ML16148A828

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Insp Repts 50-269/93-22,50-270/93-22 & 50-287/93-22 on 930725-0828.Deviation Noted.Major Areas Inspected:Plant Operations,Surveillance Testing,Maint Activities,Plant Issues & Insp of Open Items
ML16148A828
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 09/16/1993
From: Harmon P, Keller L, Lesser M, Poertner W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML16148A827 List:
References
50-269-93-22, 50-270-93-22, 50-287-93-22, NUDOCS 9309280251
Download: ML16148A828 (11)


See also: IR 05000269/1993022

Text

GRE

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

s ~101

MARIETTA STREqT, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report Nos.:

50-269/93-22, 50-270/93-22 and 50-287/93-22

Licensee:

Duke Power Company

422 South Church Street

Charlotte, NC 28242-0001

Docket Nos.: 50-269, 50-270, 50-287, 72-4

License Nos.: DPR-38, DPR-47, DPR-55, SNM-2503

Facility Name: Oconee Nuclear Station

Inspection Condu

d: July 25 - August 28, 1993

Inspect r-

A

cHarmon,

Senior Resident Inspector

Date Signed

L.

Keller, Resident Inspector

Date Signed

K. Poertner, Resident Inspector

Date Signed

Approved by:

?

L/

3

M. S. Lesser, Section Chief

Date Signed

Projects Section 3A

Division of Reactor Projects

SUMMARY

Scope:

This routine, resident inspection was conducted in the areas of

plant operations, surveillance testing, maintenance activities,

Keowee issues, inspection of open items and review of licensee

event reports.

Results:

One Deviation from commitments was identified. The Deviation

involved a failure to calibrate the Unit 1, 125 VDC ground detec

tor circuitry annually as committed in response to a previous

violation (paragraph 2.d).

One Unresolved Item (URI) was identified. The URI involved the

past operability of load shed channel 1 when powered from a 120

VAC power supply instead of 125 VDC control power (paragraph 2.c).

9309280251 930917

PDR ADOCK 05000269

0

PDR

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

H. Barron, Station Manager

S. Benesole, Safety Review Manager

D. Coyle, Systems Engineering Manager

  • J. Davis, Safety Assurance Manager

T. Coutu, Operations Support Manager

B. Dolan, Manager, Mechanical/Nuclear Engineering

W. Foster, Superintendent, Mechanical Maintenance

J. Hampton, Vice President, Oconee Site

D. Hubbard, Component Engineering Manager

C. Little, Superintendent, Instrument and Electrical (I&E)

  • M. Patrick, Regulatory Compliance Manager

B. Peele, Engineering Manager

  • S. Perry, Regulatory Compliance
  • G. Rothenberger, Work Control Superintendent
  • R. Sweigart, Operations Superintendent

Other licensee employees contacted included technicians, operators,

mechanics, security force members, and staff engineers.

NRC Resident Inspectors

P. Harmon

  • W. Poertner
  • L. Keller

NRC Personnel

  • Attended exit interview.

2.

Plant Operations (71707)

a.

General

The inspectors reviewed plant operations throughout the reporting

period to verify conformance with regulatory requirements,

Technical Specifications (TS), and administrative controls.

Control room logs, shift turnover records, temporary modification

log and equipment removal and restoration records were reviewed

routinely. Discussions were conducted with plant operations,

maintenance, chemistry, health physics, instrument & electrical

(I&E), and engineering personnel.

Activities within the control rooms were monitored on an almost

daily basis. Inspections were conducted on day and night shifts,

during weekdays and on weekends. Some inspections were made

during shift change in order to evaluate shift turnover

performance. Actions observed were conducted as required by the

2

licensee's Administrative Procedures. The complement of licensed

personnel on each shift inspected met or exceeded the requirements

of TS. Operators were responsive to plant annunciator alarms and

were cognizant of plant conditions.

Plant tours were taken throughout the reporting period on a

routine basis. During the plant tours, ongoing activities,

housekeeping, security, equipment status, and radiation control

practices were observed.

b.

Plant Status

Unit 1 operated at power for most of the reporting period. On

August 23, the Unit experienced a turbine/reactor trip from full

power on loss of DC power to a panelboard during testing

activities. The loss of power occurred due to an improperly wired

circuit breaker. Refer to paragraph 2.e for details. The Unit

was returned to power operation on August 26.

Unit 2 operated at power for most of the reporting period. On

August 25, the Unit experienced a reactor trip from full power

when an operator inadvertently pulled a Unit 2 "Z" phase relaying

potential drawer during Unit I tagging activities. Refer to

paragraph 2.f for details. The Unit was returned to power

operation on August 26.

Unit 3 operated at power the entire reporting period.

C.

Unit 3 Load Shed Channel 1

On August 3, the Licensee determined that Unit 3 load shed relay

374LSDI, located in switchgear 3TD, was fed from 120 volt AC power

instead of 125 volt DC control power as required by the wiring

diagrams. The licensee discovered this error as the result of an

ongoing wiring verification program. The licensee declared load

shed channel 1.inoperable at 4:00 p.m. and initiated a work

request to correct the wiring deficiency. The licensee also

initiated the problem investigation process (PIP) to determine how

the wiring error had occurred. The wiring was returned to normal

and load shed channel 1 was declared operable at 7:40 p.m. on

August 3.

Subsequent to this event, the licensee determined that a

modification had been performed in 1987 to provide a dedicated

fuse block for the load shed initiate coils contained in the

associated 4160 volt switchgear on all three units. During the

implementation of this modification the channel 1 load shed relay

for switchgear 3TD was connected to a 120 volt AC fuse block

located in the same breaker cubicle as the 125 volt DC fuse block

which was identified in the modification package as the proper

termination point.

3

The 120 volt AC power that was connected to the load shed relay is

supplied from a 4160V/120V transformer connected to switchgear 3TD

and used for indication and relaying on the 3TD switchgear. The

effect of supplying the 374LSD1 relay from its associated 4160

volt switchgear would be that the channel 1 load shed signal for

switchgear 3TD would not occur until after power was restored to

the switchgear following a loss of offsite power event.

The inspectors reviewed modification procedure, TN/3/A/1426/00/0,

that implemented the design change to install the dedicated fuse

block, and determined that the procedure had required that the

wiring be verified by two electricians and a QC inspector during

the installation process. The inspectors also identified that the

post modification testing performed after the modification had

been completed had not identified that the modification was wired

incorrectly and that subsequent load shed testing had also not

identified the incorrect wiring.

The inspectors held discussions with the licensee throughout the

inspection period concerning the past operability of load shed

channel 1. The licensee had not completed the past operability

evaluation by the end of the inspection period but stated that the

preliminary review indicated that the channel was operable when

connected to the 120 volt AC power supply. The inspectors

expressed concern about the operability of relay 374LSD1 when

powered from the 120 volt AC supply and requested that the

operability evaluation be provided for review when completed.

This item is identified as Unresolved Item 287/93-22-01: Load Shed

Channel 1 Operability, pending completion of the licensee's past

operability determination and review by the inspectors.

d.

DC Ground on Switchgear 1TA

On August 9, the inspector noted that the "DC System Trouble"

annunciators were in alarm for both trains of all three units.

The licensee indicated that the cause of the annunciator alarm was

a low resistance or "hard" ground (approximately 180 ohms) on the

positive leg from panelboard DIA, located downstream of breaker 31

(OEE-117-31) which is the feeder breaker for control power to

reactor coolant pump (RCP) 1B1. This portion of the DC control

system is non-safety related, but is directly tied to the safety

related 125 volt DC panelboard. At Oconee, numerous non-safety

loads are powered from the safety-related DC bus. The ground had

.been present since July 17, 1993. On July 22, I&E technicians

were able to trace the ground to the 181 RCP switchgear. After

narrowing the general location of the ground to the feeder for the

IBI RCP switchgear, the licensee deferred further work on

correcting or isolating the ground due to the perceived risk of

tripping the RCP. The licensee indicated that it was consistent

with the design of the vital DC system for a single ground to show

up on all three units due to all the units' DC systems being

interconnected through the auctioneering diode assemblies. The

4

inspector noted that these alarms would not reflash if another

positive ground occurred anywhere in the DC distribution systems

for all three units. The inspector was also concerned that there

were no compensatory actions to monitor for further positive

grounds.

The inspector noted that the control room annunciators that were

locked into alarm were shared annunciators which also provided

alarms for other conditions such as battery charger trouble,

charger output breaker tripped, and DC bus voltage low. These

other potential alarm conditions would have been masked in the

control room due to the continued presence of the ground. There

were no compensatory measures established to check for these

conditions other than normal operator rounds once a shift to check

local alarm panels.

The inspector reviewed open work requests for the vital DC system

and found that for all three units there were ten (10) open work

requests dealing with grounds (both positive and negative) and/or

the inability to calibrate ground detectors. The ground detectors

cannot be calibrated while grounds exist in the circuit. With the

exception of the hard ground discussed above, the grounds were

intermittent in nature and therefore the licensee was unable to

identify the location of the grounds. Some of the open work

requests dated back to November 1992.

A conference call between the licensee, Region II, and NRR on

Wednesday, August 12, 1993 discussed potential DC system

vulnerabilities due to the prolonged presence of the hard positive

ground and the unresolved intermittent grounds (both positive and

negative), and the licensee's schedule for corrective action. It

was the licensee's position that the ground did not present an

immediate operability concern, and that any subsequent single

failures were bounded by the single failure analysis outlined in

the FSAR. That is, the plant was designed to withstand the total

failure of a single 125 volt DC control bus. Therefore, even if a

second ground developed, causing the loss of the DC bus, that

event was bounded by the design.

The licensee indicated that

troubleshooting efforts to eliminate the ground would resume on

Monday, August 16, 1993. Subsequent to the conference call, the

inspector learned that the delay in resolving the ground was due

to high load demand on the utility grid, and technicians being on

vacation. Several members of the licensee's staff had expressed

concerns with technicians going into the RCP breaker cubicles in

search of the ground. The concern was that work in a RCP breaker

cubicle was high risk and could cause a plant trip. The

inspectors asked the licensee why power reductions during off-peak

periods were not considered which would have allowed the 1B1 RCP

to be taken off line. The licensee conceded that miscommunication

among the staff had occurred, and a power reduction to aid the

ground hunt was not fully explored. The inspectors were not able

to find evidence of any licensee planned action to resolve the

5

existing ground from July 22, when the IBI RCP breaker was

identified as the ground location, until the August 12 conference

call, initiated by the NRC. The licensee was apparently willing

to allow the ground to exist until an indeterm'inant point at which

a perceived lower risk existed. The inspectors remained concerned

with the presence of prolonged grounds in the DC system in that

the system's importance to safety requires a high degree of

reliability.

On Monday, August 16, I&E crews resumed the ground hunt. On

August 17, one full month after the ground first appeared, I&E

technicians found a short length of multi-strand copper wire in

the IBI RCP pump breaker cubicle. The wire had fallen into a

position which shorted a DC connection block to the cubicle frame.

The wire was removed and the ground alarm cleared. This evolution

did not challenge the RCP.

The inspector noted that the Unit 1 ground detectors were outside

their grace period for recalibration required by Procedure

IP/0/B/3000/024. The surveillance is scheduled on an annual

basis, with the last scheduled date being September, 1992. The

grace period for calibrating the Unit 1 ground detectors ended May

21, 1993. This procedure was originally written in response to

NRC Violation 269, 270,287/88-17-01, Maintenance Procedure

Deficiencies. In the response to this violation the licensee

committed to perform an annual recalibration of the ground

detectors. The technicians responsible for this surveillance were

not able to calibrate the detectors due to the presence of small,

high resistance grounds on the bus. The technicians requested a

deferral or hold of the surveillance. The surveillance was placed

on hold until conditions allowed the calibration. In accordance

with the licensee's policy, a surveillance can be placed on hold

(except for TS required surveillances) by the responsible

technical group. Commitment mandated surveillances are not

controlled as carefully. There was no recognition that the ground

detector calibration was a NRC commitment item. This demonstrated

a lack of controls to ensure compliance with NRC commitments.

The failure to perform an annual recalibration of the Unit 1

ground detectors is identified as Deviation 269/93-22-02: Failure

to calibrate Unit 1 ground detectors annually. The licensee

indicated that they had been unable to calibrate the ground

detectors due to the continued existence of grounds on the vital

DC system.

Following removal of the ground, technicians were able to

successfully calibrate the Unit 1 ground detectors.

e.

Unit 1 Reactor Trip

At 11:17 a.m. on August 23, Unit 1 tripped from approximately 100

percent power during performance of a peak inverse voltage test on

6

the 1ADA isolating diodes for DC panelboard 1DIA. During

performance of the peak inverse voltage test, power was lost to DC

panelboard IDIA resulting in a main turbine trip and a reactor

trip. The loss of power to panelboard 1DIA resulted from reversed

leads (reversed polarity) in the 2DCA supply breaker to isolating

transfer diode cabinet 1ADA that prevented DC power from passing

through the transfer diodes when the power supply from 1DCA was

isolated.

During the transient, the main feedwater (MFW) pumps continued to

run but adequate pump discharge pressure could not be maintained

to actually feed the steam generators. The motor driven emergency

feedwater pumps started on a steam generator dryout protection

signal when steam generator levels dropped below 21 inches for

greater than 30 seconds. Approximately 7.5 minutes after the

reactor trip, power was restored to DC panelboard 1DIA. When

power was restored to the panelboard the 1Al and 1BI reactor

coolant pumps attempted to restart. The 1Al and IBI reactor

coolant pumps had not automatically transferred to the startup

transformer due to loss of control power to the supply breaker

feeding the reactor coolant pump bus from the startup transformer.

When control power was restored, the startup transformer supply

breaker to the 1A1 and 1B1 reactor coolant pumps closed in. The

1A1 and IBI reactor coolant pump supply breaker subsequently

tripped on overcurrent.

As a result of the complications experienced during the reactor

trip, NRC Region II dispatched an electrical inspector from the

Division of Reactor Safety to assist the resident staff in

conducting a special inspection into the circumstances surrounding

the event. This reactor trip is discussed in greater detail in

NRC Inspection Report 50-269,270,287/93-23.

Unit 1 was returned to power operation on August 26, 1993.

f.

Unit 2 Reactor Trip

At 11:30 p.m. on August 25, 1993, Unit 2 tripped from

approximately 100 percent power due to a turbine trip/reactor trip

signal. The turbine generator trip resulted from a loss of load

indication and generator lockout when a non licensed operator

pulled the Z phase relaying potential drawer to the disconnect

position on the Unit 2 generator. The non licensed operator was

in the process of tagging out the Unit 1 generator for replacement

of the Unit 1 generator bus bar disconnect links and pulled the

Unit 2 drawers instead of the Unit 1 drawers.

The Senior Resident Inspector responded to the site when informed

by the licensee that Unit 2 had tripped. The trip response was

normal and the Unit stabilized in hot shutdown. The inspectors

reviewed the post trip review report prior to restart of the Unit

7

and noted no discrepancies. Unit 2 was returned to power

operation on August 26, 1993.

Within the areas reviewed, one Deviation was identified.

3.

Surveillance Testing (61726)

a.

Rod Drop Test

The following surveillance test was reviewed by the inspectors to

verify procedural and performance adequacy. The completed test

reviewed was examined for necessary test prerequisites,

instructions, acceptance criteria, technical content,

authorization to begin work, data collection, independent

verification where required, handling of deficiencies noted, and

review of completed work.

IP/O/A/0330/003A, Control Rod Drive Rod Drop Time Test. The

purpose of this surveillance is to ensure that rod drop

times are within technical specification requirements. This

surveillance test is normally accomplished during refueling

outages but was performed on the Unit 1 Group 1 and 2

control rods prior to returning the Unit to service after

the reactor trip on August 23. Group 1 rod 8 and group 2

rod 5 had experienced slow drop times during the previous

refueling outage and an emergency technical specification

change had been issued by the NRC to allow the drop times of

these two rods to be increased to 2 seconds. The licensee

had committed to test these rods at the next Unit shutdown

to verify that the drop times were acceptable. The

inspectors witnessed the rod drop time testing conducted.

The rod drop times were less than 2 seconds but the rod drop

times were significantly slower than the other rods in the

groups and were slower than the last recorded rod drop time

tests conducted in January 1993. Group 1 rod 8 dropped in

1.876 seconds and group 2 rod 5 dropped in 1.989 seconds.

The licensee intends on replacing the drive mechanisms of

these rods at the next refueling outage.

b.

Missed Emergency Feedwater Surveillance

During the inspection period the licensee identified that the

Technical Specification required monthly safety-related functional

test of the motor driven emergency feedwater pumps initiation

pressure switches had not been performed since Unit 2 returned

from its scheduled refueling outage on June 24, 1993. The

surveillance had not been performed because the procedure had been

suspended for the duration of the refueling outage and had not

been removed from this status prior to returning the Unit to

service. The Technical Specification required surveillance was

performed successfully subsequent to identifying that the allowed

grace period had been exceeded. This item will be tracked and

8

evaluated by review of the Licensee Event Report (LER) required to

be submitted to the NRC in accordance with 10 CFR 50.73.

No violations or deviations were identified.

4.

Maintenance Activities (62703)

Maintenance activity was observed and reviewed during the reporting

period to verify that work was performed by qualified personnel and that

approved procedures in use adequately described work that was not within

the skill of the trade. Activities, procedures, and the work request

were examined to verify proper authorization to begin work, provisions

for fire, cleanliness, and exposure control, proper return of equipment

to service, and that limiting conditions for operation were met.

-

TN/4/A/2078/00/BK1, Keowee Generator Air Break Interlock.

This modification package provided an interlock to prevent

the air brakes from being applied manually or automatically

during unit operation or a unit start. The modification

consisted of installing a three way solenoid valve in the

air line to the air brakes to ensure that the air system was

vented during unit operation. The inspectors observed work

in progress and reviewed the work package for completeness.

No violations or deviations were identified.

5.

Keowee Issues

On August 17, 1993 Keowee Unit 2 failed to start manually from the

Oconee control room during the performance of PT/0/A/620/17,

Keowee Manual Sync Test. A second attempt was made to start the

Keowee unit manually from the Oconee control room without success.

Keowee Unit 2 was returned to its normal automatic alignment and

the surveillance test was repeated this time from the Keowee

control room. This time the Unit responded to the manual start

signal and the performance test was completed. The operators

performed an operability check of Keowee Unit 2 after the manual

sync test was completed to verify that Keowee Unit 2 would

automatically start from the Oconee control room. The licensee

does not consider that the Keowee unit is inoperable if the manual

start circuitry in the Oconee control room is inoperable. This

position is based on the fact that the emergency start circuity in

the Oconee control room is separate from the manual start

circuitry, and under normal circumstances the Keowee units can not

be manually started from the Oconee control room because control

of the Keowee Units is maintained in the Keowee control room. The

licensee initiated the problem investigation process to develop a

plan to troubleshoot and locate the problem with the manual start

circuitry.

No violations or deviations were identified.

9

V

6.

Inspection of Open Items (92701) (92702)

The following open item was reviewed using licensee reports, inspection

record review, and discussions with licensee personnel, as appropriate.

(Closed) Unresolved Item 269,270,287/92-13-01:

RCS Hot Leg Draindown

and Loop Drop Problems.

This item addressed problems experienced with

venting the reactor coolant system hot leg high point vents during

efforts to lower or drop the level in the hot legs. Procedure

OP/1A/1103/11, Enclosure 3.1 was revised to provide guidance to vent

nitrogen into the hot legs and provide a specific valve lineup to

establish nitrogen flow. The licensee also replaced the valves in the

vent header with the valves that would pass flow in both directions.

7.

Review of Licensee Event Reports (92700)

The below listed Licensee Event Report (LER) was reviewed to determine

if the information provided met NRC requirements. The determination

included: adequacy of description, verification of compliance with

Technical Specification and regulatory requirements, corrective actions

taken, existence of potential generic problems, reporting requirements

satisfied, and the relative safety significance of the event. The

following LER is closed:

-

LER 269/92-04, Reactor Trip Results from Low Main Feedwater Pump

Discharge Pressure Due to Management Deficiency. This LER

describes a reactor trip that occurred during a Unit startup when

operators attempted to decrease hotwell level due to a high

hotwell level alarm condition during the startup. This item was

discussed in NRC Inspection Report 269,270,287/92-11. As a result

of this trip the licensee revised Procedure OP/0/A/1106/02,

Condensate and Feedwater, to add Enclosure 3.22 which provides

written instructions to reduce hotwell level and revised the

annunciator response to high hotwell level to reference the

Operating Procedure for lowering hotwell level.

No violations or deviations were identified.

8.

Exit Interview

The inspection scope and findings were summarized on August 31, 1993,

with those persons indicated in paragraph 1 above. The inspectors

described the areas inspected and discussed in detail the inspection

findings. The licensee did not identify as proprietary any of the

material provided to or reviewed by the inspectors during this

inspection.

10

Item Number

Description/Reference Paragraph

URI 50-287/93-22-01

Load Shed Channel 1 Operabil;ity (paragraph 2.c).

DEV 50-269/93-22-02

Failure to Calibrate Unit 1 Ground

Detectors Annually (paragraph 2.d)