ML15224A764
| ML15224A764 | |
| Person / Time | |
|---|---|
| Site: | Oconee |
| Issue date: | 03/08/1991 |
| From: | Belisle G, Binoy Desai, Poertner W, Skinner P NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML15224A762 | List: |
| References | |
| 50-269-91-03, 50-269-91-3, 50-270-91-03, 50-270-91-3, 50-287-91-03, 50-287-91-3, NUDOCS 9103250098 | |
| Download: ML15224A764 (13) | |
See also: IR 05000269/1991003
Text
644 REG4
UNITED STATES
o
NUCLEAR REGULATORY COMMISSION
REGION II
101 MARIETTA STREET, N.W.
z
ATLANTA, GEORGIA 30323
Report Nos.: 50-269/91-03, 50-270/91-03,
50-287/91-03 and 72-4/91-03
Licensee: Duke Power Company
P. 0. Box 1007
Charlotte, NC 28201-1007
Docket Nos.: 50-269, 50-270, 50-287 and 72-4
License Nos.: DPR-38, DPR-47, DPR-55 and SNM 2503
Facility Name: Oconee Nuclear Station
Inspection Conducted: January 27 - February 23, 1991
Inspectors:_______
P. H. Skinner, Senior Resd nt
ector
Date Signed
B. B. Desai, Reside
Ins
t r
Date Signed
-3- 2-i>F
W. K.
rtner, Re
eqt Ispe
Date Signed
Approved by-
£o'e
J-7-q
. Bel ie,
Section Chief
Date Signed
Division of Reactor Project
SUMMARY
Scope:
This routine, announced inspection involved inspection on-site in
the areas of operations, surveillance testing, maintenance
activities and inspection of open items.
Results:
One violation was identified concerning a failure to follow
procedures associated with independent verification. Two unresolved
issues were identified concerning High Pressure Injection system
instrumentation and control of activities associated with various
component circuit breakers. Controls exhibited during mid-loop
operations have improved since the previous refueling outage. One
non-cited violation concerning missed surveillance was identified.
91O3250098 910308
ADOCK 05000269
C!
REPORT DETAILS
1. Persons Contacted
Licensee Employees
- H. Barron, Station Manager
D. Couch, Keowee Hydrostation Manager
- T. Curtis, Compliance Manager
- J. Davis, Technical Services Superintendent
D. Deatherage, Operations Support Manager
- B. Dolan, Design Engineering Manager, Oconee Site Office
- W. Foster, Maintenance Superintendent
- W. Gibson, Quality Assurance
T. Glenn, Engineering Supervisor
- 0. Kohler, Compliance Engineer
C. Little, Instrument and Electrical Manager
- H. Lowery, Chairman, Oconee Safety Review Group
B. Millsap, Maintenance Engineer
M. Patrick, Performance Engineer
- D. Powell, Station Services Superintendent
- G. Rothenberger, Integrated Scheduling Superintendent
- R. Sweigart, Operations Superintendent
Other licensee employees contacted included technicians, operators,
mechanics, security force members, and staff engineers.
NRC Resident Inspectors:
- P. Skinner
- W. Poertner
- B. Desai
- Attended exit interview.
2. Plant Operations (71707)
a. General
The inspectors reviewed plant operations throughout the reporting
period to verify conformance with regulatory requirements, Technical
Specifications (TS), and administrative controls. Control room
logs, shift turnover records, temporary modification log and
equipment removal and restoration records were reviewed routinely.
Discussions were conducted with plant operations, maintenance,
chemistry, health physics, instrument & electrical (I&E), and
performance personnel.
Activities within the control rooms were monitored on an almost
daily basis.
Inspections were conducted on day and on night shifts,
during weekdays and on weekends. Some inspections were made during
shift change in order to evaluate shift turnover performance.
2
Actions observed were conducted as required by the licensee's
Administrative Procedures. The complement of licensed personnel on
each shift inspected met or exceeded the requirements of TS.
Operators were responsive to plant annunciator alarms and were
cognizant of plant conditions.
Plant tours were taken throughout the reporting period on a routine
basis. The areas toured included the following:
Turbine Building
Auxiliary Building
CCW Intake Structure
Independent Spent Fuel Storage Facility
Units 1, 2 and 3 Electrical Equipment Rooms
Units 1, 2 and 3 Cable Spreading Rooms
Units 1, 2 and 3 Penetration Rooms
Units 1, 2 and 3 Spent Fuel Pool Rooms
Unit 3 Containment
Station Yard Zone within the Protected Area
Standby Shutdown Facility
Keowee Hydro Station
During the plant tours, ongoing activities, housekeeping, security,
equipment status, and radiation control practices were observed.
b. Plant Status
Unit 1 operated at power for the entire reporting period. On
February 2, 1991, Reactor Coolant Pump 1A1 motor experienced a low
oil pot level.
This resulted in the pump being secured and a power
reduction to 40 percent. No obvious oil leak was identified.
Several gallons of oil were added to the motor, the pump was
restarted and the unit returned to 100 percent power on February 3,
1991.
Unit 2 operated at power for the entire reporting period.
Unit 3 operated at power until the generator was taken off line for
a scheduled End of Cycle (EOC) 12 refueling outage on February 13,
1991, at 3:00 p.m. While cooling down and depressurizing the
Reactor Coolant System (RCS) from hot shutdown, Reactor Protection
System (RPS) channels C and D actuated on low RCS pressure and
resulted in insertion of group 1 control rods. The reactor was
already subcritical and group 2 through 7 control rods had been
previously inserted at the time of the RPS actuation. The reactor
operator was monitoring the wide range RCS pressure meters which
were reading 30 psig higher than the narrow range (NR) RPS pressure
meters while reducing temperature and inserting group 1 rods.
During the rod insertion the RPS setpoint was reached and resulted
in the RPS actuation. A contributing factor to this unplanned RPS
actuation was that the shutdown procedure requires group 1 rods to
be inserted at 1850 - 1820 psig (RPS trip setpoint is 1800 psig),
but does not direct the operator to monitor the NR RPS pressure
3
instruments. A procedure change was submitted to change the
pressure at which group 1 rods are required to be inserted to allow
more time for rod insertion prior to reaching RPS trip setpoints. A
four hour NRC notification was made pursuant to the requirements of
10 CFR 50.72 b.2.ii.
At the end of the reporting period defueling
activities had commenced.
c. HPI Piggyback Problems
As a result of a followup item from a Self Initiated Technical
Audit, the licensee identified five potential problems that could
affect the High Pressure Iqjection (HPI) and Low Pressure Injection
(LPI) systems when in the piggyback mode of operation. These
potential problems included:
(1) potential insufficient HPI pump NPSH
(2) potential overflow/overpressurization of the Letdown
Storage Tank (LDST)
.
(3) potential inadequate Emergency Core Cooling System
(ECCS) flow
(4) inability to provide LPI pump minimum flow
(5) potential HPI pump runout.
These items are identified and addressed in a Special Report to the
NRC dated February 6, 1991.
The potential HPI pump NPSH problem during piggyback mode of
operation was resolved by removing procedural instructions which
could have allowed aligning the LPI discharge to both HPI and
Reactor Building Spray while in the piggyback mode of operation.
The potential overflow/overpressurization of the LDST during
piggyback mode of operation results from the suction pressure at the
HPI pumps due to the discharge pressure of the LPI pump potentially
being greater than the LDST relief valve set pressure of 106 psig.
This could result in the HPI pump minimum flow recirculation
returning to the LDST and eventually overfilling/overpressurizing
the tank. This could result in containment sump inventory being
lost out the relief valve to the bleed holdup tank. The piping
downstream of the relief valve and the bleed holdup tank are not
seismically qualified and are not safety related. To prevent the
LOST from overflowing/overpressurizing the licensee revised the
Emergency Operating Procedure (EOP) to open HP-363, the letdown line
to LPI pump suction isolation valve, upon entering the piggyback
mode of operation. This would divert the HPI mini-flow from the
LDST to the suction of the LPI pumps. The licensee also had the
option of shutting the HPI mini-flow recirculation isolation valves
to prevent recirculation flow back to the LDST but decided to open
HP-363 to provide mini-flow protection for the HPI pumps. The
piping downstream of the HPI mini-flow recirculation isolation
valves up to HP-363 is class "C" pipe. The inspectors questioned
whether class "C" pipe was acceptable since RCS containment sump
water would be flowing through the pipe during the piggyback mode of
II
4
operation. Review of the HPI design basis document determined that
the design basis for the HPI system states that piping that could
transport containment sump water is required to be class "B" pipe.
The licensee stated that the design basis document was incorrect and
that class "C" piping was acceptable per the original Oconee Design
Basis and that the HPI system design basis document would be
revised. The inspector is continuing the review of the
acceptability of this design evaluation. In addition, the inspector
also is reviewing the adequacy of the licensee's EOP procedure
revision in that the new procedure does not address shutting the HPI
mini-flow recirculation isolation valves if HP-363 can not be
opened, or if other single failures that could affect the mini-flow
flowpath occur. Included in this review is the appropriateness of
allowing containment sump water to be transported throughout the
non-safety portion of the HPI system with respect to radiation
levels in the Auxiliary Building. The licensee stated that a design
study would be performed to address any accessibility concerns;
however, this study was not completed prior to revising the EOP to
open HP-363. Discussions with the licensee determined that a
preliminary design study report is scheduled to be issued in mid
March. The licensee also identified that the LDST inlet and outlet
check valves were not tested in the closed direction in the
Inservice Testing Program. This item is identified as Unresolved
Item 50-269,270,287/91-03-01:
HPI Piggyback Issues, pending further
reviews of design documentation by the inspectors.
The licensee's actions with regard to potential inadequate ECCS flow
and HPI pump runout was to revise the EOP to restrict total HPI flow
during piggyback operation to less than 750 gpm, to require three
HPI pumps be operable during power operation and review of pump
runout flow requirements. The licensee's ECCS flow instrumentation
is air operated. The licensee's Instrument Air System is not safety
related, it is not seismically qualified and it does not meet single
failure criteria with respect to ECCS flow instrumentation. The
licensee's position is that these instruments fall under their
Regulatory Guide 1.97 commitments and will not fully meet safety
grade instrumentation requirements until the instruments are
modified to meet the Regulatory Guide 1.97 commitments previously
made to the NRC. The licensee is presently replacing these flow
instruments during the present Unit 3 refueling outage and stated
that the Unit 1 and Unit 2 instruments would be replaced during
their next scheduled refueling outages. The inspectors are
concerned with the extremely long time frame with respect to when
this instrumentation was identified as being deficient and the
schedule for correcting the deficiencies (over six years).
The
inspectors are also concerned with regard to the operability of the
ECCS systems due to the fact that this instrumentation must indicate
during an ECCS actuation. Further review of this issue is
identified as another example of Unresolved Item
50-269,270,287/91-03-01 discussed above.
5
d. Unit 3 Mid-loop Operations
The inspectors reviewed the licensee's actions with regard to
reducing RCS level to mid-loop operations. The licensee's
requirements for mid-loop operation are contained in Operating
Procedure (OP)3/A/1103/11: Draining and Nitrogen Purging of the RC
System. The procedure requires in part that the following items be
implemented prior to reducing RCS level below fifty inches as
indicated on reactor vessel level indicator LT-5:
-
A containment closure survey to identify containment
penetrations that would need to be closed in the event of a
loss of decay heat removal capability and to ensure that
containment closure can be achieved within 2.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />
-
Two independent RCS temperature indicators and alarms
-
LT-5 be operable and calibrated
-
-
Both main feeder buses are required to be energized and two
sources of electrical power are required to be available to
supply the main feeder buses
-
Two means of adding inventory to the RCS is required
-
Both steam generator upper primary side handhole covers removed
to provide a vent path
-
A review of maintenance and testing activities to ensure no
adverse effects on systems and components required for decay
heat removal.
The inspectors reviewed and witnessed the performance of portions of
procedure OP/3/A/1103/11. During the last Unit 2 refueling outage
the inspectors identified weaknesses in the conduct of the
licensee's actions with regard to mid-loop operations (NRC
Inspection Report 50-269,270,287/90-27). The licensee revised the
Unit 3 operating procedure since the Unit 2 refueling outage and one
of the major concerns identified has been resolved, ie: verification
of the proper operation of LT-5 prior to reducing RCS inventory to
less than eighty inches on the pressurizer level indicators. The
present procedure requires that at eighty inches pressurizer level
LT-5 agree within plus or minus five inches of indicated pressurizer
level.
When LT-5 was placed in service during the Unit 3 RCS
draindown it did not agree within five inches of pressurizer level.
Pressurizer level indicated approximately one hundred inches and
LT-5 indicated approximately eighty-five inches. The draindown was
stopped and the reactor vessel head vents were opened per the
procedure to obtain a better vent on the reactor vessel head region.
The licensee also checked LT-5 and no problems with the instrument
was identified. The licensee determined that the most logical cause
6
of the level mismatch was that the pressurizer was not properly
vented. The licensee decided to vent the pressurizer by breaking
the flange connection at the pressurizer power operated relief valve
(PORV). This corrected the level mismatch problem and the vessel
draindown was recommenced.
The licensee installed two ultrasonic level indicators on the RCS
prior to draining the RCS to less than fifty inches on LT-5. One
level detector was installed on a RCS hot leg and the other was
installed on a RCS cold leg. These level indicators indicate over a
very narrow range of RCS level ie: centerline of the hot and cold
leg to the top of the RCS hot and cold legs. The instruments
installed for this outage are scheduled to become permanently
installed indicators, provide indication via the plant computer and
provide a low level alarm in the control room. The licensee does
not consider that the installation and operability of the ultrasonic
level detectors are an absolute requirement for draining below fifty
inches. The inspectors consider that since LT-5 is the only wide
range level instrument below the level of the pressurizer level
instruments (approximately seventy-four inches) and the top of the
hot and cold legs (eighteen and fourteen inches) a second level
indication should be available to operators when operating in this
region. Discussions with the licensee determined that the addition
of another level indicator redundant to LT-5 is under consideration.
No violations or deviations were identified.
3. Surveillance Testing (61726)
a. General
Surveillance tests were reviewed by the inspectors to verify
procedural and performance adequacy. The completed tests reviewed
were examined for necessary test prerequisites, instructions,
acceptance criteria, technical content, authorization to begin work,
data collection, independent verification where required, handling
of deficiencies noted, and review of completed work. The tests
witnessed, in whole or in part, were inspected to determine that
approved procedures were available, test equipment was calibrated,
prerequisites were met, tests were conducted according to procedure,
test results were acceptable and systems restoration was completed.
Surveillances reviewed and witnessed in whole or in part:
PT/O/A/0400/15
SSF Submersible Pump Test
TP/O/B/28O/16
Turbine Overspeed Test
IP/O/A/4980/51A/RE Westinghouse Type CO-5, CO-6, CO-7, CO-8
and CO-11 Relay Test
PT/O/A/0160/06
RBCU Heat Exchanger Performance Test
7
b. Safety Related Procedures Past Due Their Two Year Review
On January 9, 1991, the licensee discovered that 50 safety related
procedures were past due their two year periodic review. Following
the discovery, the procedures were immediately put on administrative
hold, thereby enabling the procedure to be reviewed prior to use in
the field. This problem was identified during a review of the
computerized index of the I&E procedures. Duke Power Company
Administrative Policy Manual requires a comprehensive periodic
review of all station procedures at intervals not to exceed two
years for safety related, and not to exceed five years for non
safety related procedures to ensure adequacy of the procedure.
Normally, the periodic review schedule is tracked closely, and
procedures that have their reviews coming up are either reviewed or
put on administrative hold before the review due date. During the
1986-1987 time frame, a significant backlog developed on procedures
that were on administrative hold and were pending a review. The
procedure supervisor released the procedures awaiting the two year
review from administrative hold. Subsequently, the concept of
administrative hold lost significance and resulted in safety related
procedures not being reviewed at the required two year interval.
This is identified as a Non-cited Violation 50-269,270,287/91-03-03:
Failure to Periodically Review Safety Related Procedures at Intervals
Not to Exceed Two Years. This licensee identified violation is not
being cited because criteria specified in Section V.A of the NRC
Enforcement Policy were satisfied.
No additional violations or deviations were identified.
4. Maintenance Activities (62703)
a. General
Maintenance activities were observed and/or reviewed during the
reporting period to verify that work was performed by qualified
personnel and that approved procedures in use adequately described
work that was not within the skill of the trade. Activities,
procedures, and work requests were examined to verify; proper
authorization to begin work, provisions for fire, cleanliness, and
exposure control, proper return of equipment to service, and that
limiting conditions for operation were met.
Maintenance reviewed and witnessed in whole or in part:
WR 57518A
PM On 3TC-10 RBS Motor 3A Circuit Breaker
WR 57516A
PM On HPI 3A Motor Circuit Breaker
Disassembly, Inspection and Repair of 3MS-95
WR 52608J
Disassembly, Inspection and Repair of 3MS-94
WR 57115D
Perform PM On Turbine Driven Emergency Feedwater
Pump Turbine
WR 57064D
Clean Tube Side of Component Cooler 3B
WR 57514A
- 8
WR 57461B
Perform PM on 5X-51X, 50Z-51Z and 50G Relays
in 3TC-8
WR 55304B
Replace Peak Filtering Capacitor in RPS Power
Suppl ies
WR 50671K
Votes Testing of 3LPSW-19
WR 52897J
Determine Valve Position Upon Loss of IA for
3MS87
WR 52854J
Determine Valve Position Upon Loss of IA for
Installation of 6th Stage Impeller in the 3A
MDEFWP
IP/0/A/305/13 Nuclear Instrument and RPS Power Supply
Capacitor Replacement
MP/0/A/2001/3 Air Circuit Breaker Inspection and Maintenance
MP/3/A/1300/28 Motor Driven Emergency Feedwater Pump
Impeller Changeout
b. Reactor Protection System Power Supply Preventive Maintenance
The inspector observed a portion of the work activity associated
with WR 55304B, replacement and testing of the RPS power supplies
peak filtering capacitor. The preventive maintenance is performed
every third refueling outage and is accomplished by IP/O/A/305/13,
Nuclear Instrument and Reactor Protective System Power Supply
Capacitor Replacement. The inspector observed the I&E technicians
reterminating the power supply leads in the back of the RPS cabinet
prior to repowering the power supplies. Review of the controlling
procedure determined that the procedure did not control the lifting
or retermination of wires lifted by the technicians to remove and
reinstall the RPS power supplies. The technicians did not have any
documentation that identified the leads that had been lifted to
remove the power supplies and did not have any documentation that
the leads were properly reterminated. The inspector did observe
that the wires did have blue tags attached to them. The procedure
did require that a QA inspector verify that the power supplies had
been reinstalled; however, this step had already been signed off by
the QA inspector and the technicians were still reconnecting the
wires in the back of the RPS cabinet. Discussions with the
technicians determined that the QA inspector had signed only for the
power supplies being installed in the proper cabinet. Maintenance
Directive 7.5.3, Work Request Implementation, requires that
Section V of the work request "Additional Sheet" be completed
anytime temporary alterations are made to plant equipment or circuit
configurations and that the disconnection/reconnection of wiring be
listed. The Maintenance Directive also requires the date and time
the wires were disconnected/reconnected be entered, that the persons
performing the disconnection/reconnection sign each time when they
have performed the operation and that the two independent
verifications of the action be documented. The failure to meet the
requirements of Station Directive 7.5.3 with respect to
8
WR 57461B
Perform PM on 50X-51X, 50Z-51Z and 50G Relays
in 3TC-8
WR 55304B
Replace Peak Filtering Capacitor in RPS Power
Supplies
WR 50671K
Votes Testing of 3LPSW-19
WR 52897J
Determine Valve Position Upon Loss of IA for
3MS87
Determine Valve Position Upon Loss of IA for
Installation of 6th Stage Impeller in the 3A
MDEFWP
IP/0/A/305/13 Nuclear Instrument and RPS Power Supply
Capacitor Replacement
MP/0/A/2001/3 Air Circuit Breaker Inspection and Maintenance
MP/3/A/1300/28 Motor Driven Emergency Feedwater Pump
Impeller Changeout
b. Reactor Protection System Power Supply Preventive Maintenance
The inspector observed a portion of the work activity associated
with WR 55304B, replacement and testing of the RPS power supplies
peak filtering capacitor. The preventive maintenance is performed
every third refueling outage and is accomplished by IP/0/A/305/13,
Nuclear Instrument and Reactor Protective System Power Supply
Capacitor Replacement. The inspector observed the I&E technicians
reterminating the power supply leads in the back of the RPS cabinet
prior to repowering the power supplies. Review of the controlling
procedure determined that the procedure did not control the lifting
or retermination of wires lifted by the technicians to remove and
reinstall the RPS power supplies. The technicians did not have any
documentation that identified the leads that had been lifted to
remove the power supplies and did not have any documentation that
the leads were properly reterminated. The inspector did observe
that the wires did have blue tags attached to them. The procedure
did require that a QA inspector verify that the power supplies had
been reinstalled; however, this step had already been signed off by
the QA inspector and the technicians were still reconnecting the
wires in the back of the RPS cabinet. Discussions with the
technicians determined that the QA inspector had signed only for the
power supplies being installed in the proper cabinet. Maintenance
Directive 7.5.3, Work Request Implementation, requires that
Section V of the work request "Additional Sheet" be completed
anytime temporary alterations are made to plant equipment or circuit
configurations and that the disconnection/reconnection of wiring be
listed. The Maintenance Directive also requires the date and time
the wires were disconnected/reconnected be entered, that the persons
performing the disconnection/reconnection sign each time when they
have performed the operation and that the two independent
verifications of the action be documented. The failure to meet the
requirements of Station Directive 7.5.3 with respect to
9
lifting/reconnecting of wiring during the performance of WR 55304B
is identified as Violation 50-287/91-03-04:
Failure to Follow
Procedure/Inadequate Control of Maintenance Activities.
c. Electrical Breaker Maintenance and Testing
The licensee has three safety related 4160 volt switchgear for each
unit (TC, TD and TE). These switchgears supply safety related and
non-safety related load centers and motors. During observation of
Preventive Maintenance (PM) and testing conducted on the Unit 3
4160 volt electrical circuit breakers, the inspectors determined
that circuit breakers supplying non TS related loads do not receive
the same level of control and documentation with respect to
maintenance activities and testing that circuit breakers which
supply safety related loads receive.
During observation of PM activities conducted on circuit breaker
3TC-6 which supplies power to condensate booster pump 3A, the
inspectors determined that no procedure was in use to perform the
activities associated with the breaker. Discussions with the
maintenance personnel present, determined that procedures were only
required to be used when performing maintenance on circuit breakers
that supplied TS identified components. The personnel showed the
inspector the work package associated with the 3A HPI pump breakers.
This work package identified the breaker as TS related and
identified the procedure required to be used to perform the
maintenance activity. Discussion with the personnel present
indicated that the same maintenance activities were performed on
both breakers; however, the TS related breaker was required to be
performed per the procedure and the non TS related breaker was
accomplished via the skill of the craft. The inspector also
witnessed PM activities associated with the testing of 4160 volt
circuit breaker trip relays and determined that testing and setting
of the relays for TS related breakers were accomplished and
documented by procedures, however, testing of non TS related breaker
relays was accomplished via skill of the craft. The inspector held
discussions with licensee personnel and questioned the use of non TS
related work controls on circuit breakers that are housed in safety
related electrical switchgear. The inspectors consider that the
breakers for non safety related equipment contained in safety
related switchgear are safety related breakers and should receive
the same controls as the breakers supplying safety related
equipment. This item was discussed with licensee management and the
licensee is reviewing the controls for working on non TS equipment
circuit breakers contained in safety related switchgear. The
inspectors also discussed this item with regional electrical
personnel and requested guidance on whether breakers supplying non
safety related components contained in safety related switchgear are
required to be treated as safety related breakers. This item is
10
identified as Unresolved Item 50-269,270,287/91-03-02:
Circuit
Breaker Maintenance and Testing, pending further NRC and licensee
review.
No additional violations or deviations were identified.
5. Inspection of Open Items (92700)(92701)(92702)
The following open items were reviewed using licensee reports,
inspection, record review, and discussions with licensee personnel, as
appropriate:
a. (Closed) Inspector Followup Item (IFI) 50-269,270,287/89-12-02:
Review of Actions Taken Based on Findings of ECCS Valve Functional
Evaluation of February 1989. This item was opened to follow
licensee action associated with the failure of the boron dilution
flowpaths to meet single failure criteria. This was subsequently
addressed in LER 50-269/90-11. Based on the actions taken as
discussed in the LER and reviewed by the inspectors, this item is
closed.
b. (Closed) LER 50-269/90-11: Boron Dilution Systems Do Not Meet
Single Failure Design Criteria Due to Design Deficiency,
Unanticipated Interaction of Systems. This LER was provided in
correspondence dated July 26, 1990. On June 26, 1990, the licensee
identified a condition that both trains of the Boron Dilution System
contain valves that receive power from a common motor control
cubicle for all three Oconee units; therefore, these systems did not
meet single failure criteria. The temporary corrective actions for
this problem were to develop a procedure to provide temporary power
to one of these valves which would assure that one train would be
available if needed. The inspectors have reviewed the temporary
actions taken for this problem. The planned corrective actions are
to return one of the valves to an alternate power source. Station
Modification (NSM) 1, 2, 32867 has been proposed to implement this
change. The present scheduled dates for the completion of these
NSMs are refueling outages commencing in December 1991 for Unit 2,
May 1992 for Unit 3 and October 1992 for Unit 1. Based on the
temporary actions taken and the scheduled implementation of the
permanent corrective actions, this item is closed.
c. (Closed) P2189-12:
Part 21 from Limitorque Corporation Regarding
Pre -
1981 Type SMB-000 and Pre - 1976 Type SMB-00 Torque Switch
Potential Failure. The licensee received notification of this
potential problem in October 1989. This item was incorporated into
the stations Problem Investigation Report (PIR) process and
identified as 4-089-0173. Reviews were conducted to determine if
valves at Oconee were affected. A total of 14 valves were affected
on Unit 1, 12 valves on Unit 2 and 6 valves on Unit 3. The licensee
performed an operability evaluation and determined that the valves
in question were conditionally operable. This conditional
11
operability was in effect until the end of each units upcoming
refueling cycle. Unit 1 and 2 outages have been completed and each
of the identified valves have been verified to have the correct
component or the component was changed as necessary. The inspectors
reviewed the work request associated with each of the identified
valves. The valves for Unit 3 have been identified for the outage
in progress and work requests have been generated and scheduled to
address this potential problem. Based on these actions and the
review by the inspectors, this item is closed.
6. Exit Interview (30703)
The inspection scope and findings were summarized on February 25, 1991
with those persons indicated in paragraph 1 above. The inspectors
described the areas inspected and discussed in detail the inspection
findings. The licensee did not identify as proprietary any of the
material provided to or reviewed by the inspectors during this
inspection.
Item Number
Description/Reference Paragraph
50-269,270,287/91-03-01
URI - HPI Piggyback Issues, paragraph 2.c.
50-269,270,287/91-03-02
URI - Circuit Breaker Maintenance and
Testing, paragraph 4.c.
50-269,270,287/91-03-03
NCV - Failure to Periodically Review
Safety Related Procedures at Intervals Not
to Exceed Two Years, paragraph 3.b.
50-287/91-03-04
Violation - Failure to Follow
Procedure/Inadequate Control of Maintenance
Activities, paragraph 4.b.