ML15118A221

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Insp Repts 50-269/97-02,50-270/97-02 & 50-287/97-02 on 970323-0503.Violations Noted.Major Areas Inspected: Operations,Engineering,Maint & Plant Support
ML15118A221
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 06/02/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML15118A219 List:
References
50-269-97-02, 50-269-97-2, 50-270-97-02, 50-270-97-2, 50-287-97-02, 50-287-97-2, NUDOCS 9706120187
Download: ML15118A221 (45)


See also: IR 05000269/1997002

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

50-269, 50-270, 50-287, 72-04

License Nos:

DPR-38, DPR-47, DPR-55, SNM-2503

Report No:

50-269/97-02, 50-270/97-02, 50-287/97-02

Licensee:

Duke Power Company

Facility:

Oconee Nuclear Station, Units 1, 2 & 3

Location:

7812B Rochester Highway

Seneca, SC 29672

Dates:

March 23, 1997 - May 3. 1997

Inspectors:

M. Scott, Senior Resident Inspector

G. Humphrey, Resident Inspector

N. Salgado, Resident Inspector

D. Billings, Resident Inspector

R. Moore, Reactor Inspector (Sections E2.1, E8.2, E8.4,

E8.5)

R. Chou, Reactor Inspector (Sections E1.3, E1.4, E1.5)

N. Economos. Reactor Inspector (Section M1.3)

B. Carroll, Project Engineer (Sections M8.5, M8.6)

Approved by:

C. Casto, Chief, Projects Branch 1

Division of Reactor Projects

Enclosure 2

9706120187 970602

PDR

ADOCK 05000269

G

PDR

EXECUTIVE SUMMARY

Oconee Nuclear Station, Units 1, 2 & 3

NRC Inspection Report 50-269/97-02,

50-270/97-02. 50-287/97-02

This integrated inspection included aspects of licensee operations.

engineering, maintenance, and plant support. The report covers a six week

period of resident inspection; in addition, it includes the results of

announced inspections by four regional reactor inspectors.

Operations

Unit 1 was shutdown for a scheduled Reactor Coolant Pump (RCP)

outage. This was professionally and methodically accomplished

with good operator command and control.

Rod drop time testing

during the shutdown was acceptable. (Section 01.2)

The return of Unit 1 to power operation was appropriately managed

and executed. Aside from the higher than expected RCP vibration

values, the plant operated ina normal and expected manner.

(Section. 01.4)

On April 21, licensee investigation discovered unidentified

Reactor Coolant System (RCS) leakage. On April 22, the licensee

declared a Notice of Unusual Event based on unidentified Unit 2

leakage greater than 10 gpm. The 2A1 High Pressure Injection

(HPI) line had a crack in the pipe to safe end weld. During the

discovery and investigative phases of the 2A1 event, the

Operations staff performed professionally. The licensee

appropriately communicated with the NRC and other agencies. A

special NRC inspection team was formed to followup on this event.

(Section 01.5)

During the two Unit 2 drain downs to < 50 inches RCS level (mid

loop), the inspectors concluded that the licensee implemented and

.

maintained the requirements specified by procedure while

accomplishing reduced inventory operations. The inspectors

concluded that the reduced inventory evolutions were well

coordinated and controlled. (Section 01.6)

Based on initial Unit 2 HPI pipe crack event findings of the

licensee's Failure Investigation Process (FIP) team, the licensee

re-evaluated previous non-destructive examinations made on Unit 3

and voluntarily shut it down.

(Sections 01.7 and E1.6)

On May 3 at 9:20 a.m., Unit 3, which had been shutdown the

previous evening and was being prepared for further cooldown, lost

the flow from two HPI pumps. The residents were promptly notified

by the licensee and responded to the site. Aside from the failure

of the pumps, the licensee activities in response to the Unit 3

event were adequate. Post event operational management of the

Enclosure 2

2

problem was adequate. In view of the initial non-level emergency

plan action determination, the licensee's decision tQ man the

Technical Support Center (TSC) and Operations Support Center (OSC)

was conservative and practical. A NRC Augmented Inspection Team

was formed to evaluate the circumstances surrounding the unusual

event. (Section 01.8)

The licensee identified a lack of procedural controls to maintain

Low Pressure Injection (decay heat removal) cooler outlet

temperature above the minimum temperature (70 degrees F) shown on

the Technical Specification (TS) heatup and cooldown curves,

section 3.1.2. Procedural guidance permitted operation at

temperatures lower than the operating region as defined by TS

curves. A licensee engineer identified this problem during a Unit

3 outage review and a Non-Cited Violation (NCV) was identified.

(Section 03.1)

A Technical Specification required lock on a Control Rod Drive

System patch panel was found unlocked in 1995. This was reported

in a Licensee Event Report and a NCV was identified. (Section

08.1)

Maintenance

The inspector concluded that the licensee's actions were

appropriate to identify and repair a Unit 3 HPI pump oil leak

within the required Limiting Condition for Operation (LCO)

timeframe. The licensee's evaluation of the Component Cooling

(CC) system flashing during the post modification HPI performance

test was adequate. Placing the operations procedure for the CC

system on administrative hold was appropriate while the licensee

continued to review the process .of setting up flow to the letdown

coolers. (Section M1.2)

Corrective maintenance on the 1A1 Reactor Coolant Pump was being

performed in accordance with approved procedures. Craft and

supervisors were knowledgeable and carried out their tasks

satisfactorily (Section M1.3).

Operations failure to complete the procedure prerequisites prior

to performing other sections in the main body of an elevated water

storage tank (for fire protection) civil inspection procedure was

identified as a violation of procedure adherence. (Section M1.4)

Engineering

The inspectors concluded that the two remaining sections of Unit 3

Integrated Control System (ICS) testing were satisfactorily

accomplished in accordance with the licensee's procedures.

Control of all test activities was good. Positive observations

Enclosure 2

3

were made relating to test briefings. Control Room (CR) briefings,

and communication and coordination of test evolutions. (Section

E1.1)

The licensee reported an unresolved safety question to the NRC on

missile protection of the Low Pressure Service Water (LPSW) system

piping. (Section E1.2)

The inspectors concluded that the licensee performed adequate pre

operational tasks for the transporting, inserting, and retrieving

of the Dry Storage Cask from the Fuel Receiving Area to the

Horizontal Storage Module. (Section E1.3)

The inspectors considered that the licensee performed an adequate

installation of concrete base mat and Horizontal Storage Modules

for Phase III of the Independent Spent Fuel Storage Installation,

except as identified in the violation on under sized welds (first

example). (Section E1.4)

The inspectors concluded that the licensee performed an adequate

review on the vendor Calculation Evaluation for the Upper Surge

Tank Supports. The modification on the supports was acceptable,

except as identified in the violation on Upper Surge Tank

uninspected welds (second example of one above).

(Section E1.5)

The cognizant engineer controlled and directed the maintenance

activity associated with the 1A1 Reactor Coolant Pump in a well

planned and conservative manner. Additional resources contracted

to assist in vibration analysis made a positive contribution in

assessing the problem. (Section M1.3)

The licensee was proactive in rapidly forming a Failure

Investigation Process (FIP) team shortly after the Unit 2

injection line crack condition was known. The licensee called in

available industry talent to support and supplement the team. The

licensee was communicative with the NRC and provided information

as required and requested by the NRC. (Section E1.6)

Procurement Engineering performance related to upgrade and

qualification of safety-related replacement parts was good.

Engineering evaluations were technically sound and well

documented. (Section E2.1)

Deficiencies were identified in the licensee's measures to assure

the quality of equipment and services received from a 10 CFR 50.

Appendix B, vendor. A violation of regulatory requirements was

identified. (Section E2.1)

Unrelated to procurement engineering, a violation was identified

for inadequate corrective actions and design control on Reactor

Enclosure 2

4

Building Cooling Unit (RBCU) fuse failures identified in 1995.

Additionally, Engineering failed to identify the opepability

impact of the fuse failures on the RBCUs. (Section E8.4)

Plant Support

During the Unit 2 HPI pipe crack and Unit 3 HPI pump degradation

events that occurred this inspection period, inspectors were

present to observe Emergency Plan activities performed by the

licensee. Overall, the licensee performed in a conservative

manner on both events and followed their Emergency Plan

Procedures. (Sections 01.5, 01.8, and E1.6)

Enclosure 2

Report Details

Summary of Plant Status

Unit 1 operated at full power until a scheduled shutdown on March 28, 1997.

to investigate the cause of high vibration on the 1A1 Reactor Coolant Pump

(RCP). (Section 01.2) The Unit was back online on April 8. 1997 (Section

01.3). and remained at full power for the remainder of the reporting period.

Unit 2 operated at full power until April 21, 1997, when the Unit began

experiencing increased unidentified leakage. During the process of shutting

down the unit, unidentified leakage increased to approximately 12 gpm at which

time the licensee initiated a Notice of Unusual Event (NOUE). (Section 01.5)

In order to examine and repair a failed weld in the 2A1 High Pressure

Injection (HPI) line (Section E1.6). the licensee reduced Reactor Coolant

System (RCS) inventory to 16 (+\\- 2) inches on two occasions (Section 01.6).

At the end of the inspection period, the unit remained drained down to 16 (+\\

2) inches.

Unit 3 operated at full power for most of the reporting period until May 2.

1997, when the unit began shutting down in order to examine a HPI nozzle based

on re-evaluation of previous Non-Destructive Examination (NDE). During the

process of going from hot to cold shutdown, two of three HPI pumps were

potentially damaged. A NOUE was declared by the licensee on May 3. 1997.

(Section 01.8)

Review of UFSAR Commitments

While performing-inspections discussed in this report, the inspectors reviewed

the applicable portions of the UFSAR that related to the areas inspected. The

inspectors verified that the UFSAR wording was consistent with the observed

plant practices, procedures, and/or parameters. A licensee identified UFSAR

issue is addressed in Section E1.2.

I. Operations

01 - Conduct of Operations

01.1 General Comments (71707)

Using Inspection Procedure 71707, the inspectors conducted frequent

reviews of ongoing plant operations. In general, the conduct of

operations was professional and safety-conscious. Specific events and

noteworthy observations are detailed in the sections below.

01.2 Unit 1 Scheduled Shutdown (71707)

a. Inspection Scope

On March 28, Unit 1 shutdown to perform repairs on the 1A1 RCP that had

exhibited higher than normal vibration since the last inspection

period/startup from a forced outage (Inspection Report 50-269,

Enclosure 2

2

270,287/97-01, Section 01.2). The inspectors observed the'shutdown

activities and reviewed emergent problems.

b. Observations and Findings

The shutdown was normal, with all equipment operating as expected except

as indicated below. An inspector observed the satisfactory performance

of PT/0/A/0300/01, Control Rod Drive (CRD) Rod Timing Test. All rods

were within the administrative and less restrictive Technical

Specification (TS) time limits.

During the shutdown, the 1A2 RCP experienced high vibration and was

secured earlier than anticipated. An alternate RCP was used to cool the

plant to conditions permitting entry into Decay Heat Removal (DHR). The

1A2 RCP had reached approximately 30 mils displacement intermittently at

the pump's coupling spool piece which is higher than its normal at power

operation shutdown alarm setpoint of 20 mils. No damage occurred to the

pump or other plant components. Section M1.3 discusses work performed

on the 1A1 and 1A2 pumps. Section 01.4 discusses the return to power

operations of the unit.

c. Conclusions

The Unit shutdown was professionally and methodically accomplished with

good operator command and control.

Rod drop time testing performed

during the shutdown was acceptable.

01.3 Unit 1 Venting of the RCS (71707)

a. Inspection Scope

As discussed in Inspection Report 50-269.270.287/96-17. a violation was

identified regarding incomplete venting of the RCS due to valve

mispositioning. On April 5, the inspector observed the venting of the

Unit 1 RCS.

b. Observations and Findings

After repairs were performed on the 1A1 and 1A2 RCPs, the RCS loops were

refilled. The senior resident inspector observed the satisfactory

venting of the loops in accordance with OP/1/A/1103/02. Operations

performed the activities with appropriate diligence. As an independent

verification of a proper vent, when the RCPs were started no pressurizer

level changes were observed. Gaining additional information during this

venting, Operations has planned further enhancements to the procedure

prior to its next use. The RCP work is discussed in Section M1.3.

Enclosure 2

3

01.4 Unit 1 Restart (71707)

a. Inspection Scope

After RCP repairs had been performed, Unit 1 was prepared for restart.

Restart activities took place from April 7 - 11.

During the

preparation, which included various combinations of RCP pump operation,

the inspectors observed pump vibration levels and operator activities.

b. Observations and Findings

Aside from some higher than expected RCP vibration levels, the startup

preparation activities were normal and appropriately carried out by the

licensee. The unit went critical at 6:36 a.m., on April 11, 1997. The

Main turbine generator was latched to the electrical grid at 4:12 p.m.

that same day. Two minor problems occurred during startup. One

involved pressure swings in the auxiliary steam header pressure when the

operators were balancing steam load between Unit 1 and Unit 3. The

licensee had been continually looking at this problem throughout the

inspection period. The second minor problem occurred during the

approach to criticality. The startup was delayed due to Group 5. Rod 7

not moving when other rods in the group indicated movement. A corroded

connector pin was identified as the cause. Following cleaning of the

pin and testing, the Unit was started up without further problems.

Observation of the approach to criticality was found to be adequate.

During the restart activities, the 1A1 and 1A2 RCPs had higher than

expected vibrations. During low RCS pressure and temperature 1A2 RCP

runs, the pump ran with 30.3 and 25.8 mils vibration (at the pump

coupling spool piece, X and Y orientation on 4-7-97) but settled into

more expected levels of 5.5 and 4.3 mils (4-10-97) at higher pressure

and temperature with all RCPs in operation. During low RCS pressure and

temperature 1A1 RCP runs, the pump ran 46.0 and 39.0 mils (at same

locations as above on 4-7-97) and it settled into slightly higher than

expected levels of 19.6 and 20.5 mils (on 4-10-97). The recommended

emergency shutdown vibration levels provided by the pump vendor was 20.0

mils at the spool piece location. The licensee had been in

communication with the pump vendor as previously discussed in Inspection

Report 97-01, resolving that the higher than expected vibration was

mainly an economic'consideration. The RCP seal package was not

challenged by the pump vibration levels. The pump vendor was expected

on site in May 1997, to review collected data from the "A"

loop RCPs.

As of this report, the licensee planned to run the RCP with appropriate

planned contingencies, 50.59 evaluation, and engineering overview until

the next refueling outage (late August). The licensee did not yet have

a course of action for the 1A1 RCP repair/reduction in vibration level.

Enclosure 2

4

c.

Conclusions

The return of Unit 1 to power operation was appropriately managed and

executed. Aside from the higher than expected RCP vibration values, the

plant operated in a normal and expected manner.

01.5 Unit 2 2A1 Injection Line Break

a. Inspection Scope (71707. 93702)

On April 21, Unit 2 personnel detected an increase in RCS unidentified

leakage and responded to the event. The licensee called the Senior

Resident Inspector (SRI), who came to the plant to followup on the

occurrence. The leakage was not readily identified. While the licensee

performed an orderly shutdown, the leakage increased to the point that a

Notice of Unusual Event was declared.

b. Observations and Findings

On April 21. at 10:45 p.m., Operations personnel observed indications

that Unit 2 had increased unidentified RCS leakage. The licensee began

investigating in accordance with Technical Specification (TS) 3.1.6.

The normally constant level Letdown Storage Tank (LDST) was slowly

losing level and the normal Reactor Building (RB) sump required

increased pumping. As the above was observed, the RB general radiation

monitors came into alarm. A subsequent RCS leakage calculation

indicated a 2.36 gpm leak rate, which was up from the normal rate of a

few tenths of a gpm. The licensee called the SRI at 12:50 a.m., who

responded to the plant. On April 22, 1997, at approximately 1:30 a.m.,

an Operations RB entry revealed a spraying fog in the "A"

cavity near

the 2A1 RCP that could not be safely approached. The licensee began an

orderly shutdown of the unit at 3:52 a.m. and notified the NRC duty

officer at 4:26.a.m. At that time the leakage rate was 3.4 gpm. The

inspectors went into an around the clock coverage for plant monitoring

with supplemental personnel from the regional office staff.

That same day, reactor power was reduced to 20 percent (reached at 09:08

a.m.), an held for another RB entry but the licensee was still unable to

identify the leak due to spray. The leakage was seen at or near the

2HP-127 isolation valve, which is on the 2A1 normal makeup injection

line near the RCS cold leg. Leakage continued to gradually increase

until about 4:00 p.m. when it exceeded 10 gpm and the licensee declared

a Notice of Unusual Event. At 4:46 p.m., the licensee verified that RCS

boron was within the limits of the shutdown boron calculation and plant

cooldown was commenced. Later on April 22, 1997, the licensee exited

the unusual event condition at 8:32 p.m. when RCS leakage went below 10

gpm (two consecutive calculations). Maximum achieved leakage was nearly

12 gpm.

Enclosure 2

5

On April 23, 1997,

at 4:45 a.m., a third containment entry-was made. At

the time, the plant was approximately 250 degrees F and 278 psig. with

RCS leakage at 1.8 gpm. The SRI entered the building with two

operations personnel, discovering a still spraying unisolable crack in

the weld joining the 2A1 injection line pipe and the injection nozzle

safe end. The 2.5 inch diameter pipe weld was cracked between the 10:00

to 2:00 o'clock position. All hangers on the piping appeared to be

intact, as did the 2A2 injection line.

Once on shutdown cooling, Operations proceeded to drain down for

inspection and removal of the crack area for root cause determination.

Section E1.6 discusses preliminary investigation of the problem.

Section 01.6 below discusses the two draindowns to reduced inventory.

A special NRC team inspection was officially formed (Inspection Report

97-07) April 5, 1997, to follow this event to its completion. Prior to

team formation, the team leader had been on site since the day of the

event following licensee activities.

c. Conclusions

During the discovery and investigative phases of the problem, the

Operations staff performed professionally. The licensee appropriately

communicated the emergency class notification and updates to the NRC and

other agencies.

01.6 Draindown of the Unit 2 RCS to Midloop

a. Inspection Scope (71707. 93702, 40500)

As a controlled repair activity followup to the above event, the

licensee drained the Unit 2 RCS twice to levels below the RCP seal

package. Prior to, and during the draindowns, the residents attended

the prejob briefs, pre-planning meetings, Plant Operations Review

Committee (PORC) meetings, as well as observed the draindown evolutions

to achievement of stable conditions.

The inspectors reviewed the Unit 2 midloop operations as controlled by

procedure OP/2/A/1103/11. Draining And Nitrogen Purging Of Reactor

Coolant System.

b. Observations and Findings

In order to repair a failed weld downstream of 2HP-127 on the outlet

side of the tee where the warming line connects to the injection line

(Section 01.5), the licensee reduced RCS inventory to 16 (+\\- 2) inches.

The licensee achieved the required levels on April 27 and 30. The

inspectors reviewed the licensee's program prior to the reduction of RCS

inventory and verified that the requirements were met while operating at

the reduced inventory levels as specified in procedure OP/2/A/1103/11,

Enclosure 2

6

Enclosure 3.6, Requirements for Reducing Reactor Vessel Level to < 50"

on LT-5. This procedure stipulated the sequence and stepsrequired for

reduction of RCS inventory and midloop operation. It further specified

the precautions and limitations to be adhered to while in midloop.

The inspectors verified that the requirement for two independent trains

of RCS level monitoring was met while at reduced inventory. This was

accomplished through the use of two permanently installed instruments

(2LT-5A and 2LT-5B) and two temporary ultrasonic instruments.

Level

indications were displayed in the control room (CR) on the 2LT-5A and

2LT-5B indicators, the Inadequate Core Cooling Monitor, and on the

Operator Aid Computer.

The inspector verified that two trains of core exit thermocouples were

available and utilized while at reduced inventory, as well as that the

two sources of inventory makeup and cooling were available for

operation. Multiple sources of offsite power were also available. The

inspector reviewed the licensee's contingency plans to repower vital

busses from available alternate electrical power supplies in the event

of the loss of the primary source.

Once the section of pipe was cutout, and capped, the licensee commenced

makeup to raise RCS level to 80 inches on April 29, 1997. Although, the

level was increased, the licensee was maintaining < 50" requirements

until repairs were completed.

A second draindown to 16 (+/-2) inches was necessary to perform repairs

on the damaged thermal sleeve and to replace the HPI piping that had the

weld crack. The draindown commenced on April 30, 1997. The inspectors

were in.the CR to observe operations during this draindown evolution.

All the parameters described in the previous paragraphs were applicable

for this draindown. No problems were identified. The Unit remained in

the draindown condition through the end of this reporting period.

c.. Conclusion

The inspectors concluded that the licensee implemented and maintained

the requirements specified by procedure while accomplishing reduced

inventory operations without incident on two occasions. The inspector

concluded that these reduced inventory evolutions were well coordinated

and controlled.

01.7 Unit 3 Shutdown Due to Injection Line Concerns

a. Inspection Scope (71707, 93702. 40500)

Based on initial Unit 2 event findings of the Failure Investigation

Process (FIP) team, the licensee re-evaluated previous non-destructive

examinations made on Unit 3. The licensee voluntarily shutdown Unit 3

when the 3A1 injection line condition had been brought into question

Enclosure 2

7

(see Section E1.6). The inspectors monitored the activities before and

during the shutdown.

b. Observations and Findings

The unit completed a normal shutdown from 100 percent power on May 1 and

2. Aside from some minor Integrated Control System (ICS) problems at

about 12 percent power, the shutdown was routine. All parameters and

plant equipment except ICS operated normally. As power was decreasing

from the 12 percent range, the ICS transfer from constant Tave to

decreasing Tave programs was not a bumpless transfer in that power

abruptly dropped from 12 to 7 percent power (as indicated on NIs).

The

operators stopped power reduction and reset the reduction rate from 0.2

% per minute to 0.1 % per minute and a slow, predictable power reduction

resumed. Instrument & Electrical (I&E) engineers were reviewing the

occurrence at the end of the period.

01.8 Unit 3 Loss of Normal RCS Makeup

a. Inspection Scope (93702)

On May 3, at 9:20 a.m., during preparations for further Unit 3 cooldown,

the 3A and 3B HPI pumps experienced fluctuating pressure, flow, and

motor amperes. The licensee declared the pumps inoperable/out-of

service. The residents were promptly notified by the licensee and

responded to the site.

b. Observations and Findings

As indicated above, Unit 3 was preparing to cooldown with one Low

Pressure Injection (LPI) pump in RCS recirculation and the 3B1 RCP

running to cool RCS components. With the Letdown Storage Tank (LDST)

indicating approximately 55.9 inches level, a statalarm annunciated

indicating low HPI header pressure. Operators observed the running 3B

HPI pump motor amperes oscillate. The 3A HPI pump auto-started with the

low pressure and it also indicated swinging motor amperes. Both pumps

were secured. The entire episode with the pumps lasted approximately 19

minutes when the last HPI pump, the 3A, was secured. At the end of this

time, the plant was still at a stable temperature and pressure with the

heat from the running RCP maintaining pressure. All other evolutions

were stopped while the licensee evaluated the condition. Once notified,

the residents responded to the plant. Licensee evaluation of the

emergency plan indicated that no notifications were required at that

time. The licensee manned the Operation Support Center (OSC) and the

Technical Support Center (TSC) to support evaluation of the condition

and to be available should conditions worsen. The residents went into

an around the clock coverage.

During the pump problems, a non-licensed operator (NLO) was dispatched

to the HPI pump room for observation. He noted smoke and/or a vapor in

Enclosure 2

8

the air around the 3A pump and the pump was warm. He reported this to

the CR. When the SRI arrived at the site at approximately9:40 a.m.

(well after the HPI pumps had been secured), he immediately inspected

the pump areas noting no smoke or unusual heat. There was a slight

electrical odor in the air. Suction pressure was 45 to 50 psig on the

pumps. The 3A pump had a local discharge gage pressure of zero and the

3B pump had a pressure of 2030 psig (CR pressure read zero for this

value). The pump seals were observed not to be leaking fluid at that

time. Reportedly, the licensee flooded the suction line with borated

water storage tank (BWST) head pressure and the 3A pump seal leaked

water. Separately, a resident inspector also responding to the site had

entered the Unit 3 CR to followup on recovery activities.

The licensee took actions to get out of the condition of being unable to

cool down the RCS further. They took time to understand what of the HPI

system was functioning and available for use. Due to the chance that

the 3A and 3B pump were damaged, they did not want to pump/flow

associated pieces into the-rest of the HPI piping. Other than to the

LDST, the 3C HPI pump, which is normally only used during refueling

outages, can also be aligned to the BWST for makeup to the plant. A

procedure was developed to makeup to the RCS with this pump. Further, a

contingency procedure was also written to perform actions should the 3C

pump and flow path not work.

In parallel, the licensee attempted to.determine what had happened to

the two HPI pumps that had been secured. Checks on the level of the

LDST indicated that the level instruments were not reading correctly.

The reference leg of the instruments was found to be approximately 50

percent full after the tank had been re-filled. With tank level being

operated previously at around an indicated 55.9 percent, there was some

likelihood that the out-of-service HPI pumps had become air bound.

Due to the length of time it took to prepare the procedures for use of

the 3C HPI pump and the contingency plan, at the discretion of plant

management, the licensee entered into an Unusual Event Classification

from their emergency plan (May 3).

The 3C HPI pump use procedure became

available in the evening of May 3. The contingency plan procedure was

not available until the next day which was outside of the current

inspection period.

Through the night of May 3, the licensee made preparations for the next

day's operational recovery to resume plant cooldown. The licensee

flushed and vented the piping surrounding the 3C pump and made

instrument checks of components. The plant was heating up about one

degree per hour, but otherwise was in a very stable condition.

The NRC formally chartered an Augmented Inspection Team (AIT) on May 5,

1997, to evaluate the licensee's activities regarding the above event.

The manager for the AIT was sent to the site on May 3, 1997, to support

Enclosure 2

9

the resident's around the clock coverage. The AIT's findings will be

documented in IR 50-269.270,287/97-06.

c. Conclusions

Operational management of the problem was adequate. In light of the

non-level emergency plan action determination, the licensee's manning of

the TSC and OSC was conservative and practical.

01.9 10 CFR 50.72 Reports Submitted During this Inspection Period

During the inspection period, five 10 CFR 50.72 notifications were

called in by licensee. The inspectors were appropriately notified of

the reports by the licensee. The residents tracked any Limiting

Condition for Operation (LCO) conditions and followed up on any

corrective actions.

The following reports were made by the licensee:

-

On April 2. 1997, for Unit 3. it was determined that the Reactor

Building Cooling Unit (RBCU) primary side control fuses were

potentially under rated and may not have permitted the RBCUs to

start during a Loss of Coolant Accident (LOCA)/Loss of Offsite

Power (LOOP) upon receipt of an Engineered Safeguards (ES) signal.

The fuses had been replaced with fuses of a higher rating on June

21. 1995. Therefore, the potential RBCU inoperability existed on

Unit 3 prior to June 21, 1995. Section E8.4 of this report

addresses this issue..

-

On April 17, 1997, it was determined by the licensee's engineering

analysis that the travel stops on valve HP-120 may not have been

set to adequately restrict makeup flow through this valve. As a

result, during past periods in which Units 1, 2. and 3 were in a

condition where RCS temperature was less than 325 degrees F, the

second train of Low Temperature Overpressure Protection (LTOP)

may

not have been capable of mitigating certain LTOP events since less

than a ten minute delay period would have been available. This is

discussed in Section E2.2 of this report.

-

On April 26, 1997, it was determined that portions of Oconee's Low

Pressure Service Water system piping did not meet the Oconee UFSAR

design requirements for high trajectory turbine missiles. This is

discussed in Section E1.2 of this report.

-

On May 2, 1997, it was determined that Oconee Unit 2 primary

unidentified leak rate was found to exceed TS 3.1.6.1 limits of 1

gpm. Maximum leak rate was approximately 12 gpm.

Based on this

information, the licensee entered into an Emergency Plan Unusual

Event action level.

This is discussed in Section 01.5 of this

report.

Enclosure 2

10

-

On May 3, 1997, it was determined by engineering evaluation that

with an inaccurate LDST level indication the Unit 3 HPI system

would not have been able to perform its intended safety function

during power operations. At approximately 9:20 a.m. on the same

day, two of the HPI pumps had been potentially damaged by possible

air binding due to voiding of the LDST. Section 01.8 discussed

this event.

02

Operational Status of Facilities and Equipment

02.1 Engineered Safety Feature System Walkdowns (71707)

The inspectors used Inspection Procedure 71707 to walkdown accessible

portions of the following safety-related systems:

Keowee Hydro Station

Unit 2 HPI injection lines

Unit 2 HPI pumps

Unit 3 HPI pumps

Unit 3 penetration rooms

Unit 1, 2. & 3 600 Volt electrical breakers and supply

transformers

Unit 2 and 3 TDEFW pumps

Unit 2 and 3 RBs

Equipment operability, material condition, and housekeeping were

acceptable in all cases. Several minor discrepancies were brought to

the licensee's attention and were corrected. The inspectors identified

no substantive concerns as a result of these walkdowns.

03

Operations Procedures and Documentation

03.1

Inadequate Procedure for Control of LPI Temperature

a..

Inspection Scope.(71707)

The inspector reviewed Licensee Event Report (LER) 269/97-01 and

interviewed personnel associated with the issue of inadequate procedural

control of LPI temperature.

b. Observations and Findings

On December 15, 1997, Units 1 and 2 were in cold shutdown and Unit 3 was

in a refueling outage. All three units were being cooled by LPI flow

which is the B&W version of decay heat removal. A system engineer

identified a lack of procedural controls to maintain LPI (decay heat

removal) cooler outlet temperature above the minimum temperature (70

degrees F) shown on the TS heatup and cooldown curves, section 3.1.2.

Procedural guidance permitted operation at temperatures lower than the

operating region as defined by TS curves.

Enclosure 2

11

A 10 CFR 50.72 notification was made on February 13. 1997,-following the

completion of a past operability evaluation (PIP 5-96-2653.).

The

evaluation concluded that limiting values for temperature had been met

in the past.

The licensee's review of Operations procedures indicated that 70

degrees F was the minimum temperature that can be injected into the

reactor vessel. However, when compared to the TS limit, the procedure

limit was not compensated for instrument inaccuracy or operational

margin. Other Operations procedures required that the LPI pump suction

temperature be maintained between 60 and 125 degrees F.

Technical inaccuracies in the operating procedures did not include

adequate consideration and emphasis on the applicability of TS

temperature limits when heatup and cooldown activities were not in

progress. Therefore, the applicability of monitoring LPI cooler outlet

temperature as a controlling parameter was omitted. This could have

allowed LPI to enter the vessel at a temperature lower than that allowed

by TS.

Immediate corrective actions were to increase LPI cooler outlet

temperature to 81 degrees F until instrument inaccuracies could be

determined. Followup corrective actions included revising Operating

Procedures with correct instrument accuracies to specify operation at

greater than 75 degrees F at the LPI cooler outlet temperature to assure

current minimum TS limits were met.

This licensee-identified and corrected violation is being treated as a

Non-Cited Violation (NCV). which was consistent with section VII.B.1 of

the NRC Enforcement Policy. This is identified as NCV 50-269.270,

287/97-02-01, Inadequate Procedure For Control of LPI Temperature.

LER 269/96-01 has other planned corrective actions that have yet to be

implemented. Figures in TS 3.1.2 may be changed under the corrective

action scheme.

On a separate but related topic, the site's Design Basis Document (DBD.

00S-0254.00-00-1028, dated 11-27095, section 31.3.17) discusses BWST

electric heater capabilities. The heaters are supposed to maintain BWST

temperatures between 60 to 65 degrees F. The rational behind this

statement was recognizing the need to maintain the borated water supply

above 50 degrees F to lessen the potential for thermal shock of the

reactor vessel during high pressure system operation. TS 3.3.4 basis

stated the same information as the DBD. The DBD section did not discuss

HPI or LPI inadvertent injections or ES flow testing at lower BWST

temperatures. The inspectors will review other documents as it relates

to pressurized thermal shock of the RCS under Inspector Followup Item

(IFI) 50-269,270,287/97-02-09, BWST Temperature Requirements.

Enclosure 2

12

c. Conclusions

The licensee identified a lack of procedural controls to maintain LPI

(decay heat removal) cooler outlet temperature above the minimum

temperature (70 degrees F) shown on the TS heatup and cooldown curves,

section 3.1.2. Procedural guidance permitted operation at temperatures

lower than the operating region as defined by TS curves. A licensee

engineer identified this problem during a Unit 3 outage review. An NCV.

was issued.

08

Miscellaneous Operations Issues (92901, 90712)

08.1 (Closed) LER 50-269/95-05-00: Breach of Technical Specification Due To

Unlocked Control Rod Patch Panel

On July 8, 1995, at 10:15 a.m., operators discovered a Unit 1 CRD System

Patch Panel was unlocked as described in Inspection Report 50-269,270,

287/95-18. This panel was required by TS 3.5.2.7 tobe locked at all

times after confirmation of proper rod operation and sequence. The

licensee entered LCO 3.0 that required plant shutdown within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />

unless the condition is rectified and the LCO exited. The licensee

determined the panel lock to be broken, and placed a security guard at

the panel at 1:00 P.M. At that time, the LCO was exited. The lock was

repaired at 4:10 p.m. The licensee also verified that all three Units

CRD patch panels were locked. This licensee-identified and corrected

violation is being treated as a Non-cited Violation, consistent with

Section VII.B.1 of the NRC Enforcement Policy. This item is identified

as NCV 50-269/97-02-02. Unlocked CRD System Patch Panel.

08.2 (Closed) LER 50-269/95-05-01: Breach of Technical Specification Due To

Unlocked Control Rod Patch Panel

This LER supplement was sent by the licensee to correct a typographical

error documented in LER 50-269/95-05-00. This item is closed based on

the closure of LER 50-269/95-05-00 documented in section 08.1 of this

inspection report.

08.3 (Closed) VIO 50-270/96-10-01: Failure To Change Flux/Flow Imbalance

Setpoint

As described in Inspection Report 50-269,270.287/96-10 on July 6, 1996.

control rod 3 of group 7 dropped from approximately 95% withdrawn to

approximately 84% withdrawn. During the recovery attempt the rod

dropped to fully inserted. TS required a power reduction to less than

60% and a reset of the high flux and flux/flow imbalance trip setpoints.

The licensee did not reduce the Nuclear Overpower Trip Setpoints for the

flux/flow imbalance after reducing power to less than 60%. As part of

the corrective actions, the abnormal procedures for addressing a dropped

control rod, AP/1,2.3/A/1700/15, Dropped Control Rods, was to be changed

to include independent steps for resetting the high flux and

Enclosure 2

13'

flux/flow/imbalance trip setpoints. A note was to be added to the

procedure to state the necessity to perform steps in a timely manner.

Also, the alarm response guide for the quadrant power tilt statalarm was

to be updated and approved to include a separate step for changing the

high flux and flux/flow/imbalance setpoints. The inspector reviewed all

procedures and verified that the revisions were implemented

appropriately. Therefore, this item is closed.

II.

Maintenance

M1

Conduct of Maintenance

M1.1 General Comments

a. Inspection Scope (62707)

The inspectors observed all or portions of the following maintenance

activities:

PT/0/A/600/18

Emergency Feedwater Operability Test

PT/0/A/0230/01

Rad Monitor Checklist

MP/0/B/1800/121

Elevated Water Storage Tank (EWST) Civil

Inspection

TT/1/A/0150/046

Enclosure 131, 1LP-18 Functional

Verification

PT/3/A/0202/11

High Pressure Injection Pump Test

PT/0/A/0300/01

Control Rod Drive Trip Time Test

WO 97035913

Cut-out of Failed 2A1 Injection Pipe

IP 3/A/0305/014-1

CRD Trip Breakers

WO 97028206/01

IP/0/B/0326/019, Jumper Setup and Program

Installation

b. Observations and Findings

The inspectors found the work performed under these activities to be

professional and thorough. All work observed was performed with the

work package present and in active use. Technicians were experienced

and knowledgeable of their assigned tasks. The inspectors frequently

observed supervisors and system engineers monitoring job progress.

Quality control personnel were present when required by procedure. When

applicable, appropriate radiation control measures were in place.

Enclosure 2

14

The EWST civil inspection is covered in M1.4. The HPI test is discussed

in Section M1.2..

c. Conclusion

The inspectors concluded that.the Maintenance activities listed above

were completed thoroughly and professionally.

M1.2 Unit 3 High Pressure InJection Pump Oil Leak (62707)

a. Inspection Scope

The inspector reviewed Problem Investigation Process (PIP) report 3-097

1250, which addressed an oil leak in the lower bearing of 3B HPI pump

motor. The inspector also observed the performance of portions of

procedure PT/3/A/0202/11,. High Pressure Injection Pump Test.

b. Observations and Findings

On April 8, 1997, the 3B HPI pump motor lower bearing oil pot was

experiencing approximately one quart oil loss after operating times that

varied between 31 and 68 hours7.87037e-4 days <br />0.0189 hours <br />1.124339e-4 weeks <br />2.5874e-5 months <br />. The licensee initiated PIP 3-097-1250

to resolve this problem. The 3B HPI pump motor was declared inoperable

due to the inability to maintain the proper oil levels in the lower

bearing oil pot as designed during a postulated accident condition. The

failed 3B HPI pump motor was removed and replaced with a spare HPI pump

motor per Work Order (WO) 97032280.

The inspector observed portions of the post modification performance

test, PT/3/A/0202/11. The test was performed to return the pump to

operable status and to exit the-LCO. While performing the prerequisites

concerning increasing letdown flow to setup the necessary flow rate,

flashing occurred in the Component Cooling (CC) system. This caused

reduced heat transfer across the letdown coolers which resulted in an

increasing letdown temperature. Letdown flow was reduced and the

standby CC pump was started. The reactor operator bypassed and isolated

the inservice purification demineralizer at 130 degrees F. A team was

dispatched to place the standby CC cooler in service and an NLO was sent

to makeup to the CC surge tank. After these actions were taken, the CC

system temperatures began to decrease. Following system stabilization

and return to normal alignment, the 3B HPI pump performance test was

completed.

During this event the 3B letdown cooler CC outlet temperature was

observed to be 355 degrees F, which exceeded the design temperature

limit of 225 degrees F as specified by OFD 144A-3.2. The highest

observed CC outlet temperature for the 3A letdown cooler was 263 degrees

F, which also exceeded the design temperature limit. The licensee's

evaluation as documented in PIP 3-097-1315 determined that the CC system

Enclosure 2

15

was operable. The inspector reviewed the evaluation and did not

identify any problems.

During the licensee's review of this event, it was identified that there

existed insufficient CC flow to the letdown coolers. A review of

OP/1,2,3/A/1104/08, Component Cooling System, revealed a possible

procedural weakness for setting up proper CC flow to the letdown

coolers. The licensee placed the particular enclosure for setting up

this flow on administrative hold pending further review of the process.

c. Conclusion

The inspector concluded that the licensee's actions were appropriate to

identify and repair the HPI pump within the required LCO timeframe. The

licensee's evaluation of the CC system flashing during the post

modification HPI performance test was adequate. Placing the operations

procedurefor the CC system on administrative hold was appropriate while

the licensee continued to review the process of setting up flow to the

letdown coolers.

M1.3 Corrective Maintenance on 1A1 Reactor Coolant Pump (62700)

a. Inspection Scope

This inspection was performed for the purpose of observing the

corrective maintenance activity on the Unit 1, 1A1 Reactor Coolant Pump

(RCP) which exhibited high vibration during plant operation. The plant

was placed in a outage condition to identify and correct the problem.

b. Observations and Findings

Through discussions with the cognizant engineer and by review of reports

and/or related documents the inspectors ascertained the following

information.

Unit 1 entered the outage on March 28, 1997, in order to investigate the

cause for the high vibration in 1A1 RCP and to take appropriate

corrective action. Once the plant reached hot shutdown condition, the

licensee inspected the subject pump and found no signs of reactor

coolant seal leakage. The licensee observed minimal RCP motor external

oil leakage. Audible and physical evidence of vibrations observed

.during plant operation were reviewed. Instrument readings indicated

normal and stable seal flow, as well as pump and motor temperatures. A

no-load test run revealed evidence of damage and/or wear to the RCP

lower motor guide bearings.

A summary of the licensee's inspection and test results were as follows:

No major changes in pump vibration were observed from 100% power

to hot shutdown condition.

Enclosure 2

16

No evidence of misalignment due to motor movement from slippage

and/or binding occurring during shutdown or during the as-found no

load run.

Uncoupled run vibration data revealed that overall shaft vibration

in the area of the motor coupling was approximately 2.75 mils vs.

the 1.4 mils encountered in the May 1994 outage.

As-found alignment with the rotor in the mechanical center was out

approximately 19 mils and 48 mils with the rotor in the electrical

center.

Bearing Inspection and Results

The licensee's visual inspection of the lower bearing revealed no

significant bearing babbitt wear. Some measurable wear was evident on

the bearing support plates:

the worst being approximately 8 mils on the

number 6 bearing support plate. Significant wear was observed on 4 of

the 6 jack screws: the jack screw in number 4 bearing was worn more

severely than the others. A similar inspection showed the upper

bearings were in good condition; support plates and jack screws were

suitable for continued service. The licensee determined that the

probable source of the vibration was motor misalignment and associated

bearing wear. Consequently, it was decided that no further disassembly

or inspections would be necessary.

The subject pump was reassembled and aligned using Revision 1. to the

existing troubleshooting procedure, MP/0/A/1800/22. This revision

provided for motor alignment by centering the motor rotor in the stator

as opposed to aligning the motor shaft to the motor base cutout. On

April 2, 1997, the inspectors ascertained that alignment of 1A1 had been

accomplished to the acceptance criteria of the aforementioned procedure.

A review of related records verified that the alignment was

satisfactory.

RCP 1A2 Vibration Profile

The licensee's records revealed that RCP 1A2 experienced increased pump

shaft vibration during power reductions. For example, while reducing

power for the present outage, shaft vibration increased from 11 to 12

mils when the reactor was at about 15% power, then increased to between

20 - 22 mils when RCP 1B2 was shut down. Also, high vibration was noted

while decreasing power with both 1A2 and 1B1 pumps in operation. The

RCP 1A2 shaft vibration gradually increased to about 30 mils. Because

of vibration similarities during operational transients in RCPs 1A1 and

1A2, the licensee decided to perform a similar inspection and

maintenance on RCP 1A2. Results of this inspection showed the lower

motor bearing components exhibited no abnormal wear patterns with the

exception of two bearing shoes which had significant wear in the support

groove area. No significant wear or damage was observed on the upper

Enclosure 2

17

bearing components. At the close of this one week inspectton,

maintenance activities were still in progress on both RCPs.

Inspection Assessment

Based on a review of inspection results, analyses and assessments, the

inspectors ascertained the following information.

Both 1A1 and 1A2 RCPs demonstrated extreme vibration responses to

changing plant conditions. For example, major transients or step

changes occurred on the 1A1 and 1A2 RCPs when either of the two were

started or stopped. The 1A1 RCP transient occurred when the 1B1 RCP was

started to commence two pump operation. The 1A2 transient occurred when

the 1A1 RCP was stopped. Also, it appears that the magnetic and

mechanical misalignment and the lower motor bearing jack screw wear

observed in the 1A1 pump, were contributing factors to the high

vibration phenomenon. The inspectors reviewed the following

information/documents for technical content and adequacy:

MP/0/A/1800/22, Troubleshooting and/or Corrective Maintenance

MP/0/A/3009/009, Motor Reactor Coolant Pump Major Preventive

Maintenance

AP/1/A/1700/16. Abnormal Reactor Coolant Pump Operation, Revision

8, and the 10 CFR 50.59 Evaluation Screening for AP/1/A/1700/16

PIP 1-097-1043, Pre-outage Shutdown Risk Assessment For 1A1 RCP

c. Conclusion

The licensee's response to this abnormal condition was satisfactory.

In-house and contractor personnel appeared to be very knowledgeable and

attacked the problem in a well planned manner with satisfactory results.

Craft and field supervisors worked in a conscientious manner to identify

and correct the problem. Procedures and field records appeared to be

complete and accurate.

M1.4 Elevated Water Storage Tank (EWST) Civil Inspection

a. Inspection Scope (61726)

The inspector reviewed procedures and observed activities for draining

the EWST. This activity was necessary to perform an internal civil

inspection of the tank. The inspectors interviewed CR personnel,

operations staff, and system engineers.

Enclosure 2

18

b. Observations and Findings

As part of the high pressure service water system, the EWST provides

sealing water for the low pressure service water/condenser circulating

water system siphon (upon a loss of power) when lake levels are low.

On April 8, 1997, work was scheduled to drain the EWST for the civil

inspection of the tank via MP/O/B/1800/121, Elevated Water Storage Tank

Civil Inspection. Unit 2 Operations personnel were in charge of the

procedure and the evolution. During the night shift from April 8 - 9,

1997, Operations completed steps 11.3 through 11.5.4 of MP/O/B/1800/121.

On April 9, 1997, during a review of the procedure in the Unit 2 CR, the

inspector identified that section 6.0, Prerequisites, had not been

completed. Included in these prerequisites was the requirement to

maintain lake levels to prevent an impact on low pressure service

water/condenser circulating water siphon flow on a loss of power.

Nuclear Policy Manual NSD 703 Administrative Instructions for Station

Procedures. Conduct of Mechanical Maintenance Procedures Section C.16

states: "Each procedure shall list those items which are to be completed

and those conditions which are to exist prior to performing the

specified maintenance. Appropriate provisions shall be made to document

compliance with the prerequisites listed."

Operations placed the evolution on hold, conducted a meeting with

involved personnel, and initiated PIP 0-97-1215 to document the error.

This NRC identified violation is being identified as Violation (VIO)

50-269.270.287/97-02-03, Failure to Perform Procedure Prerequisites.

c. Conclusions

The inspector concluded that the failure of operations to complete the

EWST Civil Inspection procedure prerequisites prior to performing other

sections in the main body of the procedure is a violation of procedure

adherence.

M8

Miscellaneous Maintenance Issues (92902, 90712)

M8.1

(Closed) LER 50-270/96-005-00: Main Steam Relief Valves Technically

Inoperable Due To Improper Assembly Of Component

This issue was addressed in Inspection Report 50-269.270,287/96-20 as

VIO EA 96-478-01014, Failure To Follow Procedure and Properly Install

MSSV Spindle Nut Cotter Pins. Accordingly, this LER is considered

closed as this issue will be evaluated during the followup on VIO EA 96

478-01014.

Enclosure 2

19

M8.2 (Closed) Unresolved Item (URI) 50-270/96-13-06:

Lug Connections for

High Voltage Terminations

Problem Investigation Process report 2-96-1777 documented a 2B HPI pump

motor failure which occurred on September 18, 1996. The motor failure

was indicated to be due to a random failure of the winding insulation.

The subject motor was the first HPI motor to be replaced by the licensee

under a new HPI motor overhaul program in April 1996. LER 270/96-03

addressed the operational impact of the motor winding failure.

Additionally, the PIP discussed two loose motor lead lugs that did not

cause or contribute to the winding failure, but were indicated to be

improperly installed. Review indicated the reasons for the improper

lugs was mixed, but basically, the vendor had provided the wrong size

lugs (loose/unattached) with the refurbished motor. The lugs were

provided separately such that the motor phase leads could pass through

the terminal box porting and then be lugged.

The licensee installed the lugs with appropriate crimping tools for that

size lug. The lugs were tight on the subject phase leads to

appropriately pass current and did megger correctly after the motor

installation. However, at some period after installation of these

stranded wire leads, pull-out force required to separate the conductor

from the lug was/became minimal. It was observed that the electrical

phase that failed had the tightest "as-found" crimp connection. The

programmatic weakness to this "skill of the job task" was that there was

no guidance for determining proper lug size, even though the lugs

utilized were vendor provided.

The PIP intermediate response contained corrective action that scheduled

and directed issuance of procedures and training to cover the

programmatic lead termination issue. The change that provided guidance

for 600 Volt and less motor lugs, MP/0/A/3009/020B, was issued February

24, 1997. It now gives specific guidance for the lugging of the HPI

motors. This less than 600 Volt procedure had no associated remedial

training, had adequate instructions, and did provide sizing criteria for

lugging. A procedure for greater than 600 Volt motors termination.

IP/0/A/3009/018, was issued on April 28, 1997. A training task was

issued on April 29, 1997, to require training of personnel prior to new

procedure use or require previously qualified personnel task performance

under supervision during procedure utilization: thus completing the

actions of the PIP. No HPI or other safety-related motors had been re

lugged prior to issuance of the above instructions.

The absence of programmatic aspects for electric motor terminations was

a violation of Appendix B, Criterion V. Based on the facts that the

event was licensee-identified, the lug problem could not have been

prevented by corrective actions of a previous violation, the problem was

corrected in a reasonable time period, it was not a willful violation,

and the licensee prevented recurrence prior to corrective action

implementation, the requirements of Section VII.B.1 of the Enforcement

Enclosure 2

20

Policy were satisfied to consider this issue NCV 50-269,270,287/97-02

04, Failure To Have A Sizing Criteria For Electrical Lugs.*

M8.3 (Closed) IFI 50-270/96-13-05: HPI Motor Failure

The PIP identified above addressed the root cause of the HPI motor

failure as being a ground in the slot-to-slot section of the first coil

in an electrical phase of the 2B HPI pump motor. The conclusion was

supported by the motor vendor repair/refurbishment report (P.O. ON

11670, dated 4-16-97). This item is considered closed.

M8.4 (Closed) LER 50-270/96-03: Technical Specification Required Shutdown

Due to Inadequate Work Planning

The closure of IFI 50-270/96-13-05 also closed the above LER. The

licensee had completed the corrective actions stated in the LER.

M8.5 (Closed) Licensee Event Report (LER) 270/95-01: Technical Specification

(TS) Exceeded Due to Equipment Failure

This LER concerned the failure of valve 2LP-19 (Low Pressure Injection

Emergency Sump Suction) to open while performing quarterly valve stroke

testing, and its spurious opening during subsequent troubleshooting.

The problem was attributed to the periodic sticking of the B finger on

the CLOSED contactor, which when stuck open would not allow the OPEN

circuit to energize. As this type of erratic failure would most likely

occur only after the valve.was placed in the closed position, the

licensee considered 2LP-19 inoperable since its previous quarterly

stroke test.

After affected components in the motor control center (MCC) and the

control switch were replaced, 2LP-19 was successfully stroke tested and

the associated TS LCO was exited. Because the affected components were

replaced with those removed from a spare MCC compartment in the field as

opposed to a clean warehouse, the stroke test frequency for valve 2LP-19

was increased to monthly (for the next three months) and an infrared

scan was required to be conducted. Through a review of completed work

requests, the inspector verified that these additional activities were

performed satisfactorily. Associated with General Electric breaker

model No. TED 134015, the failure mode of 2LP-19 was such that the valve

could have been opened at the breaker by manually closing in the

contacts to start the motor. The redundant train valve (2LP-20) was not

affected by the failure of 2LP-19 and was available for control switch

actuation. Accordingly, having confirmed that the licensee had approved

and scheduled a Nuclear Station Modification (NSM ON-3027) for the

replacement of obsolete safety-related MCC starter compartments with new

components over the next five years, the inspector had no further

questions. This LER is considered closed.

Enclosure 2

21

M8.6 (Closed) LER 269/95-03: Low Pressure Injection (LPI) System Technically

Inoperable Due To A Design Analysis

This LER concerned two issues. The first issue, which was previously

addressed in Inspection Reports 94-38 and 95-01, involved a postulated

loss of coolant accident in which a single failure disables one of the

two reactor building emergency sump lines. Under these circumstances,

Abnormal Procedure AP/1/A/1700/07, Loss of Low Pressure Injection

System, directed the operators to secure both reactor building spray

pumps. The licensee determined that this condition was beyond the

design basis assumptions contained in the maximum hypothetical accident

safety evaluation report and 'made a procedure change to require that one

.train of reactor building spray be maintained operable. Subsequently,

the licensee performed an analysis and determined that 10 CFR Part 100

dose limits would not have been exceeded. Consequently, the associated

10 CFR 50.72 notification to NRC was determined not to be required, and

was subsequently retracted. The inspector verified that APs/1.2,3/

A/1700/07 still require one train of reactor building spray be

maintained during a postulated single failure of a reactor building

emergency sump line.

As previously addressed in Inspection Report 95-01, the second issue

reported in this LER concerned a condition outside of design basis due

to a procedural requirement to split LPI header flows in the event of a

postulated single failure of a LPI pump during emergency core cooling

system operation. Specifically, if LPI flow instrument inaccuracies and

fouling of reactor building and LPI coolers were considered coincident

with a postulated single failure of a LPI pump during emergency core

cooling system operation, then the reactor building pressure/temperature

profile required in the Equipment Qualifications (EQ) analysis could

have been exceeded. In order to resolve this issue, the licensee

revised APs/1.2.3/A/1700/07 on December 27, 1994. to require that LPI

flow not be split between headers during a loss of coolant accident.

Since that time, LPI cooler fouling has been resolved and LPI pump

capacity and maximum instrument inaccuracies have been found acceptable

to allow flow split of one LPI pump (if

no others are available) to both

LPI headers. Accordingly, the inspector verified that the APs have

since been changed to reflect this desirable alignment.

III. Engineering

El

Conduct of Engineering

E1.1 Unit 3 Integrated Control System (ICS) Testing

a. Inspection Scope (61726, 62707)

The inspectors continued to observe the complex post modification

testing of the new Unit 3 ICS.

Enclosure 2

22

b. Observations and Findings

During this inspection period the licensee completed TT/3/B/0326/ 001,

ICS/NNI Transient Testing At Power:

ICS/NNI System Upgrade, NSM ON

32989/ALl. The sections which remained to be tested were a Feedwater

(FDW) Pump Trip Transient From 70% Reactor Power and a section involving

tripping a RCP From 50% Reactor Power.

Prior to each test section the licensee conducted pre-test briefings for

all personnel involved in the testing. The inspector considered the

pre-briefs to be thorough and with the appropriate focus on nuclear

safety.

After completion of each test, a post-test brief was conducted by the

test coordinator with all personnel involved in the test. The briefs

focused on data acquisition results, test acceptance criteria, and

lessons learned. The inspectors considered the test post-briefs to be

thorough, and noted that there were no issues that required resolution

prior to continuation of testing.

The inspectors monitored testing activities from the Unit 3 CR. The

test coordinator and management designee was located in the Unit 3 CR

for all testing. Command and control in the CR during all testing was

good. The test coordinator maintained good control of all test

evolutions. The inspector concluded that testing activities conducted

in the Unit 3 CR were good and operators maintained appropriate focus on

nuclear safety at all times.

Test Results

On March. 23, 1997, the inspectors observed the performance of procedure

TT/3/B/0326/001 in the CR. Unit 3 was at approximately 70% power for

the FDW Pump Trip Transient and was at 50% reactor power for the RCP

Trip. All acceptance criteria were met for both test sections. No

discrepancies were identified.

c. Conclusions

The inspectors concluded that the two remaining sections of

TT/3/B/0326/001 were satisfactorily accomplished in accordance with the

licensee's test procedures. Control of all test activities was good.

Positive observations were made relating to test briefings, CR

briefings, and communication and coordination of test evolutions.

E1.2 Low Pressure Service Water (LPSW) Outside Design Basis

(92901)

During this inspection period, the licensee made a 10 CFR 50.72

notification when the licensee determined that some portions of the Unit

1 and Unit 2 LPSW system did not meet UFSAR Section 3.1.40 design

requirements for high trajectory turbine generated missiles.

Enclosure 2

23

Specifically, there are two portions of the LPSW system piping which are

not sufficiently separated to protect against loss of redundant LPSW

system trains if a high trajectory turbine missile were to occur. The

LPSW system serves as a safety-related heat sink during certain design

basis accidents and is considered an engineered safeguards system. The

licensee has identified this issue as an unreviewed safety question and

submitted a license amendment to the NRC on April 29, 1997, to clarify

the turbine missile design criteria in Oconee's UFSAR.

E1.3 Spent Fuel Cask Dry Run Operation

a. Inspection Scope (60854)

The inspectors observed portions of the spent fuel cask dry run (from

the spent fuel building to the storage facility) to verify that the

activities were performed in accordance with the applicable procedure.

b. Observations and Findings

The procedure used in the dry run for the transporting of the spent fuel

cask to a Phase III Horizontal Storage Module (HSM) of the Independent

Spent Fuel Storage Installation (ISFSI) was Procedure TT/O/A/1500/001.

ISFSI Phase III DSC Test Loading Storage. Rev. 0.

The licensee had already lifted the cask onto the transporter before the

inspectors arrived and was waiting for good weather to complete the

transport. The inspectors observed the licensee perform the preparation

and radiation level survey, transporting of the cask from the Fuel

Receiving Area (FRA) to the storage facility, and insertion to and

withdrawal from the HSM set in the storage facility.

The licensee followed the written procedure and the transporting,

insertion, and retrieval (or withdrawal) of the Dry Storage Canister

(DSC) proceeded without incident. However, the inspectors made the

following comments to the licensee after the DSC dry run activities:

-

The transporter speed from the FRA to the storage facility seemed

to be about 5 miles per hour (MPH). The procedure allows a

maximum of 3 MPH.

-

The four bolts remaining in the cask head after the rest of the

bolts were removed were not 90 degrees apart as required by the

procedure. They were about 70 and 110 degrees apart.

During the subsequent damage inspection, the metal debris peeled

off from the DSC was found in both of the shipping rails inside of

the cask and HSM.

With respect to the first two comments, the licensee indicated that they

would take measures to assure better control during the loading

Enclosure 2

24

operation currently scheduled for May 1997. Regarding the third

comment, the licensee plans to evaluate and take appropriate actions to

prevent DSC damage before the loading operation.

c. Conclusions

The inspectors concluded that the licensee performed adequate operations

for the transporting, inserting, and retrieving of the DSC -from the FRA

to the HSM.

E1.4 Phase III of Independent Spent Fuel Storage Installation

a. Inspection Scope (60851. 60853)

The Inspectors reviewed Phase III of the ISFSI in order to verify that

the facility was installed in accordance with the applicable procedures

and drawings.

b. Observations and Findings

The Oconee Phase I and II of the ISFSI with 40 HSMs were installed under

the specific License No. SNM-2503 and Docket Number 72-4 based on 10 CFR

72 for the storage of nuclear spent fuel material on site. The addition

(Phase III) of 20 new HSMs will be completed under a general license to

store the spent fuel on site by using the existing reactor license and

docket numbers under 10. CFR 50 for all its activities per Sections 72.6.

72.210. and 72.212 of 10 CFR 72. The licensee filed a notice of

intention with the NRC on November 7, 1996, to install Phase III of the

ISFSI by using a NUHOMS storage system manufactured by Vectra

Technologies, Inc. The inspectors reviewed the notice and determined

that it met the requirements for the general license.

The inspectors reviewed the test records and the batch data for the

concrete poured into the base slab for the slump test, air content,

temperature on air and concrete, unit weight, and compressive strength.

All the results of the tests were within the limits set in the procedure

and specification.

The licensee assembled eight HSMs on site. The inspectors, using the

manufacturing drawings, inspected HSM E21 which will be used to store a

DSC during May-June 1997 time frame. The inspectors found several welds

undersized by about 1/16" for the connections between the right beam (or

rail) web and the stiffener plates at both webs. The measured fillet

weld sizes were 1/8".

Drawing 9-354-6105, Oconee Phase III NUHOMS ISFSI

Horizontal Storage Module DSC Support Structure, Rev. 0, requires the

fillet weld be 3/16".

The High Tech Company that manufactured the steel portion of the HSM for

Vectra performed a detailed inspection the following week on all eight

HSMs installed and found more undersized welds. Vectra and High Tech

Enclosure 2

25

are currently performing analysis and evaluation of the undersized welds

and will do repairs, if required. The identified discrepancies on

installed module HSM E21 (the undersized welds) when compared with the

requirements in the drawing 9-354-6105 collectively constitute a

violation of 10 CFR 50 Appendix B, Criterion V, and, the licensee's

accepted Quality Assurance (QA) Program, Updated Final Safety Analysis

Report, Chapter 17, Quality Assurance and Topical Report DUKE 1-A,

Instructions, Procedures, and Drawings which state, in part that

activities affecting quality shall be accomplished in accordance with

documented drawings. This was identified to the licensee as Example 1

of Violation 50-269,270,287/97-02-05, Weld Undersized Or Not Inspecting

By QA.

The NRC headquarters performed several inspections of the Standardized

NUHOMS and found many deficiencies regarding the QA program. The NRC

issued a Demand for Information (DFI) on January 13. 1997, to Vectra and

requested that Vectra provide information and resolutions to the

deficiencies found in the QA program implementation for the design,

changes, and fabrication of the NUHOMS system. Duke has eight HSMs and

one DSC on site which were manufactured before the DFI was issued. Duke

is required to perform an independent review on the deficiencies based

on its own QA program if Vectra can not resolve the issue with the NRC

before Oconee loads its cask in May or June 1997. Duke plans to perform

the following activities to resolve the deficiencies found by the NRC

before its cask loading:

-

Verify fabrication drawings, specifications, and purchase orders

against the licensee requirements.

-

Verify that Noncomformance Reports, Engineering Change Notices,

and Correct Action Reports written by the manufacturers are

adequately dispositioned for the Oconee equipment.

The inspectors plan to inspect these issues before the cask is loaded to

  • see if Duke adequately addressed and resolved the issues.

c. Conclusions

The inspectors considered that the licensee performed an adequate

installation of concrete base mat and HSMs for Phase III of the ISFSI.

A violation was issued for undersized welds.

E1.5 Seismic Qualification for Upper Surge Tank Support

a. Inspection Scope (37700)

The inspectors reviewed the calculation and modification package used to

qualify and modify the Upper Surge Tank Support (USTS) for the

earthquake condition in order to verify that the supports were qualified

and installed in accordance with the applicable procedures and drawings.

Enclosure 2

26

b. Observations and Findings

The licensee's Seismic Qualification Utility Group (SQUG) engineers

reviewed the USTSs and identified: a lower and out-of-date seismic

acceleration coefficient value used by Earthquake Qualification

Engineering (EQE) International: and cover plates for columns (or legs)

of the supports were not installed in the field as required by the

drawings. Problem Investigation Process report (PIP) 0-095-1307 was

issued to resolve the problem. Based on the correct seismic

acceleration coefficient value and the existing support configurations

in the field, the licensee concluded that the applied stresses of the

support members would exceed the allowable stresses: thereby, requiring

the tank supports be modified. After the identification of the

calculational mistakes made by EQE, the licensee engineers very

carefully reviewed the assumptions and methodologies in the

calculations performed by EQE and did not find other major problems.

The inspectors reviewed other PIPs related to SQUG and did not identify

any major problems.

The inspectors inspected the modification by using the as-built

drawings. The inspectors identified several welds that did not meet the

5/16" minimum weld sizes required by the drawings. After searching for

the inspection records, the licensee stated that these welds were not

inspected by QA inspectors because the Step 4.12.4 of Procedure

TN/3/A/8979/MM/01C. Minor Modification OE-8979. for verifying the weld

sizes was marked "N/A" by the acting craft supervisor due to a

communication misunderstanding with the design engineer.

In addition, the design engineer and the QA personnel in the final

review for the closure of the package also failed to notice the problems

of not verifying the weld sizes. The licensee issued PIP 3-097-1005 for

the root cause investigation and resolution. The problem for not

verifying the 5/16" minimum weld sizes for the connections between the

tank support columns and base plates required by the Step 4.12.4 and the

attached drawing sheet 11 of 18 of Procedure TN/3/A/8979/MM/01C, Minor

Modification OE-8979, was identified to the licensee as Example 2 of

Violation 50-269,270,287/97-02-05, Welds Undersized or Not Inspecting by

QA: The Example 2 applies to Unit 3 only.

c. Conclusions

The inspectors concluded that the licensee performed an adequate review

of the EQE Calculation Evaluation for the Upper Surge Tank Supports.

The modification on the supports was acceptable except as for a failure

of QA to inspect and verify existing fillet weld sizes. A violation was

issued.

Enclosure 2

27

E1.6 Engineering Action on Unit 2 2A1 InJection Line Crack (93702, 40500)

a. Inspection Scope

As a result of the cracked injection line, on April 23. the licensee

formed a Failure Investigation Process (FIP) team to evaluate and

resolve the event described in Section 01.5 of this report.

The

resident inspectors, who were joined by a Region II DRS NRC inspector,

followed and evaluated the problem and the licensee's actions that ran

beyond this inspection period.

b. Observations and Findings

Based on the discovery of the crack, the licensee initiated PIP 2-97

1324 and formed the FIP team in accordance with Nuclear Site Directive

212, Cause Analysis. The team took a very broad based look at the

failure of the weld in the injection line. The licensee brought in

several vendors to support their investigation of the problem. The

vendors had backgrounds in metallurgy, thermal fatigue, pipe vibration,

and root cause investigation analysis. The following were areas that

the team was to evaluate:

Vibration - equipment induced, flow induced

original design - workmanship, weld material, weld configuration,

weld process, and pipe alignment

existing analysis - as built configuration, analysis review,

analysis error

miscellaneous loads - stratification, thermal interferences,

transients, modification loads, overpressure

material degradation - embrittlement, stress corrosion cracking,

chemical attack, erosion

  • .

history - thermal sleeve work, temporary work load (rigging).

shock, operational history

snubber failure

The team formation was appropriate for the complexity of the problem.

The licensee provided information in an open manner to the NRC. The

licensee, with various team members, held nearly daily phone

conversations with the NRC at the regional and headquarters offices.

The B&W owners group participated with the evaluation process.

The licensee provided a Justification for Continued Operation (JCO) on

April 28, 1997, for Units 1 and 3. which were still operating at the

Enclosure 2

28

time of the Unit 2 forced shutdown. Based on the results of the team's

investigation, Unit 3 was shutdown on May 1. 1997. due to concerns about

the 3A1 injection line thermal sleeve condition. A second JCO was

issued on May 2 for Unit 1.

Inspection Report 97-07 will address the findings of the FIP team and

subsequent corrective actions.

c. Conclusions

The licensee was proactive in rapidly forming a FIP team shortly after

the Unit 2 injection line crack condition was known. The licensee

called in available industry talent to support and supplement the team.

The licensee was communicative with the NRC and provided information as

required and requested by the NRC.

E2

EngineeringSupport of Facilities and Equipment

E2.1 Engineering Support of Facilities and Eauipment - Procurement

Engineering (37550)

a. Inspection Scope

The inspector reviewed Procurement Engineering activity related to the

purchase and receipt of safety-related replacement parts and services.

The areas reviewed included commercial grade dedication (CGD).

acceptable substitutes, verification of receipt inspection acceptance

criteria, resolution of receipt inspection deficiencies, material QA

quality level changes, and salvage/repair of equipment. The inspection

included a sample review of licensee performance in these areas to

determine if activities were consistent with applicable regulatory

requirements and licensee procedures. Applicable regulatory

requirements included 10 CFR 50 Appendix B, UFSAR, and the following:

ANSI N45.2.13-1976, QA Requirements for Control of Items and

Services for Nuclear Power Plants

RG 1.123, QA Requirements for Control of Procurement of Items and

Services for Nuclear Power Plant

Generic Letter (GL) 91-05. Licensee Commercial Grade Procurement

and Dedications Programs

b. Observations and Findings

Technical evaluations for CGD and acceptable substitutes appropriately

identified and addressed replacement parts' critical characteristics.

Acceptance criteria for critical characteristics were adequately

addressed and verified at receipt inspection. Receipt inspectors

demonstrated a strict adherence to the established acceptance criteria

Enclosure 2

29

and deficiencies were appropriately documented and resolved. Required

post installation testing identified in acceptance criteri-a was

appropriately designated on the item and tracked. Replacement parts' QA

classification changes were adequately justified. Procurement

Engineering evaluations were technically sound and well documented.

An example was identified in which equipment or services from an

approved Appendix B vendor was not consistent with procurement

documentation requirements. This involved an 8-inch safety-related

valve (LP-40) which was procured and installed in the Unit 3 Low

Pressure Injection (LPI) system. The valve did not meet the Purchase

Order (PO) requirements related to Duke valve specification CNS 1205.28

00-0001, ASME Section III Carbon and Stainless Steel Ball Valves, dated

March 3. 1982. Two valves were procured on PO 8575, dated March 26.

1996. to be installed on minor modifications ON0E 8859 and 8860 which

were to provide double valve isolation between the LPI system and the

Borated Water Storage Tank (BWST). Section 8.6.2.2 of the valve

specification stated that all valves were to close in the clock-wise

direction. The valves were received, inspected, and accepted in

November 1996. The vendor had inadvertently deviated from the PO

referenced design specification of one valve by reversing its operation

(i.e., counter-clockwise to close). The vendor, Anchor Darling Company,

had been audited and approved by the Duke Procurement Engineering

organization and was an approved 10 CFR 50, Appendix B, vendor. The

vendor documentation received with the valves certified that all PO

requirements and specifications were met. The licensee's and the

vendor's quality control programs failed to identify the procured valve

did not meet the PO requirements. This item is identified as Violation

50-287/97-02-06, Inadequate Control of Purchased Material, Equipment,

and Services. This procurement deficiency was self-identifying in that

the associated valve design error contributed to a Unit 3, loss of

Reactor Coolant System (RCS) inventory event on February 1, 1997 (NRC

Report Nos. 50-269,270,287/96-20). Performance weaknesses by

Engineering, Maintenance, and Operations which contributed to this event

are discussed in paragraph E8.3 of this report.

c. Conclusions

Procurement Engineering performance in establishing and verifying

quality requirements for upgraded replacement parts, acceptable

substitutes, and resolution of deficiencies was good. An example was

identified in which an approved 10 CFR 50, Appendix B, vendor provided

defective materials or services which demonstrated a deficiency in the

licensee's vendor qualification or oversight process. A violation was

identified on this issue.

Enclosure 2

30

E2.2 Non-conservative Setup of Controls for Low Temperature Overpressure

Protection (LTOP)

The licensee identified methods used to set the travel stops for HP-120

(make-up control valve) were potentially non-conservative during Low

Temperature Overpressure Protection (LTOP) operation. The inspectors

reviewed the operability issues concerning operation during LTOP.

On February 25, 1997, the licensee identified the procedure used to set

the HP-120 controls to limit Reactor Coolant System (RCS) make-up flow

were non-conservative. HP-120 is the normal make-up to the RCS control

valve. The controls were set for a maximum of 70 - 80 gpm with one HPI

pump in operation using OP/1.2,3/A/1104/49, Low Temperature Overpressure

Protection (LTOP). The licensee identified that more than one HPI pump

could be operating after the travel stop on HP-120 was set. The standby

pump could start on low seal injection flow. 'This would allow more than

the maximum flow through HP-120. The maximum flow through HP-120 is

based on allowing an operator ten minutes to correct HP-120 failing

open.

The licensee is evaluating the LTOP concerns through PIP 0-097-0710 and

PIP 5-097-1204. A 10 CFR 50.72 notification was made on April 17, 1997.

The inspectors also interviewed operations personnel on the duties of

the dedicated LTOP operator, a compensatory action.

At the close of the inspection period, NRC review of the issue was not

complete. This issue will be followed as URI 50-269,270.287/97-02-07,

Non-conservative Setting of LTOP Controls.

E7

Quality Assurance in Engineering Activities

E7.1 Quality Assurance in Engineering Activities - Procurement Engineering

a. Inspection Scope (37551)

The inspector reviewed the licensee's self-assessment activities

associated with procurement engineering processes. Applicable

regulatory guidance was.provided by 10 CFR 50. Appendix B. These

included two station self-assessments and one corporate consolidated

performance audit in 1995 which included Procurement Engineering

activities.

b. Observations. Findings, and Conclusion

The scope of the self-assessments was adequate to evaluate performance

of the procurement activity under review. Findings were appropriately

documented and tracked for resolution.

Enclosure 2

31

E8

Miscellaneous Engineering Issues (92903)

E8.1 (Closed) VIO 269,270,287/96-09-01:

Inoperable Hydrogen Recombiner

Condensate Pumps

This violation involved the Containment Hydrogen Recombiner System

(CHRS) not being able to satisfy TS 3.16.3 for an indeterminate

timeframe. The licensee investigation indicated that the drain pumps on

all three units failed to operate due to corrosion between the pump

casing and the impeller. Completed corrective actions included

increasing the test frequency on the pumps and machining and coating the

inside of the pump casing with epoxy. The pumps were part of a

temporary modification, a permanent modification will be implemented to

remove the accumulation of moisture in the section and discharge piping

such that the temporary modification including the pumps will no longer

be needed. The permanent modification is complete on Unit 2 and Unit 3.

The other permanent modifications are scheduled to be complete by the

end of the Unit 1 upcoming Refueling Outage (RFO). Based on the

licensee's completed/planned corrective actions, this item is closed.

E8.2 (Closed) URI 50-269.270,287/96-03-03:

Adequacy of Information Provided

for Spent Fuel Pool (SFP) Design

The Oconee SFP inspection (NRC Inspection Report 96-03. paragraph 4.4.2)

identified a design concern related to the interface between the Spent

Fuel Pools (SFP) and the Standby Shutdown System (SSS). The SSS

modification to the SFP installed in 1980 deviated from the design

described in the Standard Review Plan (SRP). Section 9.1.3 of the SRP

stated that the SFP should be designed such that the failure of inlets,

outlets, piping or drains will not result in inadvertent drainage below

a point approximately ten feet above the top of the active fuel in the

SFP. The Oconee design, which provides a three-inch diameter

seismically qualified piping connection for the SSS, would permit

draining the SFP to six feet below the top of the active fuel assembly.

Barriers to prevent this drain down included administrative controls to

monitor level during a SSS event, a low level alarm annunciated at two

foot below the normal 23.5 foot level, and the seismic qualification of

the connecting three inch diameter piping.

This issue is being addressed by NRC Task Action Plan No. M88094,

"Resolution of SFP Action Plan Issues", and will be resolved in

conjunction with this plan.

E8.3 (Closed) URI 50-269,270,287/96-20-03:

Loss of RCS Inventory

This item was related to the inadvertent Unit 3 RCS inventory reduction

event which occurred on February 1, 1997. The unit was in mode 5 with

decay heat removal provided by the LPI system. The cause of the event

was a configuration control error that occurred during a static pressure

test alignment. The test was performed to verify the acceptability of

Enclosure 2

32

welds on LP-40 and LP-42, which were installed by minor modifications.

The issue was unresolved pending further review of event precursors and

root causes.

The root cause was determined to be an inadvertent vendor deviation from

the PO requirements of LP-40. This is discussed in paragraph E2.1 of

this report as a procurement process deficiency and a violation of

regulatory requirements was identified (VIO 50-287/97-02-06).

The precursors to the event demonstrated performance weaknesses by

Engineering. Maintenance, and Operations which degraded barriers and

contributed to the installation of defective equipment in a safety

related system. Engineering post modification functional testing did

not identify the valve design defect. Additionally, Engineering did not

identify the potential shutdown risk associated with the test and did

not establish adequate precautions or configuration verification

parameters. Maintenance demonstrated a-weakness regarding a questioning

attitude for abnormal equipment conditions. A maintenance technician

had previously noted the valve was a reverse acting valve but did not

question this abnormal condition or communicate it to management or

Engineering. Operations demonstrated a weakness in configuration

control verification in that no secondary means were used to verify the

valve position. Due to routine faulty position indication, operators

did not check the position indication on the valve itself. In this

case, a clockwise turn of the valve verified the valve was full open

rather than full closed. Additionally, Operations reviewed and approved

the static test configuration and did not identify or establish

precautions for the shutdown risk associated with system misalignment.

The above weaknesses were also discussed in the licensee's Event

Investigation Team report of the loss of RCS inventory event.

Positive performance related to this event included the operators'

prompt actions to terminate the RCS inventory loss upon discovery, five

minutes after the test was initiated. Additionally, an event

investigation team was established promptly and provided a comprehensive

review of the event cause and precursors.

E8.4 (Closed) URI 50-269,270.287/96-17-03: Reactor Building Cooling Unit

(RBCU) Operability Concerns Due to Wrong Fuse in Control Circuit

This item addressed the licensee's actions to resolve a fuse deficiency

in the RBCU control circuit which was identified on February 27, 1995.

by the licensee's equipment failure trending process and documented on

PIP 0-95-0267. During an NRC inspection of open PIPs in November 1996,

it was noted that the issue was not resolved and that RBCU operability

had not been addressed. The item was unresolved pending further NRC

review of licensee corrective actions and the impact of deficient fuses

on RBCU operability.

Enclosure 2

33

The RBCU failure trend was identified for the Unit 3 RBCUs'which failed

four times between 1990 and 1995 from blown fuses after the. RBCU was

energized following maintenance. The licensee's cause determination

concluded that the wrong fuse type was installed (i.e.. instantaneous

rather than time delay fuses). The Unit 3 KTK-8 instantaneous fuses

were changed in June 1996, to KTK-15 instantaneous fuses. The PIP

corrective actions replaced the fuses on all RBCU control circuits in

Units 1, 2, and 3 with time delay CCMR-6 fuses. The CCMR-6 fuses were

installed in Units 1 and 2 in 1996. replacing the original KTK-8 fuses.

The PIP was closed on December 2, 1996. On December 23. 1996, CCMR-6

fuses were installed on Unit 3 RBCUs and two of the three RBCUs failed

during post maintenance testing. This demonstrated that the corrective

actions for the PIP were inadequate.

The original cause evaluation failed to identify the design control

deficiency that the fuses were not suitable for application in the RBCU

fan motor circuit. The fuses were rated below circuit conditions.

Following the December 1996 Unit 3 RBCU failures the licensee evaluated

the control circuit conditions and determined that the fuses were under

rated for circuit conditions. On January 16. 1997, the licensee

received information from the RBCU control transformer vendor that the

transformer in-rush current could reach 171 amps. Unit 1 and 2 possible

in-rush current was approximately 168 amps. The original KTK-8 fuses

and the replacement CCMR-6 fuses were rated at 80 and 90 amps,

respectively for in-rush current. The KTK-15 fuses which had been

temporarily installed in Unit 3 were rated at 200 amps and were adequate

for this application. This demonstrated that the licensee's cause

determination, which did not evaluate circuit conditions, was

inadequate.

The licensee categorized PIP 0-95-0267 as a less significant event issue

and no operability evaluation was documented. The under rated fuses

impacted the operability of all RBCUs in which they were installed. The

in-rush current varied due to the cycle discrepancy between the power

supply and the primary control circuit transformer when the RBCU was

energized, therefore it was not predictable which start up would exceed

the KTK-8 or CCMR-6 current capacity. During a Loss of Coolant Accident

(LOCA) the RBCU fans change from fast to slow speed and the fuse

limiting condition would not occur. The RBCUs would only need to be re

energized following a Loss Of Offsite Power Event (LOOP). Therefore,

following a LOOP the operability of the RBCUs could not be assured.

Technical Specification 3.3.5 requires three trains of RBCUs to be

operable when the reactor is critical, and two trains when the RCS

conditions are above 250 degrees F and 350 psig. The performance

history of Unit 1 and 2 RBCUs included no blown fuse failures as in the

Unit 3 RBCUs. However, the design conditions of the under rated fuses

indicated that all RBCUs were inoperable. This was demonstrated for

Unit 3 based on design and performance history. This demonstrated that

the licensee's corrective actions were inadequate in that they did not

Enclosure 2

34

adequately identify and address the significance of this condition

adverse to quality.

Following the licensee's identification in January 1997, that the fuses

were under rated in all RBCUs, adequately rated fuses (KTK-15) were

installed in all RBCUs before the Units were restarted from the extended

outage. However, at this time the licensee did not initiate a new PIP

or re-open the original PIP to evaluate the past operability of the

RBCUs or the extent of condition for this issue. Following discussion

with the inspector, the licensee initiated PIP 0-097-1109 on April 1,

1997, to investigate the inappropriate categorization of PIP 0-95-0267,

and initiated a 10 CFR 50.72 report on April 2, 1997. This item is

identified as Violation 50-269,270,287/97-02-08, Inadequate Corrective

Action and Design Control for RBCU Fuse Failures.

E8.5 (Closed) VIO 50-269.270,287/96-04-03: Failure to Follow Procedure for

Drawing Control

This item was related to the identification of controlled drawings that

had not been updated to reflect changes from a modification completed 18

months prior to the drawing control inspection. Ten Vital to Operations

(VTO) drawings in the Units 1, 2, and 3 CRs had not been updated. The

corrective actions in the licensee's June 20, 1996, response to the

violation included improvement of VTO marking designations on drawings

and a 100 percent audit of station controlled drawings to verify correct

revisions were at all drawing file locations. The inspector verified

the corrective actions were completed and concluded that the licensee's

corrective actions were comprehensive.

IV. Plant Support Areas

P1

Conduct of EP Activities (71750)

During the two major events that occurred this inspection period.

inspectors were present to observe Emergency Plan activities performed by

the licensee. These activities are discussed in Sections 01.5, 01.8, and

E1.6 of this report.

Overall, the licensee performed in a conservative

manner on both events and followed their Emergency Action Levels.

V. Management Meetings

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management

at the conclusion of the inspection on May 7, 1997. The licensee acknowledged

the findings presented. No proprietary information was identified.

Enclosure 2

35

Partial List of Persons Contacted

Licensee

T. Barron, Procurement and Engineering Manager

S. Benesole. Independent Spent Fuel Storage Installation Readiness Manager

E. Burchfield, Regulatory Compliance Manager

T. Coutu, Operations Support Manager

D. Coyle, Systems Engineering Manager

T. Curtis, Operations Superintendent

J. Davis, Engineering Manager

B. Dobson, Systems Engineering Manager

W. Foster, Safety Assurance Manager

J. Hampton, Vice President. Oconee Site

G. Hawkins, Maintenance Manager

D. Hubbard, Maintenance Superintendent

C. Little, Electrical Systems/Equipment Manager

J. McLean. Senior Engineer-Modification

B. Peele, Station Manager

J. Smith. Regulatory Compliance

A. Wells. Civil Engineer

NRC

D. LaBarge, Project Manager

Enclosure 2

36

Inspection Procedures Used

IP 71750:

Plant Support Activities

IP 71707:

Plant Operations

IP 61726:

Surveillance Observations

IP 62707:

Maintenance Observations

IP 40500:

Self-Assessment

IP 37551:

Onsite Engineering

IP 92901:

Followup - Operations

IP 93702:

Responding to Events

IP 90712:

LER Review

IP 62700:

Maintenance Implementation

IP 92902:

Followup - Maintenance

IP 60854:

ISFSI - Dry Run

IP 60853:

ISFSI - Fabrication

IP 60851:

ISFSI - Design

IP 37700:

Design, Design Changes and Modifications

IP 37550:

Engineering

IP 92903:

Followup - Engineering

Enclosure 2

37

Items Opened, Closed, and Discussed

Opened

50-269,270,287/97-02-01

NCV

Inadequate Procedure for Control of LPI

Temperature (Section 03.1)

50-269/97-02-02

NCV

Unlocked CRD System Patch Panel (Section

08. 1)

50-269,270,287/97-02-03

VIO

Failure to Perform Procedure Prerequisites

(Section M1.4)

50-269.270.287/97-02-04

NCV

Failure to Have a Sizing Criteria for

Electrical Lugs (Section M8.2)

50-269,270,287/97-02-05

VIO

Welds Undersized or Not Inspecting By QA

(Section E1.4 and E1.5)

50-287/97-02-06

VIG

Inadequate Control of Purchased Material.

Equipment, and Services (Section E2.1)

50-269,270,287/97-02-07

URI

Non-conservative Setting of LTOP Controls

(Section E2.2)

50-269.270,287/97-02-08

VIG

Inadequate Corrective Action and Design

Control for RBCU Fuse Failures (Section

E8.4)

50-269,270.287/97-02-09

IFI

BWST Temperature Requirements (Section

03. 1)

Closed

50-269/95-05-00

LER

Breach of Technical Specification Due to

Unlocked Control Rod Patch Panel (Section

08.1)

50-269/95-05-01

LER

Breach of Technical Specification Due to

Unlocked Control Rod Patch Panel (Section

08.2)

50-270/96-10-01

VIO

Failure to Change Flux/Flow/Imbalance

Setpoint (Section 08.3)

50-270/96-005-00

LER

Main Steam Relief Valves Technically

Inoperable Due to Improper Assembly of

Component (Section M8.1)

  • CEnclosure

2

38

50-270/96-13-06

URI

Lug Connections for High Voltage

Terminations (Section M8.2)

50-270/96-13-05

IFI

HPI Motor Failure (Section M8.3)

50-270/96-03-00

LER

Technical Specification Required Shutdown

Due to Inadequate Work Planning (Section

M8.4)

50-269.270,287/96-09-01

VIO

Inoperable Hydrogen Recombiner Condensate

Pumps (Section E8.1)

50-269.270.287/96-03-03

URI

Adequacy of Information Provided for Spent

Fuel Pool (SFP) Design (Section E8.2)

50-269,270,287/96-20-03

URI

Loss of RCS Inventory (Section E8.3)

50-269,270,287/96-17-03

URI

RBCU Operability Concerns Due to Wrong

Fuse *in

Control Circuit (Section E8.4)

50-269,270,287/96-04-03

VIG

Failure to Follow Procedure for Drawing

Control

(Section E8.5)

50-270/95-01-00

LER

Technical Specification Exceeded Due to

Equipment Failure (Section M8.5)

50-269/95-03-00

LER

Low Pressure Injection System Technically

Inoperable Due to.a Design Analysis

(Section M8.6)

Enclosure 2

39

List of Acronyms

AIT

Augmented Inspection Team

ANSI

American Nuclear Society Institute

ASME

American Society of Mechanical Engineers

B&W

Babcock and Wilcox

BWST

Borated Water Storage Tank

CAR

Corrective Action Report

CFR

Code of Federal Regulations

CC

Component Cooling

CFR

Code of Federal Regulations

CGD

Commercial Grade Dedication

CHRS

Containment Hydrogen Recombiner System

CR

Control Room

CRD

Control Rod Drive

DBD

Design Basis Document

DFI

Demand For Information

DHR

Decay Heat Removal

DRS

Division of Reactor Safety

DSC

Dry Storage Canister

EAL

Emergency Action Level

ECN

Engineering Change Notice

ES

Engineered Safeguards

EWST

Elevated Water Storage Tank

F

Degrees Fahrenheit

FDW

Feedwater

FIP

Failure Investigation Process

FRA

Fuel Receiving Area

GPM

Gallons Per Minute

GL

Generic Letter

HPI

High Pressure Injection

HQ

Headquarters

HSM

Honizonal Storage Module

IAW

In Accordance With

ICS

Integrated Control System

I&E

Instrument & Electrical

IR

Inspection Report

ISFSI

Independent Spent Fuel Storage Installation

JCO

Justification for Continued Operation

KHU

Keowee Hydro Unit

LDST

Letdown Storage Tank

LER

Licensee Event Report

LCO

Limiting.Condition for Operation

LOCA

Loss of Coolant Accident

LOOP

Loss of Offsite Power

LPI

Low Pressure Injection

LPSW

Low Pressure Service Water

LT

Level Transmitter

LTOP

Low Temperature Over Pressure

MP

Maintenance Procedure

Enclosure 2

40

MPH

Miles Per Hour

MSSV

Main Steam Safety Valve

MVA

Mega Volts-Amps

NCR

Nonconformance Report

NCV

Non-Cited Violation

NDE

Non-Destructive Examination

NI

Nuclear Instrument

NLO

Non-Licensed Operator

NOUE

Notice of Unusual Event

NOV

Notice Of Violation

NRC

Nuclear Regulatory Commission

NRR

Nuclear Reactor Regulation

NSM

Nuclear Station Modification

NSD

Nuclear System Directive

NUHOMS

Nutek Horizonal Modular Storage

OSC

Operations Support Center

PIP

Problem Investigation Process

PORC

Plant Operating Review Committee

PO

Purchase Order

PSIG

Pounds Per Square Inch Gage

QA

Quality Assurance

RB

Reactor Building

RBCU

Reactor Building Cooling Unit

RCP

Reactor Coolant Pump

RCS

Reactor Coolant System

RFO

Refueling Outage

0RG

Regulatory Guide

SFP

Spent Fuel Pool

SQUG

Seismic Qualification Utility Group

SRI

Senior Resident Inspector

SRP

Standard Review Plan

SSS

Standby Shutdown System

Tave

Temperature Average

TC

Transfer Cask

TDEFW

Turbine Driven Emergency Feedwater

TS

Technical Specification

TSC

Technical Support Center

UFSAR

Updated Final Safety Analysis Report

URI

Unresolved Item

USTS

Upper Surge Tank Support

WO

Work Order

VIO

Violation

VTO

Vital To Operations (drawing)

  • rEnclosure

2