ML15224A616

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Insp Repts 50-269/89-36,50-270/89-36 & 50-287/89-36 on 891112-1216.Violations Noted.Major Areas Inspected:Licensee self-assessment Capability & Onsite in Areas of Operations, Surveillance Testing & Maint Activities
ML15224A616
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 01/08/1990
From: Shymlock M, Skinner P, Wert L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML15224A614 List:
References
50-269-89-36, 50-270-89-36, 50-287-89-36, NUDOCS 9001190203
Download: ML15224A616 (18)


See also: IR 05000269/1989036

Text

a REG4

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION 11

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report Nos:

50-269/89-36, 50-270/89-36, 50-287/89-36

Licensee: Duke Power Company

422 South Church Street

Charlotte, N.C. 28242

Docket Nos.:

50-269, 50-270, 50-287

License Nos.

DPR-38, DPR-47, DPR-55

Facility Name: Oconee Nuclear Station Units 1, 2 and 3

Inspection Conduc ed:

November 12 -

December 16, 1989

Inspectors-

1//

V

n.

er, eni

Resident Inspector

Date Signed

t, esident Inspector

Date Signed

Approved by:

_____

____

____

___-___'

M. B. ShymloW(, Section Chief

Date Signed

Division of Reactor Projects

(I

SUMMARY

Scope:

This routine, announced inspection involved inspection at corporate

offices in the area of licensee self assessment capability and

on-site in the areas of operations, surveillance testing, maintenance

activities,

outage

activities, installation

and

testing of

modifications (Unit 3),

Fitness for Duty program training and

inspection of open items.

Results: A violation addressing two examples of procedural inadequacies was

cited during this period:

Inadequate program to ensure proper operation of safety related

throttle valves which resulted in a spill of reactor coolant

through the reactor building spray system into the reactor

building. (Paragraph 2.b)

-

Inadequate guidance in a switchyard component surveillance

procedure which contributed to a loss of power

on Unit 3.

(Paragraph 2.d)

9?001190*203 90010:3

F=

DR

A:0rIiCK:: 05000269

FDC

2

A violation addressing several

examples of failures to

follow

procedures was cited:

-

Failure to follow procedure during a transfer of power supplies

to an inverter resulted in an Engineered Safeguards actuation on

Unit 3 and led to a TS violation due to isolation of Reactor

Building'fire protection systems. (Paragraph 2.c)

-

Procedural requirements for operation of more than one reactor

coolant pump with reactor coolant temperatures less than

160

degrees F were not met. (Paragraph 2.e)

-

Failure to perform procedural requirements in sequence resulted

in a spill of contaminated water in the Unit 3 High Pressure

Injection Pump room. (Paragraph 2.e)

-

Performing procedural requirements out of sequence during a

cooldown on Unit 2 resulted in the low temperature overpressure

protection watchstander not having correct written procedures

pertaining to the assigned functions. (Paragraph 2.e)

A TS violation involving polar crane operation over the refueling

canal

and flagman positioning during crane operation was cited.

(Paragraph 5)

A weakness was noted concerning procedural compliance by Operations

personnel.

During detailed observation of evolutions the inspectors

noted numerous

instances where procedural

steps were performed

improperly out of sequence or not strictly in accordance with the

controlling procedures. Several instances clearly warranted formal

procedural changes which were not made.

This weakness contributed

directly to most of the violations noted in this report.

A strength was noted in that both the training and interim drawings

provided to operations personnel concerning recently installed

Nuclear -Station Modifications have significantly improved over

previous efforts.

(Paragraph 6)

I.

REPORT DETAILS

1. Persons Contacted

Licensee Employees

  • M. Tuckman, Station Manager

0. Couch, Keowee Hydrostation Manager

  • B. Barron, Assistant Station. Manager
  • J. Davis, Technical Services Superintendent

0. Deatherage, Operations Support Manager

B. Dolan, Site Design Engineer Representative

  • W. Foster, Maintenance Superintendent

T. Glenn, Instrument and Electrical Support Engineer

D. Hubbard, Performance Engineer

  • E. LeGette, Compliance Engineer
  • J. Lentz, Employee Relations Supervisor

t!

  • H. Lowery, Chairman, Oconee Safety Review Group

B. Millsap, Maintenance Engineer

  • D. Powell, Station Services Superintendent
  • G. Rothenberger, Integrated Scheduling Superintendent
  • R. Sweigart, Operations Superintendent

Other licensee employees contacted included technicians,

operators,

mechanics, security force members, and staff engineers.

NRC Resident Inspectors:

  • P. Skinner
  • L. Wert
  • Attended exit interview.

2.

Plant Operations (71707)(71710)(93702)

a. The inspectors, reviewed plant operations throughout the reporting

period to verify conformance with regulatory requirements, Technical

Specifications (TS), and administrative controls. Control room logs,

shift turnover records, and equipment removal and restoration records

were reviewed

routinely.

Discussions were conducted with plant

operations,

reactor engineering, maintenance, chemistry, health

physics, instrument & electrical (I&E), and performance personnel.

Activities within the control rooms were monitored on an almost daily

basis. Inspections were conducted on day and on night shifts, during

week days and on weekends.

Some inspections were made during shift

change in order to evaluate shift turnover performance.

Actions

De

observed were conducted as required by the Licensee's Administrative

Procedures.

The complement of licensed personnel on each shift

inspected met or exceeded the requirements of TS.

Operators were

responsive to plant annunciator alarms and were cognizant of plant

conditions.

Plant tours were taken throughout the reporting period on a routine

basis. The areas toured included the following:

Turbine Building

Auxiliary Building

Units 1, 2 and 3 Electrical Equipment Rooms

Units 1, 2 and 3 Cable Spreading Rooms

Unit 3 Penetration Room

Unit 3 Containment

Station Yard Zone within the Protected Area

Standby Shutdown Facility

Units 1, 2 and 3 Spent Fuel Pool Room

During the plant tours, ongoing activities, housekeeping, security,

equipment status, and radiation control practices were observed.

Unit 1 -

Unit 1 operated at 100 percent power for the

entire report period.

Unit 2 -

Unit 2 returned to 100 percent power on November 23, 1989

following a forced outage which began

on

November 10

following a dropped rod. Maintenance efforts were required

due to 2B1 and 2B2 Reactor Coolant Pumps vibration problems

which extended the outage.

The unit operated at

100

percent for the remainder of the report period.

Unit 3 -

Unit 3 remained in a scheduled end of cycle refueling

outage. As of December 16 the unit was proceeding to hot

shutdown condition in preparation for zero power physics

testing.

b. Unit 3 Reactor Coolant System Leak Through Building Spray Valve 3BS-1

On November 9, 1989, seat leakage through valve 3BS-1 resulted in an

approximately 2,000 gallon spill of reactor coolant through the

Reactor Building Spray (RBS) system into the Unit 3 containment (see

Inspection Report 50-269,270,287/89-34). The licensees investigation

into the cause of the seat leakage was initiated after a

comprehensive systematic plan was developed and discussed with the

inspectors.

Valve 3BS-1 had

been

maintained in

an

as

found

condition.

The licensee confirmed that there was excessive seat

leakage by 3BS-1 by using a hydrostatic test pump.

The 8 gpm pump

could not build up any pressure against the valve and leakage was

noted at a downstream drain line. The investigation then focused on

the operation and maintenance of the valve.

3

3BS-1

is

an eight inch motor operated Velan globe throttle valve

which shuts on torque (the

opening of the torque switch stops

movement in the shut direction once the valve is fully seated if the

operator is functioning properly).

By measuring circuit continuity

the licensee determined that the torque switch on 3BS-1 was not open.

Valve stem movement of approximately 1/4 inch (1.81 seconds travel

time) was observed (when the valve's control switch was held in the

shut position) before the torque switch opened. Apparently the Tast

time the valve was shut the control switch had not been held in the

shut position for a sufficient time period.

Since the operator for 3BS-1 has only two limit switch rotors

installed, the close light switch rotor also controls the open torque

switch bypass function. Consequently on a closing stroke the "close"

light will actuate before the valve is fully shut.

Operators are

aware that on this type of valve the control switch must be held in

the close position for an additional period of time after the close

light actuates in order to fully shut the valve.

The inspectors

noted several weaknesses in the operation of this type of valve;

PT/3/A/0150/22A,

Operational/Refueling Valve Functional

Test

(Enclosure 13.1), dated February 23, 1989, states that the 3BS-1

switch must be held in the 'close' position for approximately 3

seconds after the closed light is lit. A review of the MOVATS

signature traces for 3BS-1 indicates that the closed light

actuated at 8.055 seconds and the torque switch opened or

tripped at 11.45 seconds.

This indicates the operator should

have been instructed to hold the switch for at least 3.4 seconds

in order to ensure the valve is fully shut.

Signature trace analysis indicates that on the last operation of

3BS-1 the operator held the switch for about 1.6 seconds in the

closed position after the closed light actuated.

This is only

half of the time required by the procedure.

-

This aspect of the operation of this type of valve is not

discussed in detail in any documented operator training. It is

considered common knowledge of all operators that the switch

must be held in the closed position after the closed light

actuates. The licensee's investigation indicated that operators

use different time periods when operating these valves (values

from 2 to 5 seconds were stated).

-

There are nine valves of this type in various systems on each of

the three units. Only one procedure which requires these valves

to be cycled contains guidance on the time to hold the switch

after the closed light is lit

(BS-1,

BS-2 stroke test).

All

such throttle motor operated valves are distinguished by either

4

a yellow ring around the control switch or the word 'throttle'

on the control pushbutton and this is generally understood by

operators to mean the control switch must be held for 3 seconds

after the close light is received.

The licensee reviewed MOVATS traces on all 27 valves of concern. The

longest time interval from actuation of the close light until torque

switch tripping was found to be 5.28 seconds. Two other valves were

over 5 seconds and one was 4.97 seconds. Operations management will

be issuing written guidance to operators concerning time requirements

to ensure such safety related throttle valves are fully shut.

Discussion of this issue with Regional inspectors and close review of

IP/O/A/3001/10: Maintenance of Limitorque Operators,

dated June 23,

1989, indicated that there are weaknesses in the methods used to set

the valve operator limit switches during maintenance.

The clos.e

switch and the open torque switch bypass function are set by manually

closing the valve and then manually opening the valve until the disc

is free of its seat. A note preceding this step cautions that these

functions must be set to prevent torque switch actuation during

unseating of the valve.

Additional notes require ensuring that the

distance is 5 percent of open direction travel by either handwheel

turns after engagement,

stem travel or traces.

The procedure

emphasizes setting the switch after the handwheel resistance has

decreased to minimum running load. All of these statements address a

5 percent travel in the open direction as a minimum and no maximum

travel at setpoint is stated.

The information available on 3BS-1

indicates it

was set for a value of about 20 percent.

A longer

travel time in the open direction (before the open torque switch

bypass actuates) translates to the close light actuating with the

disc further from the fully shut position. The licensee is currently

evaluating changes needed to establish a program to control the

torque switch bypass time settings on these valves.

This program

will establish a maximum bypass time limit (less than or equal to 3

seconds) and ensure the valve operation is setup to meet this limit

as well as notification to operators if limit changes occur.

The

inadequacies identified in the review of this item are combined with

the example in paragraph

2.d and are identified

as Violation

50-269,270,287/89-36-01:

Failure to Provide Adequate Procedures as

Required by TS 6.4.1.a and 6.4.1.e.

C. Unit 3 Engineered Safeguards Actuation

At approximately 4:30 p.m.

on November

14,

1989

an Engineered

Safeguards

(ES)

actuation occurred on Unit 3.

The actuation was

caused by operator error during shifting of power supplies to a vital

panelboard. Unit 3 was in cold shutdown undergoing a scheduled 42

day refueling outage when this occurred. Reactor vessel water level

had been lowered to a reduced inventory condition in order to install

cold leg nozzle dams. No loss of decay heat removal capability or ES

injection into the vessel occurred.

After routine preventive maintenance had been performed on a portion

of the vital Instrumentation and Control System, power supplies were

being

transferred

in accordance

with

Operating

Procedure

OP/3/A/1107/04: Operation of the Vital Bus and Auxiliary Inverters.

The operator omitted a clearly designated step and erroneously opened

a switch supplying power prior to aligning the other source.

This

caused the 120VAC vital instrumentation bus to be de-energized which

resulted in the tripping of ES analog channel A.

Since ES analog

channel B was already tripped for unrelated testing, this two out of

three analog channels in a tripped state resulted in an -ES actuation.

The Oconee ES circuitry is designed such that the analog ES channels

trip when de-energized and. the digital channels are energized to

actuate. This resulted in a Keowee Hydrostation emergency start, a

temporary loss of the reactor building purge fan

and

several

radiation monitors,

and other miscellaneous equipment actuation.

Power was restored to the inverter and the ES circuitry was reset.

The event was reported to the NRC Operations Center at about 6:20

p.m.

in accordance-with 50.72(b)2ii.

At approximately 10:30 p.m.,

operators identified that

an

ES

valve had shut during the ES

actuation which secured fire protection to the Reactor Building.

This resulted in the violation of TS 3.17.5.3 for a period of

approximately 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.

This failure to follow procedure is combined with the example

identified in paragraph 2.e and will be identified as Violation

50-269,270,287/89-36-02:

Failure

to

Follow Procedures

During

Operation in a Shutdown and Cooled Down Condition.

d. Unit Three Momentary Loss Of Of Electrical Power

Oconee Nuclear Station is connected to the primary transmission

system through two large switching stations. Units 1 and 2 generate

power at 19KV which is stepped up to 230KV to feed the

230KV

transmission switchyard. Each unit is connected to the switchyard by

two breakers. There are eight transmission lines connecting this

switchyard to the remainder of the grid. Unit 3 also generates power

at 19KV, but its output is stepped up to 525KV and-feeds power to a

525KV switchyard through two breakers.

Three transmission lines

connect to this switchyard and the two switchyards are interconnected

through a 230/525 KV autotransformer.

At approximately 3:00 p.m., on December 3, 1989, Unit 3 experienced a

loss of electrical power which lasted for 21 seconds before power was

automatically restored. The unit was in cold shutdown, refueling had

been completed

and the Reactor Coolant System

(RCS)

level

had

recently been increased from a reduced inventory condition.

6

Prior to the loss of power event,

power was being provided to the

Unit 3 Main Feeder Buses (MFB) through the normal source breakers (NI

and N2)

by backfeeding through the generator main transformer from

the 525KV switchyard. The Startup transformer, which receives power

from the 230KV switchyard, was energized but the associated breakers

(El and E2) were open.

A surveillance test involving

the

autotransformer,

PT/0/A/0610/05B:

Electro-Mechanical

Relay Breaker

Trip Test, dated August 24,1989,

was being performed.

This is a

routine test conducted monthly. Step 12.26 of the test requires a

total of four breakers in the switchyard to be opened simultaneously.

This action separates the 230KV and 525KV switchyards.

Apparently,

due to

incorrect restoration

action following

some previous

maintenance in the 525KV switchyard, the yellow bus of the switchyard

was deenergized when the four breakers were opened (a disconnect had

been previously left open).

This caused the loss of power to the

MFB's.

Each of the MFB's provide power to each of the three

redundant Engineered Safeguards (ES) switchgear busses.

During normal operations, such a trip of the N1 and N2 breakers would

be accompanied by other control signals and a rapid transfer to the

startup transformer path via the El and E2 breakers.

In this case,

as expected, the rapid transfer did not occur.

The Main Feeder Bus

Monitor Panels (MFBMP)

are a non-safety related system designed to

assure a reliable source of power

to the MFB's during non-LOCA loss

of power events. An undervoltage condition for 20 seconds on 2 out

of 3 phases of both MFB's will initiate a MFBMP signal which provides

signals to various other breakers control logic and portions of the

Emergency Power Switching Logic (EPSL) to restore power.

Approximately 21 seconds after the MFB's were deenergized, the E2

breaker closed and energized the number 2 MFB via the startup

transformer. This action also energized the number 1 MFB since the

MFB's are connected through the ES switchgear buses they supply.

Initially there was a concern since some EPSL channel one components

appeared to have not functioned. properly during the event.

Subsequent investigation indicated that the timers involved in the

MFBMP circuitry did not actuate at exactly the expected 20 second

time period. The inspector observed testingwhich confirmed that one

set of timers actuated at about 19 seconds while the other set

actuated at about 21 seconds.

This apparently was sufficient to

cause the observed sequence of events and does not appear to be a

significant problem.

The times were adjusted to a 20 second dropout

time.

PT/0/A/0610/05B did not contain adequate guidance to ensure

electrical switchyard alignment prior to portions of the test during

certain plant conditions. This, in part resulted in the loss of

electrical power for the short duration during this test.

A

contributing factor in this event was the operators not being

aware of the status of the open switchyard disconnect.

An operator

involved in a restoration following switchyard maintenance activities

7

incorrectly performed

the restoration procedure and left the

disconnect open.

Additionally, it was noted that the 525KV

switchyard mimic bus in the Unit 1 and 2 control room does not .depict

this disconnect. This example of an inadequate procedure is combined

with the example identified in paragraph 2.b to constitute Violation

50-269,270,287/89-36-01:

Failure to Provide Adequate Procedures

e. Procedure Adherence Deficiencies

During this period the inspectors noted several incidents associated

with operators not following procedures as provided. The examples

noted are as follows:

On November 10, the inspector noted that a crud burst actuation

process

on Unit 3 was

being

performed

as controlled by

OP/3/A/1102/10, Controlling Procedure for Unit Shutdown.

This

procedure requires temperature to be maintained greater than 160

degrees F if two reactor coolent pumps are running, however, the

temperature observed by the inspectors was 155 degrees F. The

operators knew that the temperature was outside the procedure

requirements and had discussed this with Operations management

to assure no technical problems would exist when operating at a

value less than specified;

however,

the procedure

was not

formally changed to allow this deviation.

On November 11,

during cooldown on Unit 2 in accordance with

OP/2/A/1102/10, Controlling Procedures for Unit Shutdown,

Enclosure 4.2, step 2.9 was performed out of sequence.

Performance

of a step out of sequence is allowed by the

licensee's administrative .procedures. However,

as a result of

this change in the sequence,

the watchstanding procedures

associated with the

Low Temperature Overpressure Protection

(LTOP) were no longer valid. Verbal instructions were provided

to the LTOP operator but changes were not made to the procedure

to incorporate these instructions.

-

On November 17, a spill of contaminated water occurred in the

Unit 3 High Pressure Injection (HPI)

pump room.

Investigation

indicated that this was caused by a failure to follow procedures

in progress prior to performing steps in another procedure. The

licensee had just completed testing a containment penetration in

accordance with PT/3/A/0150/06, Mechanical Penetration Leak Rate

Test, and was returning the valves to the positions specified by

this procedure.

Step

19 of the enclosure being performed

included closing several valves and the installation of pipe

caps. Step 20 cleared tags associated with the component drain

pump. The Nuclear Equipment Operator (NEO)

was given the task

of returning the valves to their appropriate position and also

-nIII-

8

an additional task of performing another lineup to drain a

portion of another system using a portion of the first system.

No guidance was provided to the NEO as to the sequence of valve

manipulations. The operators cleared the component drain pump

tags and operated the system before Step 19 was completed by the

NE0. This caused the spill of water in the HPI pump room. The

NEO discovered the leak when he proceeded to the HPI room to

complete his assigned tasks. If the NEO had been redirected .to

a different job or had been delayed in entering the HPI pump

room,

the spill of water could have resulted in damage to

safety-related equipment.

These examples are being combined with the example discussed in

paragraph

2.c

and

will

be

identified

as

Violation

50-269,270,287/89-36-02:

Failure

to

Follow

Procedures During

Operation in a Shutdown and Cooled Down Condition.

f. Resolution of Concerns Relating to Operation With A Dropped Rod

Inspection Report 50-269,270,287/89-34 discussed a dropped rod event

which occurred on November 10, 1989 on Unit 2. The licensee's Design

Engineering (DE) group at that time had identified a concern that the

automatic protective system may not have had sufficiently low enough

setpoints to prevent local fuel damage under certain conditions of

high

power imbalance.

Consequently Unit 2 was placed in a hot

shutdown condition.

On

November 27,

1989,

the inspectors were

informed that the licensees

DE group

had completed a detailed

analysis of continued unit operation with a dropped rod. The results

indicated that the current TS required Reactor Protective System

Setpoints are set low enough to prevent any problems relative to

Departure

From Nuclear Boiling Ratio (DNBR)

and linear heat rate

limits.

Two violations were identified.

3. Surveillance Testing (61726)

Surveillance tests were reviewed by the inspectors to verify procedural

and performance adequacy. The completed tests reviewed were examined for

necessary test prerequisites, instructions, acceptance criteria, technical

content, :authorization to begin

work,

data collection, independent

verification where required, handling of deficiencies noted, and review of

completed work. The tests witnessed, in whole or in part, were inspected

to determine that approved procedures were available, test equipment was

calibrated, prerequisites were met,

tests were conducted according to

procedure,

test results were acceptable and systems restoration was

completed.

Surveillances reviewed and witnessed in whole or in part:

<II

9

PT/3/A/0610/01A Emergency Power Switching Logic Normal Source

Voltage Sensing Circuits dated November 8, 1989

PT/3/A/0610/01B Emergency Power Switching Logic Startup Source

Voltage Sensing Circuit dated November 21, 1989

PT/O/A/0202/12

High Pressure Injection System ES Test dated

PT/3/A/0150/22BDecember 4, 1989

PT/3/A/0150/22

Shutdown Valve Functional Test dated

January 25, 1989

PT/3/A/0150/22A Operational/Refueling Valve Functional Test dated

February 23,1989

PT/3/A/E600/22

Motor Driven Emergency Feedwater Pump Suction Check

Valve Test dated Juliy 14, 1988

PT/O/A/0230/16

Auxiliary Shutdown Panel Operability Test (Unit 3)

dated May 27,1987

IP/O/A/310/08A

Engineered Safeguards System Logic Subsystem 2 HPI

& RB Isolation Channel 2 Functional Test dated

September 17,1987

No violations or deviations were identified.

4. Maintenance Activities (62703)

Maintenance activities were observed and/or reviewed during the reporting

period to verify that work was performed by qualified personnel and that

approved procedures in use adequately described work that was not within

the skill of the trade.

Activities, procedures and work requests were

examined to verify proper authorization to begin work, provisions for

fire, cleanliness, and exposure control, proper return of equipment to

service, and that limiting conditions for operation were met.

Maintenance reviewed and witnessed in whole or in part:

MP/O/A/1800/14

Freeze Seal - NSM 2640 dated March 22, 1989

TN/3/A/2640/o/AM1 NSM 2640 -

Unit 3 Emergency Feedwater Upgrade

TN/3/A/2803/h/e

NSM 2803 - Main Feeder Bus Safety Train Cable

Separation dated Nov. 23, 1989

WR 57259D

Clean Emergency Feedwater Pump Turbine Oil Cooler

(MP/O/A/1100/12 dated January 23, 1988)

No violations or deviations were identified.

5. Unit 3 Refueling Outage (71707)

The inspectors conducted a tour of containment on November 27,

1989, to

observe activities in progress in this area. The refueling process had

begun and the inspectors were specifically monitoring this effort. During

this observation the inspectors noted that work was being performed,

III

10

simultaneously with fuel movement, using the small hook on the polar crane

to- support a ventilation fan adjacent to the transfer canal.

The

inspectors noted that the large hook, although nothing was attached to it,

was above the reactor vessel. Personnel working on the fan were using a

scaffold to allow access to the fan.

TS 3.12.1 requires that the

reactor building polar crane not be operated over the fuel transfer canal

when any fuel assembly is being moved.

When the fan was in position and

partially secured, the polar crane was moved from over the transfer canal.

The flagman, in communication with the crane operator, was located on the

third floor level.

TS 3.12.4 requires when the reactor vessel head is

removed and the polar crane is being operated in areas away from the fuel

transfer canal, the flagman shall be located on the top of the secondary

shield wall

(fourth floor) when the polar crane hook is above the

elevation of the fuel transfer canal. The inspectors notified the reactor

operator on the fuel handling crane and the senior reactor operator in

charge of refueling.

The licensee stopped the refueling process to

investigate this activity and take appropriate corrective actions prior to

continuing fuel

loading.

This finding is identified as Violation

50-287/89-36-04:

Inadequate Control

of Polar Crane Operation During

Unit 3 Refueling.

One violation was identified.

6.

Installation and Testing of Modifications (37828,37701)(Unit 3)

The inspectors selected several modifications concerning safety related

components which were not required to be submitted for approval to the NRC

(No modifications were being installed which required prior NRC approval).

Portions of the following Nuclear Station Modifications (NSMs),

their

related installation procedures, and testing procedures were inspected.

NSM 32803 Main Feeder Bus Safety Train Cable Separation

NSM 32640

Emergency Feedwater (EFW) Seismic Upgrade

NSM 32844 Auxiliary Reactor Building Coolers Seismic Upgrade

Of these three NSMs,

the EFW seismic upgrade was the most extensive and

was the most closely followed by the inspectors.

The NSM included the

replacement of several major large valves in the condensate system, the

addition of vent and drain lines to the Upper Storage Tank (UST) supply to

the Turbine Driven Emergency Feedwater Pump (TOEFWP),

removal of several

plant heating lines from the USTs,

and rerouting of some Low Pressure

Service Water piping which required a large freeze seal as well as some

other modifications. Many of these tasks were observed on a daily basis

during the modification work.

The inspectors reviewed portions of these NSM packages for compliance with

the Oconee

NSM Manual.

The required 10 CFR 50.59 documentation was

closely reviewed and no major discrepancies were noted.

The approved

implementation procedures were

reviewed and work observed to insure

compliance.

The

inspector noted that work within

sections of

TN/3/A/2640/0/AM1:

NSM 2640, Unit 3 Emergency Feedwater Seismic Upgrade,

  • 0

11

(October 9, 1989)

was being performed out of sequence despite a note

specifically requiring the steps within a section to be performed in

order. In this instance this did not adversely effect the quality of the

modification installation or personnel safety.

Report 269,270,287/89-25

discussed.two concerns associated with modifications which had also been

identified by a licensee QA surveillance.

The concerns involved interim

drawings and training provided to operators.

The

inspector noted that plant drawings which were effected by

modifications were correctly addressed by these interim drawings.

Improvements

were noted in the training of operators

on

installed

modifications.

The inspectors will review portions of the installation testing packages

during the next inspection period.

No violations or deviations were identified.

7. Resident Inspector Observation of Initial Licensee Fitness for Duty

Training (TI 2515/104)

The inspectors obtained copies of the licensee's Fitness for Duty (FFD)

initial training lesson plans and FFD program booklet.

The inspectors

reviewed this material and the requirements of Temporary Instruction

2515/104. On December 5, 1989, the resident inspector observed a training

session for employees who have unescorted access to a nuclear station.

The training consisted primarily of a lecturer reading the lesson plan

entitled "FFD

Training for Supervisors" (FFD-001

dated October 16,

1989)

with modifications to tailor the presentation to general

employees.

Several short videotapes were viewed and a question and answer session

followed the session. The training strongly emphasized that the licensee

is revising its.FFD policy and procedures based on the requirements of 10

CFR 26. The observed session lasted slightly over two hours. Along with

the printed material distributed this training should provide the

employees with a good fundamental knowledge of the licensees revised FFD

program.

Oconee's FFD initial training program consists primarily of presentations

made to two separate groups.

Lesson plan FFD-001:

FFD Training for

Supervisors,

is presented to supervisory personnel while FFD-002:

FFD

Training for Employees and Escorts, is given to other employees authorized

unescorted access. The inspector noted that section 4.0 of FFD-002:

FFD

Training for Employees and

Escorts, specifically

emphasized

the

responsibilities of an escort in observing and detecting fitness for duty

of individuals under escort. Section 4.1 of FFD-002 discusses a videotape

( shown as part of the training) entitled "Drugs in the Workplace." This

is intended to help employees recognize possible possession, use, or sale

of drugs. The observed session, which utilized a modified FFD-001:

FFD

12

Training

for

Supervisors, did

not specifically emphasize escort

responsibilities (Section

4.0 of

FFD-001

does not discuss escort

responsibilities). The Drugs in the Workplace videotape was shown during

the training.

10 CFR 26.22(b) requires that persons assigned to escort

duties be provided appropriate training in techniques for recognizing

drugs and indications of drug use,

sale or possession along with

techniques for observing aberrant behavior and procedures for reporting

problems. The inspector noted that section 4.2: Behavior Observation, of

FFD-002 was not covered in the observed session. These observations were

discussed with the Oconee Nuclear Station FFD Coordinator and the Oconee

Employees Relations Supervisor. The inspector emphasized his concern that

the training provided to employees and supervisors may not sufficiently

emphasize escort responsibilities.

The FFD Coordinator stated it would

be ensured that future training would emphasize escort duties.

In the near future FFD training session for supervisors will be observed.

All scheduled classes have already been given and a makeup session will be

attended. This will complete the requirements of TI 2515/104.

No violations or deviations were identified.

8.

Evaluation of Licensee Self - Assessment Capability (40500)

The inspector went to the general offices to perform a review of the

activities associated with the Nuclear Safety Review Board (NSRB).

This

review consisted of the following:

-

a review of meeting minutes for the past two years

-

a

review of meeting frequencies and composition to assure TS

requirements have been met

a review of qualifications and expertise of individual committee

members and their designated alternates

-

a review of selected audits and the audit schedule conducted under

the cognizance of the NSRB since January 1987

-

a review of the tracking mechanisms used by the NSRB for open items

-

-

a review of actions taken by the NSRB pertaining to proposed changes

to Oconee's TS.

In conjunction with this review the following specific documents were

reviewed:

-

Charter of the Nuclear Safety Review Board, Revision 8

-

NSRB Administrative Procedure (NSRB)/1,

dated 12/9/86,

Processing

Nuclear Safety Review Board Material

13

-

NSRB/2, dated 12/9/86, Conduct of On-Site Reviews and Audits

-

NSRB/3, dated 6/3/88, Record Retention and Handling

-

NSRB/4, dated 5/13/83, NSRB Outstanding Items Accountability

-

NSRB/5, dated 12/5/86, NSRB Review of Documentary Material

-

NSRB/6,

dated 12/5/86,

Conduct of Nuclear Safety Review Board

Meetings

NSRB/7,

dated 8/14/89,

Rev-iew of Nuclear Safety Evaluations for

Station Procedures, Procedure Changes, and Completed NSMs

NSRB/8, dated 9/12/88, NSRB Procedure for Processing Required Audits

During this review the inspector identified that there was no individual

appointed to the NSRB with expertise in the field of non-destructive

examination and testing. This was discussed. with the NSRB Chairman who

acknowledged this point, and stated this expertise had not been needed in

the past several years. If problems were submitted to the NSRB associated

with this area,

he was authorized to use consultants for this review.

Another inspector concern was that NRC inspection reports that did not

contain a Notice of Violation, were not reviewed by the NSRB.

Since

information addressed in these reports may provide insight to areas the

NRC considers to be strengths or weaknesses, the inspector recommended to

the chairman that they be considered in the review process. TS 6.1.3.3.b

and c states that the NSRB is to review proposed changes to procedures,

systems

or components,

and tests and experiments which involve an

unreviewed safety question.

This review is accomplished by use of a

subcommittee.

The results are then submitted to the NSRB for its review.

This process was discussed with regional management and considered to be

an acceptable method to meet the TS requirement.

The results of this

review indicate that the licensee has a self assessment capability that

meets the requirements of TS 6.1.3.

No violations or deviations were identified.

9. Inspection of Open Items (92700)(92701)

The following open items were reviewed using licensee reports,.inspection,

record review, and discussions with licensee personnel, as appropriate:

a. (Closed)

Unresolved

Item 50-269,270,287/89-34-04:

Resolution of

Apparently Incorrect Low Temperature Overpressure Protection (LTOP)

TS. This item addressed conflicts with TS 3.1.2.9 and the NRC Safety

Evaluation Report

(SER)

concerning that TS.

Inspection reports

50-269,270,287/88-34 and

89-05

provide additional

details and

document licensee commitments required to meet the SER assumptions.

During this inspection period the licensee discussed changing the

commitments made previously. A telephone discussion was held between

14

the licensee, NRR representatives and the inspectors on November 28,

1989, to discuss the proposed changes. A portion of the proposal was

to use some of the corrective action statements included in the

licensee's submittal of November 15, 1989 to change TS 3.1.2.9. The

discussion resulted in the following commitments:

-

The licensee will adhere to the present TS 3.1.2.9.a and b

except that both trains of LTOP must- be operable when Reactor

Coolant System (RCS)

temperature is less than 325 degrees F

(except when the reactor vessel head is removed).

The present

TS requires only one of the trains to be operable. This action

by the licensee is more conservative than the present TS and is

in agreement with the proposed TS.

This is not a change from

the previous commitment.

-

If

one of the LTOP trains become inoperable, the licensee will

take action as identified in the proposed TS

submittal .

At

present the inoperability of one LTOP train is not addressed in

the present TS (the inoperability of both trains is addressed).

This is also more conservative than the present TS requirements.

This is a change to the previous commitment.

The previous

commitment was to take the corrective action identified in TS if

either of the LTOP systems became inoperable.

-

The licensee will continue to use a dedicated operator with no

other responsibilities when plant conditions are such that LTOP

requirements are in effect.

This action will *be taken until

such

time

as other administrative procedures and hardware

modifications are implemented that would eliminate the necessity

of a dedicated operator.

(The

vulnerability to overpressure

transients with less than 10 minutes of operator action time

will be eliminated.)

Prior to removal of this dedicated LTOP

watchstander,

the

administrative

actions

and

necessary

modifications will

be discussed with the inspectors.

The

removal of the dedicated operator will be a change to the

previous commitment.

Based on the actions taken the unresolved item is being downgraded to

an Inspector Followup Item,

50-269,270,287/89-36-03:

Revised Low

Temperature Overpressure Protection System Operability Requirements.

b.

(Closed)

IFI 50-269,270,287/89-03-08:

Evaluation of Once Through

Steam Generator (OTSG) Rapid Cooling. This item documented a concern

of the Augmented Inspection Team (AIT)

investigating the fire in

switchgear 1TA (and related events) which occurred in January 1989.

The AIT asked the licensee to determine if

the subsequent rapid

introduction of subcooled water into the 1A OTSG negatively impacted

OTSG structural integrity. The inspectors reviewed documentation of

15

an OTSG transient assessment performed by Babcock and Wilcox (B&W)

dated January 16, 1989. The assessment considered the OTSG tubes,

main feedwater nozzles

and auxiliary feedwater

nozzles.

Usage

factors for this event were very small and it was concluded that this

transient had resulted in

no adverse effect on the structural

integrity of the OTSG. This item is closed.

C.

(Closed) IFI. 50-269,270,287/89-22-01: Update of Keowee Hydro Station

Alarm Response Procedures. This item addressed the concern that the

Keowee Procedures had not been updated since 1973. Modifications to

systems and changes in operating practices have been made during that

time. The Alarm Response Procedures have been completely reviewed

and updated. The response procedures are organized according to the

clearly labeled annunciator titles. This item is closed.

d.

(Closed) LER 50-269/86-02: EFW And LPSW Piping And Valves Not In Full

Compliance With FSAR Seismic Criteria. This LER was submitted in

correspondence dated March 5,

1986.

Modification

NSM

2640

was

completed on Unit 1 on February 24, 1989, on Unit 2 on June 29, 1989,

and was completed on Unit 3 during the present outage. Based on the

completion of these modifications, this item is closed.

e.

(Closed) LER 50-269/87-09: Two Functional Units Of Emergency Power

Switching Logic Taken Out Of Service Due To A Management Deficiency.

This LER was submitted in correspondence dated December 15,1987. The

corrective action for this item included a TS change which was due to

be submitted by July 15, 1988. Changes to this commitment were made

in subsequent correspondence by the licensee. The proposed change to

the TS was submitted August 31,

1989.

Based on this action in

conjunction with the earlier completion of the other prescribed

corrective actions, this item is closed.

f. (Closed) LER 50-269/88-04: Emergency Power Switching Logic Retransfer

To Startup Logic Defeated Due To Design Deficiency.

This LER was

submitted in correspondence dated April 6, 1988.

A portion of the

corrective action for this problem was to complete a self initiated

internal Quality Assurance audit. This was originally scheduled to

be accomplished in the third and fourth quarters of 1988, but was

delayed until the third quarter of 1989. This audit was completed in

September 1989,

and completes all corrective action for this item.

Based on this action, this item is closed.

g.

(Closed)

LER 50-270/88-02: Inoperability Of A Portion Of Emergency

Power Switching Logic Due To A Design Deficiency.

This LER was

submitted in correspondence dated May 26,

1988.

The licensee has

completed

all corrective actions identified in this LER.

The

inspector reviewed the corrective actions and considers this item

closed.

16

10.

Exit Interview (30703)

The inspection scope and findings were summarized on December 18, 1989,

with those persons indicated in paragraph 1 above.

The inspectors

described the areas inspected and discussed in detail the inspection

findings.

The licensee did not identify as proprietary any of the

material provided to or reviewed by the inspectors during this inspection.

Item Number

Description/Reference Paragraph

269,270,287/89-36-01

Violation - Failure to Provide Adequate

Procedures as Required By TS 6.4.1.a

and 6.4.1.e, paragraph 2.c and 2.e

269,270,287/89-36-02

Violation

-

Failure

to

Follow

Procedures

During

Operation

in a

Shutdown

and Cooled

Down

Condition,

paragraph 2.d and 2.b

287/89-36-04

Violation - Inadequate Control of Polar

Crane

Operation

During

Unit 3

Refueling, paragraph 5

269,270,287/89-36-03

IFI -

Revised LTOP System Operability

Requirements, paragraph 9.a