ML15224A582

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Insp Repts 50-269/89-25,50-270/89-25 & 50-287/89-25 on 890717-0819.Violations Noted.Major Areas Inspected:Maint Activities,Operations,Surveillance Testing,Facility Mods, Loss of DHR Actions & Insp of Open Items
ML15224A582
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 09/07/1989
From: Shymlock M, Skinner P, Wert L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML15224A580 List:
References
50-269-89-25, 50-270-89-25, 50-287-89-25, NUDOCS 8909150070
Download: ML15224A582 (11)


See also: IR 05000269/1989025

Text

,t

REG(,

UNITED STATES

o

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report Nos:

50-269/89-25, 50-270/89-25, 50-287/89-25

Licensee: Duke Power Company

422 South Church Street

Charlotte, N.C. 28242

Docket Nos.:

50-269, 50-270, 50-287

License Nos.

DPR-38, DPR-47, DPR-55

Facility Name:

Oconee Nuclear Station

Inspection Conducted: July 17 - August 19, 1989

Inspectors: .

,

(7

,-

--

Ff)

P. H. Skinner, Seni

Resident Inspector

Date Signed

lieI '2( /~

_")2C

L. D

r, Reside

Inspector

Date Signed

Approved by:

97-9

M B. S

Section Chief

Date Signed

ivision of Reactor Projects

SUMMARY

Scope:

This routine, announced inspection involved resident inspection

on-site in the areas of operations, surveillance testing, maintenance

activities, facility modifications, loss of decay heat removal (GL 88-17) actions, electrical power system self initiated technical

audit and design basis documentation analysis, and inspection of open

items.

Results:

During this period the inspectors noted a weakness in the licensees

program to take appropriate action to assure problems of a similar

nature do not recur and also a weakness in the maintenance of

physical examinations for licensed operators. A strength was noted

in the area of control of activities during the period of the time a

unit is in mid-loop operation as addressed by Generic Letter 88-17.

8909150 070 890808

PDR

ADOC:K 05000269

Q

FC

REPORT DETAILS

1. Persons Contacted

Licensee Employees

  • M. Tuckman, Station Manager
  • S. Baldwin, Compliance

C. Boyd, Site Design Engineer Representative

  • T. Curtis, Compliance Manager
  • J. Davis, Technical Services Superintendent

D. Deatherage, Operations Support Manager

W. Dukes, Medical Doctor

W. Foster, Maintenance Superintendent

T. Glenn, Instrument and Electrical Support Engineer

  • D. Havice, Instrument & Electrical Engineer

D. Hubbard, Performance Engineer

E. Legette, Assistant Engineer Compliance

  • H. Lowery, Chairman, Oconee Safety Review Group
  • G. Rothenberger, Integrated Scheduling Superintendent
  • R. Sweigart, Operations Superintendent

Other

licensee employees

contacted

included technicians,

operators,

mechanics, security force members, and staff engineers.

NRC Resident Inspectors:

  • P.H. Skinner
  • L.D. Wert
  • Attended exit interview.

2. An Unresolved Item is a matter about which more information is required to

determine whether it is acceptable or may involve a violation. There was

one unresolved item identified in this report (paragraph 3.b).

3. Plant Operations (71707)

a. The inspectors reviewed plant operations throughout the reporting

period to verify conformance with regulatory requirements,

technical

specifications (TS), and administrative controls. Control room logs,

shift turnover records, and equipment removal and restoration records

were reviewed routinely.

Discussions were conducted with plant

operations, maintenance, chemistry,

health physics,

instrument &

electrical (I&E), and performance personnel.

Activities within the control rooms were monitored on an almost daily

basis. Inspections were conducted on day and on night shifts, during

week days and on weekends.

Some inspections were made during shift

change in order to evaluate shift turnover performance.

3

told that this was covered by Corporate Medical Guidelines.

The

station up until 1984, had Station Directives to address this process

but at that time the medical groups at all sites were shifted to the

direction of the corporate office.

At that time the Station

Directive was deleted. The medical exams were not a problem prior to

1984 since at that time it

was a part of the application for a

license renewal every two years, but when this was changed provisions

for assuring this was done appear to have been inadequate.

A system had been established by corporate to list all Duke required

physicals (crane operators, fire brigade members, licensed operators,

asbestos handlers, etc.)

on a computer system, but it

appears that

this system was incorrect and inefficient in that many operators were

getting as many as three physicals a year (license, fire brigade, and

respirator).

As a result the licensee was

in the process of

correcting this inefficiency when the problem of missed medical

examinations was identified.

Medical

personnel

responsible for

maintaining

operator records would send notification to

the

operations supervision for supervisors to schedule examinations for

their personnel.

Since these notifications did not contain dates the

supervisors did not know that the operators had exceeded their

required dates. Review of the information provided to the operations

department indicated that the operators did obtain their physicals

upon notification by the medical department.

A computer program has now been established on site in the medical

facility that has a list of all operators and the dates that their

physicals are due.

This list has also been provided to the

supervision of each of the groups that has licensed operator

personnel that maintain their license. Another factor affecting this

process was that supervision normally scheduled the medical

examinations for the operators without notification to the operator

concerned until three days prior to the exam.

This was due to the

company policy associated with drug testing.

Although the operators did not get the required medical examinations

during the prescribed period, each did have a physical conducted by a

nurse. This 'nurse physical'

is comprehensive and includes most

checks provided in the physical given by the doctor except for X-ray,

EKG,

blood work, and drug screening.

In addition, if

problems are

identified during the 'nurse physical' the individual is required to

see a doctor. Discussions were held with the doctor that provides

these examinations concerning the individuals that had exceeded their

time intervals. None of these persons had any problems that would

have prevented them from fulfilling their watchstanding duties.

10

CFR 50.54(k) requires

an operator or senior operator licensed

pursuant to Part 55 to be present at the controls at all times during

operation of the facility. 10 CFR 55.21 requires a licensed operator

to have a medical examination by a physician every two years to

determine

that

the

operator

meets

the

requirements

of

10 CFR 55.33(a)(1). Pending further review of these requirements

4

by

NRR

this

will

be

identified

as

an

Unresolved

Item

50-269,270,287/89-25-01:

Apparent Failure to Provide

Personnel

Licensed Pursuant to 10 CFR 55 at the Controls at All Times During

Operation of the Facility.

c. Unit 1 Reactor Trip From 40% Power

On August 10,

1989, Unit 1 tripped from 40% full power at 3:41 p.m.

The plant responded as expected. Two main steam relief valves did

not reseat as expected and header pressure was reduced to

approximately 970 psig to allow the valves to reseat.

Upon

evaluation, the licensee determined that the valves reseated within

the prescribed operating tolerance of the valves.

The unit was

returned to critical operation at 9:10 p.m.

on August 10 and was

restored to 100% power operation on August 11.

This trip was caused

by an Instrument and Electrical (I&E) technician placing two Reactor

Protective System (RPS)

channels in a tripped condition at the same

time.

The inspectors reviewed this occurrence in detail.

The

sequence of events was the following:

At approximately 7:00 a.m.

on

August 10,

a low oil level alarm was received on the 1A2 reactor

coolant pump (RCP) motor. The licensee commenced a power reduction

at 7:45 a.m. in order

to

remove

the pump

from service.

At

approximately 10:00 a.m.

the pump was secured and the unit was in

operation in a three pump configuration. At noon the plant exceeded

the steady state quadrant power tilt

(QPT)

limit specified in

TS 3.5.2. Corrective actions were commenced by operations at that

time to try to reduce the QPT to the limits allowed by TS.

At

2:05 p.m. maintenance personnel had entered containment, added oil to

the RCP motor and the pump was restarted.

Also at approximately

2:00 p.m.,

the operators had not been successful in restoring the

QPT, so I&E was contacted to reduce the RPS Nuclear Overpower Trip

Setpoints according to the

requirements of

TS 3.5.2b.2.

I&E

personnel performed procedure IP/O/A/0301/003U,

Procedure To Reset

The Flux/Imbalance/Flow

and High Flux Trips For Operation With

Excessive Power Tilt Or Other Conditions, to adjust the RPS for this

condition.

Discussions with various operating and

IE personnel

identified the following points:

-

The procedure used for this activity is a very complex procedure

-

several

time

consuming calculations prior to actual

manipulations of the RPS controls.

-

It

has been used infrequently and a minimum number of I&E

personnel are qualified to perform this activity.

-

Sign offs in the procedure for step tracking are infrequent.

-

Several steps have multiple action steps within the step.

In addition to the problems described above with the procedure and

personnel qualifications, the individual performing the procedure

6

EHC trip circuitry and shorted out some components causing the loss

of EHC signal.

The plant responded normally to the trip although one

main

steam relief valve . (3MS-6)

did not reseat properly

and

operations personnel

had to reduce main steam header pressure to

approximately 970 psig to reseat the valve.

The licensee dried out

the panel,

replaced the faulted components in the EHC system and

restarted the unit.

The unit was taken critical at 5:47 p.m.

and

returned to 100% at 6:15 p.m. on August 19. The relief valve has

been identified as a work item for the upcoming outage presently

scheduled to start on November 15, 1989.

One violation was identified.

4.

Surveillance Testing (61726)

Surveillance tests were reviewed by the inspectors to verify procedural

and performance adequacy. The completed tests reviewed were examined for

necessary test prerequisites, instructions, acceptance criteria, technical

content, authorization

to begin work,

data collection, independent

verification where required, handling of deficiencies noted, and review of

completed work. The tests witnessed, in whole or in part, were inspected

to determine that approved procedures were available, test equipment was

calibrated, prerequisites were met,

tests were conducted according to

procedure,

test results were acceptable and systems restoration was

completed.

Surveillances reviewed and witnessedin whole or in part:

WR 57855A

Perform Test on Keowee Line Relays (Annual Testing)

(21L1,50P,51,50,51G,67G,87L,74PW)

PT/O/A/0610/02

Electrical Grid Trouble Protection System Logic

and Switchyard Isolation Testing

MP/1/A/2200/06

Inspection and Maintenance of Keowee Unit 1

Permanent Magnetic Generator

IP/3/A/305/9

RPS 'A' Main Feedwater to Main Turbine Trip

Calibration

PT/1/A/0202/11

High Pressure Injection System Performance Test

IP/0/A/0310/013C

Engineered Safeguards System Logic Subsystem 2 RB

Isolation and Cooling Channel 6 On Line Test

(Unit 3)

IP/1/A/0305/001E

Reactor Protective System Channel 'A' RC

Temperature Instrument Calibration

No violations or deviations were identified.

5. Maintenance Activities (62703)

a. Maintenance activities were observed and/or reviewed during the

reporting period to verify that work was performed by qualified

personnel and that approved procedures in use adequately described

work that was not within the skill of the trade.

Activities,

7

procedures

and

work requests were

examined to verify proper

authorization to begin work, provisions for fire, cleanliness, and

exposure control, proper return of equipment to service,

and that

limiting conditions for operation were met.

Maintenance reviewed and witnessed in whole or in part:

WR 55162B PM Control Rod Drive Breaker for Units 2 & 3 AC-3

WR 55406B PM Control Rod Drive Breaker for Units 2 & 3 AC-6

WR 22434C Investigate lB LPSW Pump Abnormal Start

WR 22405C Repack Outboard Rearing LPSW Pump 2B

b.

Inadequate Retesting of Valve 3LWD-1 (62703)

On August 11, 1989, the licensee discovered that valve 3LWD-1 (Normal

Reactor Building Sump Suction, Unit 3) had been returned to service

following maintenance without all required retests having been

performed. The torque switch on the valve's operator had

been

adjusted and no leak rate test was performed before this Engineered

Safeguards Containment Isolation valve was returned to service. The

leak rate test is required by TS 4.0.4 which requires testing in

accordance with Section XI of the ASME Code.

The leak test was

subsequently

performed with satisfactory results.

Since this

incident is similar to a previous

issue (LER

269/88-01:

TS

Violations Due to Missed ASME Section XI Testing Resulting From

Management Deficiency), involving valve 1RC-7, the

inspectors

examined the circumstances in detail.

At Oconee, the control and

planning of maintenance including

retesting

requirements

is

accomplished through the Work ,Request (WR)

process.

SD 3.2.1: Work

Request, and Maintenance Directives (MD) 7.5.1 through 7.5.5 contain

most of the applicable guidance concerning WRs.

The root cause of

the 1RC-7 incident as stated in the LER was a management deficiency

due to the failure of management to insure the proper implementation

of the station WR program used to control the work on 1RC-7. Several

problems including inadequate training, failure to follow WR

procedures,

problems

with

the

directives,

and

inadequate

communications

caused that

incident.

The

LER

states

that

programmatic problems associated with the directives and individual

groups methods of implementing these directives caused the majority

of the mistakes. Numerous corrective actions were identified and

implemented.

After investigation,

the inspectors

concluded that the

3LWD-1

incident occurred primarily due to a miscommunication between the job

supervisor and the Performance

(PE)

representative concerning the

scope of the maintenance actually performed on the valve.

Although

the fact that adjustment had been made to the torque switch is

clearly documented in the "action taken" section of the WR,

a phone

conversation between the job supervisor and PE failed to communicate

to

PE

that the torque

switch

had

been adjusted.

This PE

representative was well aware of the 1RC-7 incident and its causes.

9

NSM 2458 AL Replace Valves 2FDW-107 and 2RC-7

NSM 2458 AM Replace Valves 2FDW-107 and 2RC-7

NSM 2759 AK1 PORV Low Range Pressure Control Instrumentation

NSM 2755 AL1 Replace Pneumatic Control Loop For PORV (RC 66) With

Electrical Current Control Loop and Add Time Delay

Two areas of concern were identified associated with returning a system to

operation following a modification.

These were training provided to

operations personnel and interim drawings potentially needed by operations

upon restart of the system.

These problems were recently identified by

the Quality Assurance group on-site following a surveillance (0-S8853) of

the startup following the Unit 1 outage and a surveillance (0-S89/ST-5)

conducted during the Unit 2 outage.

Problem Investigation Report (PIR)

2-089-0114 has been issued with the response to be provided by the

operations and projects groups management.

Licensee management has

indicated that these problems will be corrected prior to the upcoming

refueling outage for Unit 3 which is scheduled to begin in mid - November.

Pending satisfactory resolution of this PIR, the inspector is identifying

this concern as

an

Inspector Followup Item

269,270,287/89-25-04:

Resolution of PIR 2-089-0114.

No violations or deviations were identified.

7.

TI 2515/101 Loss of Decay Heat Removal (GL88-17) (71707)

Inspection Report 50-269,270,287/89-17 discussed the review of two of the

six applicable expeditious action items required by Generic Letter(GL) 88-17. During this report period the inspectors completed the remaining

requirements of TI 2515/101.

The third applicable expeditious action item requires at least two

independent,

continuous temperature indications whenever the Reactor

Coolant System (RCS)

is in a mid-loop condition and the reactor vessel

(RV)

head is on the vessel.

The GL requires that these temperature

indications be periodically checked and recorded by

an operator or

automatically and continuously monitored and alarmed,

depending on the

location of the monitoring.

The licensee committed to monitoring of the

temperature indications by control room operators and formally logging

those indications every two

hours.

Enclosure 4.7 of Operating

Procedure(OP)/2/A/1103/11: Requirements for Reducing RV level Less Than

50 Inches On LT-5 (LT-5 is Oconee's RV level instrument: 50 inches on LT-5

corresponds to about 32 inches above the top of the hot leg flow area),

contains independence criteria for temperature indications and monitoring

requirements if

the RV head is in place.

Core exit thermocouple (CETC)

indications from each train of the Inadequate Core Cooling Monitor (ICCM)

are normally selected.

If

both trains of ICCM are not available, an

operable CETC output is selected from the Operator Aid Computer (OAC)

to

be utilized along with an operable ICCM train CETC.

The alarm setpoints

of the selected CETC's are reduced to 140 degrees F.

Performance Test

(PT)/2/A/600/01:

Periodic Instrument Surveillance, requires recording of

the selected two primary CETC indications every two hours.

During the

10

last Unit 2 refueling outage the inspectors observed operator compliance

with these procedures and noted no problems.

The fourth expeditious action item requires at least two independent,

continuous RCS water level indications whenever the RCS is in a reduced

inventory condition (below about 48 inches on LT-5 at Oconee).

These

indications should also be either periodically checked and recorded by an

operator or automatically and continuously monitored and alarmed. In the

response to the GL, the licensee stated that only one permanent RCS water

level indication is available per unit in the control room, with other

alternatives being evaluated.

The installed RV

level instrumentation

(LT-5)

operable during draindown is a differential pressure transmitter

which is connected to a water filled reference leg (which is

open to

containment atmosphere) and to the RCS cold leg piping.

The connection

tap is on the elevation center line of the cold leg piping.

These

characteristics make LT-5 very sensitive to variations in containment

pressure or RCS pressure. In discussions with the inspectors, operators

indicate that they are well aware of the limitations of LT-5.

The

inspectors have observed some problems with the LT-5 indication system

during past outages.

It

was noted that although normally a temporary

level indication system (tygon tubing) is installed before level

is

reduced below 28 inches, during the most recent outage due to a high

radiation area near the connection point, this installation was

not

performed.

The tygon tubing level *indicator system,

due to its RCS

connection location and complications involved with running tubing over

such a large elevation, has not been a reliable level indication system.

During an inspection visit to McGuire Nuclear Station the inspector

observed an ultrasonic detector (temporary installation) in operation.

This system, based on control room operator comments,

works very well.

Oconee

management

has indicated similar options (as

well as other

alternatives)

are

being

considered for Oconee.

Enclosure 4.7 of

OP/2/A/1103/11:

Requirements for Reducing RV Level Less Than 50 Inches On

LT-5,

requires that LT-5 (and

any other redundant level

indication,

excluding tygon tubing) be verified operable.

PT/2/A/600/01:

Periodic

Instrument Surveillance, requires recording of this level indication every

two hours whenever level is less than 50 inches.

The fifth applicable expeditious action requires the implementation of

procedures and administrative controls to generally avoid operations

which knowingly lead to perturbations to the RCS or to systems necessary

to keep the RCS stable while in a reduced inventory condition. Enclosure

4.7 of OP/2/A/1103/11 requires that the Operating Engineer or designee

sign a step which states that testing or maintenance which may adversely

affect the performance of systems or components required for decay heat

removal is not scheduled for the period of operation less than 50 inches.

While this step appears very broadly worded and requires significant

judgement and coordination effort on the part of the Operating Engineer's

staff, no problems have been noted in this area to date. During the last

outage the inspectors followed several maintenance activities which could

have affected decay heat removal capability. In all cases work was either,

12

particularly rely on extensive coordination and involvement on the part of

the operating staff, no significant problems have been noted by the

inspectors. During the inspection the observations included in the NRR

letter dated May 17,

1989,

in response to the licensees' submittal that

were considered. While the licensee's formal response appeared to contain

insufficient detailed information in several areas, a closer onsite review

into each of the applicable actions resulted in most of the comments being

fully resolved. The licensee is continuing to evaluate installation of an

additional, more reliable water level indication system in order to fully

comply with the GL recommendation on water level indications.

No violations or deviations were identified.

8.

Electrical Power System Self Initiated Technical Audit (SITA)

and Design

Basis Documentation (DBD) Analysis Programs

During this report period the licensee continued both of these programs.

A meeting with NRR was held on June 22,

1989 in Washington,

D.C.

to

discuss Oconee's Electrical

Power System and related Licensee Events

Reports.

Followup meetings were held onsite on July 13,

1989 with AEOD

personnel and July 19-21, 1989 to discuss the SITA process in more detail.

Inspection Report 269,270,287/89-17 contains details of several additional

electrical system problems identified by these efforts.

On August 4, 1989, as a result of the DBD effort on the 4 KV System, the

licensee identified that the '2B' Reactor Building Spray (RBS) pump motor

had been

replaced with another motor which had different starting

characteristics from the original motor. A DBD review of the calculation

disclosed that under a Loss of Coolant Accident coincident with a Loss of

Offsite Power

event

(LOCA/LOOP),

the motor may

have tripped while

starting. The licensee immediately declared the spray pump inoperable and

entered a 7 day Limiting Condition for Operation in accordance with TS 3.3.6.c.(2).

The overcurrent relays were reset to the new calculated

settings and the pump was declared operable at 1155 on August 5, 1989.

Because incorrect or inappropriate motor overcurrent settings have been a

problem in the recent past at Oconee (LER

269/87-05: High Pressure

Injection (HPI) Pumps Potential Tripping, LER 269/88-13: Lee Gas Turbines

Unacceptable as Backup Emergency Power), the inspectors examined closely

this latest issue in regards to the corrective actions of the earlier

issues.

The licensee informed the inspectors that after the HPI pump

motor overcurrent issue had been identified, all safety equipment that

would be actuated on a LOOP or a LOCA was reviewed to ensure that the

overcurrent relays were set correctly.

During those reviews the Design

Engineering (DE)

personnel involved utilized the starting characteristics

of the original spray pump motors.

Review of the spray pump motor

calculations as part of the DBD analysis revealed that the motors had been

replaced with motors of different starting characteristics.

Although

several spray pump motors had been replaced, analysis revealed that only

the '2B' motor had this incorrect overcurrent setting problem. The motor

had been replaced in 1980 which was prior to the licensee's initiation of

The Overall Plan for Organizational Review of Modifications (TOPFORM)

13

program which contains requirements specifically designed to prevent such

occurrences during modifications. The licensee informed the inspectors

that all other safety related motors have been examined to ensure that

their overcurrent settings are correct. The

'2B'

RBS pump motor appears

to have been a unique problem caused by an error during the analysis

(after the HPI motor incident) of LOCA loads fed via the underground

emergency power path. The licensee's present modification process ensures

that this problem would not occur on a pump motor replaced or added in the

future. This item will be identified as a Noncited Violation;

NCV

270/89-25-03:

Reactor Building Spray Pump Motor Incorrect Overcurrent

Relay Settings.

This licens identified violation is not being cited

because criteria specified in Section V.G.1 of the NRC Enforcement Policy

were satisfied.

Another potential problem was identified by the SITA team on July 20, 1989

during the onsite portion of their 4160V system audit. During a tour of

the Keowee Hydro Station battery room, the team identified that cable

trays and

HVAC duct work above the batteries appeared to not

be

seismically qualified.

A Problem Identification Report (PIR) was

initiated. A subsequent DE review found that the cable trays and ductwork

are not seismically designed.

Although the FSAR does not specifically

require review of interactions between

QA Condition I components and

non-seismic components,

DE looked into this issue and concluded that

seismic interaction between the trays or ducts and the Keowee batteries

are not a safety concern.

A memorandum to file documents this conclusion

and supporting information. This memo notes that the overall issue of

seismic interaction for equipment necessary for safe shutdown will be

addressed when Unresolved Safety Issue (USI) A-46 is resolved by walkdowns

in accordance with Seismic Qualification Utilities Group (SQUG)

guidelines.

In response to observations stated during the July 19-21 meeting between

NRR representatives and the licensee and the inspectors concerns (see

Inspection Report 269,270,287/89-17 and

LER 269/89-09),

the licensee

established a task force to revise TS 3.7, Auxiliary Electrical Systems.

The inspectors were concerned that significant problems with the TS which

had recently been discovered would not be corrected in a timely matter.

While it would be premature to submit a complete detailed revision to TS 3.7 before the DBD and SITA efforts are complete, the significant concerns

recently discovered should be addressed promptly such that operation in an

unanalyzed or not permitted configuration is prevented.

The task force

met on July 19, 1989 and decided that the recent TS 3.7 submittal will be

revised and

resubmitted

by about September 1, 1989.

The licensee

discussed these changes with the inspectors and ensured that their

immediate concerns would be satisfied. A complete rewrite of the TS is

expected to be submitted about June 1991. This revision is intended to

improve the format of the TS, make it less confusing and improve its ease

of use for the operators, in addition to incorporating the results of the

SITA/DBD programs and other concerns of the operators.

The inspectors

will continue to closely follow the SITA and DBD efforts and results.

'

15

be complete by June 1, 1989. The inspectors conducted a review to

determine if this LER could be closed. The chemistry department had

initiated action to have the degraded valves replaced.

Five valves

had been identified but only two had been replaced.

The second

action had also been accomplished, in that, the chemistry department

had performed an evaluation and determined that the facility was

understaffed, but no action has been taken by management to address

this problem. Since the LER implies, although not stated, that the

actions taken will preclude a similar occurrence from happening, the

inspectors considers that insufficient actions have been taken to

prevent this problem.from recurring although the specific action was

taken. The inspectors discussed this with upper management

and a

review of this issue is being performed. This item will remain open

pending further review and action taken by management.

10.

Exit Interview (30703)

The inspection scope and findings were summarized on August 19, 1989,

with those persons indicated in paragraph 1 above.

The inspectors

described the areas inspected and discussed in detail the inspection

findings listed below. The licensee did not identify as proprietary any

of the material provided to or reviewed by the inspectors during this

inspection. Dissenting comments were not received from the licensee.

Item Number

Description/Reference Paragraph

UNR 269,270,287/89-25-01

Apparent Failure to Provide Personnel

Licensed Pursuant to 10 CFR 55 At The

Controls At All Times During Operations

Of The Facility, paragraph 3.b.

VIO 269,270,287/89-25-02

Inadequate

Corrective

Action

to

Preclude

Recurrence of Events

(two

examples) paragraphs 3.c and 5.b.

NCV 270/89-25-03

Reactor Building Pump Motor Incorrect

Overcurrent

Relay

Settings,

paragraph 8.

IFI 269,270,287/89-25-04

Resolution

of

PIR

2-089-0114,

paragraph 6.