ML16138A590
| ML16138A590 | |
| Person / Time | |
|---|---|
| Site: | Oconee |
| Issue date: | 04/30/1987 |
| From: | Youngblood B Office of Nuclear Reactor Regulation |
| To: | |
| Shared Package | |
| ML16138A591 | List: |
| References | |
| NUDOCS 8705060378 | |
| Download: ML16138A590 (12) | |
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UNITED STATES NUCLEAR REGULATORY COMMISSION WASHINGTON, D. C. 20555 DUKE POWER COMPANY DOCKET NO. 50-269 OCONEE NUCLEAR STATION, UNIT 1 AMENDMENT TO FACILITY OPERATING LICENSE Amendment No. 157 License No. DPR-38
- 1. The Nuclear Regulatory Commission (the Commission) has found that:
A. The application for amendment to the Oconee Nuclear Station, Unit 1 (the facility) Facility Operating License No. DPR-38 filed by the Duke Power Company (the licensee) dated August 15, 1984, as revised July 3, 1985, complies with the standards and requirements of the Atomic Energy Act of 1954, as amended (the Act) and the Commission's rules and regulations set forth in 10 CFR Chapter I; B. The facility will operate in conformity with the application, the provisions of the Act, and the rules and regulations of the Commission; C. There is reasonable assurance (i) that the activities authorized by this amendment can be conducted without endangering the health and safety of the public, and (ii) that such activities will be conducted in compliance with the Commission's regulations set forth in 10 CFR Chapter 1; D. The issuance of this license amendment will not be inimical to the common defense and security or to the health and safety of the public; and E. The issuance of this amendment is in accordance with 10 CFR Part 51 of the Commission's regulations, and all applicable requirements have been satisfied.
- 2. Accordingly, the license is amended by changes to the Technical Soecifications as indicated in the attachments to this license amendment, and Paragraph 3.B of Facility Operating License No. DPR-38 is hereby amended to read as follows:
3.B Technical Specifications The Technical Specifications contained in Appendices A and B, as revised through Amendment No. 157, are hereby incorporated in the license. The licensee shall operate the facility in accordance with the Technical Specifications.
6705060378 670430 PDR ADOCK 05000269 P
-2
- 3. This license amendment is effective as of its date of issuance.
FOR THE NUCLEAR REGULATORY COMMISSION B.J. Youngblood, Director Project Directorate 11-3 Division of Reactor Projects -
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Attachment:
Technical Specification Changes Date of Issuance: April 30, 1987 PII l3nRP-I/II PDI -/DRP-I/II aLPDI Ij9 5'riIP-oIIi 04 an/rad HP s
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0 UNITED STATES NUCLEAR REGULATORY COMMISSION 0
o WASHINGTON, D. C. 20555 DUKE POWER COMPANY DOCKET NO. 50-270 OCONEE NUCLEAR STATION, UNIT 2 AMENDMENT TO FACILITY OPERATING LICENSE Amendment No. 157 License No. DPR-47
- 1. The Nuclear Regulatory Commission (the Commission) has found that:
A. The application for amendment to the Oconee Nuclear Station, Unit 2 (the facility) Facility Operating License No. DPR-47 filed by the Duke Power Company (the licensee) dated August 15, 1984, as revised July 3, 1985, complies with the standards and requirements of the Atomic Energy Act of 1954, as amended (the Act) and the Commission's rules and regulations set forth in 10 CFR Chapter I; B. The facility will operate in conformity with the application, the provisions of the Act, and the rules and regulations of the Commission; C. There is reasonable assurance (i) that the activities authorized by this amendment can be conducted without endangering the health and safety of the public, and (ii) that such activities will be conducted in compliance with the Commission's regulations set forth in 10 CFR Chapter 1; D. The issuance of this license amendment will not be inimical to the common defense and security or to the health and safety of the public; and E. The issuance of this amendment is in accordance with 10 CFR Part 51 of the Commission's regulations, and all applicable requirements have been satisfied.
- 2. Accordingly, the license is amended by changes to the Technical Specifications as indicated in the attachments to this license amendment, and Paragraph 3.B of Facility Operating License No. DPR-47 is hereby amended to read as follows:
3.B Technical Specifications The Technical Specifications contained in Appendices A and B, as revised through Amendment No. 157, are hereby incorporated in the license.
The licensee shall operate the facility in accordance with the Technical Specifications.
-2
- 3. This license amendment is effective as of its date of issuance.
FOR THE NUCLEAR REGULATORY COMMISSION B.J. Youngblood, Director Project Directorate 11-3 Division of Reactor Projects -
I/II
Attachment:
Technical Specification Changes Date of Issuance: April 30, 1987 POI 3DRP-I/II P
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0VS UNITED STATES NUCLEAR REGULATORY COMMISSION WASHINGTON, D. C. 20555 DUKE POWER COMPANY DOCKET NO. 50-287 OCONEE NUCLEAR STATION, UNIT 3 AMENDMENT TO FACILITY OPERATING LICENSE Amendment No. 154 License No. DPR-55
- 1. The Nuclear Regulatory Commission (the Commission) has found that:
A. The application for amendment to the Oconee Nuclear Station, Unit 3 (the facility) Facility Operating License No. DPR-55 filed by the Duke Power Company (the licensee) dated August 15, 1984, as revised on July 3, 1985, complies with the standards and requirements of the Atomic Energy Act of 1954, as amended (the Act) and the Commission's rules and regulations set forth in 10 CFR Chapter I; B. The facility will operate in conformity with the application, the provisions of the Act, and the rules and regulations of the Commission; C. There is reasonable assurance (i) that the activities authorized by this amendment can be conducted without endangering the health and safety of the public, and (ii) that such activities will be conducted in compliance with the Commission's regulations set forth in 10 CFR Chapter 1; D. The issuance of this license amendment will not be inimical to the common defense and security or to the health and safety of the public; and E. The issuance of this amendment is in accordance with 10 CFR Part 51 of the Commission's regulations, and all applicable requirements have been satisfied.
- 2. Accordingly, the license is amended by changes to the Technical Specifications as indicated in the attachments to this license amendment, and Paragraph 3.B of Facility Operating License No. DPR-55 is hereby amended to read as follows:
3.B Technical Specifications The Technical Specifications contained in Appendices A and B, as revised through Amendment No. 154, are hereby incorporated in the license. The licensee shall operate the facility in accordance with the Technical Specifications.
-2
- 3. This license amendment is effective as of its date of issuance.
FOR THE NUCLEAR REGULATORY COMMISSION B.J. Youngblood, Director Project Directorate 11-3 Division of Reactor Projects -
I/II
Attachment:
Technical Specification, Changes Date of Issuance: April 30, 1987 P I 3//RP-I/II
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ATTACHMENT TO LICENSE AMENDMENTS AMENDMENT NO. 157 TO DPR-38 AMENDMENT NO. 157 TO DPR-47 AMENDMENT'NO. 154 TO DPR-55 DOCKET NOS. 50-269, 50-270, AND 50-287 Replace the following pages of the Appendix "A" Technical Specifications with the attached pages. The revised pages are identified by amendment number and contain vertical lines indicating the areas of change.
Remove Insert Page Page iv iv 3.6-1 3.6-1 3.6-2 3.6-2 3.6-3 3.6-3 4.4-20
Section Page 3.10 RADIOACTIVE GASEOUS EFFLUENTS 3.10-1 3.11 SOLID RADIOACTIVE WASTE 3.11-1 3.12 REACTOR BUILDING POLAR CRANE AND AUXILIARY HOIST 3.12-1 3.13 SECONDARY SYSTEM ACTIVITY 3.13-1 3.14 SNUBBERS 3.14-1 3.15 PENETRATION ROOM VENTILATION SYSTEMS 3.15-1 3.16 HYDROGEN PURGE SYSTEM 3.16-1 3.17 FIRE PROTECTION AND DETECTION SYSTEMS 3.17-1 4
SURVEILLANCE REQUIREMENTS 4.0-1 4.0 SURVEILLANCE STANDARDS 4.0-1 4.1 OPERATIONAL SAFETY REVIEW 4.1-1 4.2 STRUCTURAL INTEGRITY OF ASME CODE CLASS 1, 2 AND 3 4.2-1 COMPONENTS 4.3 TESTING FOLLOWING OPENING OF SYSTEM 4.3-1 4.4 REACTOR BUILDING 4.4-1 4.4.1 Containment Leakage Tests 4.4-1 4.4.2 Structural Integrity 4.4-14 4.4.3 Hydrogen Purge System 4.4-17 4.4.4 Reactor Building Purge System 4.4-20 4.5 EMERGENCY CORE COOLING SYSTEMS AND REACTOR BUILDING 4.5-1 COOLING SYSTEMS PERIODIC TESTING 4.5.1 Emergency Core Cooling Systems 4.5-1 4.5.2 Reactor Building Cooling Systems 4.5-6 4.5.3 Penetration Room Ventilation System 4.5-10 4.5.4 Low Pressure Injection System Leakage 4.5-12 4.6 EMERGENCY POWER PERIODIC TESTING 4.6-1 4.7 REACTOR CONTROL ROD SYSTEM TESTS 4.7-1 4.7.1 Control Rod Trip Insertion Time 4.7-1 4.7.2 Control Rod Program Verification 4.7-2 4.8 MAIN STEAM STOP VALVES 4.8-1 OCONEE -
UNITS 1, 2 & 3 iv Amendment No. 157 (Unit 1)
Amendment No. 157 (Unit 2)
Amendment No. 154 (Unit 3)
3..6-REACTOR BUILDING Applicability Applies to the containment when the reactor is in conditions other than refueling shutdown.
Objective To assure containment integrity during shutdown (other than refueling shutdown), startup and operation.
Spec4 fication 3.6.1 Containment integrity shall be maintained whenever all three (3) of the following conditions exist:
- a.
Reactor coolant pressure is 300 psig or greater
- b.
Reactor coolant temperature is 200oF or greater
- c.
Nuclear fuel is in the core 3.6.2 Containment integrity shall be maintained whenever the reactor is subcritical by less than 1% Ak/k or whenever positive reactivity insertions are being made which would result in the reactor being subcritical by less than 1% Ak/k.
3.6.3 Exceptions to 3.6.1 and 3.6.2 shall be as follows:
- a.
If either the personnel or emergency hatches become inoperable, except as a result of an inoperable door gasket, the hatch shall be restored to an operable status within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, or the reactor shall be in cold shutdown within the next 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />.
If a hatch is inoperable due to an inoperable door gasket:
- 1. The remaining door of the affected hatch shall be closed and sealed. If the inner door gasket is inoperable, momentary passage (not to exceed 10 minutes for each opening) is permitted through the outer door for repair or test of the inner door, provided that the outer door gasket is leak tested within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> after opening of the outer door.
- 2.
The hatch shall be restored to operable status within seven days or the reactor shall be in cold shutdown within the next 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />.
- b.
The Reactor Building purge supply and exhaust isolation valves shall be closed except as allowed by Specification 3.6.3.b.1 and 3.6.3.b.2.
- 1.
The Reactor Building purge system may be operated, with the supply and exhaust isolation valves open, when the Reactor Coolant System temperature is below 250aF and pressure is below 350 psig.
OCONEE -
UNITS 1, 2 & 3 3.6-1 Amendment No. 157 (Unit 1)
Amendment No.
157 (Unit 2)
Amendment No. 154 (Unit 3)
- 2.
For plant conditions when the Reactor Coolant System temperature is above 250 0F and pressure is above 350 psig but the reactor is at or below hot shutdown, one Reactor Building Purge isolation valve on each penetration may be open for testing and/or maintenance-per Specification 4.4.4.1 and 3.6.6.
- 3.
For plant conditions other than contained in Specification 3.6.3.b.1,.2 above, with one or more Reactor Building purge valves open, the open valves shall be closed within one hour, or the plant shall be in hot shutdown within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and within an additional 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, Reactor Coolant System temperature below 250aF and pressure below 350 psig.
- c.
A containment isolation valve, other than a Reactor Building Purge isolation valve, may be inoperable provided either:
- 1.
The inoperable valve is restored to operable status within four hours.
- 2.
The affected penetration is isolated within four hours by the use of a deactivated automatic valve secured and locked in the isolated position.
- 3.
The affected penetration is isolated within four hours by the use of a closed manual valve or blind flange.
- 4.
The reactor is in the hot shutdown condition within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and cold shutdown within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
3.6.4 The reactor building internal pressure shall not exceed 1.5 psig or five inches of Hg if the reactor is critical.
3.6.5 Prior to criticality following refueling shutdown, a check shall be made to confirm that all manual containment isolation valves which should be closed are closed and tagged.
3.6.6 The combined leakage rate for all penetrations and valves shall be determined in accordance with Specification 4.4.1.2.
If, based on the most recent surveillance testing results the combined leakage rate exceeds the specified value and containment integrity is required then,
- 1) corrective action of Specification 3.6.3.c is met, or
- 2) repairs shall be initiated immediately and conformance with specified value shall be demonstrated within 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> or the reactor shall be in cold shutdown within an additional 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />.
OCONEE -
UNITS 1, 2 & 3 3.6-2 Amendment No. 157 (Unit 1)
Amendment No. 157 (Unit 2)
Amendment No. 154 (Unit 3)
Bases The Reactor Coolant System conditions of cold shutdown assure that no steam will be formed and hence no pressure buildup in the containment if the Reactor Coolant System ruptures.
The selected shutdown conditions are based on the type of activities that are being carried out and will preclude criticality in any occurrence.
The reactor building is designed for an internal pressure of 59 psig and an external pressure 3.0 psi greater than the internal pressure. The design external pressure of 3.0 psi corresponds to a margin of 0.5 psi above the differential pressure that could be developed if the building is sealed with an internal temperature of 120aF with a barometric pressure of 29.0 inches of Hg and the building is subsequently cooled to an internal temperature of 801F with a concurrent rise in barometric pressure to 31.0 inches of Hg. The weather conditions assumed here are conservative since an evaluation of National Weather Service records for this area indicates that from 1918 to 1970 the lowest barometric pressure recorded is 29.05 inches of Hg and the highest of 30.85 inches of Hg.
Operation with a personnel or emergency hatch inoperable does not impair containment integrity since either door meets the design specifications for structural integrity and leak rate. Momentary passage through the outer door is necessary should the inner door gasket be inoperative to install or remove auxiliary restraint beams on the inner door to allow testing of the hatch.
The time limits imposed permit completion of haintenance action and the performance of a local leak rate test when required or the orderly shutdown and cooldown of the reactor. Timely corrective action for an inoperable containment isolation valve is also specified.
When containment integrity is established, the limits of 10CFRI00 will not be exceeded should the maximum hypothetical accident occur.
The Reactor Building purge system was designed to allow cleanup of the Reactor Building atmosphere. It is normally operated during a unit shutdown which will require entry into the Reactor Building. It is used to purge the Reactor Building with fresh air to reduce the contaminant levels within the Building atmosphere, thus reducing overall personnel exposure. At times, certain safety related functions necessitate entry into the Reactor Building prior to cold shutdown conditions. These include isolation of leaking primary coolant system valves and visual inspections following outages. Use of the purge system tends to minimize any personnel exposure while not significantly contributing to overall plant risk.
The Reactor Building Purge System is required to be isolated whenever the RCS temperature is above 250aF and pressure is above 350 psig. The maximum pressure limit of 350 psig is based on the Oconee Unit 1 NPSH curve for RC pump operation. This will give a reasonable operating margin for the pumps while operating the purge. The LCO allows one isolation valve to be open on each penetration at or below hot shutdown for testing/or maintenance.
REFERENCES FSAR, Section 3.8 OCONEE -
UNITS 1, 2 & 3 3.6-3 Amendment No. 157 (Unit 1)
Amendment No. 157 (Unit 2)
Amendment No. 154 (Unit 3)
4.4.4 Reactor Building Purge System Applicability Applies to the Reactor Building Purge System.
Objective To verify that the Reactor Building Purge System is operable.
Specification 4.4.4.1 Each shutdown, when the purge valves have been operated, leakage integrity tests shall be performed on the containment purge isolation valves after final closing and prior to going above hot shutdown. If the purge valves have not been operated, leakage integrity tests shall be performed prior to going above hot shutdown unless such tests have been conducted within the proceeding six months. If the acceptance criteria of Specification 4.4.1.2.3 are not met, Specification 3.6.6 shall apply. Unit shutdown to conduct the test and/or effect repairs is specifically not required.
4.4.4.2 Monthly, when the unit is above 250aF and 350 psig, the containment purge isolation valves shall be verified closed.
4.4.4.3 Each refueling the valve seals of the containment purge isolation valves shall be visually inspected and adjusted or replaced as appropriate.
4.4.4.4 Prior to use of the purge system at conditions between cold shutdown and 250aF and 350 psig, the isolation valves shall be exercise tested in accordance with the requirements (except test frequency) of the applicable edition of the ASHE Boiler and Pressure Vessel Code,Section XI.
4.4.4.5 The pneumatically operated purge isolation valves shall be verified to close in response to a control signal from RIA-45 when the system is tested prior to refueling operations per Specification 3.8.10.
Bases Leakage integrity tests of the purge supply and isolation valves are conducted in order to identify excessive degradation of the resilient seals. Excessive leakage past resilient seals is typically caused by severe environmental conditions and/or wear due to frequent use.
The pneumatically operated purge isolation valves are tested prior to refueling operations because the only automatic isolation system in service at refueling is through RIA-45, which only closes the pneumatic isolation valves.
OCONEE -
UNITS 1, 2 & 3 4.4-20 Amendment No. 157 (Unit 1)
Amendment No. 157 (Unit 2)
Amendment No. 154 (Unit 3)