ML14191A915

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Insp Rept 50-261/88-01 on 880111-15 & 0125-29.Violations Noted.Major Areas Inspected:Maint,Design Control,Operations, Commercial Grade Procurement & Qa/Qc
ML14191A915
Person / Time
Site: Robinson 
Issue date: 03/21/1988
From: Belisle G, Mellen L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14191A913 List:
References
50-261-88-01, 50-261-88-1, NUDOCS 8804260114
Download: ML14191A915 (34)


See also: IR 05000261/1988001

Text

0% REQ 1XUNITED

STATES

NUCLEAR REGULATORY COMMISSION

-REGION

II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report No.:

50-261/88-01

Licensee:

Carolina Power and Light Company

P. 0. Box 1551

Raleigh, NC

27602,

Docket No.:

50-261

License No.:

DPR-23

Facility Name: H. B. Robinson 2

Inspection Conducted:

January 11 -

15 and January 25 -

29, 1988

Inspector:

, 3 2.1VEff

U. Mellen, Team Leader

Date Signed

Team Members: T. Cooper

L. Moore

L. Wharton

R. Wright

Approved By:

1

WG.

Belisle,-Chief

Dat'e Stgned

Quality Assurance Programs Section

Division of Reactor Safety

SUMMARY

Scope:

This special, announced quality.verification inspection was

conducted in the areas of maintenance, design control, operations,

commercial grade.procurement, and quality assurance/ quality control.

Results:

Four violations were identified involving failure to meet

reportability requirements, failure to perform post-modification

testing, failure to maintain records, and failure to follow procedures

relating to temporary repairs, work requests, and the trend analysis

program. One unresolved item was identified related to use of

commercial grade procured items and use of commercial grade procured

items in EQ applications.

8804260114 880414

PDR

ADOCK 05000261

GI

DCD

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

R. Barnett, Maintenance Supervisor, Instrumentation and

Controls

D. Baur, Supervisor, Quality Assurance

  • G. Beatty, Site Vice-President

J. Cribb, Supervisor, Quality Control

  • J. Curley, .Director, Regulatory Compliance
  • W. Flanagan, Manager, Design

R. Fronckowiak, Supervisor, Warehouse

W. Gainey, Supervisor, Operations

  • E. Harris, Director, Onsite Nuclear Safety
  • F. Lowery, Manager, Operations
  • R. Morgan, Plant General Manager

M. Page, Supervisor, Technical Support

  • D. Quick, Manager, Maintenance
  • B. Rieck, Manager, Materials and Administration

D. Whitehead, Supervisor, Performance Evaluation Unit

L. Williams, Manager, Security

  • H. Young, Director, QA/QC

Other licensee employees contacted included engineers,

technicians,

operators, mechanics, security personnel, and office personnel.

REGION II Attendees

  • G. Belisle, Chief Quality Assurance Programs Section

NRC Resident Inspectors

  • L. Garner, Senior Resident Inspector

R. Latta, Resident Inspector

  • Attended exit interview on January 29, 1988

2,

Exit Interview

The inspection scope and findings were summarized on January 29, 1988,

with those ,persons

indicated in paragraph 1 above.

The inspectors

described the areas inspected and discussed in detail the inspection

findings.

No dissenting comments

were received from the licensee.

Proprietary information is not contained in this report.

Note: A list of abbreviations used in this report is contained

in paragraph 11.

2

Item Number

Status

Description/Reference Paragraph

261/88-01-01

Open

VIOLATION -

Failure to meet

reportability .requirements (paragraph 8.f).

261/88-01-02

Open

VIOLATION -

Failure to perform

post-modification testing (paragraph 7.c).

261/88-01-03

Open

VIOLATION -

Failure to maintain

records (paragraph 8.f).

261/88-01-04

Open

VIOLATION -

Failure to follow procedure for:

1) use of a temporary repair that results in an

FSAR change (paragraph 7.a), 2) maintaining trend

analysis program records (paragraph 6.b), 3) job

descriptions for various operations positions

(paragraph 8.e).

261/88-01-05

Open

URI -

1) Use of commercial "off-the-shelf" -items

in safety-related applications without special

quality verification testing being performed

(paragraph 9.c). 2) Lack of definite correlation

between purchased item and tested item for use of

commercial grade

item

in

an

EQ application

(paragraph 9.c).

3.

Licensee Actions on previous Enforcement Matters

This subject was not addressed in this inspection.

4.

Unresolved Items

Unresolved items are matters about which more information is required to

determine whether they are acceptable or may involve violations or devia

tions. One new unresolved items was identified during this inspection and

is discussed in paragraph 9.c.

5. Quality Verification (T12515/78)

The objective of this inspection

was

to assess quality assurance

effectiveness.

For this report, quality assurance effectiveness is

defined as the ability of the licensee to identify, correct, and prevent

problems. The term quality assurance effectiveness is used in this

application, but it

is not meant to be limited to the licensee's Quality

Assurance Department. It

is the total sum of all efforts to achieve

quality results.

This was a performance-based inspection.

The principal effort was to

determine whether the results that the Quality Assurance program was

designed to accomplish were actually achieved.

However, when problems

were identified, appropriate regulatory requirements were enforced.

3

The inspection effort was divided into the following area.s:

Maintenance

Design Control

Operations

Commercial Grade Procurement

Quality Assurance/Quality Control

Each area is addressed separately in this report.

6.

Maintenance

The inspector witnessed various electrical/I&C and mechanical activities

in process. The activities were completed in a highly professional manner

by

knowledgeable personnel.

The overall performance of the maintenance

activities was acceptable. The inspector noted the level of knowledge and

experience as a strength in the maintenance area.

The inspector also examined the use of Work Requests,

the Maintenance

Trend Analysis program, and the Predictive/Preventive Maintenance program.

a.

Use of Work Requests

The inspector reviewed the administrative requirements for the use of

Work Requests, conducted interviews with technicians, mechanics,

and

work planners, and reviewed documentation, including NCRs, QA

surveillances/audits, and completed work packages.

Procedure PLP-013, "Maintenance Program", Revision 2, allows work to

be performed on routine skill-of-craft activities without the use of

approved procedures, with the Maintenance Supervisor administratively

controlling the performance of the activity.

The work planners are charged with providing the work instructions to

the mechanics and technicians on the Work Requests.

Other than a

general

instruction to provide work instructions in

MMM-003,

"Maintenance Work Requests",

Revision 16, and a list of what is

considered skill-of-craft in PLP-013, there are no specific guide

lines available to the work planners.

A review of 50 recently

completed work requests by the inspector determined that there is a

wide difference in .the detail provided by the work planner.

Work instructions for similar tasks can vary greatly from simple

statements to detailed step-by-step instructions..

For example, Work

Requests 87-AQJD1 and 87-AMZQ1 were both written to repack leaking

valves.

WR

87-AMZQ1 contains the instruction to replace valve

packing using 1/8 Chestron 1000 packing. WR 87-ADJQ1 contains six

specific steps to be performed in sequence. Both WRs are designated

as skill (i.e., skill-of-craft).

4

The lack of specific administrative control over the content of the

work instructions included on a WR is considered a weakness in the

maintenance area.

b.

Maintenance Trend Analysis

The

inspector reviewed

requirements for the maintenance

trend

analysis program,

interviewed maintenance engineers concerning the

implementation of the program, and reviewed a sample of trend reports

generated under this program.

The type of trending program utilized

at HBR,

if

used in conjunction with existing programs such as the

preventive -maintenance program,

has the potential of reducing the

amount

of. corrective maintenance

required to repair recurring

problems.

The inspector noted that a problem with the utilization of the

existing trending program was the lack of follow-up

on

items

identified during the trend reviews. Of the ten reviews conducted by

the inspector, nine of the packages did not fulfill the requirements

of MMM-011,

"Trend Analysis",

Revision 3.

Problems varied from

failure to be administratively closed out, even though corrective

action had been completed during the last refueling outage,

to

several corrective actions being past the target date without a

revision to -the schedule being approved by

the Maintenance

Supervisor.

The trend analysis program is not being utilized

according to procedure,

which has the potential of reducing its

effectiveness. Identified adverse trends in safety related equipment

need to be handled in a timely manner and corrective actions need to

be monitored to assure adequate completion.

Failure to maintain the Trend Analysis program requirements is

collectively combined with other examples of failure to follow

procedure in paragraphs 7.a and 8.e, and is considered an example of

violation 261/88-01-04.

c.

Preventive/Predictive Maintenance

The Preventive/Predictive Maintenance program

is designed to be

utilized to reduce the amount of corrective maintenance required on

certain safety-related and important-to-safety equipment.

The

program at HBR is presently being transferred

from Maintenance

Engineering to Technical Support. The personnel and responsibility

have already been transferred and approval of the interdepartmental

interface agreement was pending at the time of the inspection, which

would allow for the revising the.governing procedures.

According to MMM-005,

"Preventive/Predictive Maintenance Program",

Revision 9, the SPC, which consists of a list of the equipment placed

in the PM/PDM program for each system, with PM/PDM tasks for each

piece of equipment identified, is used by the maintenance planners to

5

develop the PM/PDM schedules.

The SPC will be controlled as an

instruction, requiring the Maintenance Supervisor to approve any

changes. The SPC was requested to be computerized in December 1986

in order to increase the efficiency of the utilization of the

program. The

SPC has not been updated since this request was

submitted.

The responsible engineer for the PM/PDM program demonstrated to the

inspector that the required changes to program procedural

and

computer software development are in-process, which alleviated all

concerns expressed by the inspector concerning the deviation from the

established program.

The

PM/PDM

program thoroughly addresses safety-related equipment

needs for the systems reviewed by the inspector. The components have

been evaluated and schedules developed for any components requiring

routine PM. The PM scheduling has been successfully implemented by

the work planners. The inspector determined that the PM/PDM program

adequately addresses the objectives established for it.

7.

Design Control

.Assessment

of the design control

functional area included: a design

process and interface review, justifications for continued operation and

temporary modifications review, previously identified findings

and

associated corrective actions review, and a sample design change package

review. The design process at HBR was generally adequate except for

temporary modifications and post-modification testing.

Specific problems

in these areas are discussed in later paragraphs of this section.

A

strength was identified relating to the licensee's identification of a

problem associated with an excessive number of design change notices to

approved modifications

and management's effective corrective action

initiative.

The majority of HBR modification packages are developed by NED,

the

corporate design organization. The onsite design group acts as a liaison

engineering group between onsite and offsite design activities.

The

liaison group is

separated into disciplines and. generally provides

constructability reviews, and coordination of modification implementation

and close out.

Modifications can originate via LER,

PIR,

temporary

modifications, or management initiative.

The design approval/development process typically begins with a PIR.

A

PIR can be initiated by any site personnel to propose a plant improvement

or request engineering evaluation.

There were 359 open PIRs on

January 14, 1988, which included major projects/modifications, non-routine

budget items, and non-safety-related improvements not handled by

maintenance work requests.

A review of the volume and subject of

6

modification associated PIRs did not identify any safety concerns with

respect to backlogged modification requests.

Following initiation, the

PIR receives management and discipline reviews to verify the validity of

the proposed plant improvement.

Those modification PIRs which receive

Site Vice-President approval

are further developed to establish the

detailed scope and. then modification package development is performed by

NED. Discussions with site design personnel and review of -design change

packages indicated an adequate interface between the principal design

group (NED) and the onsite implementation and coordination group.

a. Temporary Modifications and JCOs

The

inspector reviewed temporary modifications and JCOs for

conformance to programmatic requirements, longevity, and impact on

procedures and plant design basis documents. Administration of both

temporary modifications and JC0s was weak and these problems had been

previously identified by the licensee and were in the process of

being corrected.

Temporary modifications/repairs were administra

tively controlled by the maintenance group in accordance with

MMM-013,

"Temporary

Repairs",

Revision 4.

This procedure did not

require time limits on temporary repair installation nor periodic

reevaluations of temporary repairs to verify the need of continued

installation.

Due to the lack of administrative controls in these

areas, this is identified as a weakness.

The inspector reviewed the following temporary repairs/modifications:

TRP 85-07

Service Water MIC Repair

TRP 86-01

Mechanical Block of SI Mini-flow

Recirculation Valves

TRP 86-02

Commercial Grade Insert in Pressurizer

Safety Valve

TRP 86-10

Containment Penetration Bellows Repair

TRP 87-10

Jumper on SI Valve Interlock

Temporary modification

TRP 86-01 blocked the SI

pump mini-flow

recirculation isolation valves,

SI -856A

and B, into the

open

position, to ensure a SI pump flowpath. The safety evaluation stated

that these valves were required closed only during transfer from hot

leg recirculation to cold leg recirculation and that removal of the

blocks presented no impediment to this operational transition.

The

inspector reviewed the

procedure

governing this evolution

and

verified the specific requirement for. mechanical

block removal.

Although this temporary modification involved no apparent safety

concern it

did violate the programmatic controls for temporary

modifications.

Administrative procedure, MMM-013 requires that

modifications involving FSAR changes cannot be processed via MMM-013

without the required reviews.

TRP 86-01 did involve an FSAR change

in that FSAR Figure 6.3.2.1, the flow diagram for the SI system,

identified these as fail-close valves.

The mechanical blocking open

of these valves was not identified or processed as an FSAR change.

.7

This failure to follow MMM-013 is collectively combined with other

examples of failure to follow procedure in paragraphs 6.b and 8.e,

and-is identified as an example of violation 261/88-01-04.

The inspector's review of JCOs indicated that there was no specific

programmatic controls to address this mechanism.

Due to EQ require

ments established over the past years, the JCO has assumed a focused

identity as a mechanism to document justification of plant conditions

which do not exactly conform to plant design or commitments.

The

JCOs are performed at HBR in accordance with MOD-001, "Procedure for

Preparing Engineering Evaluations",

Revision 8.

This procedure

provides a format for evaluation and requires a 10 CFR 50.59 safety

review, but does not provide administrative controls for JC~s.

It

appeared that the majority of JCOs are reviewed by at least one PNSC

member. This is due to a required review of engineering evaluations

by discipline managers. Discipline managers are also members of the

PNSC. The evaluations could be tracked via the PNSC action item list

or other plant tracking system; however,

no single mechanism exists

to ensure a consolidated control and tracking of JCOs. Additionally,

the JCO process is not specifically defined nor does any one group

have administrative responsibility for JCOs.

The

need for JCO

administrative responsibility was verified by a review of.JCOs. For

example, JCO87-101 addressed a justification for a non-EQ qualified

valve to operate in an

EQ environment.

The restriction on the

justification was to ensure the valve was deenergized one hour after

an SI actuation due to steam break or LOCA, since valve operation in

the subsequent environment could not be guaranteed after one-hour.

Although the evaluation received PNSC approval, no responsibility was

assigned to verify implementation in plant procedures. The inspector

reviewed the implementation in the impacted procedures and noted that

the valve motor-operator deenergization requirement was event

designated rather than a specific one-hour limit.

Discussions with

the cognizant engineer identified a scenario (small

break LOCA with

one SI pump running) where the one-hour limit could be exceeded.

Upon identification of this item the licensee initiated corrective

action revising the associated procedures to state the EQ precaution

as a specific time limit. - This example illustrates the need to

designate administrative responsibility for JCO implementation.

b.

Corrective Actions

The licensee has identified weaknesses in the administration of

temporary modifications and JCOs and initiated corrective action.

Procedure MMM-013 was superseded on January 29,

1988,

by MOD-018,

"Temporary Equipment Modifications", Revision 0, which provides more

specific administrative and technical

controls and transfers

administrative responsibility to operations. The JCO administrative

weakness was identified by PNSC action item 87-08 from PNSC meeting

minutes dated 5/25/87. An action completion date of 12/31/87 was not

8

met since the corrective action scope proposed to the

PNSC was

determined inadequate. An interim corrective action to revise the

Engineering Evaluation Procedure to address JCOs specifically and

require a PNSC review was committed for February 29, 1988. Long term

corrective action was to establish a program/procedure specifically

for JCO control with administrative responsibility assigned to the

onsite design group. The long term commitment date was December 31,

1988.

The inspector reviewed corrective actions initiated by the licensee

for weaknesses identified with design basis documents and DCNs. Lack

of consolidated design base documents and indexed calculations had

been identified by the licensee and the NRC in previous inspections.

Programs to correct these problems are in the organizational- stage,

i.e., funds approved,

responsibilities and scope established,

and

guidelines developed for the process of compilation and evaluation of

design basis data. No actual man-hours had been expended on actual

data collection. PIR 87-038 initiated on April 1, 1987,

recommended

consolidation of design basis documents which were previously held by

various A/E or vendor groups, i.e.,

EBASCO

and Westinghouse.

The

design bases are presently available at various vendor locations

primarily due to the proprietary nature of the information and the

A/E information controls in effect during the construction period.

Design basis information is presently acquired by the design engineer

via an extensive search of specifications, FSAR, drawings, purchase

orders, etc. The DBD program will require review of post operating

license commitments with the original.design basis data retrieved

from the A/E and subtier vendors.

This updated data will then *be

entered into a consolidated controlled

system to provide for

retrieval of design base information. The projected completion date

for safety-related systems is 1991.

Closely associated to the DBD program is the calculation control

program- which will provide the collection and indexing of design

calculations.

This program was proposed on

PIR 87-141,

dated

September 8, 1987. This program is still in the proposal/approval

process although management indicated.the calculation indexing should

be under development by June 1988.

This program parallels the DB0

program in some aspects due to identical sources of information. The

DBD and Calculation control programs are long term corrective actions

to resolve a basic weakness in the HBR design control program.

A shorter term corrective action initiated by the licensee was the

DCN

reduction program.

The

licensee reviewed a sample

of 46

modifications from the period of 1982 to 1986 to determine the volume

of DCNs being used on modifications.

The evaluation identified a

problem with excessive DCNs which is illustrated by the following

table:

9

Average No.

No. of Mods

Highest

No.

Category

DCNs/Mod

Evaluated

DCNs/Mod

New Systems

26

13

100

Modified Systems 42

14

142

Modified Comps.

15

19

88

In conjunction with this evaluation, design management initiated an

assessment program and established-goals to reduce the number of DCNs

for Refueling Outage No. 11. The assessment requiredia review by the

Design Manager of each DCN to determine the reason for the DCN and if

the DCN could have been prevented.

The following are the goals

established and the results from the outage:

Category

Goal

Actual DCNs

New Systems

15

19

Modified Systems

11

5

Modified Components

6

6

The assessment of DCNs identified the two major causes of DCNs as

inadequate construction walkdowns (27 percent) and inadequate design

review (28

percent).

Additionally,

it

was identified that the

highest number of DCNs were on I&C

and electrical modifications

assigned to the contract A/E.

These were also the most complex and

extensive modifications.

The licensee was in the process of further

breakdown of root causes *and formulation of specific corrective

actions; however, the DCN reduction achieved by management focus on

the area represents a strength in the design control program.

The

licensee efforts to identify the problem scope, evaluate causes, and

provide initial improvement of the problem are commendable.

C.

Design Modification Packages

The

inspector reviewed a sample of modification packages for

documentation of design input, 10 CFR 50.59 safety evaluations, and

post-modification testing.

This review included the- following

modifications:

Modification No.

Title

M-912

Pressurizer PORV Block Valve

Replacement

M-883

Degraded Grid Bypass

Indication

M-920

AFW Control Wiring Reroute

M-890

-Upgrade

of PT Fuses on 480V

Emergency Bus

10

Documentation

of

input requirements was adequate

for those

modifications reviewed, consisting of a standard checklist and

references which more fully described the design document input.

Safety evaluations were expansive and generally comprehensive.

A

violation was identified with respect to performing post-modification

testing. Modification M-920, involving rerouting of the AFW control

wiring, stated as acceptance criteria that the AFW pumps and header

discharge valve (V2-16B) control circuits perform as designed and as

specified in FSAR section 7.3.1.1.1.

The referenced FSAR section

lists the auto start signals for the AFW pumps.

Contrary to this,.

the modification was closed out with only a circuit continuity check

performed for a post-modification test.

On June 15, 1987, the "B"

AFW pump failed to start on a loss of main feed pump auto-start

signal (LER 87-018).

The cause was a wiring error during modifica

tion implementation which would have been identified if the required

post-modification testing had been performed.

Corrective action for

this LER was implemented by Special Procedure 781, "Special Procedure

for Testing Auxiliary Feedwater Pumps A and B",

Revision C.

This

procedure tested two of the four auto-start signals.

The SL and

black out start signals were not tested at this time. Review of the

control wiring diagram, Drawing No. B-190628, illustrated that the SI

and black out circuits are physically separate from the Low-Low Steam

Generator Level and Loss of Main Feed Pump circuits and were not

impacted by this. modification.

Performance of SP-781 and'OST-201,

"Motor Driven AFW System Component Test", on June 17, 1987, provided

reasonable

assurance

of

AFW

pump operability.

However,

these

activities needed to have been performed prior to modification close

out.

An additional failure to perform specified post-maintenance testing

was identified on M-912,

"Replacement of Pressurizer

PORV

Block

Valve". The modification performance requirements stated the valves

must close in 40 seconds or less.

No verification of this closure

time was performed prior to modification close-out although a

performance test was

done

on

the valve several

months after

modification close out and the closure time was within the required

limit. Modifications M-912 and M-920 stated specific acceptance

criteria to be verified by post-modification testing.

This failure

to perform post-modification testing is identified as violation

261/88-01-02.

8. Operations

a.

Licensee Event Reports (LERs)

The inspector reviewed the licensee's preparation and handling of

LERs.

HBR

LERs are presently governed by Plant Operating Manual

Administrative Procedure AP-030, which requires compliance with 10

CFR 50.73, "Licensee Event Report System",

as well ,as NUREG-1022,

"Licensee Event Reports" and its Supplements, Nos. 1 and 2.

.

11

The

AEOD provided CP&L their second evaluation of Robinson

LER

quality in a QER dated August 6, 1987. This QER covered a sample of

15

LERs submitted by

HBR

between November

1985 and June 1987.

Robinson's overall evaluation was below the industry average and was

attributed to inattention

to detail

in completing the

LER

documentation.

Although the inspector noted similar occurrences in recently issued

LERs,

there was a marked decrease in the number of LER deficiencies

and a marked increase in the quality of the issued LERs.

The

licensee is in the process of implementing an LER quality improvement

program which will include the following:

Implementing the guidelines of NUREG-1022

Required peer evaluation of LER drafts

Improved AP-030, "Licensee Event Reports"

Improved Regulatory Compliance instructions

Development and use of an LER checklist

Obtaining an independent assessment of LER quality by

the Onsite Nuclear Safety unit

Improved -communication with other CP&L sites on

regulatory reporting matters

Developing a consistent LER format

Required Plant Nuclear Safety Committee review of LERs

prior to submittal

Preparing an LER Handbook for training and reference by

LER writers and reviewers

Developing a group instruction on LER preparation

Starting a training program for LER writers

Assessing whether prior LERs should be revised

Using an LER checklist based on NUREG-1022 and

Supplements 1 & 2

Involving more management and plant personnel in LER

review

Portions of this program have been implemented with a significant

improvement in LER quality.

b.

ISI Program

The inspector reviewed the results of various revisions of OST-151,

"Safety Injection Component Test", and determined there was an error

in the equation for.calculating SI pump suction pressure. The error

was in the constant used for suction height of the Safety Injection

pumps.

The inspector noted this method was used for calculating

suction pressure of other safety related pumps.

The licensee

assigned a team of two people to resolve the question immediately..

One individual measured the piping locally to determine the height of

the eye of the pump suction from the base elevation.

The othe'

researched the plant drawing file and procedure files to determine

12

the basis for the original height.

As a result, the listed height

correction was determined to be inaccurate in the round off to the

nearest foot. The measured height was determined to be 29 inches and

should have been rounded off to 2 feet instead of 3 feet.

The root

cause was not determined, but was speculated to involve the use of

the top of the piping as reference instead of the centerline of the

piping (eye of the pump).

The licensee agreed that the eye of the

pump would have been the correct reference for establishing the pump

suction pressure. To determine the effect of the one foot error, it

was evaluated against the current pump operating conditions.

One

foot of suction error would introduce a maximum error of 0.43 psig,

or 0.03% of the operating delta pressure of approximately 1450 psid.

The actual effect was insignificant since the accuracy was set by the

maximum reading error of the instrumentation.

This was set at the

resolution of the discharge pressure gauge (2000 psig) which was 10

psig minimum.

Although the error was insignificant, the licensee

stated that a change would be made to the OST to correctly indicate

the suction pressure.

The licensee is

also investigating the

likelihood of a similar condition existing on the other pumps tested

by the ISI program.

While the investigation was proceeding,

the

licensee reviewed the effect of another potential error on low

pressure pumps.

Due to the piping sizes involved, the error will

still most likely be one foot or less (0.43 psig). The RHR pumps.are

the most sensitive, but due to their elevation being lower than the

RWST the error would be conservative. It would represent an error of

approximately 0.3%, still below the resolution of the gauges.

The

licensee stated that they would complete the review to ensure no

other similar errors existed and initiate procedure changes where

applicable.

The licensee's prompt attention and immediate corrective actions are

considered an example of responsiveness and management concern in the

ISI program.

c.

OST Scheduling

The inspector reviewed the licensee's methods used for scheduling

OSTs and noted the scheduling appeared to be complete and accurate.

All OSTs reviewed were accomplished within the required interval.

d.

Conduct of Operations

The inspector reviewed the conduct of on-shift operators and the

conduct of operators during plant events. The inspector concluded

the .operators were knowledgeable of plant conditions, their assigned

duties, and events that significantly effected plant operations. All

operational activities witnessed by the inspector were completed in a

highly professional manner. The overall conduct of operations was

satisfactory.

13

e.

Procedure OMM-001

The inspector reviewed OMM-001, "Operations -

Conduct of Operations",

Revision

12.

The

inspector noted that job descriptions for

operations personnel were not consistent with lower tier documents or

actual work performed. An example of this practice is the require

ment of section 3.10, Shift Technical Advisor, delineating an STA

duty as "Review plant LERs for completeness,- applicability, and

compliance with reporting requirements."

The STA is not in the

review cycle for all

LERs.

This duty is

performed by Senior

Specialists in Regulatory Compliance.

This example of failure to follow procedure is collectively combined

with other examples in paragraphs 6.b and 7.a, and is identified as

an example of violation 261/88-01-04.

f.

Diesel Generators (D/G)

The inspector reviewed operation of the diesel generators. During

the attempt to reconstruct

the

events of August

26,

1987,

September 8, 1987,

November 4, 1987,

and November. 5,

1987,

the

inspector noted the Shift Foreman's log and the Control Operator's

log did not contain appropriate log entries as required by OMM-001.

OMM-001,

Section 5.7.3, "Shift Logs",

paragraph 1, requires the

Control Operators log to record the plant status and events in

chronological order.

Log entries include the following:

Date

Plant Status

Changes in Generator Output

Changes in Reactor Power Level

Starting and stopping of major equipment

Change of Auxiliary System and Configuration

Changes in Reactor Control Rod group positions

Performance of surveillance tests

Reactor Trips

Instrument or equipment.malfunctions or failures

Unusual trends or conditions observed

Major in-plant electrical switching

Starting and stopping of gaseous or liquid waste releases

Setpoint changes

Performance of AOPs both immediate and subsequent actions

Performance of EOPs both immediate and subsequent actions

OMM-001, Paragraph 2, requires the Shift Foreman's log book to record

the following events:

Change in status.of equipment

Reportable occurrences

Unusual occurrences

14

Set point changes

Liquid or gas releases

Changes of major auxiliary equipment service

Significant events

Entering the emergency plan

Changes of emergency classification

Additionally, 10

CFR

50,

Appendix

B, Criterion XVII,

Quality

Assurance Records, required that sufficient records be maintained to

furnish evidence of activities affecting quality. The records shall

include at least the following:

operating logs.

Contrary to the requirements,

log entries were not adequately

.maintained on multiple occurrences during the diesel generator events

between August 26,

1987 and

September 8,

1987,

as shown in the

following chart. These examples are not all inclusive and are used

to illustrate operator log problems.

Date

Time

Missing log entry

8/26/87

0145

Both D/Gs inoperable, did not record

entry into TS 3.0 in Shift foreman's or

Control operator's log.

8/26/87

0145 -

0157

Did

not

record

D/G

investigation

.performed by Shift Foreman

in shift

foreman's log.

Two additional D/G

starts and one additional D/G trip were

not recorded in the control operator's

log.

8/26/87

1400

Seven day LCO for "A" diesel generator

inoperability not recorded in shift

foreman's or control operator's log.

8/27/87

1349 -

2330

No records of testing of "A" Diesel

generator, or, diesel generator trip in

control operator's log.

9/8/87

0545

Seven day LCO for "B" diesel generator

inoperability not recorded in shift

foreman's or control operator's log.

9/8/87

2230

Both D/Gs inoperable, did not record

entry into TS 3.0 in shift foreman's or

control operator's log.

Failure to make appropriate log entries as required by 10 CFR 50

Appendix B, Criterion XVIII and OMM-001 is considered to be violation

261/88-01-03.

15

As a result of the incomplete and conflicting information available,

the inspector requested that the licensee reconstruct a sequence of

events for 4 diesel generator events and the activities concerning

the diesel generators between the related events of August 26, 1987,

and September 8, 1987,

and the events of November 4, 1987,

and

November 5, 1987.

Although some inconsistencies exist between these

sequences of events

and existing records

and interviews,

the

inspector evaluated the sequences of events to determine procedural

and regulatory adherence during the events.

SII

SII

DIESEL GENERATOR SEQUENCE OF EVENTS

8/25/87 -

9/17/87

Date/Time

Event

8/25 0205

"A" Diesel Generator was tested in order to take "B" Diesel

Generator out of service for preventative maintenance, standby

jacket water cooling system maintenance, and other miscellaneous

work.

0348

OST-401 was successfully completed for "A" Diesel

0800 "B" Diesel Generator was removed from service under a 7-day LCO for

preventative maintenance.

8/26

-

0130

Licensed operator was sent to perform the OST-401 operability

check on "A" Diesel Generator (D/G).

0145 "A" D/G tripped on overspeed during the initial start and was

declared inoperable resulting an 8-hour LCO (T.S. 3.0).

The Shift Foreman investigated the problems with "A" D/G:

o

Governor linkage was inspected.

o

Injection

pump

inspection

covers

were

removed

for

inspection.

No apparent problems were revealed during this investigation.

"A" D/G was started again.

o

Shift Foreman observed engine governor linkage:

-

Governor appeared to be controlling engine speed

(speed indicator not provided).

-

Engine again tripped.

"A" D/G was started again.

o

This start appeared normal, and the engine was shut down by

the operator.

The Operations Manager was notified (On-Call Manager):

0

Both D/Gs were out of service.

0

No apparent cause of trips had been found.

o

The last start was successful.

0

Engine operation appeared normal.

0

There was no known history of overspeed tripproblems.

Overspeed trips were believed to have been spurious.

Date/Time

Event

17

o

The decision was then made to perform OST-401

(Normal

Operability Surveillance Test).

o

Maintenance was directed to expedite reassembly of "B" D/G.

0157 "A" Diesel was started to run OST-401 operability check.

0202 "A" Diesel paralleled to the grid.

While OST-401

was in progress, Operations Manager discussed

operability and reportability with the Director

-

Regulatory

Compliance:

0

It was determined that this event constituted a 4-hour

report.

0

It was decided that if the OST-401 testing was successful,.

"A" D/G would be declared operable.

0

It

was decided that if

the OST-401 testing was

not

successful,

Unit No. 2 would be shutdown since "B"- D/G

could not be returned to service within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />.

The Operations Manager directed the Shift Foreman to:

0

Complete OST-401 to return "A" D/G to service.

0

o

Perform an additional start approximately one hour after

the D/G was shutdown to increase confidence that the D/G

was operable under relatively cold start conditions.

0340 "A" Diesel separated from the grid.

0343 "A" Diesel stopped.

0350

OST-401 was completed satisfactorily. (Exit TS 3.0)

0400 "A" Diesel declared back in service.

0404

NRC Resident notified that both-diesels had been out of service.

0408

Red Phone call made to notify that both diesels had been out of

service. (10 CFR 50.72 B.2.iii)

0501 "A" Diesel restarted

successfully as directed earlier. by the

Operations Manag.er.

0506 "A" Diesel stopped. No operability problems had been noted.

0730

At the daily Unit Managers'

meeting, this event was discussed,

Although "A" D/G had started successfully the last three times,

it was decided to further investigate the overspeed trip on "A"

D/G. A technical representative from Fairbanks Morse was called

in to help investigate the trips.

Date/Time

Event

18

1118 "B" Diesel was started for an operability check to place it back in

service.

1121 "B" Diesel was paralleled to the grid.

1259 "B" Diesel was -separated from the grid.

1315

OST-401

was satisfactorily completed,

and

"B" Diesel

was

declared back in service.

1400

"A" Diesel

taken out of service under a 7-day

LCO for

preventative maintenance

and to investigate the previous

overspeed trips which had occurred at 0145 hours0.00168 days <br />0.0403 hours <br />2.397487e-4 weeks <br />5.51725e-5 months <br />.

(WR87-AMER1)

Later in the day, the technical representative arrived and found

that one fuel injection pump control rod was hanging in the open

position.

It

was believed that the trips were caused by

excessive fuel being pumped into the engine.

The pump was

replaced early the next morning.

8/27 1349

-

"A" Diesel Generator testing was conducted.

2330

1631

Unit No. 2 was shutdown due to an E-H Oil leak.

1957 "B"

Diesel was started for operability testing because "A" Diesel

remained out of service.

2145

OST-401 was satisfactorily completed for "B" Diesel.

2330 "A" Diesel was started to run the operability check.

8/28 0130

"A" Diesel declared back in service per the satisfactory

completion of OST-401.

0250

Unit 2 was returned on line due to successful E-H Oil leak

repair.

8/31 2143

"B" Diesel was started to run an operability check. "A" Diesel

was to be taken out of service to replace exhaust manifold heat

shields.

2340

"B" Diesel

was stopped and operability performance declared

satisfactory due to the completion of OST-401.

9/1

0830

"A" Diesel was taken out of service to install exhaust manifold

heat shields.

1345

"A" Diesel was declared back in service due to the successful

.completion of OST-401.

Date/Time

Event

19

9/7

2240

"A" Diesel started for operability check to remove "B" Diesel

from service for maintenance not previously completed on 8/26.

NOTE:

At this time, "A" D/G had been successfully cold started

on 2 separate occasions since 8/28/87.

9/8 0028

"A" Diesel was stopped and OST-401 was satisfactorily completed.

0545

"B" Diesel was taken out of service for maintenance under a

7-day LCO.

2236

"A" Diesel was started to perform an operability check.

o

"A" Diesel tripped on overspeed.

-

Declared out-of-service resulting in an 8-hour LCO.

2238

"A"Diesel was again started, and again tripped on overspeed.

0

Shift Foreman notified the Operations Supervisor.

O

Conference call was set up between the Shift Foreman,

Operations Supervisor, and the Operations Manager.

-

No

confidence

in "A" -diesel operability due

to

overspeed trips (apparent repeat of the 8/26 event).

-

"B" D/G could be returned to service within the Tech.

Spec. 3.0 LCO.

-

Start Plant shutdown if the "B" D/G OST is not started

within five hours.

-

If

OST-401

was

not satisfactory,

proceed to -hot

shutdown within the T.S. LCO.

P ~

On-Call Manager and the Director-Regulatory Compliance were

involved in the discussion and concurred with the

decisions.

2350

The

NRC Resident was notified of a 4-hour immediate

notification.

9/9 0208 "B" Diesel was started.for. an operability.check because "A"

Diesel

was currently out of service.

0219

Red Phone call was made to the NRC for a 4-hour significant

event.

0406

OST-401 was completed,

and "B" Diesel was declared back in

service.

0419

NRC was notified, when they called for a Daily Plant Status

Check, that "B" Diesel was operable at 0406 and that "A" Diesel

was out of service. under a 7-day LCO.

Date/Time

Event

20

1300

A PNSC was conducted to review the "A" D/G concerns.

The PNSC

appointed a project team consisting of Tech.

Support,

Mech.

Maint., ONS, and Operations personnel. The task team took steps

to obtain technical assistance representatives from Fairbanks

Morse, Woodward Governor, and independent engineering consulting

services from Trident Engineering.

9/10 0136

"B" Diesel started for operability testing because "A" Diesel

was still out of service.

0404

OST-401 was satisfactorily completed.

2015

Unit 2 was taken off-line due to a turbine generator hydrogen

cooler leak.

2046

Reactor was shut down. Redundant diesel testing is no longer

required by Technical Specifications.

9/14 0633

"A" Diesel

was

started for testing after injection pump

replacement.

1351

"A" Diesel was stopped.

1451

OST-401 was unsatisfactorily completed.

When speed droop was

reset to zero the engine speed drifted badly.

2108 "A" Diesel was run to allow governor compensation adjustment.

2239 "B" Diesel was started for operability check.

9/15 0045

OST-401 operability check for "B" Diesel was satisfactorily

completed.

-

0200

Test run of "A" D/G to test governor operation.

0615

-

"A" Diesel was run to test the governor operation per

0747

OP-604 in order to gather load indicator vs. load data.

1010

-

"B" Diesel was run to gather data for Engineering so that

1051

the maximum starting RPM's for "B" D/G could be compared to "A"

D/G.

1640

-

"A" Diesel was run for testing after the governor oil

1707

was changed.

9/16 2100

"A" Diesel was started. This run was to perform an overspeed

trip test after the trip mechanism was adjusted to give a higher

trip point. This test was satisfactory.

2102 "A" Diesel was paralleled to the grid.

Date/Time

Event

21

2212 "A" Diesel was separated from the grid and subsequently stopped.

OST-401 was completed.

Evaluation of data revealed that

improvement could be made in the balance between cylinder

temperatures.

9/17 1400

-

"A" Diesel was run for an operability check following

1541

maintenance work to balance the cylinder temperatures.

2140

OST-401 was satisfactorily completed,

and

"A" diesel

was

returned to service.

11/3/87

0401 -

"B" Diesel Generator (D/G)

was tested for operability

0545

per OST-401 (using the inboard solenoid) to take "A" D/G

out of service to perform work on its service water system.

0600 "A" D/G was taken out-of-service.

11/4/87

0505 "B" D/G was tested for operability per OST-401 (using the

outboard solenoid) because "A". D/G was still out of service.

11/5/87

0250-"B" D/G local start was attempted by a licensed operator (using

the inboard solenoid).

The

start sequence was stopped

(pushbutton released) due to audible evidence of air leaking to

atmosphere in the vicinity of the

starting air solenoid

manifolds.

The

operator notified the Shift

Foreman,

who

proceeded to the Diesel Generator Room.

The Shift Foreman

0

Inspected air system

O

Instructed the operator repeat start sequence, while he watched

the air start system,

in the exact manner as was previously

performed.

11/5/87

0256 A second attempt to local start "B" D/G resulted in a successful

start.. At that time, the Shift Foreman notified the operating

supervisor and was instructed to start the diesel a third time.

11/5/87

0310 A third attempt to local start "B" diesel resulted in a

successful start using the inboard solenoid.

Shift Foreman was directed to set up a conference call between

Operations Supervisor, Operations Manager,

and the Director

Regulatory Compliance.

The following is a summation of the

conference call.

0

Reviewed sequence

O

Decided on-2 potential causes

(1) Sticking check valve (non-tested side)

(2) Sticking.solenoid valve (tested side)

Date/Time

Event

22

11/5/87

0

After the successful starts:

-

It

was determined that the most probable cause was a

sticking check valve

1. Check valve flow path was used in the previous day's test.

2. The check valve apparently became unstuck during -or after

the aborted start attempt as a result of reverse airflow or

mechanical vibration.

It was recognized that, had both solenoids been lined up for

normal operation (not in the test configuration), the D/G would

have auto-started as required.

o

The D/G was considered to be operable because it

was the

local start test configuration that caused the failure to

start.

(Later,

the PNSC

recognized that the D/G should

have been considered technically inoperable prior to its

successfully starting).

o

The Shift Foreman was instructed to complete the OST.

0507

OST-401 on "B" D/G was successfully completed.

0730

The event.was discussed during the Daily Unit Managers' Meeting.

(Managers

of Operations and Maintenance later discussed the

event with Project Vice President).

It was decided to gather

pertinent information for review by PNSC.

11/5/87

1330 The

PNSC

was convened to review the EDG testing concerns,

discuss reportability issues, and recommend follow-up actions.

The PNSC directed that the following actions be taken:

0

Inspect check valves on "B" D/G.

0

Check strainers for debris.

0

If no problems found, check solenoid valves.

o

Operations to write an NCR to track resolution.

0

"B" D/G should be considered technically inoperable for the

six minutes until the

successful

start, and that a

four-hour report be issued.

Declared reportable at 1500

hours.

11/5/87

1500 The NRC Resident was notified of this event.

1847 A four-hour immediate notification was made to the NRC via the ENS.

11/5/87

1500 -

The following work was performed:

11/6/87

0525 0

A starting air solenoid from stock was set up in the I&C

Shop to give the I&C Technicians a feel for a properly

operating solenoid.

Date/Time

Event

23

o

Since "A" D/G was out of service, its strainers and check

valves were

disassembled

and

inspected.

No debris,

discoloration, or freedom of movement problems were found.

o

"B"

D/G

was

started (using

the outboard solenoid),

synchronized to the grid,

separated from the grid, and

stopped. It was verified to be operable per OST-401.

0525-0542 "A" D/G was test operated prior to installing heat shields.

0828-1030 "A" D/G was test operated per OST-401 and returned to service.

1135-1510 (The following is a summary of actions taken as directed by the

PNSC):

O

The "B" D/G

outboard strainers and check valves were

disassembled and inspected. No debris, discoloration, or

freedom of a movement problems were found.

The outboard solenoid valve was disassembled and inspected

for signs of trash or other material.

The solenoid main

plunger was checked for free operation and any signs of

sticking.

Condition of components

appeared

to

be

satisfactory.

0

"B"

D/G

was then satisfactorily started for outboard

solenoid valve testing.

1515-1643 o

The "B" D/G

inboard strainers and check valves were

disassembled and inspected. No debris, discoloration, or

freedom of a movement problem were found.

o

The inboard solenoid valve was disassembled and inspected

for signs of trash or other material.

The solenoid main

plunger was checked for free operation and any signs of

sticking.

Condition

of

components

appeared to be

satisfactory.

o

"B" D/G was then satisfactory started for inboard solenoid

valve testing.

The NCR remains open at this time.

NOTE: The licensee omitted a November 4, 1987, diesel generator

event from the sequence of events. This event involved the

inoperability of both diesel generators for less than one minute

after a motor control center was inadvertantly disabled.

24

Following the event of August 26,

1987, the licensee's cursory

corrective actions appeared inadequate to preclude repetition.

This is identified as a management weakness.

Following an

identical

failure

on

September 8, 1987,

the

licensee

aggressively began troubleshooting diesel generator problems.

Several days later the licensee found that the problem was a

defective overspeed trip mechanism and performed corrective

action.

During the Diesel Generator events of August 26, 1987,

September 8, 1987,

November

4,

1987,

and November 5,

1987

the licensee determined that these events were reportable as

four-hour events and notified the NRC as required by 10 CFR

50.72.b.2.iii.

This requires the licensee to notify the NRC

as soon as practical and in all cases within four hours of the

occurrence of any of the following;

-

Any event or condition that alone could have prevented the

fulfillment of the safety function of structures or systems

that are needed to:

o

Shutdown the reactor and maintain it

in a safe

shutdown condition,

So

Remove residual heat,

o

Control the release of radioactive material, or

0

Mitigate the consequences of an accident.

For the events of November 4, 1987,

and November 5, 1987, the

reporting requirements for 10 CFR 50.72.b.2.iii were not met in

that they were not reported within four hours as required.

Date

Report Time (following event)

8/26/87.

2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> 38 minutes

9/8/87

3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> 41 minutes

11/4/87

21 days

11/5/87

approximately 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br />

In reviewing these events, it was determined that the

requirements of 10 CFR 50.72.b.2.iii are not. applicable.

The

requirements of 10

CFR 50.72.b.1.ii

are applicable.. This

requires that the licensee notify the NRC as soon as practical

and in-all cases within one hour of the.occurrence of any of the

following:

-

Any event or condition during operation that results in the

condition of the

nuclear powerplant,

including* its

principal safety barriers, being seriously degraded; or

results in the nuclear power plant being:

o

In

an

unanalyzed condition

that

significantly

compromises plant safety;

25

o

In a condition that is outside the design basis of the

plant; or

o

In a condition not covered by the plant's operating

and emergency procedures.

The failure to follow reporting requirements of 10 CFR 50.72 is

identified as violation 261/88-01-01..

g. Technical Specification Interpretation

TS 3.3.2.2.b requires that "If

one containment spray pump becomes

inoperable during normal reactor operations, the reactor may remain

in operation for a period not to exceed 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> provided the four

fan cooler *units are operable and the remaining containment spray

pump is demonstrated to. be operable prior to initiating repairs."

The normal operating practice at HBR is not to retest the remaining

containment spray pump if it has been demonstrated operable prior.to

entering the TS action statement. This practice appears to conflict

with the literal interpretation of the TS action statement. -The

inspector did not view this as a significant safety-related problem

although this does not appear to comply with the current wording of

the TS. This issue is being referred to NRR requesting an inter

pretation of the TS.

26

9.

Commercial Grade Procurement

The licensee's nuclear procurement program was inspected with the major

focus

on

the procurement of commercial

"off-the-shelf"

items.

The

inspection was accomplished by reviewing procurement records, engineering

evaluations, and interviewing plant personnel.

a. Program Controls

The nuclear procurement program requires engineering and quality

assurance reviews for all purchase orders prior to the order being

placed. The planning staff initiates the material requisition.

The

technical support group and qualit'y assurance group then review the

material requisition to determine' the need for any technical and

quality requirements. The reordering of spare and replacement items

is generated through a computerized material management system.

b.

Implementation and Program Review

The nuclear procurement program as it relates to commercial "off-the

shelf" items has administrative controls which

are

implemented

-through the corporate material management system.

This system is

programmed to require engineering and QA approvals if any .changes are

entered. Commensurate approvals are required for the purchase of any

new item.

c.

Review of Commercial Grade Procurement

The inspector performed detailed reviews of various engineering

documents related to upgrades, re'lacements-in-kinds, and classifica

tion changes. The EEs that were written as justification for these

actions were detailed, in-depth, and adequately addressed all

concerns.

The inspector reviewed commercial1

"off-the-shelf" procurements for

selected electrical and mechanical

spare

and replacement parts.

Purchase requests for replaceme nt .items are reviewed by the

engineering technical

support group to verify that the original

specification identified the item as commercial

grade.

For items

where additional controls were or ginally required, similar controls

are again delineated.

The eng neering evaluation sufficiently

identified originally procured commercial grade items for the

procurements. reviewed.

However,

since items were originally purchased as commercial grade,

there is no way of assuring tha

later items purchased by the same

procurement

process

meet

the

original

item's

critical

characteristics.

Critical characteristics are the

identifiable

and/or measurable attributes of commercial grade items.

Commercial

27

grade vendors are not audited by the licensee; therefore,

some

special verification requirements need to be established for the

procurement of commercial grade items.

Several

mechanisms are

available to verify critical characteristics; however,

they are not

being performed.

The licensee's interpretation is that a receipt

inspection verifies an item's critical characteristics.

A receipt

inspection; however, only verifies the item's unique identification,

cleanliness, physical state, and workmanship.

FSAR Section 17.2.7 requires that for the purchase of commercial

"off-the-shelf" items where spedific quality assurance controls

appropriate for nuclear applications cannot be practically imposed,

special quality verification requirements shall be established and

described, if required, to provide the necessary assurance to CP&L of

the acceptability of the item.

CP&L Corporate Quality Assurance! Program,

Revision 10,

Part 5

Material and Equipment Control,

Section 5.5, "Off-the-Shelf Items",

requires that an engineering evaluation be performed prior to an

"off-the-shelf" item being used

n a safety-rel.ated application to

establish the suitability of the item for its intended use.

The use of commercial "off-the-shelf" items in safety-related

applications without special quality verification requirements to

0provide

assurance of the item'I acceptability is considered an

example of unresolved item 261/88-01-05 and will be forwarded to NRR

for resolution.

The inspector reviewed approximately two years of engineering

evaluations and identified that one (87171)

justified the use of

Scotch 70 tape, which was purchased as non-Q, for EQ applications.

This was justified based on an upgrade of the tape to commercial

grade.

The evaluation documented that only a visual inspection of

the tape was performed. The basis of the upgrade was a seven year

old EQ test report for Scotch 70 tape.

The use of commercial grade

items in EQ applications is acceptable only if a definite correlation

can be made between the item plurchased and the item originally

tested. This is considered to be a- further example of unresolved

item 261/88-01-05 and will be forwarded to NRR for resolution.

10.

Quality Assurance/Quality Control

Reviews of the _HBR

QA organization

effectiveness consisted of an

evaluating both the site's QA/QC organization and the co.rporate

PEU.

Assessment of each unit's activities was conducted by interviews with each

Unit Supervisor.

The inspector also conducted a detailed review of

audit/surveillance schedules,

schedulling compliance, audit/surveillance

findings, nonconformance reports, adequacy and timeliness of corrective

actions,

and the project's trend analysis programs.

The evaluation

28

concluded that the HBR

QA program

was adequately accomplishing

its

assigned function of identifying, correcting and preventing problem

recurrence. This conclusion is based on observations, discussions with

responsible management personnel and documentation reviews.

The audit/surveillance unit size and experience level is adequate.

The

inspector examined the experience, training, and qualification records for

the HBR Director of QA/QC and 22 site CP&L QA/QC personnel and determined

they were qualified in their respective areas of engineering,

surveillance, or inspection responsibilities.

Examination of the above

records and discussions with several site QA/QC personnel confirmed that

this organization has a good blend of experience (multidisciplined

backgrounds), large number of years in the nuclear (15.6 years average)/QA

(10.5

years average)

industry,

has

been rather stable with minimal

turnover of personnel,

and maintained its independence while keeping

excellent rapport with plant craft and management personnel.

These

characteristics were identified as a noteworthy strength of the QA/QC

organization.

The NRC inspector accompanied a QA/QC technician during the performance of

the surveillance of MST-021,

"Reactor Protection Train 'B' At Power",

Revision 1. Discussions with this individual concerning the subject test

procedure and systems 'involved indicated that he was well qualified to

monitor

the test and was

knowledgeable of good audit/surveillance

principles.

NCR 88-033 was generated by the I&C group to identify a

control room status light (LC-475B1)

which did not light as required

during step 31 of MST-021.

The NRC inspector witnessed the trouble

shooting of the problem authorized by WR 88-ABB11.

The relay contacts

that feed the status light were spray cleaned and subsequently tested

satisfactory.

The

in-process

QA/QC

surveillance test checklist and

MST-021 documentation recorded by I&C and control room personnel were

examined and found satisfactory.

The qualifications of six PEU audit

personnel were recently reviewed and the results were documented in NRC

Inspection Report No. 50-400/87-38 by this inspector-and determined to be

appropriate.

A formalized audit/surveillance system was in place and adherence to

schedules was

adequate.

Operations QA/QC Section Procedure 0QA-201,

"Surveillance Program", Revision 1, and Corporate QA Departmental

Procedure CQAD 80-1,

"Procedure for Corporate QA Audits", Revision 13,

require formalized systems.

The

inspector examined the HBR audit/

surveillance planning and scheduling matrices for 1986 -

1987,

the

approved first quarter

1988

schedules,

and the tentative audit/

surveillance schedule for the remainder of year 1988.

The inspector

determined that the subject audit/surveillance schedules

contained

satisfactory coverage of quality related activities and commitments

contained in the FSAR and Technical Specifications.

Adherence to these

schedules was adequate.

29

Audits/surveillances conducted appeared to be satisfactory in depth and

scope and identify some relatively significant problems for management

corrective action.

The inspector reviewed the following audits/

surveillances and their respective checklists that were performed at HBR

during 1986 -

1987:

Audit/Surveillance No.

Activity Examined

QAA/0020-86-01

HBR Operations

QAA/0020-87-01

HBR Operations

QAA/0020-87-06

Modification Process - All

Aspects

QAA/0020-87-07

HBR Activities

QAA/0104-86-01

HBR Design Engineering

Section

QAA/0127-86-01

HBR QA/QC Unit

QAA/0127-86-02

HBR QA/QC Unit

QAA/0127-87-01

Operations QA Unit

QASR/86-012

QC Activities

QASR/86-015

Procurement Control

QASR/86-057

Locked Valve List

QASR/86-081

Material and Equipment Control,

Storage and Shipping

JQASR/86-097

Personnel Training and Records

QASR/86-114

Safety Reviewer Qualifications

QASR/86-136

Control of Special Processes

QASR/86-137

Spare Parts Evaluation

QASR/87-003

Construction Activities

QASR/87-036

Outage Activities 4/5 - 4/11/87

QASR/87-056

Maintenance Work Request Program

QASR/87-063

Control of Measuring and Test

Equipment

QASR/87-099

Procurement Control

QASR/87-106

QA/QC Activities

In general, the inspector noted that the audit/surveillance reports and

related checklist items examined were verified to the depth and scope

necessary to ascertain the activities' compliance or noncompliance with

the accepted QA program. However,

comments and responses to some audit/

surveillance checklist items were very brief to the point that reconstruc

tion of the audit data would be difficult. The specifics as to what was

examined,

how examined,

sample size considered, accept/reject criteria

used, and the acceptability of the audited item were often not documented..

Also, occasionally, the response given for an audit/surveillance checklist

item either did not verify the acceptability of that item or was not

relevant to the checklist item being examined.

A few examples that

illustrate the above identified audit/surveillance weaknesses are:

30

QAA/0104-86-01

Checklist Items 2.2.24 thru 2.2.28

QAA/0127-86-01

Checklist Items 4.3, 5.1.2.5 thru

5.1.2.8

QAA/0127-86-02- Checklist Items 6.4, 6.8

QASR/86-015

Checklist Items -

Most

QASR/86-114

Checklist Items -

Most

QASR/86-136

Checklist Items -

Most

QASR/86-137

Checklist Items -

Most

QASR/87-003

Checklist Items -

Most

The inspector observed that audit/surveillance reports and related

checklist content appeared to have continually improved since January

1987. Discussions with the Project QA/QC Surveillance Specialist and the

HBR Lead PEU

QA Specialist identified that increased emphasis had been

placed in this area.

The inspector noted that checklist line items,

cancelled or not inspected on an audit/surveillance, were being conscien

tiously

examined

on

subsequent

audits/surveillances

as

stated.

Discussions conducted with the

PEU

Supervisor (Region

II

Inspection

50-400/87-38) and with the HBR QA Supervisor identified CP&L's new audit/

surveillance philosophy is changing to a more performance based concept.

A good example of this transformation at HBR is performance based audit

QAA/0020-87-06,

which examined three safety significant modification

packages-from their conception in design through installation, inspection,

turnover and filing of the record packages.

This comprehensive audit

resulted in 11 adverse findings being identified.

The fact that HBR

audits/surveillances are

becoming

more

performance

based

versus

documentation oriented was identified as another strength of the QA

organization.

A potential violation in the audit area relating to the protection of

safeguards information was identified to appropriate licensee personnel

and will be examined further by Region II Security Inspectors during their

next routine inspection.

Discrepancies identified by either site QA/QC,

Corporate audits or plant

personnel receive timely, appropriate corrective action.

The inspector

reviewed the following NCRs and ADRs for the above attributes:

ADR/NCR No.

Title

ADR/0020-87-06-F2

No Structural/Seismic Safety

Review

Conducted for Modification 908

ADR/0020-87-06-F4*

No Documented Evidence in

Modification

Package 908 of an ALARA Review

ADR/0104-86-01-C1

Training Program and Schedule Had

Not Been.Formally Established

ADR/0127-87-01-C1

"Comment Due Date" Change Did Not

Require Approval

31

NCR/86-110

RPC Craft Personnel Not Required to

Read Procedures

NCR/86-154

Quarterly Calibration Checks Not Performed

as Required

NCR/86-155

Welding and Brazing Material Control Record

Filled Out Improperly .

NCR/86-178

QA Records Not Filed in Fireproof Cabinet

NCR/87-012

Personnel Certified to Operate Forklift

Before Demonstrating Their Ability

NCR/87-013

Gripper Not Listed on Material Control Tool

List as Required

ADR/NCR No.

Title

(cont'd)

NCR/87-056

OP-305, Step 6.14.4.3 Revised Without

Temporary Change

NCR/87-069

Inspections Not Performed as Required

NCR/87-118

Indeterminate QC Witness of EQ Splice Kits

NCR/87-128

OST-10 Not Performed Within Grace Period

NCR/87-138

Engineering Evaluation Not Performed on

Torque Wrench Found Out of Tolerance.

NCR/87-155

Valve V2-26 Failed to Operate During OST-206

NCR/87-184

Reports.Not Completed for Inspections

Performed

NCR/87-185

EE 86-145 Was Not Performed Prior to

Performance of Work

NCR/87-191

QA/QC Does Not Review Work Request for

Maintenance Performed on EQE

NCR/87-222

EE 87-103 Did Not Address FSAR

Section 3.5.1.2 Requirement

Examination of the above ADR/NCR discrepancies identified that they were

properly handled. Satisfactory corrective actions were specified and the

close out of the subject discrepancies was accomplished by reinspection/

verification

of details

as

necessary.

The

PEU

has performed

satisfactorily in follow up and closing out ADRs.. A total of 14 ADRs were

identified in 1986 and 22 during 1987.

Currently, there are eight ADRs

(all issued in 1987)

open;

seven of which are pending completion of

corrective actions and are progressing satisfactorily.

The eighth ADR

(20-87-06-F5)

has been granted an extension to March

15,

1988,

for

submittal of a new response.

There were 174 NCRs issued in 1986 and 264

in 1987.

As of December 31,

1987, there were 31 "Q" and 9 "Non-Q"

type,

or a total of 40 NCRs outstanding.

The majority of these 40 open NCRs

were issued during November -

December 1987 and corrective actions are

still ongoing. Only 5 of the 40 outstanding NCRs are older than 6 months.

The oldest NCR (86-110, issued August 11, 1986) remains open deliberately

by .QA/QC to verify that the training of RPC crafts on new procedures was

being implemented properly.

NCR 87-037,

issued March

16,

1987,

has

32

generic implications affecting other plants and resolution required

extensions and escalation which has resulted in approved corrective

actions to be implemented by April 1, 1988.

Review of the remaining 3

NCRs (87-003,87-030, 87-123) determined that these items were in the

process for resolution and their long term resolution was not due to

inattention by management.

Based on the above current statistics and

discussions with responsible PEU/QA/QC personnel, the inspector concluded

that the ADR/NCR corrective action systems have been responsive and well

controlled. A strength was identified in that HBR management has placed

increased emphasis on plant personnel's use of the NCR system to identify

and correct deficiencies. This has resulted in a substantial increase in

the number of NCRs being identified during the latter half of 1987 which

were subsequently corrected.

Mechanisms were in place to recognize and prevent recurring or repetitive

discrepant conditions and upper management was made aware of these trends.

The Senior Executive Vice-President reviews and signs each corporate audit

report issued. The QA Department used several excellent nonconforming

trending/status programs that help identify adverse trends and recurring

discrepant conditions.

The inspector examined the following

HBR

and

Corporate QA discrepancy trend/status reports that are routinely presented

to CP&L's upper level management and found them satisfactory for their

intended purpose:

Corporate Quarterly Nonconformance Trend Reports (4th Quarter 1985

through 3rd Quarter 1987)

HBR QA/QC.Monthly Reports (November and December 1987)

HBR QA/QC Quarterly Surveillance Program Status Reports (1st Quarter

1986 through 3rd Quarter 1987)

11.

List of Abbreviations

ADR

Audit Deficiency Report

AEOD

Office of the Analysis and Evaluation of Operational Data

AFW

Auxiliary Feedwater System

A/E

Architect/Engineer

CP&L

Carolina Power and Light Company

DBD

Design Basis Document

DCN

Design Change Notice

EE

Engineering Evaluation

EQ

Environmental Qualification

EQE

Environmentally Qualified Equipment

FSAR

Final Safety Analysis Report

HBR

H.B. Robinson Nuclear Plant

I&C

Instrumentation and Controls

ISI

Inservice Inspection

JCO

Justification for Continued Operation

33

LER

Licensee Event Report

LOCA

Loss of Coolant Accident

MIC

Microbiologically Induced-Corrosion

MST

Maintenance Surveillance Test Procedure

NCR

Nonconformance Report

NED

Nuclear Engineering Department

NRC

Nuclear Regulatory Commission

OST

Operations Surveillance Test Procedure

POM

Predictive Maintenance

PEU

Performance Evaluation Unit

PIR

Plant Improvement Report

PM

Preventive Maintenance

PNSC -

Plant Nuclear Safety Committee

PORV

Power Operated Relief Valve

PT

Potential Transformer

QA

Quality Assurance

QAA

Quality Assurance Audit

QASR

Quality Assurance Surveillance Report

QC

Quality Control

QER

Quality Evaluation Report

RPC

Robinson Plant Construction

SI

Safety Injection System

SPC

System Program Chart

TRP

Temporary Repair Procedure

.

TS

Technical Specifications

URI

Unresolved Item

WR

Work Request