carbon dioxide

and halon fire protection systems as a warning device for system

activation. The licensee agreed that the use of chemicals with

wintergreen odor for other than fire protection would defeat the

original purpose for detecting a carbon dioxide or halon release.

The licensee subsequently discontinued the use of wintergreen odor

in the plant with the exception of the fire protection system.

No violations or deviations were identified.

6.

Review of Licensee Event Reports (92700)

The below listed Licensee Event Reports (LER) were reviewed to determine

if the information provided met NRC requirements. The determination

included: adequacy of description, compliance with Technical

Specification and regulatory requirements, corrective actions taken,

existence of potential generic problems, reporting requirements

satisfied, and the relative safety significance of each event. The

following LER is closed:

a.

(Closed) LER 270/93-04, Emergency Feedwater Required Technical

Specification Surveillance Interval Exceeded Due To Management

Deficiency.

The licensee identified that the required surveillance for the

initiating circuitry for the Unit 2 Motor Driven Emergency

Feedwater (MDEFW) pumps had not been performed in the time

interval required by the Technical Specification.

The problem was

identified on August 23, 1993,' with the unit at 100 percent power.

The time allowed by the surveillance had been exceeded by 28 days.

As a result, the surveillance was immediately performed with

satisfactory results.

The licensee determined that the deficiency had occurred as a

result of placing the surveillance in the "suspend" mode at the

time the test was due. It was further determined that the

personnel involved believed that once the test was in the suspend

mode, the computer program would reschedule the test prior to

exceeding the Technical Specification time limit. However, the

program did not have this feature, and therefore,' the surveillance

was not rescheduled. This resulted in the failure to perform. the

work within the required time period with a 28 day over-run.

The licensee's corrective action was to revise Maintenance

Directive 7.3.6, Preventative Maintenance Program, step 5.5.4,

Suspending Or Deferring a Predefined Work Order, -to require an

15

engineering evaluation for suspending work orders that cannot be

performed within the allowable time frame.

The inspectors reviewed the licensee's documentation that the

surveillance was performed, reviewed the revised Maintenance

Directive, and verified that the commitment was properly

implemented.

No violations or deviations were identified.

7.

Exit Interview

The inspection scope and findings were summarized on June 2, 1994, with

those persons indicated in paragraph 1 above. The inspectors described

the areas inspected and discussed in detail the inspection findings

addressed in the summary and listed below. The licensee did not

identify as proprietary any of the material provided to or reviewed by

the inspectors during this inspection.

Item Number

Description/Reference Paragraph

50-269/94-16-01

Apparent Violation:

Failure to Follow

Refueling Procedures -

two examples

(paragraph 2.c).

50-287/94-16-02

Violation: Failure to Follow Procedure

Results in Inadvertent Dilution of the RCS

(paragraph 2.,d).

50-269,270,287/94-16-03

Unresolved Item:

Engineered Safeguards

Wiring Discrepancies (paragraph 4.b).

50-269/94-16-04

Inspector Followup Item:

HPI pump run-out

flow testing (paragraph 3.b.(3)).