ML16148A832

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Insp Repts 50-269/93-23,50-270/93-23,50-287/93-23 & 72-0004/93-23 on 930823-28.Violations Noted.Major Areas Inspected:Evaluated Circumstances Surrounding 930823 Reactor Trip Following Loss of 1DIA 125 Volt Dc Panelboard
ML16148A832
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 09/23/1993
From: Harmon P, Lesser M, George Macdonald, Poertner K
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML16148A831 List:
References
50-269-93-23, 50-270-93-23, 50-287-93-23, 72-0004-93-23, 72-4-93-23, NUDOCS 9310150100
Download: ML16148A832 (13)


See also: IR 05000269/1993023

Text

SREGj

UNITED STATES

0 oNUCLEAR

REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report Nos. 50-269/93-23, 50-270/93-23, and 50-287/93-23

Licensee: Duke Power Company

422 South Church Street

Charlotte, NC 28242-0001

Docket Nos.: 50-269, 50-270, 50-287 and 72-4

License Nos.: DPR-38, DPR-47 DPR-55 and SNM-2503

Facility Name: Oconee Nuclear Station

Inspection Conducted:

ugus 23 - 28, 1 3

Lead Inspector:

.

c-3

P. Harmon, enior Reside t Inspector Date Sighed

  • A3I,

Inspectors:

G. MacD nald, Reac or Insp t r

Date Signed

6

K. Poertner, Resid t Inspkc or

Date Signed

Approved by:

M. S. Lesser, Section Chief

Date Signed

Projects Section 3A

Division of Reactor Projects

SUMMARY

Scope:

This special inspection was performed to evaluate the

circumstances surrounding the Unit 1 Reactor Trip on August 23,

1993 following loss of the 1DIA 125 Volt DC panelboard. The

inspectors reviewed the sequence of events, plant response,

operator response, maintenance and testing activities and the

effectiveness of the licensee's Significant Event Investigation

Team.

Results:

1.

The cause of the loss of DC power and reactor trip was due

to reversed power leads associated with the redundant diode

power supply to panelboard 1DIA.

2.

The Main Feedwater System did not respond properly following

the trip due to an incorrect pump speed control circuit card

which had previously been installed. This prevented the

Main Feedwater pump from developing adequate pressure to

feed the steam generator.

9310150100 930924

PDR ADOCK 05000269

0

PDR

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

  • H. Barron, Station Manager

S. Benesole, Safety Review Manager

D. Coyle, Systems Engineering Manager

  • J. Davis, Safety Assurance Manager

T. Coutu, Operations Support Manager

B. Dolan, Manager, Mechanical/Nuclear Engineering

W. Foster, Superintendent, Mechanical Maintenance

  • J. Hampton, Vice President, Oconee Site

D. Hubbard, Component Engineering Manager

C. Little, Superintendent, Instrument and Electrical (I&E)

  • M. Patrick, Regulatory Compliance Manager

B. Peele, Engineering Manager

S. Perry, Regulatory Compliance

  • G. Rothenberger, Operations Superintendent
  • R. Sweigart, Work Control Superintendent

Other licensee employees contacted included technicians, operators,

mechanics, security force members, and staff engineers.

NRC Resident Inspectors

  • P. Harmon
  • W. Poertner

L. Keller

NRC Personnel

  • G. MacDonald
  • M. Lesser
  • Attended exit interview.

2.

Introduction

a.

Background

DC power at each Oconee unit is provided to the DC loads from four

125 vdc panelboards. Major loads from each panelboard include 125

vdc Control Power, and a 120 vac Static Invertor for vital

instrument power. Each panelboard receives power through a dual

set of isolating transfer diodes, referred to as Normal and

Backup. Either set of diodes will provide full power to the

panelboard. The diode set which provides power is automatically

determined by the highest voltage present. The Normal supply for

each of the Unit 1 panelboards is from the Unit 1 battery bus, and

2

the Backup is supplied from the Unit 2 battery bus. Each diode

pair has an input and an output breaker provided for isolation and

testing of the diodes.

On the day of the Unit 1 trip, all three Oconee Units were at 100

percent power with no major problems and no Technical

Specification (TS) Limiting Conditions for Operations (LCOs) in

effect. A scheduled surveillance test was underway to test the

isolating transfer diodes' ability to transfer and provide power

when the Normal diode pair's input breaker was manually opened.

When the test was performed, the Backup diode pair did not provide

power, and the 125 vdc panelboard was lost along with its

attendant loads.

b.

Event Summary

On August 23, at 11:17 a.m., Oconee Unit 1 tripped from 100

percent power. The trip was initiated during a maintenance

surveillance of the Unit 1 DC panelboards' isolating diodes. When

the IDIA panelboard's supply was shifted to the backup source, the

panelboard deenergized, causing a loss of the DC loads fed from

IDIA. The turbine electrohydraulic control system and several

turbine supervisory instruments were deenergized, causing a

turbine generator trip and a subsequent reactor trip. The control

room operator's response to this trip was complicated by the loss

of several related power supplies. The main feedwater pumps did

not respond properly to the trip, and Emergency Feedwater was

automatically initiated when steam generator levels decreased to

the automatic initiation setpoint. Operators were able to

stabilize the plant at hot shutdown with systems within normal

parameters.

Several complications occurred due to the loss of DC control power

from the 1DIA panel board. These included the loss of main feeder

bus #1 and the Reactor Coolant Pump (RCP) supply bus 1TA not

automatically transferring to the Startup Transformer CT1. The two

RCPs on bus 1TA lost power and coasted down with their pump

breakers remaining closed. Several minutes later, when power to

the pump buses was restored, the RCPs attempted to restart.

Additionally, numerous control room instruments and alarms were

lost, adding additional confusion to the incident.

The event investigation found that a maintenance related error was

the principal cause of the trip. The leads to the backup supply's

isolating diodes for the IDIA circuit had been inadvertently

reversed during a breaker replacement evolution in May 1993. As a

result, the diodes' input polarities were reversed, and the diodes

did not conduct current. When the normal power supply was

deenergized as part of the surveillance test, the backup supply

did not provide power to the IDIA panelboard.

0II

3

The inability of the Main Feedwater Pumps (MFWP) to supply

feedwater to the steam generators was also found to be maintenance

related. A printed circuit card was replaced in the MFWP control

circuit during the previous refueling outage. The new card was

installed to replace a malfunctioning card in the circuit and was

not properly modified by removing an integration limiter which is

part of the basic card as a shelf item. As a result, MFWP speed

did not increase to a high enough value to force water into the

generators at the higher, shutdown pressures. As the water levels

in the SGs decreased, the motor driven Emergency Feedwater pumps

were automatically initiated when level dropped below 20 inches

for 30 seconds and valves 1FDW-315 and 1FDW-316 automatically

opened to supply emergency feedwater to the steam generators.

3.

Sequence of Events on August 23, 1993

1100 I&E Technicians started performing surveillance test

IP/0/A/3000/6, Peak Inverse Voltage Test, on the isolating diodes

for the IDIA 125 vdc Panelboard. (This 125 vdc panelboard

receives normal supply from Unit 1 Battery Bus 1DCA via an

isolating transfer diode. A backup supply, with its own isolating

transfer diodes, is fed from Unit 2 Battery Bus 2DCA, with an

auctioneering circuit which will select the highest potential from

the two available diode pairs.)

1115 Technicians checked the availability of power from the backup

source prior to opening the normal isolating diodes' input

breaker. This check consisted of verifying the backup breaker

position, and verifying no voltage drop across the breaker.

1117 Technicians opened the input breaker to the Unit 1 diodes. The

following occurred:

-

Power lost to lDIA (feeds IKVIA static invertor, D.C.

control power for breaker control, and EHC control power.

among other loads).

-

Power lost to static invertor 1KVIA (feeds Inadequate Core

Cooling Monitor train A, RPS Channel A, ES channel A among

others).

-

Main Turbine trip due to loss of Electrohydraulic Control

(EHC) power.

-

Reactor trip due to turbine trip.

-

Station auxiliary loads transferred from IT (Auxiliary

Transformer) to CT-1 (Startup Transformer).

-

Reactor Coolant pump bus 1TA did not fast transfer to the

Startup Transformer due to loss of DC control power. With

4

the Auxiliary transformer deenergized, the two RCPs (1A1 and

181) on bus ITA coasted down and stopped.

-

Power lost to the Radiation Monitor (RIA) monitor in the

control room (no cause determined at time of this report).

1118 Operators responded to trip as follows:

Verified that the Main Feedwater system was responding to

the reactor trip and the Feedwater startup valves were

opening to control Steam Generator (SG) level to the no-load

setpoint of 25 inches. The Main Feedwater pump speed

increased automatically to overcome the increased SG

pressure, but did not provide enough speed and discharge

pressure to overcome SG pressure. (This was later

determined to be caused by installation of an incorrect

printed circuit card which limited pump speed).

Continued

steaming of the SGs caused levels in the SGs levels to

decrease further.

-

Controlled Makeup Control Valve 1HP-26 to control RCS

makeup.

Started High Pressure Injection (HPI) Pump 1B and noted that

the 1A HPI pump had no indicating light, but had normal

running amps. HPI pump 1A could not be stopped.

-

Noted the Condenser Circulating Water (CCW) gravity flow

valves opening.

1124

I&E Technicians performing the surveillance reclosed the normal

isolating diodes' input breaker, reenergizing iDIA. This

restoration of DC control power caused several additional events:

RCP bus 1TA transferred to the startup transformer,

restoring power to the 1A1 and 181 RCPs.

-

RCPs 1A1 and 181 started to roll.

-

High starting current on 1Al and 181 RCPs was noted by the

operator.

-

High (long term) current tripped the RCP breakers approxi

mately 7 seconds after trying to restart the RCPs. RCPs 1A1

and 181 stopped.

-

1KVIA power fuse blows, and the breaker to the 1KVIA Static

Invertor opens.

1131 Steam Generator levels reached 20 inches, initiating the dryout

protection feature and starting the motor driven emergency

feedwater pumps. (The dryout protection feature is not a Technical

5

Specification required feature, but was available during this

event).

1132 Emergency Feedwater (EFW) flow rates reached 500 gpm, operators

took manual control of valves 1FDW-315 and 1FDW-316, the EFW level

control valves, to raise SG levels slowly. Both valves go shut

(Valves do not have a bumpless transfer feature). Operators

reopened the valves in Manual mode of operation.

1133 Operators attempted to place the 1FDW 315/316 valves back in

Automatic, but both valves shut. Operators regain Manual control

(Operators did not realize that placing valves in manual reset the

automatic level control associated with the SG dryout start

feature). Operators concerned that Automatic control of 1FDW

315/316 was not working properly.

1135 SG levels returned to normal.

Operators were controlling the

plant within normal post-trip conditions. Forced circulation was

in effect with two RCPs running. Trip review and event

investigation begins.

4.

Event Investigation and Findings

a.

Trip Report and Significant Event Investigation Team (SEIT) Team

Response

Shortly after the trip, licensee management decided to ask for an

independent review of the event by their Significant Event

Investigation Team (SEIT). A SEIT was formed and dispatched to

the Oconee site. Individual team members began arriving at

approximately 7:00 p.m. on August 23.

The team conducted

interviews and witnessed the licensee's trip review process. The

SEIT team concurred in the plant staff's trip review and readiness

for restart. The SEIT team's report contained items to be

resolved prior to startup, recommendations which should be

considered for subsequent corrective actions, and items to be

reviewed without specific recommendations. Each of the team's

issues to be resolved prior to restart were adequately addressed.

The inspectors observed the SEIT team's participation in the event

review and trip review. The team's recommendations appeared to be

reasonable and conservative, and included appropriate items for

further review. Final disposition or resolution of the team's

recommendations will be addressed by the Oconee staff in the

Licensee Event Report (LER) covering this event. The resident

inspectors will review resolution of these items during review of

the LER.

The trip report identified the root cause of the trip, event and

system anomalies, and ensured appropriate corrective actions were

initiated. For the instances identified where maintenance errors

had resulted in a loss of configuration control in the isolating

6

transfer devices and the feed pump control circuits, the licensee

determined that the same devices on the other two units were

properly configured.

b.

Cause of the Trip_

The trip was caused by a deenergized 125 vdc panelboard, and loss

of loads associated with that panelboard. The electrohydraulic

control circuitry powered from the panelboard deenergized and

tripped the turbine. The reactor tripped as designed when the

turbine tripped. The panelboard was deenergized during a

surveillance test which required the backup power supply to

function. A maintenance error had previously reversed the leads

to blocking diodes supplying the panelboard. When the normal

supply was deenergized as part of the test, the backup source did

not automatically supply the panelboard. This item is discussed

further in paragraph 6.

5.

Plant and System Response

a.

Feedwater System Response

Following a reactor trip, the Main Feedwater System (MFW) is

designed to provide feedwater and bring SG levels to 25 inches.

Due to installation of an incorrect printed circuit card in the

MFW pump control circuit, pump speed did not increase to a point

high enough to bring feedwater pressure above steam generator

pressure. Steam pressure increases from approximately 850 psig at

full power to approximately 1000 psig at hot shutdown. The feed

pump circuit problem is discussed further in paragraph 6.b.

b.

Emergency Feedwater (EFW) Response

The EFW system would not normally actuate to provide water to the

SGs following a reactor trip. Since main feedwater did not

respond properly and control levels at 25 inches, SG levels

decreased below approximately 20 inches for 30 seconds, and the

motor driven EFW pumps started. The start signal for the motor

driven EFW pumps was a SG Dryout signal. This signal is not

considered an emergency start signal, but is a backup to the "Both

Feed Pumps Tripped" signal which is considered an emergency start.

Since the MFW pumps did not trip in this instance, EFW operation

was different than operators had experienced or trained for.

Operators typically take Manual control of EFW control valves FDW

315 and FDW 316, throttle them to minimize the thermal transient

on the SGs, and return the valves to Automatic when levels reach

the control point, 30 inches. Since the Emergency start is sealed

in by the MFW pumps being tripped, automatic control is still

available and will control to the SG level setpoint. When the

Dryout protection signal initiated the start of the motor-driven

EFW pumps, the operators took manual control, and the valves

immediately shut. Taking the valves to Manual resets the

7

actuation signal following a Dryout Protection start, and sends a

zero position signal to the valves. Operators reopened the valves

and fed the SGs to approximately 25 inches. The valves were then

placed in Automatic, and the valves were reclosed. Since the

operators were not aware of the different actuation and control

circuitry for the valves in the "Dryout Protection" mode, they

assumed the valves were malfunctioning. The valves were returned

to Manual, and the operators maintained SG levels. In conclusion

the EFW System responded properly although not as expected by

operators.

c.

Reactor Coolant Pump Response

When the reactor tripped, 125 vdc control power was not available

to fast transfer the RCPs on bus 1TA to their alternate power

supply. When power on the ITA bus was lost, the pumps slowed

down, but did not trip from the bus. The undervoltage protection

scheme does not sense reduced voltage or hertz on the bus, but

instead "anticipates" low voltage by monitoring breaker position

of the normal and startup feeder breakers to the 1TA (1TB bus for

pumps 1A2 and 1B2) pump supply bus. The undervoltage condition is

sensed by both breakers being open for 2 seconds. Since DC power

to the 2 second time delay circuit was lost, the undervoltage

circuit did not actuate and open the RCP breakers. Consequently,

the 1A1 and 1BI RCPs remained connected to a dead bus.

Approximately 7 minutes after the reactor trip and RCP coastdown,

technicians restored power to the deenergized 1DIA panelboard.

This also restored power to the 125 vdc control circuit. The 125

vdc control circuit then performed the fast transfer of the ITA

power supply to the startup transformer, reenergizing the two idle

RCPs. The 1A1 and 181 RCPs began to roll, even though a normal

pump start interlock had not been satisfied. The interlock, Oil

Lift Pump running for at least 2 minutes and oil pressure normal,

is only designed for preventing closure of the pump breakers. Due

to the high starting current applied to start two pumps

simultaneously, the RCPs tripped within approximately 7 seconds on

overcurrent. Operators witnessed this series of events, and

confirmed that high starting current and RCS flow indicated that

the pumps had indeed started, but then tripped. Prior to

restarting these pumps for the subsequent plant startup, the

licensee conferred with the manufacturer, Westinghouse, on the

possibility of pump damage due to starting without proper oil

pressure from the oil lift pumps. Westinghouse recommended

additional monitoring of pump vibration, but concluded that damage

should not have occurred. The pumps were later started with no

problems indicated.

d.

Loss of Radiation Monitors (RIAs)

When the reactor tripped and station power transferred to the

startup transformer, the process radiation monitors for the steam

line and condenser air ejectors were lost. These monitors provide

8

crucial information relative to operators determining whether a SG

tube rupture has occurred. The loss of the monitors was origi

nally thought to be part of the instruments directly affected by

the IDIA panelboard power loss. Later investigation revealed that

the RIAs should have been unaffected by the 125 vdc power loss.

The RIAs for Unit 3 had also been lost during the previous Unit 3

trip on January 26, 1993. The licensee had initiated a Problem

Investigation Process (PIP 93-375) on the Unit 3 event. Since the

RIAs use the plant computer for signal processing, the licensee

believes that the momentary power drop when the plant auxiliary

power shifts to the startup transformer may cause a computer

related problem in the RIAs. This is still under investigation by

the licensee's corrective action program. After the Unit I trip

resulted in the loss of RIAs, operators were notified of the

possibility of RIA loss during future plant trips.

6.

Review of Maintenance Activities

a.

Maintenance/Surveillance On Isolating Transfer Diode Cabinet 1ADA

The inspectors reviewed the troubleshooting plans for the transfer

of diode 1ADA. The licensee troubleshooting consisted of

performing procedure IP/O/A/3000/006 to attempt to reproduce the

failure. IP/O/A/3000/006 contained a check of the diode cabinet

circuit breakers and diodes. Troubleshooting concentrated on the

circuit breakers in the diode cabinets because of previous

problems encountered with these breakers. The licensee did not

have a written troubleshooting plan to systematically assess the

diode cabinet power supply components and all diode cabinet

components. The vendor manual/drawings were not initially present

at the job site. The inspectors reviewed the vendor manual for

the diode cabinets and noted that it contained a troubleshooting

section. Once the licensee determined that the diode cabinet

circuit breakers were acceptable, additional planning was required

to develop testing to locate the problem. A comprehensive and

systematic planning effort prior to beginning troubleshooting

could have reduced the time to correct the problem and the time

the unit was in an LCO for troubleshooting.

The inspectors witnessed the licensee's troubleshooting efforts on

the diode cabinet. The licensee determined the cause of the

failed diode cabinet power supply and completed the repairs within

the time allowed by the plant technical specifications. Temporary

modification TM1091 was implemented to reverse the DC power leads

inside diode cabinet 1ADA and restore proper polarity to the unit

2 diode power supply. The inspectors witnessed the testing of

diode cabinet 1ADA after the temporary modification was complete.

The test results were satisfactory. The remaining diode cabinets

were tested to verify that both power sources were operable. All

power supplies to the diode cabinets were operable.

9

The licensee determined that the Unit 2 powersupply circuit

breaker leads had been reversed on the circuit breaker in DC Motor

Control Center 2DCA Compartment 3A. During circuit breaker

testing, the circuit breaker in 2DCA Compartment 3A was found to

be cracked and was replaced under Work Order 9204935901 on May 18,

1992.

Licensee Maintenance Directive 4.4.13 original revision, "ONS I&E

Configuration Control Work Practices" Step 5.3.1, requires that a

"Component Out Of Normal Sheet" be completed when station I&E

equipment is placed in an out of normal state. Lifting electrical

leads was listed as an example requiring the use of the "Out Of

Normal Sheet."

The inspectors reviewed Work Order 9204935901 and noted that the

2DCA Compartment 3A circuit breaker shunt trip leads were listed

on the "Out Of Normal Sheet."

The circuit breaker line and load

side DC power cables were not listed on the "Out Of Normal Sheet."

Step 10.3 of procedure IP/0/A/3011/013 required that the line and

load side cables be marked and disconnected. A procedure step

completion signoff was required by the performer for Step 10.3.

Step 10.21 of IP/O/A/3011/013 required that the breaker cables be

connected as marked in Step 10.3. Step 10.21 required a

completion signoff by the performer and a verifier. From the

review of the work package, it appeared that one individual marked

and disconnected the breaker power cables and two different

individuals reterminated the cables. The convention for marking

leads could not be determined by the inspectors.

The post maintenance testing for Work Order 9204935901 consisted

of performing circuit breaker overcurrent testing in accordance

with IP/0/A/3011/013. The only control mechanism for maintaining

configuration control was the marking of the breaker leads. The

inspectors examined the circuit breaker power cables in 2DCA

Compartment 3A and found no cable markings. The incorrect

connection of 2DCA Compartment 3A circuit breaker rendered the

Unit 2 DC supply to diode cabinet 1ADA inoperable.

Review of Work Order 9204935901 indicated that the 2DCA

Compartment 3A circuit breaker power cables were not adequately

controlled to ensure proper termination by a different individual.

The "Out Of Normal Sheet" was not utilized to control the

configuration of the circuit breaker power cables. This item is

identified as an example of Violation 50-269,270,93-23-01: Failure

to Follow Procedures to Maintain Configuration Control.

b.

Maintenance/Surveillance on Unit 1 Main Feedwater Pump Speed

Controls

On December 28, 1992, the main feedwater pump speed control

proportional plus integral module failed its time specification

during surveillance testing. The installed controller module was

10

a Bailey Meter Company Type 6620255A-9. Procedure IP/0/B/0325/003

calibration data sheet required a Type 6620255A-9 controller which

did not have a speed limiter. Work Order 51316L installed a new

Type 6620255A-10 controller which contained a speed limiter.

Licensee personnel obtained the spare module by referencing the

MMIS number. The MMIS data indicated that part number 6620255A-10

was issued. It appeared that licensee personnel did not compare

the part number of the old controller to the part number of the.

new controller. The part number on the calibration data sheet in

IP/0/B/0325/003 was also not compared with the part number of the

new module. The vendor manual clearly explained that the type

6620255A-9 module did not contain a speed limiter while the type

6620255A-10 contained a speed limiter. It appeared that the

licensee relied solely on the MMIS data to identify the correct

replacement module.

The inspectors reviewed the post installation calibration checks

performed after the installation of the type 6620255A-10 module.

The calibration checks did not input test values which could have

detected the presence of a limiter card.

Subsequent to the trip the licensee verified that the feedwater

speed controllers for Units 2 and 3 did not contain speed limiter

cards in their proportional plus integral modules. The inspectors

reviewed WR 93028973 for Unit 2 and WR 93028974 for Unit 3 which

verified that the speed controllers for Units 2 and 3 did not have

limiter cards.

There have been previous instances where incorrect Bailey modules

were installed in the integrated control system. LER 287/90-01

Revision 2, reported that on January 19, 1990, an incorrect relay

module was discovered in the Integrated Control System. The I&E

procedures contained no requirements to compare or otherwise

ensure exact replacements. On April 25, 1990, a memorandum was

issued to all I&E Technicians, Supervisors, and General

Supervisors in response to LER 287/90-01. The memorandum

indicated that the MMIS number could not be relied on solely to

ensure correct part replacements. The memorandum required that

new and old part numbers should be compared and that the part

numbers on the new part and the calibration data sheet should be

compared. The licensee developed Maintenance Directive 4.4.13,

"ONS I&E Configuration Control Work Practices", on February 25,

1993, to maintain I&E configuration control.

Despite the

memorandum, the procedure, and the management directive, licensee

personnel still did not follow procedures and failed to maintain

configuration control.

This item is identified as another example

of Violation 50-269,270,287/93-23-01: Failure to Follow Procedures

to Maintain Configuration Control.

The inspectors observed that the licensee's MMIS database

contained several different Bailey controller part numbers under

11

the same MMIS number (stock number). This represents a problem to

personnel required to maintain configuration control of the ICS.

7.

CONCLUSIONS

a.

Root Cause of the Trip

The root cause of the event is considered to be maintenance errors

during work 4ctivities conducted during the previous refueling

outage for Unit 2. These errors resulted in the loss of

configuration control of a power supply to safety related DC

panelboard IDIA. In addition to the maintenance errors, lack of a

rigorous post-maintenance testing program prevented prompt

identification of the errors at the time they were made. Instead,

the errors went undetected until the failed device was challenged.

b.

Maintenance-related errors

The maintenance practices detailed in this report indicate

weaknesses in the Maintenance Program at Oconee. This event and

several similar events precipitated by maintenance activities have

unnecessarily challenged the safety systems and operators.

C.

Post-maintenance testing inadequacies

Post-maintenance testing in the instances detailed was inadequate.

The purpose of testing after a maintenance activity such as

lifting and relanding leads should determine that the activity was

properly performed. A lack of a rigorous approach to testing is

indicated by this and several similar events at Oconee.

d.

Evaluation of Operator Response

The Operations shift personnel performed well during the

transient. They adequately verified the post-trip parameters, and

maintained the plant at stable shutdown conditions. The

complexity of a losslof 125 vdc panelboard concurrent with the

trip introduced several anomalous indications and events the

operators were not familiar with. Adherence to procedures and

knowledge of the plant and systems were demonstrated during this

event. A lack of adequate training and familiarity was indicated

in the operation of the Emergency Feedwater System in the dryout

protection mode.

8.

Exit Interview

The inspection scope and findings were summarized on August 27, 1993,

with those persons indicated in paragraph 1. The inspectors described

the areas inspected and discussed in detail the inspection findings.

The licensee did not identify as proprietary any of the material

provided to or reviewed by the inspectors during this inspection.

12

Item Number

Description/Reference Paragraph

VIO 50-269,270/93-23-01

Failure to Follow Procedures

to Maintain Configuration Control, two

examples(paragraphs 6.a and 6.b).

0