ML16154A568

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Insp Repts 50-269/94-01,50-270/94-01 & 50-287/94-01 on 940102-29.Violation Noted.Major Areas Inspected:Plant Operations,Surveillance Testing,Maintenance Activities & Engineering & Technical Assistance
ML16154A568
Person / Time
Site: Oconee  
Issue date: 02/16/1994
From: Harmon P, Lesser M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML16154A564 List:
References
50-269-94-01, 50-269-94-1, 50-270-94-01, 50-270-94-1, 50-287-94-01, 50-287-94-1, NUDOCS 9402280114
Download: ML16154A568 (14)


See also: IR 05000269/1994001

Text

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UNITED STATES

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NUCLEAR REGULATORY COMMISSION

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REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report Nos.:

50-269/94-01, 50-270/94-01 and 50-287/94-01

Licensee:

Duke Power Company

422 South Church Street

Charlotte, NC 28242-0001

Docket Nos.: 50-269, 50-270, 50-287, 72-4

License Nos.:

DPR-38, DPR-47, DPR-55, SNM-2503

Facility Name:

Oconee Nuclear Station

Inspection Conducted: January 2 - January 29, 1994

Inspector:

a

-'

/O

P. E. Hafmon, Senior Resident Inspector

Date Signed

W. K. Poertner, Resident Inspector

1. A. Keller, Resident Inspector

P. G

umphrey, Resident Inspector

Approved by:"

M. S. Lesser, Section Chief,

Date Signed

Reactor Projects Section 3A

SUMMARY

Scope:

This routine, resident inspection was conducted in the areas of

plant operations, surveillance testing, maintenance activities,

and engineering and technical assistance. Activities were

monitored during the Unit 3 End of Cycle 14 refueling outage.

Results:

One violation was identified, which involved inadequate procedures

controlling steam generator tube plug processes. Due to

inadequate installation, 14 tube plugs separated from their

respective tubes and were later recovered during refueling

operations (paragraph 2d).

Two Unresolved Items were identified. One URI involved improperly

sized orifice plates installed in High Pressure Injection lines

(paragraph 2c).

The second URI involved a temporary loss of power

to Unit 3 during refueling activities (paragraph 3).

Refueling activities continued on Unit 3. The resident staff

witnessed several major maintenance and modification activities

and in general considered these activities to be well planned and

executed.

9402280114 940217

PDR ADOCK 05000269

PDR

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

  • B. Peele, Station Manager

S. Benesole, Regulatory Compliance Manager

D. Coyle, Systems Engineering Manager

J. Davis, Engineering Manager

  • B. Dolan, Safety Assurance Manager

W. Foster, Superintendent, Mechanical Maintenance

J. Hampton, Vice President, Oconee Site

D. Hubbard, Component Engineering Manager

C. Little, Superintendent, Instrument and Electrical (I&E)

  • D. Patterson, Regulatory Compliance
  • S. Perry, Regulatory Compliance
  • G. Rothenberger, Operations Superintendent

R. Sweigart, Work Control Superintendent

Other licensee employees contacted included technicians, operators,

mechanics, security force members, and staff engineers.

NRC Resident Inspectors

  • P. Harmon
  • W. Poertner
  • L. Keller
  • G. Humphrey

NRC Personnel

  • K. Kavanagh
  • Attended exit interview.

On January 21, 1994, the Chairman of the NRC conducted a routine visit

to the site, and held a press conference to discuss items of interest

with the local media. The Regional Administrator, Region II,

accompanied the Chairman on his tour and was also onsite to meet with

licensee management, and resident inspectors.

2.

Plant Operations (71707)

a.

General

The inspectors reviewed plant operations throughout the reporting

period to verify conformance with regulatory requirements,

Technical Specifications (TS), and administrative controls.

Control room logs, shift turnover records, temporary modification

log and equipment removal and restoration records were reviewed

routinely. Discussions were conducted with plant operations,

2

maintenance, chemistry, health physics, instrument & electrical

(I&E), and engineering personnel.

Activities within the control rooms were monitored on an almost

daily basis.

Inspections were conducted on day and night shifts,

during weekdays and on weekends.

Inspectors attended some shift

changes to evaluate shift turnover performance. Actions observed

were conducted as required by the licensee's Administrative

Procedures. The complement of licensed personnel on each shift

inspected met or exceeded the requirements of TS. Operators were

responsive to plant annunciator alarms and were cognizant of plant

conditions.

Plant tours were taken throughout the reporting period on a

routine basis. During the plant tours, ongoing activities,

housekeeping, security, equipment status, and radiation control

practices were observed.

b.

Plant Status

Units 1 and 2 operated at 100 percent power throughout the

inspection period. Unit 3 .remained shutdown the entire reporting

period for a scheduled refueling outage.

c.

Unit 3 High Pressure Injection Orifice

On January 15, 1994, the licensee identified that the normal and

emergency injection pressure breakdown orifice in the 3B2

injection line was a 7/8 inch (.875 inch) diameter orifice versus

a .78 inch diameter orifice as documented in the system flow

diagrams and design calculations. The increased orifice size

would result in HPI flows in excess of calculated flow rates and

could potentially result in pump runout concerns under certain

design events or reduced flow rate into the RCS assuming a failure

of an injection line.

The incorrect orifice was identified by the system engineer during

maintenance activities to correct a leaking flange connection.

The system engineer had questioned the higher flow rates seen on

the Unit 3 high pressure injection (HPI) full flow tests when

compared to the Unit 1 and 2 tests and decided to inspect the

orifice during the scheduled maintenance activity. The licensee

completed inspection of the three other orifice plates on Unit 3

and found that they were also 7/8 inch orifice plates. The

licensee was still reviewing this item at the completion of the

inspection period and had not completed an operability evaluation.

This item is identified as Unresolved Item 287/94-01-01:

Improperly Sized HPI Orifice Plates.

3

d.

Steam Generator Tube Plugs Found in Unit 3 Reactor Vessel

On January 9, 1994, while performing a post-defueling video.camera

inspection of the Unit 3 reactor vessel, the licensee discovered.

eight steam generator tube plugs on the lower grid assembly of the

reactor vessel.

During the previous operating cycle there were no

indications of higher primary-to-secondary leakage, Loose Parts

Monitor alarms, or any other indications that tube plugs had

separated from the steam generator tubesheet(s) and entered the

RCS. -Subsequent steam generator inspections revealed that there

were 14 missing tube plugs from the bottom head of the 3B Once

Through Steam Generator (OTSG).

The 14 missing tube plugs were

all part of a single batch of Inconel-690 rolled plugs installed

during the previous Unit 3 refueling outage by the Babcock &

Wilcox Nuclear Service Company (BWNS). -A review of the audio and

video records of the installation of this batch of tube plugs,

conducted by BWNS, indicated that there were 33 plugs (including

the 14 missing plugs) which may not have received the proper

torque value. Proper torque assures adequate expansion of the

plug in the steam generator tube. BWNS also reviewed all the

available tapes for Steam Generator 3A and the Unit 1 & 2 steam

generators for plugs that were installed during their last

refueling outages. Only one additional questionable tube

installation was identified. This was-located in the upper

tubesheet of Steam Generator 2B.

BWNS utilized a remote air motor control roll process to install

the tube plugs in question. The tool used in.this process was a

"ROGER" (Remotely Operated Generator Examination and Repair) roll

tool.

The ROGER roll expansion tool consisted of a torque

controlled air motor which drove the mandrel of the roll expander.

When operating properly, the amount of torque delivered to the

tube plug is achieved by adjustment of a clutch within the air

motor assembly. Upon reaching the target torque, the clutch

mechanism closes a valve within the air motor. When this valve

closes, supply air will not enter the vanes of the air motor and

the air motor turns off.

A device called the flow verification assembly was used to monitor

the air flow (by use of a rotameter) and air pressure (using a

pressure gauge) to the air motor. The rotameter was used to

ensure the air motor reached the target torque and did not stop

due to stalling out. When the target torque was reached and the

clutch mechanism turns off the air supply to the air motor, the

flow of air through the flow verification assembly stops, and the

rotameter stops rotating. If the rotameter continues to rotate,

then the air motor has stalled and the proper torque is not

assured.

The flow verification assembly also monitors the air pressure

delivered directly to the input of the air motor. This air

4

pressure is also monitored during the expansion process. The air

pressure corresponding to the proper torque is determined during

the calibration of the tool which is done prior to rolling any

plugs.

During the roll expansion process, the air pressure will

read a dynamic level, usually 5 to 10 psi below the static air

pressure. Upon reaching torque-out, the air pressure will

increase back to the static pressure and remain there for

approximately 3 seconds when the control computer shuts off the

air supply to allow retraction of the tool.

Monitoring of the flow verification assembly to assure proper

torque-out should have been done by the tooling operator during

the installation process. As stated above, proper torque-out is

assured when correct air pressure is indicated on a gage and zero

air flow is indicated by a rotameter, on the air flow verification

assembly. Video tapes of the installation of the 33 tubes in

question revealed that the pressure gauge on the air flow

verification assembly went to zero prematurely, following cut-out

of the air motor. Additionally, the characteristic sound of

proper torque-out could not be heard, and the roll times were

considerably shorter for these plug installations.

The faulty installation of tube plugs in Steam Generator 3B

occurred during a single shift by one crew. This crew installed a

total of 52 plugs in the lower head of the Steam Generator 3B

during this shift, of which 33 did not receive proper torque-out.

According to.BWNS, the individuals who performed the plug

installations had received all required training for this process

and were considered to be fully qualified to perform this task.

The controlling procedure for this activity did not provide

appropriate acceptance criteria for determining that proper torque

out was achieved, independent verification accomplished or QC

verification that proper torque-out was achieved. Furthermore,

the video tapes were not reviewed by licensee or BWNS personnel

following the activity to verify proper torque-out. Steam

generator tube plugging is an activity that is important to safety

both from the aspect of tube integrity and preventing debris

hazards to the reactor coolant system. The inspectors concluded

that the lack of independent verification and procedural guidance

to determine proper torque-out was inappropriate and resulted in

the failure to identify improperly installed steam generator tube

plugs. This matter is identified as Violation 287/94-01-02:

Inadequate Procedure for Steam Generator Tube Plugging Activities.

All 14 missing plugs were recovered. Two of these plugs were

found trapped in the lower end fittings of fuel assemblies. The

14 missing plugs and the remaining questionable plugs for Steam

Generator 3B were replaced. The questionable plug in the upper

tubesheet of Steam Generator 2B will be replaced during the next

Unit 2 refueling outage.

5

d.

Plant Tours

During a tour of the Unit 3 Reactor Building on January 7, 1994,

the inspector noted that large amounts of plastic had been used to

bag mirror insulation during the outage, 3EOC14. The insulation

had been removed from systems for work during the outage and was

inserted in plastic bags to avoid the spread of contamination.

However, the plastic material did not appear to be fire retardant.

Oconee Nuclear Site Directive 3.2.7, Control of Combustible

Materials, was reviewed to evaluate the licensee's program to

control fire loading in the reactor building. The inspector could

not find where the directive specifically addressed the fire

loading requirements in that area. The licensee confirmed that

fire loading in the reactor building was not addressed in the site

directives or procedures.

The licensee later informed the inspector that the omission of

fire loading requirements for the reactor building was being

corrected through a revision to the site directive. Based on the

licensee's corrective actions, this issue will not be opened as an

item for tracking.

f.

Condenser Circulating Water (CCW) Piping Seismic Interactions

On January 18, 1994, the licensee identified a potential piping

interaction in which the CCW pump discharge vents could be damaged

in a seismic event by the metal restraints placed around the CCW

intake piping to stabilize the lines while the piping is

unwatered. The licensee commenced to increase Keowee lake level

to above 798.1 feet to ensure gravity flow would be available to

supply suction to the Low Pressure Service Water Systems until an

evaluation could be completed to determine the seismic adequacy of

the piping configuration. In parallel with these actions the

licensee initiated exempt changes to modify the piping restraints

to increase the clearance such that adequate clearance would be

maintained during a seismic event. The licensee completed the

exempt changes to the Unit 1 and 2 CCW systems at 5:00 p.m. on

January 19, 1993. The licensee plans to modify the Unit 3 CCW

restraints prior to completion of the Unit 3 refueling outage.

This item was identified during the initiation of the problem

investigation process (PIP) to resolve drawing discrepancies in

the CCW system flow diagrams identified by the system engineer.

As a result of the PIP process, the seismic adequacy was also

questioned. The licensee had not completed the past operability

evaluation at the end of this reporting period. The inspectors

plan to review this item further after the operability evaluation

has been completed.

6

Within the areas reviewed, one violation for inadequate procedural

guidance for steam generator tube plugging activities, and one URI

concerning improperly sized HPI orifice plates were identified.

3.

Unit 3 Loss of Power to the Main Feeder Buses

At approximately 2:06 p.m., on January 27, 1994, Unit 3 experienced a

loss of electrical power to the main feeder buses (MFBs) which lasted

for approximately 21 seconds, due to PCB-59 inadvertently opening. This

resulted in a subsequent load shed of the non-vital loads from the Unit

3 MFBs. Approximately 21 seconds after the MFBs were deenergized, the

El breaker closed and energized the number 1 MFB via the startup

transformer. This action also energized the number 2 MFB since the MFBs

were connected through the ES switchgear they supplied.

The unit was in cold shutdown with all fuel offloaded to the spent fuel

pool.

The spent fuel cooling pumps were load shed during this event.

Power was restored to the spent fuel cooling pumps after approximately 4

minutes. There was no increase in spent fuel temperature. Both Keowee

units started as expected but did not tie onto the MFBs because the

buses were reenergized from the startup transformer path via the El

breaker. Units 1 and 2 were unaffected by this event.

Prior to the loss of power-event, power was being provided to the Unit 3

MFBs through the normal source breakers (NI and N2) by backfeeding

through the generator main transformer (3T) from the 525 KV switchyard

via PCB-59. A preventive maintenance activity which involved replacing

terminal strip lugs inside the number 4 Main Steam Stop Valve (MSSV)

power cabinet was ongoing. A terminal lug was inadvertently grounded

which created enough ground fault current to pick up the loss of load

relay (62GX/3), in the same 125 Vac circuit as the stop valve lugs.

Picking up the loss of load relay caused PCB-59 to open (per design).

The control room supervisor who approved the Work order (94007093- 01)

stated that he was unaware that this activity had the potential to pick

up the loss of load relay. As of the end of the inspection period,.the

adequacy of the work control process for this activity was still under

review. This matter is identified as Unresolved Item 287/94-01-03:

Maintenance Activity Results in Loss Of Power.

Within the area inspected no violations were identified.

4.

Maintenance and Surveillance Testing (62703), (61726)

a.

CCW Relay Replacement (Work Order 9400122 02)

The inspector witnessed work in progress during the changeout of

Control Relay, CCWPX2B. The changeout was a result of relay

overheating caused by a contact that did not open when required.

The work was performed per Work Order Task 9400122 02 which

implemented a special temporary instruction for the activity,

7

TI/2/1/3000/14, Temporary Instruction and Electrical Procedure To

Repair Damage Caused By Failed Coil For CCWPX2B.

The relay that was in.the CCW control circuitry affected all of

the Oconee Condenser Circulating Water Systems. To avoid a

potential loss of the normal water flows to the units, the relay

was replaced without de-energizing the circuit. This required

close co-ordination with the operations personnel and detailed

instructions for the activity.

The inspector reviewed the work activity and the required post

maintenance testing, and determined that the activity had been

carefully planned and implemented.

b.

Control Rod Drive System Test (OP/O/A/1105/09)

On January 6, 1994, the inspector witnessed operator performance

of test, OP/O/A/1105/09, Control Rod Drive System. The purpose of

the test was to verify transfer of control rod power between the

"normal" and "auxiliary" power supplies while on-line. The test

was performed in conjunction with PT/O/A/600/15, Control Rod

Movement, to verify operability of the rods with power from each

supply.

During the test, computer indication for rod Number 9 in Group 4

did not respond to the rod movement and as a result a work request

was initiated. However, rod movement was verified on the

indicating meter.

The inspector determined that the test had been properly

authorized, was performed in accordance with the procedures, and

the activities were documented as required.

c.

Calibration of LT-97 (Work Order 93057524 01)

Implementation of activities described in Work Order Task 93057524

were reviewed by the inspector on January 4, 1994.

The work

effort consisted of calibration of Differential Pressure

Transmitter LT-97. The equipment is utilized for measuring the

level in Flash Tank 3C2 and was calibrated per procedure

.IP/O/B/275/11A.

The inspectors determined the work performance and documentation

was in accordance with the applicable procedures.

d.

Turbine Driven Emergency Feedwater Test (PT/2/A/600/12)

In progress testing of the Unit 2 Turbine Driven Emergency

Feedwater Pump was observed by the inspector. The test was

performed to demonstrate operability of the pump as required by

the Technical Specifications ( TS Sections 3.4, 4.0.4, and 4.9.).

8

At the beginning of the test, an excessive amount of steam was

being emitted from the drain line. The system engineer determined

the steam was a result of condensation that had accumulated in the

steam header prior to the pump start. The steam emission stopped

as the pump continued to operate.

In addition, a cooling water leak was observed on the outboard

pump bearing. A maintenance request was made to repair the leak.

The packing was tightened which corrected the leak problem.

The inspector determined that the testing activity was performed

in accordance with the procedure and deficiencies identified were

properly dispositioned.

e.

EPSL Startup Source Voltage Sensing Circuit Test (PT/3/A/0610/01B)

This test verified proper operation of the Emergency Power

Switching Logic (EPSL) undervoltage sensing circuitry for 4160

Volt Startup Source (CT-3), proper operation of the Unit 3 Startup

Breaker Anti-Recycle (STAR) logic, and tested the contact

development for the new relays installed under TN/3/A/2886/0/0.

The test was completed satisfactorily indicating the equipment

operated as designed. The inspector noted good procedural

compliance and good communications between the technicians in the

field and the control room operators.

f.

Condenser Circulating Water Pump Discharge Pressure Test

(PT/1/A/0261/09)

The inspector reviewed PT/1/A/0261/09, Condenser Circulating Water

Pump Discharge Pressure Test, which was performed on January 26,

1994. The stated purpose of this test procedure is to demonstrate

the operability of the condenser circulating water pumps. The CCW

pumps were operated in various pump combinations and the discharge

pressures were recorded. The CCW pumps are considered operable if

recorded discharge pressures are greater than 3.48 in. HG on the

header with two CCW pumps operating. The test reviewed by the

inspector was the initial performance of the procedure and was not

a technical specification required test. The test was written as

a result of isolating the continuous vacuum priming system to the

CCW intake. The acceptance criteria was based on a design

engineering calculation that determined that 3.48 inch HG would

maintain air in solution and prevent air accumulation in the CCW

intake piping that could adversely affect operation of the

emergency condenser cooling water system.

The pressure values recorded met the acceptance criteria stated in

the test procedure. However, the acceptance criteria did not

account for operation at lower lake levels. The licensee has

established administrative limits for lake levels based on CCW

pump combinations required to maintain pressure above 3.48 inch

HG. The administrative limit for three CCW pump operation is 789

9

feet. The lake level at the time the test procedure was performed

was 797.49 feet. This item was discussed with the system engineer

and he agreed to review the acceptance criteria to determine if

normalizing the pressure indications would be appropriate.

g.

Convert 3B CST Pump to Mechanical Seals (Work Order 92014350)

Implementation of activities described in Work Order 92014350 were

reviewed by the inspector. The work effort observed consisted of

reinstalling Condensate Storage Tank Pump 3B after converting the

pump to mechanical seals as opposed to packing.

The inspectors found the work performance and documentation to be

in accordance with the applicable procedures. The inspectors did

note that the work activity was designated as non-QA. The

Condensate Storage Tank can be used as a water source to makeup to

the Upper Surge Tanks and is addressed in the Technical

specifications. The inspectors are reviewing the design

requirements of the emergency feedwater suction supplies and the

water volumes required by the TS. This item will be reviewed in

further resident inspection reports.

h.

Reactor Coolant Leakage Verification (PT/1/A/600/10)

The inspector reviewed the performance of procedure PT/1/A/600/10

conducted on January 24, 1994.

The procedure verifies reactor

coolant system (RCS) unidentified leakage was less than 1 gpm

(assuming .5 gpm evaporative losses) and calculated total combined

RCS leakage to verify operability of the Standby Shutdown Facility

Reactor Coolant Makeup Pump. The inspectors questioned the

enclosure used to calculate total combined RCS leakage in that the

enclosure did not take into account the assumed .5 gpm evaporative

loss included in the unidentified leakage calculation. The

licensee reviewed the item and revised the enclosure to account

for evaporative losses. The revision was considered an

enhancement of the procedure.

Within the areas reviewed, licensee activities were satisfactory and no

violations were identified.

5.

Engineering (71707)

Modification of Unit 3 EPSL to Automatically Close Standby Breakers in

the Event Startup Breakers Fail to Close (TN/3/A/2886/0/0):

Prior to this modification, the Emergency Power Switching Logic (EPSL)

would not automatically close the standby breakers if both startup

breakers failed to close while there was adequate voltage present at the

startup transformer. This modification installed a relay (3SBC3A,

3SBC3B) in each channel of EPSL, which is energized whenever both

startup breakers are open coincident with undervoltage on both main

feeder buses. These relays provide contacts which when closed help to

make up the circuit to energize the closing coils for the standby

breakers. The inspector reviewed the modification package and observed

cable and relay installation in the field. All activities observed were

satisfactory.

No violations or deviations were identified.

6.

Inspection of Open Items (92701) (92702)

The following open items were reviewed using licensee reports,

inspection record review, and discussions with licensee personnel, as

appropriate:

a.

(Closed) IFI 269,270,287/92-09-04, CBAST Pump Testing.

This item involved apparent inadequacies in the licensee's testing

of the Concentrated Boric Acid Storage Tank (CBAST) pumps. The

inspectors were concerned that the testing performed may not be

sufficient, in that only pump pressure and vibration were observed

and recorded. The system did not have instrumentation which would

allow flow determination. Without obtaining pump flow,

degradation and performance could not be determined. After

reviewing their program, the licensee agreed that pump flow should

be obtained, but requested relief from that requirement. The

relief request was denied, and the licensee modified the system on

all three units to provide acceptable flow instrumentation.

Testing was then performed which conformed to ASME Section XI

requirements.

b.

(Closed) URI 269,270,287/91-17-01, Density of HSM Reinforced

Concrete.

An NRC inspector previously reviewed the licensee's records for

construction of the Independent Spent Fuel Storage Facility, SNM

2503, and found that the concrete density did not meet the

requirements of the facility's TS Section 5.5. The required

density is a minimum of 145 pounds per cubic foot, which would

ensure an acceptable compressive strength. Construction records

indicated densities of various concrete building components of

approximately 144 pounds per cubic foot. The licensee submitted a

TS change which changed the requirements to a "Nominal" density

requirement having the same compressive strength. The change was

approved and implemented, clearing the inconsistency.

c.

(Closed) URI 269,270,287/92-24-01, Testing MG-6 Relay and Keowee

Overhead Path.

Following an observed failure of a breaker to close in the Keowee

Unit tie to the overhead emergency power path, the licensee found

that a permissive relay, type Westinghouse MG-6, had failed.

Further investigation determined that the relay had never been

tested, that the failure could have existed for an indeterminate

time, and the failure had resulted in Keowee Unit 2 being

inoperable when it was aligned to the overhead path. This issue is

further described in LER 269-92-014.

Following an Enforcement Conference conducted on November 8, 1993,

the NRC concluded that violations of requirements had not occurred

since the licensee had tested the relay originally and TS did not

specifically require testing of the overhead path and the

attendant MG-6 relay.

d.

(Closed) URI 269/93-03-03, Past Operability of Valve 1HP-97

During the performance of a periodic test, Check Valve 1HP-97

failed to.fully seat when pressure was applied in the reverse flow

direction.

This item was further discussed in NRC Inspection

Report 50-269,270,287/93-05 and a potential single failure concern

was identified.

The licensee performed a past operability

evaluationffor the'valve failing to fully seat and determined that

the valve had been past operable based on a mechanical inspection

of the valve internals. The NRC Office of Nuclear Reactor

Regulation reviewed the potential single failure concern and

determined that the licensee met licensing requirements for

Oconee.

7.

Review of Licensee Event Reports (92700)

The below listed Licensee Event Reports (LER) were reviewed to determine

if the information provided met NRC requirements. The determination

included: adequacy of description, compliance with Technical

Specification and regulatory requirements, corrective actions taken,

existence of potential generic problems, reporting requirements

satisfied, and the relative safety significance of each event. The

following LERs are closed:

a.

(Closed) LER 269/92-05, Equipment Failure and Defective Procedure

Result in Operation in Violation of Technical Specification. The

issues raised by this LER were dispositioned under violations 92

14-01 & 02. These violations were closed in inspection report 93

20.

b.

(Closed) LER 287/91-07, Equipment Failure Closes Pneumatic Valve

in Condensate Demi.neralizer System Causing Loss of Feedwater and

12

Reactor Trip. This event was documented in NRC Inspection Report

269,270,287/91-16.

c.

(Closed) LER 287/91-08, Excessive Reactor Coolant Leak, Reactor

Trip, and Inadvertent Protective System Actuation Result from

Management Deficiencies and Equipment Failures. This event was

documented in NRC Inspection Reports 269,270,287/91-31 and

269,270,287/91-34.

d.

(Closed) LER 269/92-14, Equipment Failure Results in the

Inoperability of Keowee Unit 2 Overhead Power Path and a Technical

Specification Violation

This issue is discussed in the closure of URI 269,270,287/92-24-01

in paragraph 6 of this inspection report.

e.

(Open) LER 269/92-17, Inadequate Seismic Support Of Vital

Instrumentation And Control Batteries Due To Unknown Cause,

Possible Installation Deficiency.

The report identified three areas associated with the 125v battery

banks where the installation of the equipment did not agree with

the applicable vendor drawings. The deficiencies involved were:

(1) a vertical support was missing on the Unit 2CB battery rail,

(2)

missing splice plates on Units 2 and 3 battery racks, and (3)

battery cells located above the butt joints on the mounting racks.

The licensee evaluated the issues and determined that the battery

rail with the missing vertical support was sufficient to meet the

seismic criteria required for an operability determination. The

determination was based on an engineering analysis that the test

data from racks with seven vertical supports had sufficient margin

such that those with six supports were acceptable.

The issue of-missing spli'ce plates where the support rails butt

together was evaluated. The results of that evaluation revealed

that the splice plates were necessary to seismically qualify the

battery racks. As a result, the missing splice plates were

installed and the installation was verified by the inspector.

The third issue involved battery cells located above the butt

joints of the mounting rails. The vendor manual was revised by the

licensee to allow batteries to be placed above the butt joints on

racks with installed seismic protection. The inspector could not

find the basis for the licensee's revision to the vendor manual

even when considering the addition of the seismic structure.

This LER will remain as an open item based on the resolution of

the third issue.

No violations or deviations were identified.

13

8.

Exit Interview

The inspection scope and findings were summarized on January 31, 1994,

with those persons indicated in paragraph 1 above. The inspectors

described the areas inspected and discussed in detail the inspection

findings. The licensee did not identify as proprietary any of the

material provided to or reviewed by the inspectors during this

inspection.

Item Number

Description/Reference Paragraph

URI 50-287/94-01-01

Improperly Sized HPI Orifice Plates

(paragraph 2.c).

VIO 50-287/94-01-02

Inadequate Procedure for Steam Generator

Tube Plugging Activities (paragraph 2.d).

URI 50-287/94-01-03

Maintenance Activity Results in Loss Of

Power (paragraph 3).