ML15239A004

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SALP Repts 50-269/86-02,50-270/86-02 & 50-287/86-02 for Sept 1984 - Feb 1986
ML15239A004
Person / Time
Site: 05000000, Oconee
Issue date: 06/19/1986
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML15239A003 List:
References
50-269-86-02, 50-269-86-2, 50-270-86-02, 50-270-86-2, 50-287-86-02, 50-287-86-2, NUDOCS 8607100493
Download: ML15239A004 (38)


See also: IR 05000269/1986002

Text

JUN 19 1986

ENCLOSURE 1

SALP BOARD REPORT

U. S. NUCLEAR REGULATORY COMMISSION

REGION II

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

Inspection Report Numbers

50-269/86-02; 50-270/86-02; 50-287/86-02

DUKE POWER COMPANY

OCONEE NUCLEAR STATION UNITS 1, 2, AND 3

September 1, 1984, through February 28, 1986

8607100493 860619

PDR ADOCK 05000269

PDR

I. Introduction

The Systematic Assessment of Licensee Performance

(SALP)

program is an

integrated NRC staff effort to collect available observations and data on a

periodic basis and to evaluate licensee performance based

upon this

information.

The SALP program is supplemental to normal

regulatory

processes used to determine compliance with NRC rules and regulations. The

SALP program is intended to be sufficiently diagnostic to provide a rational

basis for allocating NRC resources and to provide meaningful guidance to

licensee management to promote quality and safety of plant construction and

operation.

An

NRC

SALP Board,

composed of the staff members listed below,

met on

April 23,

1986,

to review the collection of performance observations and

data to assess licensee performance in accordance with guidance in NRC

Manual Chapter 0516,

"Systematic Assessment of Licensee Performance."

A

summary of the guidance and evaluation criteria is provided in Paragraph II

of this report.

This report is the SALP Board's assessment of the licensee's safety

performance at the Oconee Nuclear Station for the period September 1, 1984,

through February 28, 1986.

SALP Board for Oconee Nuclear Station

R. D. Walker, Director, Division of Reactor Projects (DRP), RII (Chairman)

A. F. Gibson, Director, Division of Reactor Safety (DRS), RII

J. P. Stohr, Director, Division of Radiation Safety and Safeguards, RII

V. L. Brownlee, Chief, Reactor Projects Branch 3 (RPB3), DRP, RH

G. E. Edison, Deputy Project Director, PWR Licensing Division B, NRR

H. Pastis, Project Manager (Oconee), PWR Licensing Division B, NRR

J. C. Bryant, Senior Resident Inspector, Oconee, DRP, RII

Attendees at SALP Meeting

R. D. Walker, Director, Division of Reactor Projects (DRP), RH (Chairman)

A. F. Gibson, Director, Division of Reactor Safety (DRS), RII

J. P. Stohr, Director, Division of Radiation Safety and Safeguards, RH

L. A. Reyes, Deputy Director, DRP, RII

V. L. Brownlee, Chief, Reactor Projects Branch 3 (RPB3), DRP, RII

G. E. Edison, Deputy Project Director, PWR Licensing Division B, NRR

H. Pastis, Project Manager (Oconee), PWR Licensing Division B, NRR

J. C. Bryant, Senior Resident Inspector, Oconee, DRP, RII

K. D. Landis, Chief, Technical Support Staff (TSS), DRP, RII

C. W. Burger, Project Engineer, RPB3, DRP, RII

J. K. Rausch, Reactor Engineer, TSS, DRP, RII

T. C. MacArthur, Radiation Specialist, TSS, DRP, RII

Enclosure 1

2

II. Criteria

Licensee performance is assessed in selected functional areas depending on

whether the facility has been in the construction,

preoperational,

or

operating phase during the SALP review period.

Each functional area

normally represents an area which is significant to nuclear safety and the

environment and which is a normal programmatic area. Some functional areas

may not be assessed because of little or no licensee activity or lack of

meaningful NRC observations.

Special areas

may be added to highlight

significant observations.

One or more of the following evaluation criteria was used to assess each

functional area; however,

the SALP Board is not limited to these criteria

and others may have been used where appropriate.

A. Management involvement in assuring quality

B. Approach to the resolution of technical issues from a safety standpoint

C. Responsiveness to NRC initiatives

D. Enforcement history

E. Reporting and analysis of reportable events

F. Staffing (including management)

G. Training and qualification effectiveness

Based upon the SALP Board assessment,

each functional area evaluated is

classified into one of three performance categories.

The definitions of

these performance categories are:

Category 1:

Reduced NRC attention may be appropriate. Licensee management

attention and involvement are aggressive and oriented toward nuclear safety;

licensee resources are ample and effectively used such that a high level of

performance with respect to operational safety or construction quality is

being achieved.

Category 2:

NRC attention should be maintained at normal levels.

Licensee

management attention and involvement are evident and are concerned with

nuclear safety; licensee resources are adequate and are reasonably effective

such that satisfactory performance with respect to operational safety or

construction quality is being achieved.

Enclosure 1

3

Category 3:

Both NRC and licensee attention should be increased. Licensee

management attention or involvement is acceptable and considers nuclear

safety, but weaknesses are evident; licensee resources appear to be strained

or not effectively used such that minimally satisfactory performance with

respect to operational safety or construction quality is being achieved.

The functional area being evaluated may have some attributes that would

place the evaluation in Category 1, and others that would place it in either

Category 2 or 3. The final rating for each functional area is a composite

of the attributes tempered with the judgement of NRC management as to the

significance of individual items.

The SALP Board may also include an appraisal of the performance trend of a

functional area.

This performance trend will only be used when both a

definite trend of performance within the evaluation period is discernible

and the Board believes that continuation of the trend may result in a change

of performance level.

The trend, if used, is defined as:

Improving:

Licensee performance was determined to be improving near the

close of the assessment period.

Declining:

Licensee performance was determined to be declining near the

close of the assessment period.

III. Summary of Results

Overall Facility Evaluation

During this SALP assessment period, the Oconee facility was effectively

managed and achieved a satisfactory level of operational safety.

Strengths

were noted in the areas of plant operations, surveillance, fire protection,

emergency preparedness and outages.

The plant operations and the fire

protection functional areas have shown improvement due to well qualified

operating staffs.

Weakness was noted in the area of maintenance as

evidenced by the number of reactor trips attributed to maintenance work.

The radiological controls functional area needs improvement in its QC

programs and management review areas. The security functional area shows a

lack of interface between security departments and other departments in the

remainder of the plant. Of special note is the establishment of a new

division for integrated scheduling.

This effort should be effective in

improving overall operations particularly in the maintenance, surveillance,

and outages functional areas.

Enclosure 1

4

May 1, 1983 -

September 1, 1984

Functional Area

August 31, 1984

February 28, 1986

Plant Operations

1

1

Radiological Controls

2

2

Maintenance

1

2

Surveillance

1

1

Fire Protection

Not Rated

1

Emergency Procedures

1

1

Security and Safeguards

1

2

Outages

1

1

Quality Programs and

2

2

Administrative Controls

Affecting Quality

Licensing Activities

2

2

Training

Not Rated

2

IV. Performance Analysis

A.

Plant Operations

1. Analysis

During the evaluation period, routine inspections were performed

by the resident and regional staffs.

On day and night shifts

operations personnel were found to be alert, professional

and attentive to their duties. Plant housekeeping has improved

during the evaluation period,

and a major cleanup,

paintup,

decontamination program is in progress throughout the plant.

A special inspection was made by the Office of Nuclear Reactor

Regulation (NRR)

concerning plant susceptibility to "wrong unit

wrong train" events. In general, the plant was found satisfactory

in its approach to prevention of such events. During the assess

ment period,

one reactor trip occurred when

an

I&E mechanic

tripped the wrong train during a surveillance test.

The licensee

has a program for identifying all equipment with color coded, by

unit, signs listing the unit, system and equipment.

An INPO evaluation was conducted during the period.

The resident

inspectors reviewed the report and found that no serious problems

were identified. By inspection, the residents determined that the

licensee has taken positive action on those criticisms listed in

the INPO report.

Station management demonstrates commendable awareness of plant

operating conditions.

The inspectors have found the station

manager

and the department superintendents to be sufficiently

informed to discuss any event in detail.

The several layers of

management provide guidance and stay in touch without interfering

with SRO's and ROs in performance of their duties.

Enclosure 1

5

An evaluation of the content and quality of a representative

sample of the 38 Licensee Event Reports (LERs)

submitted by

Oconee 1, 2 and 3 during the SALP period was performed using a

refinement of the basic methodology presented in NUREG/CR-4178.

The results of this evaluation indicate that Oconee 1, 2 and 3

have an overall LER score in the top quarter of proficiency as

compared to the 49 units (i.e.,

licensees) that have

been

evaluated to date using this methodology.

The resident inspectors are kept informed of plant events and

reportable events are handled according to regulations.

The

approach to resolution of technical issues usually is very

thorough,

and the licensee has sufficient technical staff to

perform these duties.

The resident inspectors have found the

licensee to be responsive to issues expressed by themselves or

other NRC personnel.

During the reporting period, the licensee

initiated programs for rework of main steam code safety valves and

use of motor operated valve actuator testing (MOVATS) prior to

official NRC publications on the issues. Training of operations

personnel is kept current.

The inspectors witnessed simulator

training of personnel

concerning an event which occurred at

another site. The training took place just a few days after the

event and was quickly accomplished by calling in personnel on days

off where necessary.

The reactor operating staff is considerably larger than that

required by Technical Specifications (TS). Whereas TS require one

shift supervisor (SRO)

and two additional SROs for three unit

operation, the normal shift complement is the shift supervisor

plus six additional SROs. There are six RO's on shift rather than

the required five. Five nuclear equipment operators are required,

but the normal complement is eleven or twelve.

There are two

relief SRO's available; two SRO's on training at the Oconee

Technical Training Center (OTTC);

15 in the RO training class at

the OTTC;

and ten learners at the Technical Training Center

located near the McGuire site.

A degreed STA was added to the staff of each shift during the

reporting period.

These individuals are SRO licensed and STA

trained.

They report

to the Superintendent of Integrated

Scheduling.

One of their

normal

shift duties is priority

scheduling of shift maintenance personnel.

In addition to the shift operating engineer and his staff, to

support each reactor unit there is a unit operating engineer and

four assistant operating engineers.

These individuals are SRO

licensed and provide assistance, scheduling and continuity to the

operating staff. All licensed pesonnel are licensed on all three

units.

Enclosure 1

6

During the assessment period, Oconee Unit 2 completed a continuous

power production run of 439 days. Licensee efforts to improve the

quality of performance, aided by the plant simulator which became

operable at the end of the previous evaluation period, are having

a positive effect. There were no reactor trips caused by operator

error during the evaluation period.

Though there was an increase of one violation cited against

operations as compared to the previous assessment period, this in

not considered to be indicative of declining performance in

operation of the plant. The increase is partially due to a longer

evaluation period with a commensurate

increase in inspection

activity. One violation cited below concerns failure to delegate

administrative duties of the shift supervisor to non on-duty

personnel. This violation was essentially for failure to specify

in writing how these duties would be handled. As described above,

there are four extra SRO's on shift above technical specification

requirements.

These additional people normally handle any

required administrative duties.

Violations which were cited

against operations are as follows.

a.

Severity Level

IV violation for failure to delegate the

administrative duties of the shift supervisor to non-on duty

personnel.

(84-16, 15, 26)

b. Severity Level IV violation for exceeding permissible control

rod position limit at 15% power during power ascension.

(85-10)

c. Severity Level

IV violation for failure to log a valve

failure to open. All other required actions, including a

priority work request, were taken. (85-37)

d. Severity Level

IV violation for delay in shutdown for a

reactor coolant system leak.

Over a period of 40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br />,

hourly samples varied from 0.65 gpm above the Technical

Specifications limit of 1.0 gpm to 0.38 gpm below the limit

while the licensee attempted to identify the leak. (85-41)

e.

Severity Level V violation for incomplete documentation of

the controlling procedure prior to startup.

All required

actions had been taken.

(84-36)

f.

Severity Level V violation for a work request not properly

classified as safety related. (85-21)

Enclosure 1

7

2. Conclusion

Category:

1

3. Board Recommendation

No recommended.changes in NRC inspection resources.

B.

Radiological Controls

1. Analysis

During the evaluation period, inspections were performed by the

resident and regional

staffs.

This

included confirmatory

measurements using the Region II mobile laboratory.

The licensee's health physics staffing level was adequate and

compared favorably to other utilities of similar size in that an

adequate number of ANSI qualified licensee and contract health

physics technicians were available to support routine and outage

operations. The radiological effluents control staffing levels

and staff qualifications were acceptable. Key positions in the

radwaste management program and

environmental

surveillance

programs were filled with qualified staff.

The strengths of the health physics program were the quality of

the health physics technicians and the experience level of the

corporate and site health physics staffs.

The staff has a low

turnover rate and an effective training program.

The understanding of technical issues and approaches to technical

problem solving were deficient in several areas of the licensee's

radiological measurements and measurements quality control

(QC)

program. Failure to resolve previously identified measurement and

calibration items regarding liquid scintillation and gamma

spectroscopy system analyses resulted in violations concerning

inaccurate liquid and gaseous effluent measurements,

failure to

meet required lower limits of detection for gaseous effluent

measurements, and failure to complete radiochemical analyses of a

significant proportion of environmental samples. Review of spiked

sample confirmatory measurement results indicated a need for

improvement in QC programs and in management review areas to

assure the capability to identify and correct inaccurate measure

ments associated with vendor nuclide analyses.

Additional technical areas needing timely managment evaluation and

action included evaluation of

systematic biases

noted for

whole-body

counting

activities,

improved

surveillance

and

maintenance of radiation effluent monitoring instrumentation to

ensure operability, and the evaluation and resolution of

identified inaccurate

measurements

associated with the

Post

Enclosure 1

8

Accident Sampling Systems

(PASS).

Although the licensee was

responsive to the violations as noted by their prompt corrective

actions, more timely evaluation and resolution of the effluent

monitor and PASS issues is needed.

The licensee submitted the required effluent and environmental

reports; however, the second half 1984 report was submitted one

month late. Failure of licensee representatives to review and

resolve delays concerning radiochemical analyses by their approved

vendor laboratory resulted in the late submittal.

Liquid and

gaseous data were within established limits for total quantities

and concentration of material released. No significant trends in

releases or in estimated dose were noted.

During the rating

period, the licensee met the reporting requirements for anomalous

results in selected environmental

samples;

however,

licensee

management

involvement was considered deficient in that they

failed to thoroughly evaluate dose estimates using all environ

mental pathways to meet the intent of 40 CFR

190.

Following

additional review, dose estimates were determined to be within

40 CFR 190 limits.

During the evaluation period, the licensee's radiation work permit

and respiratory protection programs were found to be satisfactory.

Control of contamination and radioactive materials within the

facility was adequate.

From January 1985 to January 1986,

the

amount of contaminated area decreased from approximately 56,000 to

17,000 square feet which represents a 69 percent decrease.

In

1985, there was a 10 percent decrease in the number of clothing

and skin contamination incidents when compared to 1984.

During the evaluation period from January 1, 1985 to December 31,

1985, the licensee's collective occupational dose was 1303 man-rem

or 434 man-rem per unit. This compares favorably to the national

average exposure of 425 man-rem per unit for pressurized water

reactors.

The licensee has established and implemented an

aggressive control program.

During the evaluation period from January 1 to December 31, 1985,

the licensee disposed of 33,507 cubic feet of solid radioactive

waste containing 2,069 curies.

This is quite close to the

national average of 11,650 cubic feet per unit shipped by other

PWR facilities. However,

the radwaste shipping area resulted in

one violation for failure to transport radioactive material in a

strong, tight container.

Enclosure 1

9

Nine violations were identified:

a. Severity Level III for failure to transport radioactive

material in a strong, tight package as required by 10 CFR

71.5(A).

(85-03)

b. Severity Level IV for failure to have adequate procedures for

radiological effluent measurements. (84-30, 29, 32)

c. Severity Level IV for failure to meet detection limits for

radiological environmental samples.

(84-19, 18, 20)

d. Severity Level IV for failure to document E-bar calculations

correctly on

some occasions and,

in one case,

to base

calculations on 45 minutes elapsed time rather than the

actual elapsed time of 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />, 15 minutes. (85-26)

e. Severity Level

IV for failure to adequately control the

access to high radiation areas

as

required

by

10 CFR

20.203(c)(2).

(85-42)

f. Severity Level V for failure to meet required lower limits of

detection (LLD) for effluent measurements.

(84-30, 29, 32)

g. Severity Level V for failure to label containers of radio

active material as required by 10 CFR 20.203(f).

(85-30)

h.

Severity Level V for failure to post an airborne radio

activity area as required by 10 CFR 20.203(d).

(85-33)

i. Severity Level V violation for failure to address inoperable

effluent monitors in a semi annual report. (85-20)

2.

Conclusion

Category:

2

3. Board Recommendations

Licensee attention in this area was evident; particularly in the

staffing of health physics key positions.

It appears, however,

that there is room for improvement in the licensee's timeliness in

evaluating and resolving issues,

i.e., effluent monitor

and

post-accident sampling system.

Enclosure 1

10

C. Maintenance

1..

Analysis

During the evaluation period, maintenance performance was

inspected by regional and resident inspection staffs. Units 2 and

3 were each refueled during the assessment period; Unit 1 began

the period during a refueling outage and ended the period in

another refueling outage. Much of the maintenance work inspected

occurred during these outages and is discussed in the outage

section of this report.

The

maintenance

program

is well

organized and demonstrated

evidence of adequate planning and priority assignment; maintenance

procedures were generally adequate, complete and well maintained.

Licensee reponse to resident inspector and other NRC initiatives

has been satisfactory. The maintenance department is well staffed

and has made several major changes in staffing in the past three

years. In addition, there are initiatives in work to improve

capabilities of the personnel.

These changes are discussed below.

In

1983,

prior to the current assessment period, maintenance

personnel joined the operations rotating shifts.

Mechanical

maintenance has a supervisor and six mechanics on each shift,

while there is an Instrument and Electrical (I&E)

supervisor and

four technicians on each shift. This closer working relationship,

in addition to improved availability of maintenance personnel,

appears to be having a positive effect.

The maintenance department has a planning and scheduling section

for mechanical, I&E, and outage maintenance. While priorities and

timing are established by the Integrated Scheduling Department, as

described in the Surveillance Section of this report, the details

are handled by this 41 person section.

In addition to the scheduling section, plant maintenance has a

mechanical maintenance staff of about 160 persons and an I&E staff

of approximately 130. Also stationed at the Oconee site is the

Duke Power

Company

Construction

and Maintenance

Department

(CMD)-Southern Division, with a staff of approximately 350 persons

in the maintenance portion of CMD. These people are scheduled by

the Planning and Scheduling Section,

as needed,

to augment the

Plant Maintenance Department. CMD also supplies vendor assistance

as needed. Other off-site divisions of Duke Power Company provide

assistance where needed. The construction portion of CMD performs

modifications to the plant and also supplies, as needed, builders

for scaffold erection and other such work, bringing the available

work force for outages to about 1000 people.

This large pool of

personnel available for maintenance is a major asset.

Enclosure 1

11

Training of maintenance

personnel

is conducted at the DPC

facilities near Charlotte, at the Oconee site, and at vendor

training facilities where appropriate. A part of the DPC Employer

Training Qualification System

(ETQS),

which is a formalized

program including verification and documentation of skills, is

evaluation of each employee by his own supervisor and another for

the specific training needed to prepare him for any work to which

he may be assigned.

CMD maintenance employees are being brought into the ETQS program

with the goal of bringing them to the same level of proficiency as

the plant maintenance staff. The ETQS will verify the qualifica

tions of Oconee maintenance and interfacing maintenance support

personnel prior to their performing work.

Other initiatives in work include bringing the engineering groups

into closer relationship with mechanics and technicians to form

logical working groups and allow engineers to better understand

maintenance; concentration of persons on major problems; review of

equipment for the quality of maintenance and study by management,

engineers,

and other qualified personnel to improve the quality;

upgraded procedures, tooling, training and dedicated personnel to

specific work to enhance quality; electrical circuit analysis; and

bringing ALARA into planning and the work group to establish

responsibility there.

Planned to begin in 1986 and to be

completed in 1987 is a maintenance training center at Oconee.

The resident inspectors latest review of the maintenance backlog

revealed no problem with maintenance being kept current, but there

was a considerable backlog of station modifications.

During the

assessment period,

DPC assigned 14 additional engineers to the

site for a period of two years to study the backlog items for

relevance and to get the work brought up to date.

Four of the 15 reactor trips which occurred during the assessment

period may be attributed to maintenance work in progress at the

time.

a.

On April 26,

1985,

Unit 2 tripped from 72% power due to a

problem in the electro hydraulic control (EHC)

system.

At

the time,

maintenance personnel

were working inside the

cabinet. Examination revealed no questionable components.

b.

On July 10,

1985,

Unit 2 tripped while a mechanic was

investigating a problem with the ICS turbine header pressure

control. As he plugged in a test meter, a noise signal was

introduced causing turbine control and intercept valves to

close.

Enclosure 1

12

c.

On January 31, 1986, Unit 2 tripped while switchyard breaker

testing and maintenance were in progress.

A misalignment of

circuits, when a test signal was introduced, caused a load

rejection

resulting

in a generator/turbine/reactor

anticipatory trip.

d.

On January 31, 1986, Unit 1 tripped while switchyard breaker

testing and maintenance were in progress.

A combination of

one bus being out of service related to the Unit 2 trip four

hours earlier, and a miscommunication between a switchyard

mechanic and the control room caused Unit 1 generator output

to transfer to a single breaker.

The single breaker is

designed to accept the full load, but it failed to do so.

The maintenance personnel at work during trips c and d are

not a part of Oconee maintenance. Eight of the remaining 11

trips were the result of equipment failure.

Three violations were identified in the maintenance area as listed

below.

a. Severity Level IV violation for failure to file a noncon

forming item report in a timely manner. A Cuno filter in the

low pressure service water system had been installed in the

reverse direction.

When the error was discovered after the

system had been in operation for some time, corrective action

was taken immediately but the NCI report was not filed.

(84-28)

b. Severity Level IV violation for returning a modified sample

line to service prior to Design Engineering review of the.

change. Material of below required wall thickness had been

used. (85-41)

c. Severity Level V violation for inadequate development and

implementation

quidance for

CRD

breaker inspection and

maintenance activities.

Specific recommendations in the

vendor manual had not been included. (85-21)

2.

Conclusion

Category: 2

3.

Board Recommendation

The Board notes indications of strong management participation in

this area. No change in NRC inspection activity is recommended.

Enclosure 1

13

D. Surveillance

1. Analysis

During the assessment period, inspections of surveillance

activities were performed by the regional and resident inspection

staffs. The inspectors witnessed selected operational surveil

lances of reactor protective systems,

pump and valve operations,

calibration of instruments and others, and reviewed completed test

procedures. Startup tests and low power physics testing were

witnessed.

During outages, the inspectors witnessed and/or

reviewed inservice inspection activities, reactor vessel examina

tion,

performance testing of pump and valves,

and tendon and

snubber surveillance.

The quality of procedures in use was found to be good, and there

was evidence of prior planning and assignment of priorities.

Procedures were controlled and contained sufficient detail for the

control of activities.

Completed procedures were reviewed by

managers and by senior reactor operators. Surveillance activities

were conducted by qualified personnel,

and as witnessed by the

inspectors, suitable levels of management

became involved when

problems arose. Surveillances were supported by a competent QA

organization.

The Performance Section, which conducts surveillances, has a staff

of 33. These are knowledgeable engineers and technicians.

The

inspectors have found this group to be very professional. Actual

manipulation of equipment is performed by operators and mainte

nance personnel.

During the assessment period,

the licensee established a new

division for integrated scheduling.

This division handles the

overall schedule for operations, surveillance, maintenance and

outages. While the affected divisions do the detailed job

planning and manpower allocation, the new division considers the

overall plant needs and establishes priorities and time frames for

work performance. The permanently assigned integrated scheduling

engineer for each unit conducts the daily outage meetings when a

unit is shut down.

The division produces the integrated schedule

for the entire refueling outage to avoid conflicts between the

various departments, and resolves conflicts on a daily basis when

they occur.

The division also schedules the priorities for

surveillance and maintenance during operation.

The integrated scheduling division is headed by a superintendent,

indicating the priority assigned to the group.

This superinten

dent is completing SRO training.

While this training is not an

NRC requirement for the position, all of the plant superintendents

are SRO trained or are being trained.

Enclosure 1

14

Some

problems identified in the surveillance area included a

determination that the temperature and humidity of the instrument

calibration shop was not routinely verified although specified

requirements for temperature and humidity were in effect for some

instrument calibrations.

The licensee relied on

the

air

conditioning system to maintain the shop within the necessary

parameters during calibration. Another inspection determined that

trains A and B of the containment hydrogen monitoring system were

technically inoperable for a twenty day period due to inability to

calibrate the instruments to the specified tolerance.

The

licensee was aware of the problem and was attempting to resove it.

A technician,

while performing

a reactor protection

system

calibration and test, mistakenly tripped breakers in the wrong

channel. This resulted in a reactor trip.

This was a personnel

error and the only instance of wrong unit-wrong train error

identified during the assessment period.

The three violations cited against surveillance are listed below.

a.

Severity Level IV violation for failure to verify on a

regular basis that instrument shop temperature and humidity

met procedure requirements. (85-04)

b. Severity Level

IV. violation for allowing the containment

hydrogen monitor to be technically out of service for a

period of twenty days. (85-25)

c.

Severity Level IV violation for failure to follow procedure,

despite independent verification, in surveillance of a

reactor protection system,

resulting in a reactor trip.

(86-01)

2. Conclusion

Category:

1

3. Board Recommendation

The Board notes that the licensee's new division for integrated

scheduling has a potential for providing new initiatives in this

area. No change in NRC inspection activity is recommended.

E.

Fire Protection

1. Analysis

During this assessment period, inspections were conducted by the

regional and resident inspection staffs of the licensee's fire

protection and fire prevention program.

The licensee's imple

mentation of the 10 CFR 50,

Appendix R, safe shutdown capability

and associated fire protection features was not reviewed during

Enclosure 1

15

this assessment period. Resident inspectors witnessed a number of

fire drills including those where offsite support organizations

reported to the site and participated in the drill.

The licensee has issued procedures for the administrative control

of fire hazards within the plant, surveillance and maintenance of

the fire protection systems and equipment,

and organization and

training of a plant fire brigade.

These procedures were reviewed

and found to meet NRC requirements and guidelines.

The inspectors reviewed the licensee's implementation of the fire

protection and administrative controls. General housekeeping and

control of combustible and flammable materials were in need of

improvement

in several plant areas but corrective action was

promptly initiated. The fire protection extinguishing systems,

detection systems and fire barriers and fire barrier penetrations

were found to be in service.

Surveillance inspection and tests

and maintenance of the fire protection systems and features were

satisfactory except for the failure to conduct the semi-annual

surveillance on the licensee's C02 system. However, this item was

properly identified and reported to the NRC.

Organization and staffing of the plant fire brigade meet the NRC

guidelines. The training and drills for the brigade members meet

the frequency specified by the procedures and the NRC guidelines.

The annual fire protection/prevention audit and 24 month QA fire

protection

program audit by offsite organizations and the

triennial audit

by

an

outside fire protection organization

required by the Technical Specifications were reviewed.

These

audits were conducted within the specified frequency and covered

all essential elements of the fire protection program.

The

licensee had

implemented

corrective action

on

discrepancies

identified by the audit.

The licensee apparently identified, analyzed, and reported fire

prevention

events and discrepancies

as required

by

license

condition or Technical Specifications.

These reports were

reviewed and found to be satisfactory.

In general,

the management involvement and control in assuring

quality in the fire protection program is evident due to frequent

involvement in the site fire protection program and well

developed, issued and implemented protection administrative

procedures. The licensee's approach to resolution of technical

fire protection issues indicates an understanding of issues, and

is geared toward meeting the

requirements.

However, the

licensee's implementation of the 10 CFR 50, Appendix R fire

protection and

safe shutdown requirements have not yet been

verified by the NRC.

The responsiveness to NRC initiatives are

generally timely and thorough. Fire protection related violations

Enclosure 1

16

are rare. However, when violations do occur, effective corrective

action is promptly taken.

Licensee identified fire protection

related events or discrepancies are properly analyzed, promptly

reported and effective corrective action taken.

Staffing for the fire protection program is adequate to accomplish

the goals of the position within normal work hours with only

occasional overtime or backlog of work.

Fire protection staff

positions are identified and authorities and responsibilities are

clearly defined.

Personnel

are qualified for their assigned

duties. The fire brigade training program is well defined and

implemented.

No violations or deviations were identified during this assessment

period.

2. Conclusion

Category:

1

3. Board Recommendations

The Board notes that the licensee's implementation of the

10 CFR 50,

Appendix R was not reviewed during this period.

The

Board recommends that NRC inspection activities determine this at

an early date.

F. Emergency Preparedness

1. Analysis

During this assessment period,

inspections were performed by

regional

and

resident

inspection

staffs.

These included

observation of a small-scale exercise and two routine inspections

addressing emergency response and related implementing procedures.

The resident inspectors participated in the technical

support

center during a number of drills.

Routine inspections and exercise observations indicated that the

emergency organization and staffing were adequate. The corporate

emergency planning organization provided adequate support to the

plant. Key positions in corporate and plant emergency response

organizations were filled.

Corporate management appeared to be

committed to maintaining an effective emergency response program,

and was directly involved in the annual exercise and the followup

critique. Critiques were held following periodic drills as well

as the annual exercise and appropriate corrective actions were

taken to resolve identified problems.

Enclosure 1

17

Personnel assigned to the emergency organization understood their

emergency response roles and were adequately trained in required

areas

of emergency

response.

During

routine

inspection

interviews, walkthroughs and exercise observations, the emergency

response

personnel

adequately

identified

and

classified

hypothetical emergency events. The emergency response organiza

tion

promptly made

required

notifications,

and

provided

appropriate protective action recommendations. During the annual

exercise, however, the following findings were identified by the

NRC for corrective action: (1) radiological field teams failed to

define plume dimensions and identify the plume center line;

(2) frequent prompting of players by controllers and excessive

dialogue between controllers and players.

Corrective actions

initiated by the licensee for these findings included additional

training of radiological field teams and training regarding the

limit of interactions between controllers and players.

No

violations were issued for actions during the exercise, because

one purpose of such exercise is to identify weaknesses in program

implementation so that corrective actions can be taken by the

licensee.

The following essential elements for emergency response were found

acceptable: Emergency classification; notification and communica

tions; public information; shift staffing and augmentation;

emergency preparedness training, except as noted above;

dose

projection and assessment;

emergency worker protection;

post

accident measurements and instrumentation;

changes to the

emergency preparedness program;

and annual

quality assurance

audits of the plant and corporate emergency preparedness programs.

The exercise demonstrated that the plan and procedures could be

effectively implemented in the areas of communications, accident

assessment, and exposure control.

The emergency response

facilities, namely the TSC and OSC,

and the equipment therein,

were adequate to support radiological emergency events.

The

interim EOF,

however, requires additional available space and an

improved configuration. A permanent facility is planned. Current

use, however,

does not compromise

response capability.

The

licensee demonstrated

an adequate working relationship with

offsite emergency support organization.

No violations were identified regarding the licensee's implementa

tion of the emergency preparedness program.

2. Conclusion

Category:

1

3.

Board Recommendation

The Board recognizes an improving trend and has no recommended

changes in NRC inspection resources.

Enclosure 1

18

G.

Security and Safeguards

1. Analysis

During this evaluation period, various routine inspections were

performed by the resident and regional

staffs.

The

NRC's

Regulatory Effectiveness Review was also performed during this

period.

The licensee utilizes a contract security force which is monitored

by proprietary Security Technical Associates who continually audit

the

contractor

and

resolve

licensee

identified issues.

Additionally,

the contractor has its own Contract Compliance

Review Program which ensures each security shift adheres to the

licensee's approved security procedures.

During

this

evaluation

period,

inspectors witnessed

the

performance of the security force during various back-shifts.

During these irregular hours the security force appeared well

staffed, adequately equipped and professional in the conduct of

its routine duties.

A small turnover rate has allowed the

licensee to establish a reliable corps of experienced and

knowledgeable security officers. As noted in the previous SALP

report,

one strength in the licensee's security program is an

aggressive implementation of its Training and Qualification Plan.

The security shifts are not encumbered with extensive compensatory

measures necessary for failed security equipment.

This reflects

plant management's

attention

to

maintenance

and

setting

appropriate priority to the repair of security related hardware.

The licensee is in the final transition of upgrading its security

alarm system to include a new alarm station facility.

While the licensee has experienced an unusual increase in the

number and severity level of security related violations, they are

not indicative of a major security breakdown.

Upon analysis of

the trend, it appears that the majority of the violations are

symptomatic of problems associated with people,

procedures and

documentation, versus hardware and equipment. Specifically, two

of the five violations listed below concern degraded security

barriers and are attributable to a lack of a comprehensive

interface between the security organization and other departments

of the plant.

A third violation deals with

an

inadequate

procedure and a fourth violation concerns inadequate documenta

tion.

Although the licensee has corporate and site management support of

its security program,

it

appears that intraplant communication

needs to be emphasized so that non-security individuals are aware

of their security responsibilities.

Enclosure 1

19

The violations identified were as follows:

a. Severity Level III due to inadequate security barriers.

(85-39) Civil Penalty of $25,000 issued.

b. Severity Level IV for having an unattended security barrier

breach. (85-28)

c. Severity Level IV due to an electronic alarm annunciation

failure. (85-28)

d. Severity Level V for failing to have adequate records.

(85-28)

e.

Severity Level V due to

an

inadequate alarm testing

procedure. (85-05)

2. Conclusion

Category: 2

3.

Board Recommendation

No change in NRC inspection activity is recommended.

H. Outages

1. Analysis

During this evaluation period, routine inspections were performed

by the resident and regional inspection staffs.

All three units

were refueled during the period.

The inspectors reviewed the

comprehensive shutdown schedule which integrates work schedules

for all groups; operations,

maintenance, testing and surveil

lances. The newly established integrated scheduling division is

discussed under Surveillance.

The inspectors reviewed prepara

tions for refueling, including controls on receipt, inspection and

storage of new fuel,

inspection of facilities for fuel handling,

reviewed records on selected new fuel assemblies, verified that

adequate procedures were on hand for all phases of the operation,

and verified that procedures met Technical Specification

requirements.

The inspectors witnessed refueling from the refueling floor, the

control room and the spent fuel area to verify that preparations

and conditions prior to and during core alteration were

in

accordance with licensee and NRC requirements.

Enclosure 1

20

Major work performed during

the outage

included inservice

inspection activities, reactor vessel examination,

performance

testing of pumps

and valves,

replacement of main feedwater

nozzles, letdown cooler replacement, reactor coolant pump and main

turbine refurbishment,

sludge lance and water slap cleaning of

steam generators, rework of several hundred valves on each unit,

installation of reactor vessel level instrumentations (RVLIS)

on

Unit 1, installation or adjustment of safe shutdown makeup pumps,

rework of main steam code safety valves, installation of control

room display system,

and Motor Operated Valve Actuator Testing

System (MOVATS) analysis of several motor operated valves.

Areas

inspected included replacement of main feedwater flow

nozzles,

letdown cooler replacement, reactor coolant pump

refurbishment, activities associated with IE Bulletins 79-02 and

79-14, disassembly and repair of an emergency feedwater

pump

turbine, rework of code safety valves, repair of a control rod

drive, replacement of an inner hatch seal, RVLIS installation, and

MOVATS testing.

The large Duke Power Company work force available on site and from

off site is discussed in the maintenance section of this report

along with qualification and training of the force.

Also, the

integrated scheduling group,

which plays a large part in outage

performance, is discussed in the surveillance section. Refueling

outages are scheduled to last about 59 days,

and the outages

usually are very close to this schedule unless unanticipated

problems are encountered.

The licensee had been responsive to inspector concerns as

evidenced by an extensive program to rework main steam code safety

valves due to a delay in reseating of some valves after a reactor

trip. The normal relief settings for some of the valves is 1050

psig, with blow down set at 3%. The turbine stop valves maintain

pressure after trip at 1025 psia to control pressurizer level,

bringing the maintained pressure

and

blow

down

very close

together. The problem is under study by the licensee.

In addition to refueling outages and reactor trips, there were 12

shut downs for maintenance during the assessment period.

a. Units 1 and 3 were each shut down once for steam generator

tube leaks.

b. Unit 2 was shut down for steam generator pulse cleaning and

water slap cleaning.

c. Unit 1 was shut down to repair a leak on the nitrogen decay

tank drain valve and was returned to criticality on the same

day.

Enclosure 1

21

d. Unit 2 was shut down to repair a leak on an instrument root

valve and again three months later to repair a leak on

another instrument root valve.

e. Unit 3 was shut down to repair leaks in a moisture separator

reheater tube bundle.

f..

Unit 3 was shut down twice to add oil to a reactor coolant

pump reservoir.

g. Unit 3.was shut down due to leakage past "O" rings on the

reactor vessel

head soon after start up from refueling.

Several other leaks were repaired.

h. Unit 3 was shut down due to an overheated bearing on the high

pressure turbine. This bearing had been replaced during the

recently completed refueling outage during routine turbine

overhaul.

The same bearing failed the second time after

about a weeks operation.

At this time,

extensive efforts

were made to bring the entire turbine into as near perfect

alignment as possible. The shaft and bearing surfaces were

also reworked. No other problems were experienced.

It

appears that the leaks after startup and turbine problems

indicate possible weakness in the maintenance

program.

The

licensee has stated that, although turbine alignment was within

specifications, apparently it would be necessary to bring them

into original, or as new, alignment.

Considering the large number of workers and the scope of shutdown

work, few violations were cited during the refueling outages. A

violation was cited concerning welding of the main feedwater

nozzles in that weld filler metal in use had no coupons tested in

the heat treated condition, while some of the welds in which this

material

was used had

been heat treated.

Another violation

involving the feedwater flow nozzles concerned failure to apply

post weld heat treatment to the weld procedure qualification test.

A third violation concerned release of reactor coolant pump studs

for use, installation of the studs, and declaration of the pumps

to be operable even through a documentation problem existed on the

material

used for stud fabrication.

The violations cited are

listed below.

a. Severity Level IV violation for use of weld filler material

which had not been tested to code requirements stipulated by

the purchase order. (85-27)

b. Severity Level IV violation for use of a weld procedure which

had not been properly qualified for the work being performed.

(85-27)

Enclosure 1

22

c. Severity Level IV violation for use of reactor coolant pump

studs for which Duke Quality Assurance Manual cerification

requirements had not been met. (85-27)

2. Conclusion

Category: 1

3. Board Recommendation

The Board notes that a new division for integrated scheduling has

been established which should result in new initiatives and

positive attributes.

I. Quality Programs and Administrative Controls Affecting Quality

1. Analysis

During this assessment period, routine inspections were performed

by resident and regional

staffs.

The following areas

were

reviewed by the regional staff during this period:

QA program,

QA/QC administration, procurement, receipt, storage and handling,

design control,

test and

experiments, measuring and test

equipment,

and surveillance testing and calibration control.

In

addition, a special,

announced team inspection was performed by

regional, resident and contract personnel to assess the licensee's

compliance with Generic Letter 83-28, "Required Actions Based on

Generic Implications of the Salem ATWS Events".

Areas inspected

included:

Post-trip review; equipment classification; vendor

interface and manual control; surveillance and post maintenance

testing; and reactor trip system reliability.

The licensee

management appeared to be adequately involved in assuring quality

and has been responsive to NRC initiatives. This was observed by

the scheduling, developing, reviewing and submittal of adequate

responses to GL 83-28 which entailed management participation.

The licensee's responses reviewed for GL 83-28 were determined to

be timely, concise, and adequate.

Review of licensee responses

revealed that they understood the requirements of GL 83-28 and had

adequately resolved technical issues.

Review of the test and experiments program identified that it was

well developed and procedurally delineated.

Technical issue

resolution from a safety standpoint was clearly demonstrated by

use of a nuclear evaluation checklist for performance of nuclear

safety evaluations.

Additional management involvement in this

area was further demonstrated by the licensee's present.effort to

enhance and improve the nuclear evaluation checklist for better

evaluation of nuclear safety issues.

Enclosure 1

23

The licensee was responsive to

NRC concerns as evidenced by

successful closure of violations relating to quality, which were

identified in various functional areas.

QA/QC administrative procedures were found to be exemplary in

style and scope,

and the personnel within this group appeared

knowledgeable

of

QA program

changes

and

implementation.

Additionally, QA program procedures appeared well written. The QA

staff had a positive attitude toward the implementation of the QA

program. The commitment tracking system was well developed.

In samples reviewed by the inspectors, the Q-list appeared well

defined, clear, and concise in defining those structures, systems,

components,

documents,

and activities to which the QA program

applies. During this assessment period, a special review by IE

headquarters personnel found the Q-list to be one of the best they

had reviewed. During this assessment period, a team inspection

was conducted which reviewed the licensee's response to Generic

Letter 83-28. This team identified two violations. One concerned

failure to follow procedures for classifying safety-related work

requests. This violation was attributed by the inspectors to be

due to a lack of detail in one area of the Q-list and inadequate

training provided for classifying safety-related work activities.

The resident inspectors have also discussed with the licensee

possible loopholes in use of the Q-list in determining the need of

QA review of job plants.

Another violation concerned failure to incorporate appropriate

vendor recommendations and acceptance criteria into the procedure.

The inspectors noted that this appeared to be an isolated instance

and not a program breakdown.

However,

it

is listed in this

section of the report since the work is performed by non-site

personnel.

The team inspections found that in the area of post-trip review,

the licensee has prepared

and revised procedures to define

responsibilities, authorities, methods of assessment, training,

and equipment

needed to perform a timely technical post-trip

review. Interviews revealed that plant personnel preparing and/or

reviewing the post-trip documentation were familiar with plant

systems, equipment, and operations.

Examination of documentation and interviews with

licensee

personnel confirmed that the licensee's administrative controls

were being implemented during the procurement of safety-related

items and services.

Observations of the receipt, storage,

and

handling process made it

apparent that these activities were

accomplished in accordance with regulatory standards and the

licensee's QA program.

Enclosure 1

24

The current data and information collection systems used at the

plant are considered adequate for the evaluation of unplanned

reactor trips; however, the licensee is planning and installing

enhancements to the plant's data collection. The Safety Parameter

Display system is operational on all units.

Other violations listed in this section were identified during

inspections of other areas, but were considered to be of corporate

origin or of a programmatic

nature.

These include late or

incomplete reports to the NRC.

The craft personnel

performing surveillances appeared to be

knowledgeable of the procedures and equipment.

QA records of

surveillances and maintenance were well maintained and retriev

able.

Four violations were identified:

a.

Severity Level IV violation for failure to determine

inspection requirements and other variables affecting quality

prior to implementation of a modification.

(85-06)

b.

Severity Level IV violation for failure to comply with a

Technical Specification which requires the Shift Technical

Advisor (STA)

to report to the Operating Engineer and to

advise the shift Supervisor. (84-16, 15, 26)

c. Severity Level IV violation for failure to submit an annual

report of nuclear station modifications within the required

time frame. (85-11)

2. Conclusion

Category: 2

3. Board Recommendation

The Board notes that there is a lateness of reports.

Further

attention on the part of licensee management is needed. No change

in NRC inspection activity is recommended.

J.

Licensing Activities

1. Analysis

This performance assessment is based on our evaluation of the

licensee's performance in support of licensing actions that had a

significant level of activity during the evaluation period. These

actions include licensee request for amendments and exemptions or

Enclosure 1

25

relief from regulatory requirements, responses to generic letters,

and various submittals of information for multi-plant and

NUREG-0737

actions.

Licensing

actions were completed as

delineated in Supporting Data,Section V.C.

Management's

involvement and control in assuring quality has

improved somewhat since the last reporting period.

Submittals

have improved in quality,

including the descriptions

for

pre-noticing under

a no significant or significant hazards

determination. Management has also shown aggressive participation

in resolving the problem of disposing of low-level contaminated

waste to areas other than licensed low-level radioactive waste

burial sites.

Participation has improved to resolve the

issue, III.D.3.4,

"Control

Room Habitability".

Improvement has also been observed

in visits to headquarters and the Oconee site.

Meetings have

become more effective, management participation has increased, and

participants have all the necessary information.

The Duke staff and key personnel

possess an excellent working

knowledge

and

history of the plant.

The efforts of the

engineering staff have been effective in resolving technical

problems.

An area that continues to need improvement is management attention

for anticipating potential problems with,

and scheduling,

the

submittal of major reviews.

An emergency TS change was processed

in April 1985 for Oconee Unit 3 and much of the information to

support the amendment could have been given to the staff earlier

in the event. Also the lack of information delayed resolution of

the delayed response regarding certain General Electric reactor

trip breakers under-voltage trip attachments.

Many submittals

that could have been anticipated have been given to the staff with

minimal time for review. This can be seen in the steam generator

sleeving submittal and request for a license extension.

Usually,

submittals are timely but recently there have been several

untimely submittals.

Usually, management attention is evident on major issues and in

difficult issues needing resolution.

Additionally,

Duke

has

generally improved on submitting reload reviews on a more timely

basis to allow adequate time for NRR review.

One exception to

this however, occurred for Oconee 1 cycle 9 when the amendment had

to be issued before the prenotice comment period expired.

Enclosure 1

26

Duke has continually exhibited an excellent understanding of

technical issues and has usually endorsed resolutions which have

been acceptable to the

Commission's

staff.

When resolving

technical issues, Duke has generally expressed conservatism from

the safety standpoint and has usually presented a sound approach

to resolving issues. When proposing an approach to resolve any

safety concern or to meet any regulatory requirements,

Duke has

usually proposed acceptable solutions.

Duke seems to follow closely the regulatory environment and takes

an active role from the safety standpoint.

Duke consistently

takes the lead for the nuclear industry to help resolve matters of

generic concern.

For example, Duke has participated in Babcock

and Wilcox Owner's Groups and has proposed to participate in

programs or studies that have or will be used at other utilities.

Some examples include Duke participating in the regulatory

effectiveness program to improve the regulations and the TS

improvement program to improve the TS. Other programs include the

reliability engineering study and probabilistic risk assessment

study.

NRR has met with the licensee several times during this review

period. Duke has generally been well prepared,

responsive and

made a concerned effort to resolve the issues.

When

major

differing positions occurred between the staffs, Duke was

professional and endeavored to resolve all questions.

Overall,

the meetings were generally informative and productive.

However,

some licensing actions (e.g., overtime limits and Shift Technical

Advisor) required repeated submittals and several years to resolve

and the delays were attributable to the licensee.

Oconee Nuclear Station has been visited by various staff members

and consultants for gathering information. Although under a heavy

schedule, Duke has been courteous, cooperative, and informative.

Duke has tried to meet deadlines and notified NRR when they cannot

be met.

Our observations from various plant tours is that housekeeping is

excellent. A concerted effort to maintain a clean facility was

evident throughout the plant and especially so in the common

turbine bay.

Regarding control room behavior, our observations indicate that

the operators act in a professional and responsive manner.

The

operators were attentive to plant conditions and responsive to

control room annunciators.

Enclosure 1

27

Based on an

NRR evaluation of licensing activities during the

period from September 1, 1984 to February 28,

1986,

no major

deficiencies affecting licensing activities became apparent. Duke

has improved

on

the quality- of the

submittals.

However,

continuing effort needs to be devoted for the timeliness of some

submittals.

The licensee's approach to the resolution

of

technical issues is generally sound and conservative; and the

licensee is usually responsive to NRC initiatives.

One violation was identified in the licensing activities area.

Severity Level V violation for failure to report revisions to

the FSAR within the required time frame. (85-20)

2. Conclusion

Category: 2

3. Board Recommendation

None noted.

K. Training

1. Analysis

During the assessment period, routine inspections of plant

training programs were performed by Regional and resident

inspection staffs. A special team assessment of Oconee training

programs was conducted early in the SALP period to determine the

effectiveness of the licensee's overall training

program

in

supporting safe operation of the facility. Toward the end of the

SALP period, the Division of Human Factors Technology conducted a

special post-accreditation audit of INPO accredited training

programs.

The Oconee Training Center is located adjacent to the Oconee site

and is used to train plant specific (Oconee)

operators.

The

facility has

11,600 sq.

ft. of space devoted to classrooms,

offices, and the Oconee simulator including a public viewing area.

The Mount Holly Training facility located approximately ten miles

north of the Duke Corporate Office in Charlotte, N.C. is used for

Mechanical Maintenance Training and Health Physics training. This

facility was just recently put into use in January 1986 and

occupies 31,600 sq. ft.

of classrooms, shop facilities, and

offices.

These facilities and those mentioned in the McGuire training

section represent an extensive commitment to training.

Enclosure 1

28

Although inspections revealed several specific and programmatic

weaknesses in the various plant training programs,

management

responsiveness and commitment, in general, resulted in an overall

improvement in the area of training.

A notable example of management's initiative was the development

of the Employee Qualification and Training System

(EQTS)

to

control

and implement formalized on-the-job (OJT) training

requirements.

The

EQTS,

once fully implemented,

will correct

programmatic deficiencies apparent in the non-licensed operator

(NLO)

and maintenance OJT programs during the assessment period.

Adequate facilities were provided for the support of plant

training and the enhancement of instructional delivery.

The training department appears well staffed and has a low

turnover rate. The facility has, in general, a low turnover rate

of both licensed and non-licensed personnel.

This is attributed

primarily to Duke's hiring and training practices of local

personnel.

Operating staff training, knowledge of the facility, and attitude

appeared to be good.

Sixteen persons took the Senior Reactor

Operator (SRO)

examination with ten passing; five persons took

partial Reactor Operator

(RO)

examinations,

carried over from

previous licensing applications, and all of these persons passed.

This performance was not as good as the last rating period, but

still is comparable to the industry norm.

Simulator instruction was well

structured; however, several

scenarios were not included in the simulator portions of initial

reactor operator and senior reactor operator training programs.

These programs did not provide for proficiency demonstrations in

solid plant pressure control, inert gas bubble pressure control,

and filling the pressurizer to a solid condition and creating a

steam bubble. A direct approach to combat an ATWS malfunction was

not available and the senior operator training program did not

provide sufficient real time practice in

performing routine

heatup, startup, shutdown, and cooldown.

The licensee performed a table top analyses of the NLO and RO

programs to produce a list of the tasks that are performed in

these jobs which were linked to learning objectives in lesson

plans; however, there was no task list for the SRO/STA position.

In many cases, the learning objectives did not include conditions

or standards, or were too broad and vague to link to test

questions. Because of these shortcomings,

the training program

did not meet two to five elements necessary for effective

performance-based training contained in the Commission's Policy

Statement on training and qualifications.

Enclosure 1

29

Administrative deficiencies were noted in the operator training

and retraining programs.

A controlled administrative procedure

was not available to define the licensed operator (LO)

training,

license requalification training and the non-licensed requalifica

tion training programs and to ensure the appropriate administ

ration of revision, review and

approval of these training

programs. Contradictions observed in the participation of backup

licensees and

licensed instructors in the licensed operator

requalification program and the licensee's failure to provide a

formal program description for the Accelerated Requalification

Program were also symptomatic of the lack of controlled documents

detailing the administration of plant training programs.

A significant programmatic weakness in the licensee's operator

training program was the lack of system texts coupled with the

inconsistent format of instructor lesson plans.

These deficiencies in instructional and student training materials

impacted the consistency and sequencing of learning objectives and

diminished their aid to the student in learning the skills and

knowledge necessary to perform the function of plant operator.

The training of maintenance personnel

was determined to be

sufficient to support plant maintenance activities. The lack of a

formalized on-the-job training program was being corrected by the

development of EQTS.

A major weakness in the maintenance area

during the assessment period was the licensee's failure to

establish

and

implement procedures to ensure that pertinent

operating experience is fed back to all levels of maintenance

personnel.

The licensee's general employee training (GET)

was considered

effective; however,

certain weaknesses in the

GET

areas of

physical security and QA were apparent. The generic nature of the

GET video tape and attempts to maintain its applicability to all

Duke Power Plants resulted in certain Oconee security specifics

such as card reader usage and vital area locations not being

presented to the employee during GET.

Related GET omissions in

the area of QA such as the day-to-day role of QA inspectors and

how to report QA deficiencies were also observed.

The following violation was identified.

Severity Level IV violation for failure to establish and

implement adequate procedures to permit timely dissemination

of operating experience to mechanical and I&E maintenance

personnel.

(84/25-24-27)

Enclosure 1

30

2.

Conclusion

Category:

2

3. Board Recommendation

The Board notes that the training has been effective in spite of

weaknesses noted in the Security and Quality Assurance areas.

No

change in NRC inspection activity is recommended.

V. Supporting Data and Summaries

A.

Licensee Activities

During this evaluation period,

major licensee activities included

normal

power operations, four refueling outages, and extensive

modifications and repairs.

Some of these items are listed in the

individual sections of this report.

Two items of particular note are

completion of the safe shutdown facility and of a waste compaction and

incinerator facility.

B. Inspection Activities

In addition to a review concerning importance to safety, a review on

regulatory effectiveness, operator licensing examinations,

ten site

inspections by NRR,

and several other special audits, 62 inspections

involving approximately 7400 inspector-hours on site were performed by

regional and resident inspectors.

C.

Licensing Activities

Summary of significant licensing actions and other activities during

the SALP evaluation period.

1.

NRR/Licensee Meetings - 30

2.

NRR site visits -

10

3.

Commission briefings -

none

4. Schedule extensions granted -

none

5. Reliefs granted - 1 (in-service inspection relief granted)

6. Exemptions granted - 2

a.

Fire protection technical exemptions (lighting)

b.

ISI/IST common start date exemption

7.

Licensee Amendments Issued - 48 (16 for each unit)

Enclosure 1

31

8.

Emergency technical specification changes issued -

one (reactor

building cooling fan '3A')

9.

Orders issued -

none

10.

NRR/Licensee Management Conferences - None

11.

Li-censee Actions

0

118 Plant specific actions were completed. Included in this

category and used to provide input to this evaluation are:

-

ISI/IST Exemption

Cycle 9 Review, Oconee 1

-

Fire Protection Exemption Request (Lighting)

-

Review of Guidelines for Determining Core Damage

-

EOF Location

-

ISI Relief Request

-

Mark BZ Fuel

-

Air Lock Testing Frequency Technical Specification

Change

-

STA Bachelor's Degree or Equivalent

-

Regulatory Effectiveness Program

-

Disposal of Five Feedwater Heaters Onsite

-

Minimum Operator Staffing Technical Specification Change

-

Interpretation of 10 CFR 20.203(e)

-

Startup Physics Report Revisions

-

Emergency Technical Specification Change for "3A"

Fan Cooler

-

Licensing Operators Requalification Program

-

Technical Specification Improvement Meeting

-

Inverter Alert

-

Administrative Technical Specification Change

-

FSAR Reference Amendment

-

Emergency Drill

-

Waste Gas Holdup Tanks Technical Specification Review

-

DCRDR Program Plan

-

Keowee Batteries Inoperability Extension

-

Oconee 1 Spent Fuel to McGuire

-

Confirmatory Items on GK 83-28, Item 4.3

-

RTB UVTA

-

Reload Methodology

-

Cycle 9 Review, Oconee 3

-

RCS Leak Test Technical Specification changes

-

Disposal of Contaminated Sand in Controlled Area

-

Cycle 8 Fuel Assembly, Oconee 2

-

Nuclear Equipment Operators

-

Overtime Limits

-

II.B.3 Technical Specification Change

-

II.F.1.2 Technical Specification Change

-

Definition of "Accessible/Accessibility"

-

H2 Penetrations

Enclosure 1

32

0

38 Multi-Plant actions completed. Included in this category

and used to provide input to this evaluation are:

-

Technical Specification Review of "Reportable

Occurrence" Requirements

-

Item 4.3, Automatic Actuation of Shunt Trip Attachment

fo.r Westinghouse and B&W Plants

-

Masonry Wall Design, Response to I&E Bulletin 80-11

-

Environmental Qualification of Safety Related Electrical

Equipment

-

Item 1.1, Post Trip Review Program Description and

Procedures

-

Natural Circulation Cooldown (GL 81-21)

-

Control of Heavy Loads _ Phase II

-

Item 3.1.3, Post Maintenance Testing

-

Item 3.2.3, Post Maintenance Testing

-

Items 3.1.1. and 3.1.2, Post Maintenance Testing

Procedures

-

Diesel Generator Reliability Technical Specifications

(GL 84-15)

-

Items 3.2.1 and 3.2.2, Post Maintenance Testing

Procedures

-

Item 4.1, Reactor Trip System Reliability

-

Item 4.5.1, Reactor System Functional Testing

a

17

TMI

(NUREG-0737

actions completed.

Included in this

category and used to provide input to this evaluation are:

-

Item I.D.2, Safety Parameter Display System

-

Procedures Generation Package Review

-

Item I.D.1.1, Detailed Control Room Design Review

Program

-

Item I.D.1.2, Detailed Control Room Design Review

Summary Report

-

Item II.K.3.30, Small Break LOCA Outline

-

ICC Guidelines

D.

Investigation and Allegation Review

No allegations were received during the evaluation period. A meeting

was held in the Regional Office on October 5, 1984, at the licensee's

request to discuss allegations received during the previous assessment

period. No action was prescribed against the licensee.

Enclosure 1

33

E. Escalated Enforcement Actions

1. Civil Penalties

Severity Level III violation concerning access control of the

plant, Civil Penalty -

$25,000.

2. Orders

None

F. Management Conferences Held During the Evaluation Period

Conferences held in the Regional Office

-

An enforcement conference was held at the Region II office on

March 26, 1985,

to discuss the radioactive material transport

event.

-

An enforcement conference was held at the Region II office on

July 3, 1985,

to discuss the failure to report the inoperability

of both trains of containment hydrogen monitors.

-

An enforcement conference was held at the Region II office on

January 14,

1986, to discuss the yard drainage system

and

barriers.

G.

Confirmation of Action Letters

None

H. Licensee Event Report Analysis

During the evaluation period,

13

LERs for Unit 1, eight LERs for

Unit 2, and three LERs for Unit 3 were evaluated by the NRC staff to

determine event cause.

Enclosure 1

34

The Distribution of these events was as follows:

CAUSE

NUMBER

Unit 1

Unit 2

Unit 3

Component Failure

5

3

2

Design

Construction/Fabrication/

Installation

Personnel

-

Operating Activity

2

4

1

- Maintenance Activity

1

- Test/Calibration Activity

2

1

-

Other Activity

1

Out of Calibration

1

Other

1

_

Total

13

8

3

I. Enforcement Activity

UNIT SUMMARY

FUNCTIONAL

NO. OF DEVIATIONS AND VIOLATIONS IN EACH

AREA

SEVERITY LEVEL

D

V

IV

III

II

I

UNIT NO.

1/2/3

1/2/3

1/2/3

1/2/3

1/2/3 1/2/3

Plant Operations

1/0/1

1/3/2

Radiological Controls

4/4/4

4/4/5

1/0/0

Maintenance

1/1/1

0/0/2

Surveillance

3/2/2

Fire Protection

Emergency Preparedness

Security

2/2/2

2/1/1

1/1/1

Outages

2/3/2

Training

1/1/1

Quality Programs and

2/3/2

Administrative Controls

Affecting Quality

Licensing

1/1/1

TOTAL

9/8/9

15/17/17

2/1/1

Enclosure 1-

35

FACILITY SUMMARY

FUNCTIONAL

NO. OF DEVIATIONS AND VIOLATIONS IN EACH

AREA

SEVERITY LEVEL

D

V

IV

III

II

I

Plant Operations

2

4

Radiological Controls

4

5

1

Maintenance

1

2

Surveillance

3

Fire Protection

Emergency Preparedness

Security

2

2

1

Outages

3

Training

1

Quality Programs and

3

Administrative Controls

Affecting Quality

Licensing

1

TOTAL

10

23

2

J.

Reactor Trips

Fifteen unplanned reactor trips and twelve shutdowns for maintenance

occurred during the evaluation period. Also during this period, Unit 1

was shut down twice and Units 2 and 3 once each for end of cycle

refueling outages. The unplanned trips are listed below.

Unit 1

December 2, 1984 -

Unit 1, during startup after refueling,

tripped from 43% power due to a loose wire in an Amphenol

connector which caused a relay to open,

resulting in

isolation of the generator from the grid.

Opening of the

generator breaker resulted in a turbine trip followed by an

anticipatory reactor trip.

December 3, 1984 - Unit 1 tripped from 57% power when "B"

main feedwater pump tripped after the auxiliary oil pump was

shut down. The oil pump was shut down procedurally since the

feedwater pump was at 4100 RPM and the shaft driven oil pump

should have provided sufficient oil pressure.

Since "A"

feedwater

pump was not operating at the time,

reduced

feedwater pressure caused an anticipatory reactor trip.

January 22, 1985 - Unit tripped from 100% power when moisture

separator reheater valves

(MSRV)

closed,

resulting in a

reactor trip from high pressure. Cause of the valve closure

could not

be determined at the time.

The reactor was

returned to power.

Enclosure 1

36

April 11,

1985 - Unit 1 tripped from 100% power when MSRV's

closed for reasons unknown,

resulting in a reactor high

pressure trip. Following the trip, a thorough examination of

turbine control circuits identified a loose connection on a

card which, when manipulated, signaled shaft overspeed and

caused the MSRV's to close.

April 11,

1985 -

Unit 1 tripped from 17% power due to

fluctuations in turbine header pressure which caused

a

reactor trip. The reactor was restarted shortly thereafter.

April 25, 1985 - Unit 1 tripped from 100% power after most of

the control room Statalarms were lost due to failure of an

inverter and its failure to transfer to another power source.

Power was also lost to the ICS. The reactor remained stable

with positive instrument indications while power was lost.

When power was restored, demands which had built into the ICS

caused feedwater fluctuations which resulted in tripping both

feedwater pumps, causing a reactor anticipatory

trip.

Modifications to the inverters to improve circuit reliability

and additions to the operator training program have been

completed.

January 31,

1986 -

Unit 1 tripped at 3:47 p.m.

from 100%

power due to a turbine trip and anticipatory reactor trip.

The turbine/generator trip was the result of an error by

electricians performing tests and maintenance in the 230Kv

switchyard which tripped one bus being fed by the Unit 1

generator. This caused one generator output breaker, PCB-21,

to open, transferring the entire generator output to a single

breaker,

PCB-20.

PCB-20 was designed to accept the full

load; however,

apparent failure of PCB-20 breaker contacts

caused the breaker to explode.

Unit 2

April 20,

1985 -

Unit 2 tripped from 20% power during power

ascension following refueling outages when power was lost

from a 600 volt motor control center (MCC). This led to loss

of a feedwater auxiliary oil pump, resulting in a trip of the

feedwater pump which caused an anticipatory reactor trip.

Investigation revealed that loss of the MCC was due to a

ground fault in another system.

April 26,

1985 -

Unit 2 tripped from 72% power due to a

problem in the electro hydraulic control system (EHC).

At

the time,

maintenance personnel were working in the

EHC

cabinet. A false power imbalance signal was received which

resulted in a reactor trip.

Examination identified no

questionable components. Apparently, the trip was caused by

a mechanic's error.

Enclosure 1

37

July 10,

1985 - Unit 2 tripped from 94% power due to high

reactor coolant pressure resulting from an erroneous signal

which closed the turbine control and intercept valves.

The

trip apparently was caused by a mechanic who was investi

gating a problem with the

ICS turbine header pressure

control. He plugged in a test meter which introduced a noise

signal causing the valves to close.

January 31,

1986 -

Unit 2 tripped at 11:31 a.m. from 100%

power following a load rejection which caused a generator/

turbine trip and anticipatory reactor trip.

At the time,

electricians were performing maintenance

and testing of

microwave circuits in the 230Kv switchyard. Input of signals

into a circuit unexpectedly caused a breaker fault relay to

actuate, resulting in a generator trip.

February 4, 1986 - Unit 2 tripped from 100% power due to a

technicians error during a surveillance test.

Unit 3

July 23, 1985 -

Unit 3 tripped while in three reactor coolant

pump operation at 74% power due to reactor coolant system

high pressure.

The trip was the result of a feedwater

transient caused by a failed feedwater ratio multiplier in

the ICS.

October 24, 1985 - Unit 3 tripped from 10% power due to loss

of feedwater,

caused by failure of an auxiliary steam

regulating valve to work properly during reactor power

increase following a startup.

January 31,

1986 -

Unit 3 tripped at 7:08 a.m.

from 57%

power. The trip was

caused

by a feedwater

pump flow

transmitter which failed high, causing a feedwater runback

and subsequent reactor high pressure trip.

Only one

feedwater pump was operating at the time, since the unit was

returning to power following a reduction to 15% power in

order to repair a turbine intercept valve.