ML16148A603

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Insp Repts 50-269/91-34,50-270/91-34 & 50-287/91-34 on 911123-1221.Violations Noted.Major Areas Inspected:Rcs Leakage That Occurred on Facility & Loss of 87,000 Gallons of Reactor Coolant Water to Reactor Bldg
ML16148A603
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 01/14/1992
From: Belisle G, Binoy Desai, Harmon P, Poertner W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML16148A602 List:
References
50-269-91-34, 50-270-91-34, 50-287-91-34, NUDOCS 9202140232
Download: ML16148A603 (20)


See also: IR 05000269/1991034

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

.

REGION H

a

101 MARIETTA STREETN.W.

&1

ATLANTA, GEORGIA 30323

Report Nos. 50-269/91-34, 50-270/91-34 and 50-287/91-34

Licensee:

Duke Power Company

422 South Church Street

Charlotte, NC 28242

Docket Nos.: 50-269, 50-270 and 50-287

License Nos.: DPR-38, DPR-47 and

DPR-55

Facility Name:

Oconee Nuclear Station

Inspection Conducte

November 23 - December 21, 1991

Inspectors:

.

/. /4

P. E. Harmo ,

enio

es den

spector

Date Signed

de

Bp

esaDate

Signed

W. K. Poertne/

Resid itIns

c or

Date Signed

Accompanying Inspectors: J. J. Lenahan, Reactor Inspector, Region II (RH),

Division of Reactor Safety (DRS)

L. S. Mellen, Reactor Engineer, RH, DRS

R. B. Shortridge, Radiation Specialist, RII,

Division of Radiation Safety and Safeguards (DRSS)

E. D. Testa,

Em

gency Preparedness Specialist, RII,

Approved by: G.A./1te,

a

Signed

Division of Reactor Pr jects

SUMMARY

Scope:

This inspection was conducted to follow-up on the primary Reactor

Coolant System (RCS)

leakage that occurred on Unit 3 on November 23

and 24,

and the resulting loss of approximately 87,000 gallons of

reactor coolant water to the reactor building.

Results: Two violations were identified, concerning the failure to follow

procedures (paragraph 2.c) and inadequate installation and inspection

procedures to ensure proper installation of a compression fitting

(paragraph 3).

9202140232 920114

PDR ADOCK 05000269

Q

PDR

2

The evolution was well controlled by the Technical Support Center

(TSC).

Numerous

problems were encountered and solved in a

conservative, safety-conscious manner.

During the actual plant

shutdown, operatcr actions led to an inadvertent Reactor Protection

System actuatio

which had no direct consequences.

Operators

exhibited sound judgement, knowledge of plant, safety consciousness,

and an overall appropriate conduct of responsibility with one

exception noted above.

The licensees radiological response was

prudent and effective.

Emergency response activities were

satisfactory.

REPORT DETAILS

1. Persons Contacted

  • H. Barron, Station Manager
  • J. Davis, Quality Assurance Manager
  • G. Rothenberger, Superintendent, Integrated Scheduling
  • R. Sweigart, Superintendent, Operations

C. Little, Superintendent, Instrument and Electrical(I&E)

W. Foster, Superintendent, Mechanical Maintenance

Other licensee employees contacted included technicians, operators,

mechanics, security force members, and staff engineers.

NRC Resident Inspectors:

  • P. Harmon

W. Poertner

  • B. Desai
  • Attended exit interview

2. Event Description

a. Event Overview

Prior to the event, the unit was at 100 percent power with RCS

temperature and pressure being controlled at 580 degrees F and

2155 psig respectively.

The core was at 232 effective full power

days burnup (complete cycle being 410 effective full power days).

One of the three high pressure injection (HPI) pumps was in service

maintaining pressurizer level.

The other two HPI pumps were in

standby with both trains of.the HPI system operable. Both trains of

the low pressure injection (LPI)

system were operable and in the

standby.mode.

Containment integrity was maintained and the reactor

building spray and the reactor building cooling systems were

operable. All offsite power supplies were operable.

At the time of the event there were indications of defective fuel

pins and the licensee had been monitoring the Iodine(I) concentration

in the reactor coolant.

Based on concentration of 1-131, 132, 133,

134 and 135, the licensee had projected that. there were potentially

eight fuel pins with small defects.

Reactor coolant activity was

higher than normal as a result of the defective fuel pins.

The Inadequate Core. Cooling Monitor (ICCM)

instrumentation was

installed at Oconee as part of a post Three Mile Island (TMI)

modification.

This modification had been completed on Unit 3 during

the refueling outage that ended in March 1987. A portion of the ICCM

includes the "A" and the "B" hot leg level indications. The hardware

for hot leg level instrumentation consists of two impulse lines (one

2

for each loop) that taps into the high point vent line located at the

apex of each hot leg.

This line feeds the low pressure side of a

differential pressure (dp) cell.

The high pressure impulse. line taps

into the decay heat drop line.

A RCS pressure transmitter serving

the ICCM subcooling margin monitor as well as providing control room

indication also taps into the impulse line feeding the high pressure

side of the "A" hot leg level dp cell.

Prior to the event, the

control room RCS pressure indication (off ICCM)

was reading the

normal value of 2155 psig.

Both trains of ICCM were .operable;

however, the hot leg level indications were not valid (normal) due to

forced flow conditions.

At approximately 1:41 a.m.

on November 23,

1991, operators in the

Unit 3 control room received alarms indicating problems with the ICCM

"A" train as well as fire alarms in the reactor building.

The

operators noted that the letdown storage tank (LDST)

level and

pressurizer level were decreasing.

The operators also noted that

reactor coolant makeup through the pressurizer level control valve

and reactor building normal

sump level were increasing.

With

symptoms of an RCS leak, the operators entered the Abnormal Procedure

for excessive RCS leakage.

The RCS leak was estimated by the

operators at approximately 70 gpm. AT 2:14 a.m., an ALERT emergency

classification was declared and per the emergency plan, the Technical

Support Center (TSC),

the Operations Support Center (OSC)

and the

Crisis Management Center (CMC) were activated. A controlled shutdown

and a subsequent depressurization of the unit was initiated.

Based

on the fault on the ICCM "A" train, as well as the failure to zero of

a wide range

RCS' pressure gage,

the source of the leakage was

suspected to be the hot leg level portion of the Reactor Vessel Level

Indication System (RVLIS)

instrumentation connection located at the

apex of the "A" hot leg (candy cane). . The RCS was completely

depressurized at approximately 5:00 p.m.

on November 24, at which

time the leak was stopped.

After purging the reactor building,

personnel entered the building and positively identified the source

of the leak.

A

compression fitting, 3/4 inch in diameter,

associated with the RVLIS hot leg level instrumentation, had failed.

Approximately 87,000 gallons of reactor coolant leaked from the

failed compression fitting within a time frame of approximately

40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br />.

The RCS leakage was caused by the failure of an improperly installed

compression.fitting. Some difficulty was experienced in cooling down

and fully depressurizing the RCS to stop the unisolable leak.

Containment atmosphere samples detected radioactive iodine and noble

gas concentration as high as 1380 times the Maximum Permissible

Concentrations (MPC).

Radiation dose to the public as well as to

plant personnel as a result of the accident was minimal.

3

After the reactor shutdown was completed and the reactor containment

was purged, the licensee walked down all compression fittings in the

Unit 3 Reactor Building and found a high percentage had not been

properly made up.

All accessible fittings were either tightened to

manufacturers'

specifications, or analyzed as acceptable for those

which could not be brought into conformance.

b.

Sequence of Events

Date/Time

Event

November 23, 1991

0100

Units 1, 2, and 3 operating at 100%.

0120

RCS leakage calculation performed for the last hour

indicated 0.18 gpm.

0141

Operators received alarm indicating problem with ICCM

"A" train and also received fire alarms in the reactor

building.

0143

Operators noted Letdown Storage Tank (LDST) level

decreasing, Pressurizer. level decreasing,

reactor

coolant makeup increasing, and reactor building normal

sump level increasing.

Operators referred to

AP/3/A/1700/02, Excessive RCS Leakage.

0155

Radiation Instrument Alarm (RIA)-47 (Reactor Building

Particulate) alarmed high.

0203

Operators initiated a controlled shutdown of the unit

at 15 MW/min.

Reactor coolant leak estimated to be

70 gpm.

0214

Emergency classification of ALERT declared based on

RCS leak greater than 50

gpm.

Site Assembly

commenced. Leak estimated at 60-70 gpm.

0217

With unit power at 78%,

Integrated Control System

(ICS)

Asymmetric

Rod indication resulted in unit

runback to 60%.

Operators placed SG/Rx Master and Rx

control in Manual and inserted control rods to reduce

power.

0218

Site Assembly requested

0221

NRC, State, and Local Counties notified.

4

0231

OSC Activated

0239

Received reactor building High Iodine alarm on RIA-48.

0250

Site Assembly Complete

0300

Unit at 48%, control rods being manually inserted to

achieve 1% per minute decrease.

0305

Technical Support Center (TSC) established.

0325

RCS leak estimated to be stable at 60-70 .gpm.

0327

Reactor trip occurred at approximately 35% power due

to a divergent steam pressure oscillation.

0330

Crisis Management Center (CMC) established.

0339

Reactor building sample results indicated Iodine at

2 MPC, and Noble Gas at 407 MPC.

0530

RCS at 1735 psig and 535 degrees F, Hot Shutdown

Conditions.

0629

RCS Chemistry results received; boron concentration

933 ppm.

0635

Operators placed RPS channels A, B, C, D in shutdown

bypass.

0638

Operators reset control rod drive (CRD) breakers. Turbine

Bypass Valves (TBV)

opened due to shift in Main Steam

header bias setpoint, initiating an inadvertent rapid

cooldown of the RCS.

Main Steam and reactor coolant

pressure began increasing from about 1620 psi when

operators manually closed turbine bypass valves.

0639

Turbine Bypass Valve Controller placed in Automatic.

0641

RPS actuation as reactor coolant pressure increased to

1700 psi (no control rod movement as rods were already

at the bottom).

Operators subsequently reset the CRD

breakers and withdrew group one rods to 50% per

procedure. Cooldown and depressurization continued.

1427

Unit cooldown reached 250 degrees F.

1550

LPI pumps A and B started for decay heat removal.

1718

Unit cooldown reached 200 degrees F (Cold Shutdown).

5

1720

ALERT terminated and Crisis Management Center

deactivated (leak less than 10 gpm).

2054

Reactor Coolant Pump 3B1 (final pump) secured.

2156

Pressurizer cooldown initiated.

November 24, 1991

0002

5,000 gallons. pumped from reactor building to the

miscellaneous waste.holdup tank for sampling,

processing, and eventual release.

0800

Leak estimated to be 5 to 10 gpm.

1700

Leak stopped after unit completely depressurized.

Final depressurization involved opening pressurizer

relief valves to allow colder RCS loop water to enter

the pressurizer and collapse the -remaining steam

bubble.

High point RCS hot leg vents were opened,

allowing higher elevation hot leg water to drain down

and enter the pressurizer. Although the "A" hot leg

level dropped as expected, the "B" loop hot leg hung

up because the vent arrangement did not provide

effective venting into the RCS.

The "A" hot leg was

effectively vented inward by the failed instrument

tube.

NOTE:

On Novembver 24-25, Emergency Notification

Updates and Event News Releases were given as required

by established procedural controls.

November 25, 1991

0100

Reactor Building Purge initiated.

1300

Damage assessment team entered reactor building and

identified failed RVLIS compression fitting.

11/27/91

Completed pumping water from reactor building

basement for processing.

11/28/91

Reactor building decontamination activities in

progress.

11/30/91

RVLIS valve and tubing sent to B&W for analysis.

Commenced inspections of valves, penetrations,

instruments, etc. in reactor building.

6

12/08/91

All inspections in the reactor building

complete. Unit 3 in hot shutdown with RCS at 536

degrees F and 2190 psig. Startup activities in

progress. While pulling Rod Group 5 to achieve

criticality, Rod 6 of Group 5 dropped into the core.

Shutdown (cooldown and depressurization) was

commenced.

12/09/91

A reactor building entry confirmed that the stator

rod 6 of group 5 was bad. Remeggering of.control rod

drive stators initiated.

12/11/91

26 of 69 stators did not meet meggering acceptance

criteria.

12/12/91

RCS cooldown and depressurization initiated to drain

RCS to 200 inches on the pressurizer to enable work on

CRD stators.

12/13/91

Reactor vessel head vented, 29 stators pulled

for troubleshooting and drying.

12/14/91

RCS fill begun, 4 stators replaced, all 29 stators

dried, 24 connections replaced.

All stators

remeggered.

12/15/91

Small RCS leak noticed during a building walkdown.

The leak was identified as a crack in the decay heat

drop line.

12/16/91

Shutdown.Cooldown commenced to isolate and repair

leak.

c. Event Details

Resident inspectors arrived on site shortly after the initiation of

the event.

Control room activities as well as TSC/OSC activities

during recovery were monitored on a "round the clock" basis by the

resident staff. In addition, inspectors interviewed plant personnel,

reviewed logs, attended meetings, as well as observed portions of

activities in the reactor building associated with the event.

The

following information was gathered from the above inspector

activities.

Prior to the event, on the morning of November 23,

1991, Units 1,

2 and 3 were operating at 100 percent power. Unit 3 was staffed with

one unit supervisor (SRO), one control room supervisor (SRO) and two

reactor operators.

A RCS

leakage calculation performed at

approximately 1:20 a.m. on November 23, indicated a RCS leakage of

approximately 0.18 gpm which was

well within the Technical

Specification (TS) limitations.

7

At 1:41 a.m.,

operators in the Unit 3 control

room received a

statalarm indicating problems with the ICCM "A" train and also

received statalarms indicating a fire in the Reactor Building.

Shortly thereafter, the operators noticed that the vertical panel

board indicated that the letdown storage tank (LDST) level as well as

the pressurizer level were decreasing and that the reactor coolant

makeup and reactor building normal sump level were increasing. LDST

level decrease is attributed to increased makeup flow as the high

pressure injection pump draws suction from the LDST during normal

operation.

The operators immediately recognized the symptoms of

excessive RCS leakage and referred to the abnormal procedure for

excessive RCS leakage, AP/3/A/1700/02.

Per the instructions of

AP/3/A/1700/02, efforts were initiated to determine the leak size.

At approximately 1:55 a.m.,

Radiation Instrument Alarm (RIA)-47,

which monitors reactor building particulate activity, alarmed high.

By 2:03 a.m.,

the RCS leak rate calculation was completed and the

leak rate was estimated to be 70 gpm.

This leakage exceeded the

TS 3.1.6 limits of unidentified leakage greater than 1 gpm as well as

total RCS leakage greater than 10 gpm. A unit shutdown was initiated

with a load reduction of 15 MW/min. Operators also isolated letdown

to minimize further inventory loss.

At this time, there was no

conjecture as to the location of the leak.

At 2:14 a.m.,

an ALERT emergency classification was declared, per

Enclosure 4.1.1 of Emergency Classification Procedure RP/0/1000/01,

based on an unisolable RCS leak greater than 50 gpm and subcooling

margin greater than 0 degrees F. .A site assembly was also commenced

per the -requirements of RP/0/A/1000/03 which was the applicable

emergency procedure while in the Alert emergency classification.

Notifications were made to activate the TSC, OSC and the CMC.

During the controlled shutdown, while at 78 percent power, the unit.

experienced an ICS runback to 60 percent power due to an asymmetric

rod caused by indication of a safety rod in Group 3 not at its out

limit. However, all rods were verified by the operators to be at

their required positions.

The cause of the runback was later

determined to be a failed out limit indication and not an actual

dropped rod.

The runback was terminated at 60 percent power by

taking the Reactor Diamond Control to manual.

The operators

continued to reduce power by manually inserting the control rods. By

3:05 a.m.,

the TSC and the OSC had been fully activated and the

Station Manager

had assumed responsibility as

the emergency

coordinator. The unit was at 42 percent power and manual shutdown

was continuing at the rate of 1 percent per minute.

Field

monitoring teams were dispatched to identify any changes in the

offsite dose rates.

8

At 3:24 a.m., with the unit at 35 percent power, operators placed the

3B Main Feedwater pump (MFWP) in manual in anticipation of securing

the pump.

This resulted in a divergent steam pressure oscillation

due to an inherent. instability of turbine pulser control at low

power.

The slower response of the feedwater system in manual

initiated the divergent steam pressure oscillation.

As the speed of

the pump was reduced, the discharge feedwater pressure reached a low

enough pressure to trip the Reactor Protection System (RPS)

trip

bistable for the 3B MFWP on RPS channels A and D.

To dampen the

divergent steam pressure oscillation, operators tried to increase the

speed of the 3B MFWP. This caused the speed of the 3A MFWP (which

was in auto) to decrease.

The 3A MFWP reached the low discharge

pressure setpoint of approximately 800 psig, tripping the RPS

channels A and'.D trip bistables.

Since the bistable trip caused by

the 3B MFWP was already locked in, the two MFWPs were now perceived

by the .RPS to be tripped.

Therefore, the RPS actuated on loss of

both MFWPs and the unit tripped. The post trip response of the plant

was normal with reactor coolant leak still in progress.

All control

rods were inserted into the core.

Both 4 KV and.7 KV electrical

power supplies transferred to the startup source. Unit 3 stabilized

at hot shutdown. No Engineered Safeguards (ES) or pressurizer relief

valve actuations occurred.

Both MFWPs continued to pump into the

steam generators, removing decay heat through the turbine bypass

valves and into the condenser. "A" MFWP was later secured by the

operators.

The licensee's review of the operators'

actions

regarding the feedwater pump shutdown and control of the ICS

concluded that operator familiarity with various combinations of

auto/manual station controls should be increased.

Increased training

in this area is planned by the training staff.

By 3:30 a.m., the Crisis Management

Center

(CMC)

had been

established.

The unit was stable at hot shutdown. RCS leakage at

this time was estimated at approximately 130 gpm. This leak rate was

suspected to be in error on the high side due to the inherent large

uncertainties, associated with leak rate calculations during transient

conditions.

Reactor building sample results indicated that the

concentration of radioactive Iodine in the building was two times the

maximum permissible concentration (MPC) and noble gas was 407 times

MPC.

Field monitoring teams did not detect any offsite increase in

activity. Operators noted through the reactor building video camera

that a significant amount of steam was rising from the "A" cavity.

The steam was condensing on virtually all visible walls, handrails

and equipment.

No significant rise in reactor building pressure was

noted.

A boron concentration sample of the RCS,

requested earlier by the

TSC,

indicated the RCS concentration to be 579 ppm.

At 4:45 a.m.,

cooldown of RCS to 532 degrees F was begun. Further boration of the

RCS was initiated to ensure adequate long-term shutdown margin.

Contents of the bleed hold up tanks, as well as the concentrated

.9

boric acid mix tank were constantly pumped into the LDST to keep up

with the inventory loss.

By the controlling procedure for unit shutdown, OP/3/A/1102/10, at

approximately 5:30 a.m.,

the ES system was bypassed to enable

lowering RCS. pressure to below the ES high pressure setpoint of

1750 psig.

Further cooldown was in progress by controlling secondary

pressure using the ICS turbine header pressure setpoint control with

the turbine bypass valves in the automatic mode of operation.

Shutdown Procedure OP/3/A/1102/10, Enclosure 4.2, step 2.3, requires

the,%turbine bypass valves to be placed in Manual.

The CRO, after

consulting with the CRSRO,

decided to leave the TBVs in Auto

and

control the TBVs by manually lowering the demand signal.

The

operator and the CRSRO believed this method of control to be

equivalent to placing the controller in Manual.

The method chosen

was based on a desire to reduce operator duty and attention during

the transient.

However, the consequences of leaving the controls in

Auto were not properly analyzed or recognized.. *When the reactor trip

breakers are reset, the ICS automatically removes a bias that

increases the setpoint by 125 psig.

If the TBVs are in auto, the

removal of the bias results in the TBS-sensing a pressure error of

125 psig. At approximately 6:33 a.m., the RPS was placed in shutdown

bypass to allow the RPS system not to actuate while RCS pressure was

reduced below the low pressure trip setpoint. An over-pressure trip

setpoint of 1710 psig RCS pressure is automatically reinstated by

this evolution to prevent inadvertent re-pressurization when the

reactor is reset.

At 6:38 a.m., the control rod breakers were reset in preparation for

partially withdrawing one group of control rods as a standby source

of negative reactivity. When the CRD breakers were reset, the ICS

removed the 125 psig steam header pressure automatic bias applied to

the turbine header pressure setpoint following a reactor trip.

As a

result the turbine bypass valves opened to achieve the new lowered

turbine header setpoint. This created a cooling transient on the RCS

and the RCS pressure dropped to approximately 1620 psig.

The

operator took the turbine bypass valves to Manual and started driving

them closed creating a reduction in heat removal from the primary

side. RCS pressure and.temperature started increasing. RCS pressure

reached the over-pressure setpoint and tripped the RPS.

The CRD

breakers opened. However, all control rods were already in the core

so no other consequences occurred.

RCS pressure continued to

increase to approximately 1720 psig when the operator took the. bypass

valve back into Manual and reopened them to stabilize pressure.

Subsequently, the operators reset the CRD breakers, withdrew one

group of control rods to 50 percent in accordance with the shutdown

procedure and continued the cooldown.

10

During the transient, the operator and his supervisor chose to not

perform a step required by the relevant procedure.

While performing

steps out of sequence or changing the procedures is allowed after

careful analysis and review, the transient imposed by the procedure

deviation indicates that full cognizance of the ICS functions and the

rationale for the step requiring placing the TBVs in Manual were not

adequately considered. This is a violation for failure to follow

procedures, VIO 287/91-34-01: Failure -to Follow Procedures..

At approximately 7:30 a.m.,

the RCS was at 1500 psig and 480

degrees F. The operators noted that intermediate nuclear range

instrument NI-4 had failed low.

Samples obtained from the reactor

building indicated Noble gas concentrations of 1023 MPC and Iodine

and particulate concentrations of 970 MPC.

-No offsite dose

indications were found. RCS leakage was approximately 50 gpm.

Cooldown continued and at about 3:30 p.m.,

Low Pressure Injection

(LPI) pumps A and B were aligned to remove decay heat. At 5:18 p.m.,

cold shutdown was reached and subsequently the Alert was terminated.

An

RCS leak rate of 10-15 gpm still existed.

The leakage was

suspected to be in the A hot leg RVLIS instrumentation as the CR

indication had failed low.

HP personnel were sampling the reactor

building every four hours.

Unit 3 reactor building samples taken at

9:15 p.m.

showed Iodine concentrations at 1386 MPC.

Noble gas

concentrations at 1416 MPC,

particulate concentrations at .84 MPC

and tritium concentrations at less than 1 MPC.

By 2:00 a.m., on November 24, 1991, operators had started pumping the

reactor building sump water into the waste holdup tanks located in

the Auxiliary Building for processing. The airborne Iodine activity

in the reactor building was estimated at 1382 MPC.

By 8:00 a.m.,

the RCS leak was still estimated at 5 to 10 gpm, and the pressurizer

was at saturation temperature and at 30 psig.

This pressure was

being maintained by the temperature and saturated conditions in the

pressurizer. Although all pressurizer heaters had been turned off,

the hot pressurizer continued to hold pressure above atmospheric.

The normal cooldown process requires personnel entry into the reactor

building to align valves to establish flow through the pressurizer to

cool it. However,

the airborne activity in the reactor building

precluded the normal cooldown path. The dose rate to the skin from

the airborne concentration of noble gas in the reactor building was

estimated at 321 .mrem/hour. A special procedure was written to vent

the pressurizer and the hot legs to reduce the hot leg levels.

This

involved opening the pressurizer relief valve to vent the pressurizer

to the Quench Tank, allowing the colder water from the loops to enter

the pressurizer. To enable the inrush of cooler water to enter.the

pressurizer and cool it down,

the high point vents on the hot legs

were opened to drop the loop levels.

The "A" hot leg dropped since

the hot legs are higher than the pressurizer, and an effective vent

into the RCS existed through the break. The

"B" loop did not drop,

however,

because an adequate vent is not available without a

containment entry.

Kerotest valves in the vent line act as

stop-checks and prevent flow from atmosphere into the loops, and the

vent line configuration can allow loop seals to develop.

Hot leg

venting problems are a known phenomenon at Oconee.

The hot legs are

very difficult to vent inwards,

and pressurized nitrogen into the

vents is routinely used to positively vent the hot legs as the levels

are dropped.

As soon as the "A" hot leg level was dropped, the leak

stopped.

By 5:00 p.m.,

November 24,

1991, the unit was completely.

depressurized and the leak stopped.

Approximately 87,000 gallons. of contaminated water had accumulated in

the reactor building basement.

Plans were established to remove,

treat, and discharge the radioactive water as well as to perform a

filtered/controlled release of the radioactive concentrations of the

reactor building air.

On November 25, at 1:00.a.m.,

the reactor building purge was started

to reduce the activity for building entry.

At 1:00 p.m., airborne Iodine activity was reduced to 27 MPC.

An

inspection team entered the reactor building and identified the

location of the leak. The inspectors witnessed the containment entry

on the video monitor in the control room. The leak was confirmed to

be from a 3/4 inch diameter instrument line that had pulled out of a

compression fitting just downstream of the instrument root valves for

the A hot leg RVLIS.

Within this area, one violation was identified.

3. Engineering Review

The configuration of the instrument line was as follows:

A 1 inch

diameter pipe is attached to the apex of the hot leg pipe.

At about

12 inches above the hot leg there is a tee junction.

One portion of the

tee goes to the high point vent system and the other portion, the line of

interest, is the line associated with the RVLIS instrumentation.

Downstream of the tee is a 3/8 inch diameter restrictor followed by a

3/4 inch isolation valve.

A 3/4 inch adapter is butt welded to this

isolation valve.

Then a 4 inch piece of stainless steel tubing is

attached to this adapter using a Parker/Hannifin compression fitting. A

series of tubing reducers were used to transition from the 3/4 inch tubing

to the 3/8 inch tubing which resulted in a total of six compression joints

per instrument line. At the end of the 3/8 inch tubing is a dp cell.

The

3/4 inch tubing was found to have been pulled out of the 3/4 inch tubing

adaptor at the valve, causing the RCS leakage.

The leakage was limited by

the 3/8 inch ID restrictor located just downstream of the tee and upstream

of the root valve. The root valve, fittings and tubing were subsequently

removed from the system for inspection and analysis.

12

Analysis of the tubing/fitting concluded that the tube pulled out of the

compression fitting due to inadequate engagement of the ferrule to the

tube. This conclusion was based on:

-

The gap measurement between the nut and the fitting was found to be

0.182 inch versus a nominal gap of 0.153 inches specified by the

manufacturer.

The manufacturer stated that the nominal valve did not

constitute acceptance criterion or specifications,

but rather

provided indication of proper installment.

-

Though the ferrule had been installed in the correct orientation,

visual examination of the tubing identified that the ferrule had not

been compressed onto the tubing.

An analysis performed by B&W indicated that, based on the shallow axial

score marks,

the ferrule had not bitten deeply into the tube.

In

addition, the crimping of the tube made by the ferrule was much less than

expected. The inside diameter of the tube was not appreciably deformed,

confirming improper crimping or swaging.

The outside diameter of the

tubing met specification requirements.

Based on the above,

the B&W

analysis concluded that improper makeup of the. fitting joint caused the

tube fitting to detach.

The ferrule had not been compressed enough to

hold the tube in place and allowed system pressure to force the tube out

of the ferrule and fitting. The licensee concluded that the compression

fitting nut was not tightened enough.

Oconee uses both Swagelock and Parker/Hannifin compression fittings.

Both manufacturers provide installation instructions which specify that

fittings should be installed "finger tight," then tightened an additional

number of turns depending on the tubing's outside diameter.

Scribing the

nut to positively indicate the: number of turns past finger tight is

recommended.

Swagelok provides specific acceptance criteria for the gap

between the nut and the fitting and provides a go/no-go inspection gage to

assure that fittings were properly tightened.

While installation

technicians are trained in this requirement, procedures for installation

di.d not contain instructions to reinforce the requirement.

The failed

fitting and the high number of other deficiencies, discussed below,

indicated that skill of the craft was inadequate as a means of ensuring

the manufacturers'

requirements were met in this area.

The installation

procedure, TN/3/A/32401/00/AK1, consists of a single sentence:

"Install

3/4 inch SS tubing, 3/4 inch x 1/2 inch union,

1/2 inch SS tubing, 1/2

inch x 3/8 inch union and 3/8 inch SS tubing between the root valve at the

Reactor Vessel Head and the 3/8 inch compression fitting between the tee

connection bellows sensor xxxx (bellows number specific to instrument).

Reference drawings xxxx."

Skill-of-the-craft as to how to actually put

fittings, unions tubing and ferrule together was implicit.

Manufacturers'

requirements,

recommendations and precautions were not specified in the

installation procedures.

After the single sentence installation

13

procedure, a sign-off space is provided for the individual performing the

installation (craft), a second space for an independent verifier (IV),

and

a third space for Quality Assurance (QA).

The completed procedures

reviewed by the inspector had initials in each -of the required spaces,

but

there are no requirements or acceptance criteria to any of the three

parties signing each space what is expected for that signature.

QA

inspection procedure QAE2,

Instrumentation Installation, Modification and

Maintenance Inspections,

Rev.

14,

governs the inspection.by the QA

individual for the case at issue.

The specific instructions to the QA

inspector consist of a single item in Section 5.7.c. requiring "For QA-1

and QA-3, verify that all fittings are tight."

"Tight" is a relative term

and could mean anything past finger tight.

10 CFR 50, Appendix B, Criterion V, Instructions, Procedures and Drawings

requires, in part, that for activities affecting quality, "instructions,

procedures

and drawings shall include appropriate quantitative or

qualitative acceptance criteria for determining that important activities

have been satisfactorily accomplished.

10 CFR 50, Appendix B, Criterion

X, Inspection, requires,

in part, that "If

inspection of processed

material or products is impossible or disadvantageous, indirect control by

monitoring processing methods, equipment, and personnel shall be provided.

Both inspection and process monitoring shall be provided when control is

inadequate without both."

Attributes of these requirements are not

contained in the records of the installation of the fittings for the RVLIS

modifications.

The inadequate procedure which resulted in an improper installation of a

compression fitting is identified as VIO 287/91-34-02: Failure in Quality

Assurance Process to Detect an Improper Installation of a Compression

Fitting.

The root valve tubing and associated fittings on both the "A" and "B" hot

legs RVLIS instrumentation were replaced with a modified design.

The

licensee inspected a sample of other Parker and Swagelok fittings located

in the reactor building. Approximately ten percent of the fittings were

found to be out of nominal range.

Consequently the licensee performed an

inspection of all similar fittings on the RCS and HPI system.

This

inspection included 455 fittings (191 Swagelok and 264 Parker/Hannifin).

Of these, twenty eight percent were found out of nominal range.

The

licensee attempted to tighten all of these fittings; however, 23 fittings

were left out of range as they could not be further tightened into nominal

range without use of excessive force.

The licensee performed an

.

engineering evaluation and concluded that it was acceptable to leave the

23 fittings out of range.

The licensee also inspected a broad range of components in the reactor

building due to exposure to humid atmosphere during the event.

These

included:

-

4 of 11 Environmentally Qualified (EQ)

transmitters were opened and

visually inspected. No evidence of water intrusion was found.

14

-

8 of 8 Target Rock EQ solenoid valves were successfully cycled and

tested.

26Limitorque limit switch housings were inspected. No moisture was

noted.

-

All 22 Fire detectors were checked..

One was found bad and was

replaced.

-

5 electrical penetration junction boxes were opened. No moisture was

evident.

-

2 Pressurizer heater junction boxes were inspected and 3 cables were

meggered.

No defects were found.

-

Sample of Incore instruments were checked.

No problems were

identified.

-

5 resistance temperature detectors on RCS were checked and were found

to respond satisfactorily.

-

The power operated relief valve acoustic leak monitor was visually

inspected.

-

2 of 4 reactor coolant pumps

(RCP)

were Hi Pot tested.

Oil was

changed on 1A2 RCP when.water was found in the upper oil pot.

In addition, 20 of 69 CRDs were meggered. The initial resistance values

obtained were within the tolerance limits. However, during startup, just

prior to criticality, a control rod in group 6 dropped into the core.

As

a result, the licensee initiated shutdown and decided to remegger all 69

CRDs.

Of these,

29 CRDs did not meet the acceptance criteria.

The

dropped rod's stator indicated a phase to phase fault.

It is postulated

that the heatup caused the intruded moisture to vaporize and affect the

resistances in the CRD mechanisms.

The 29 CRDs were purged with nitrogen

and remeggered.

Four new CRD stators were installed and 24 cable

connectors replaced.

Startup activities were initiated.

During a reactor building tour, a

small leak from the decay heat drop line was noted. The unit was cooled

and depressurized in order to accommodate work to change out portions of

piping in.the decay heat drop line. Details of the leak will be provided

in a future report.

At the end of this inspection period, the unit was in cold shutdown with

repairs on the decay heat dropline in progress.

Within this area, one violation was identified.

15

4.

Operational Review

Upon receiving indications of a fire in the reactor building as well as

indications of increased makeup to the RCS, increase in reactor building

sump levels, and decreasing pressurizer levels, operators in the Unit 3

control room correctly diagnosed the problem as being excessive RCS

leakage.

They began a rapid controlled shutdown, and correctly declared

an ALERT emergency classification.

Some difficulties were experienced at

35 percent power and a reactor trip occurred.

The trip -was due to

divergent steam pressure oscillations and was unavoidable due to the short

period of the oscillations.

Another difficulty experienced during

shutdown was caused by the failure of operators to adhere to a step in the

shutdown procedure. The operators exhibited sound judgement, knowledge of

plant arrangement and safety consciousness.

With one exception noted

above, all procedures were followed.

Communications between the control

room and TSC and within the control room were carried out satisfactorily.

Emergency as well as operating procedures were adequate to diagnose,

respond to and mitigate the event.

Within this area, no violations or deviations were identified.

5. Radiological Review.

The failure of the compression fitting on Unit 3 resulted in approximately

87,000 gallons of reactor coolant leaking from the instrument line.

The

leakage was contained within the reactor building. Activity levels in the

reactor building due to Iodine and noble gases were also significantly

elevated following the event.

High dose rates as well as contamination

levels were produced in portions of the reactor building. The licensee's

response during the event was both prudent and effective. The licensee

correctly assessed the root cause of the event and took steps to ensure

plant personnel's and the public's radiological safety.

Reactor.coolant from the leak through the instrument line had accumulated

in the basement of the reactor building. This was gradually pumped to the

Miscellaneous Waste Holdup tanks

(MWHUT)

located in the auxiliary

building. The MWHUT has a capacity of approximately 15,000 gallons. From

the MWHUT,

the reactor coolant was pumped to the Feeder tanks located in

the Radwaste facility for processing. From the Feeder tanks, the coolant

was channeled through a set of filter/demineralizers to reduce the

activity levels to below regulatory requirements. The processed coolant

was then held up in waste monitor tanks where it was sampled.

After

ensuring acceptable levels of radioactivity, the contents of the waste

monitor tanks were released to Lake Hartwell.

The licensee started

transferring the effluent from the reactor building at 11:58 p.m.,

on

November 24, 1991. The releases were completed by 5:15 p.m.,

November 28,

1991.

16

Airborne radioactivity concentrations were high, particularly Iodine, due

to the leaking fuel pins as well as the unit trip from 35 percent power.

The reactor building purge system was used to lower airborne activity in.

the reactor building. The reactor building purge system is a once through

ventilation system which filters reactor building air through High

Efficiency particulate air and carbon adsorber filters prior to release

through the unit vent. The purge.exhaust system was.started at 1:08 p.m.,

on November 25, 1991.

Concentrations of Iodine and noble gas ranged

downward over the 25th and 26th of November. During this release, neither

the licensee's nor the. state of South Carolina's environmental survey

teams detected any increase of radioactivity in the airborne environment.

On November 26,

1991, with Iodine concentrations between 7.12 and 12.55

MPC, fourteen licensee personnel made entry into the unit 3 reactor

building. The survey results obtained by Health Physics were as follows:

RADIATION DOSE RATES (mR/hr)

Area

High Contact (1")

General Area (18")

1st floor

100

5-8

2nd floor

60

5-15

3rd floor

5-20

4th floor

700 10-300

"A" cavity

-at leak

450

150-200

-West stairs

150-200

"A" cooler

120

10-60

"D" cooler

160

"C" cooler

120

CONTAMINATION LEVELS

1st floor -

10,000 cpm/100 cm2 up to 2 mR/hr gamma;.09 MRAD Beta

2nd floor -

2,000 cpm up to 66 mRrad Beta

3rd floor - 19.6 mrad Beta up to 135 mrad Beta; 6 mR/hr gamma

4th floor -

5-40 mR gamma; 2,440 mrad Beta

"A" cavity (at leak) -

180 mR gamma; 6,420 mrad Beta

17

All personnel wore a full set of protective clothing, wet suits, .and self

contained breathing apparatus (SCBAs) during the entry.. Upon exiting at

5:10 p.m. on November 26, no personnel were found to be contaminated after

removing the protective clothing.

The licensee performed decontamination of the reactor building in

conjunction with repair of the leak and investigation for damage to.

components.

The target levels of 5,000 to 15,000 disintegrations per

minute per 100 centimeters square (dpm/100 cm2) were not achieved. After

using high pressure spray equipment in various areas,

smearable

contamination levels ranged as high as 1 to 10 mrad Beta on the floors and

up to 100 mrad Beta in the area of the leak.

During heatup and

pressurization on December 2, 1991,

Iodine levels began to increase.

Iodine concentration increased from 12 times MPC. to 45 times MPC on

December 4, 1991.

On December 5, 1991, just prior to criticality the unit

experienced a rod drop caused by a problem with a stator.

During

cooldown, Iodine and noble gas levels decreased to less than 1 times MPC

upon entry.

The licensee calculated the dose to public due to the releases.

The

numbers indicate the dose that a person would get if the person were to be

present.at the site boundry (approximately 1 mile) for the duration of the

release.

.

SOURCE/CURIES

DOSE TO WHOLE BODY

DOSE TO THYROID

Liquid .0305 Ci gross

.00139 mrem

.0122 mren

.0165 Ci Tritium (.015% of annual limit) (.0407% of annual

limit)

.293 Ci Noble Gas

Noble Gas 672 Ci

.00218 mrad

N/A

(.00727% of annual limit)

Iodine Gas

.0004 mren

(estimated)

(.114 percent of annual

limit)

Within this area, no violations or deviations were identified.

6. Emergency Preparedness Review

An ALERT emergency classification was declared as a result of the RCS

leak. A site assembly was performed; the TSC, OSC and the CMC were also

activated.

The inspector reviewed the emergency response activities

associated with the recognition, declaration, initial and followup

notifications, and activation of the emergency response facilities.

The

licensee used approved procedures and emergency response plan.

Trained

18

personnel made timely recognition, classification, initial notification,

and followup notifications.

Site assembly.was completed in a timely

manner and a field team was appropriately dispatched. Cellular telephone

compensated for radio communication difficulties with the field team.

The

licensee's emergency organization responded and performed in a

satisfactory manner.

Within this area, no violations or deviations were identified.

7. Exit Interview

The inspection scope and findings were summarized on December 23,

1991,.

with those persons indicated in paragraph 1 above.

The inspectors

described the areas inspected and discussed in detail the inspection

findings listed below.

No dissenting comments were received from the

licensee.

The licensee did not identify as proprietary any of the

material provided to or reviewed by the inspectors during this inspection.

Item Number

Description/Reference Paragraph

VIO 287/91-34-01

Failure to Follow Procedures (paragraph

2.c)

VIO 287/91-34-02

Inadequate Installation and Inspection

Procedures (paragraph 3)