ML14191A910

From kanterella
Jump to navigation Jump to search
Insp Rept 50-261/88-03 on 880111-0210 & 0307.Violations Noted.Major Areas Inspected:Followup on Previous Insp Items, Operational Safety Verification,Physical Protection, Surveillance Observation & Maint Observation
ML14191A910
Person / Time
Site: Robinson 
Issue date: 03/11/1988
From: Fredrickson P, Garner L, Latta R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14191A909 List:
References
50-261-88-03, 50-261-88-3, NUDOCS 8803280166
Download: ML14191A910 (16)


See also: IR 05000261/1988003

Text

8 REc.

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report No.:

50-261/88-03

Licensee:

Carolina Power and Light Company

P. 0. Box 1551

Raleigh, NC 27602

Docket No.:

50-261

License No.: DPR-23

Facility Name: H. B. Robinson

Inspection Conducted: January 11 -

February 10,

and March 7, 1988

Inspectors:

A I

L. W. G~rner, Senior Resident Inspector,

Date Signed

M. Latta, Resident Inspector,

Date Signed

Contributing

B.

Breslau,.Reactor Engineer

Inspectors:

. J. Kel ogg, Rea tor Engi

er

Approved by: U

/

S /1/

P. E. Fredrickson, Chief

Date Signed

Reactor Projects Section 1A

Division of Reactor Projects

SUMMARY

Scope: This routine,

announced inspection was conducted in the areas of

followup on previous inspection items, operational

safety verification,

physical protection,

surveillance observation, maintenance observation,

ESF

system walkdown, onsite followup of events at operating power reactors, onsite

review committee, and natural circulation cooldown.

Results: One violation was identified involving four examples of failure to

operate the plant within the design basis (paragraph 10.c).

An additional

related violation was identified involving failure to identify and correct

conditions adverse to quality as required by 10 CFR 50 Appendix B, Criterion

XVI ( paragraph 10.c).

0

8803280166 80-314

PDR

A

05000261

DCD

REPORT DETAILS

1. Persons Contacted

Licensee Employees

R'.

Barnett, Maintenance Supervisor,. Electrical

+*G. Beatty, Vice President, Robinson Nuclear Project Department

  1. C. Bethea, Manager, Training
  1. H. Bryon, Instructor

R. Chambers, Engineering Supervisor, Performance

0..Crocker, Supervisor, Radiation Control

+*J. Curley, Director, Regulatory Compliance

J. Eaddy, Supervisor, Environmental and Chemistry

R. Femal, Shift Foreman, Operations

W. Flanagan, Manager, Design Engineering

  1. W. Gainey, Support Supervisor, Operations

P. Harding, Project Specialist, RadiationControl

+*E. Harris, Director, Onsite Nuclear Safety

D. Knight, Shift Foreman, Operations

E. Lee, Shift Foreman, Operations

F. Lowery, Manager, Operations

D. McCaskill, Shift Foreman, Operations

R. Miller, Maintenance Supervisor, Mechanical

R. Moore, Shift Foreman, Operations

+#R. Morgan, Plant General Manager

D. Myers, Shift Foreman, Operations

D. Nelson, Operating Supervisor

M. Page, Engineering Supervisor, Plant Systems

D. Quick, Manager, Maintenance

B. Rieck, Manager, Control and Administration

  1. D. Sayre, Senior Specialist, Regulatory Compliance

D. Seagle, Shift Foreman, Operations

R. Steele, Shift Foreman, Operations

+#H. Young, Director, Quality Assurance/Quality Control (QA/QC)

Other

licensee employees

contacted included

engineers,

technicians,

operators, mechanics, security force members, and office personnel.

Region II Attendees

  • B Breslau
  • P Kellogg

NRC Resident Inspectors

+#*L. Garner

+#R. Latta

  • Attended exit interview on January 27, 1988

BAttended exit interview on Mbrso 7 , 1988

  1. Attended exit interview on eari s,

1988

2

2.

Exit Interview (30702, 30703)

The inspection scope and findings were summarized on January,27, February

11,

and March 7, 1988, with those persons indicated in paragraph 1.

The

inspectors described the areas inspected and discussed in detail the

inspection findings listed below. Dissenting comments were not received

from the licensee.

Proprietary information is not contained in this

report.

No written material was given to the licensee by the Resident

Inspectors during this report period.

Note:

A list of abbreviations used in this report is contained in

paragraph 13.

Item Number

Status

Description /Reference Paragraph

261/84-45-01

Open

IFI -

Service Water Degradation

261/88-03-01

Open

UNR* -

Review OT Delta T Safety

Analysis Results

261/88-03-02

Open

IFI -

Review Finalized Transition

Document and Step Deviation Forms

261/88-03-03

Open

IFI -

Review Step Deviation Forms

For-Plant Specific Soak Time

and Subcooling Margin

261/88-03-04

Open

VIOLATION -

Failure to Comply with

Criterion 35 of 10 CFR 50 Appendix A

261/88-03-05

Open

VIOLATION -

Failure to Comply with

Criterion XVI of 10 CFR 50 Appendix B

  • Unresolved items are matters about which more information is required to

determine whether they are acceptable or may involve violations or

deviations.

3.

Licensee Action on Previous Enforcement Matters (92702)

Not inspected

4.

Licensee*Action on Previously Identified Inspection Items (92701)

a.

(Open) IFI 261/84-45-01

Service Water Degradation

Inspection in this area has previously been reported in Inspection

Reports nos. 261/84-45, 261/84-48, 261/85-12, 261/85-22, 261/86-12,

261/87-03 and 261/87-35. This report documents the December 1987,

3

weld control

group radiographic examination results and the

subsequent actions taken by the licensee in response to the indicated

increased MIC growth rate.

During the week of December seventh, 29 service water pipe welds were

radiographed. Results available on January 5, 1988, indicated that

the average annual growth rate for 6 inch diameter pipe had

increased from 5/8 inch to 1.6 inches circumferentially. None of the

welds had MIC lengths greater than the structural limit.

Based on

the new growth rate, all welds which were projected to exceed 9

inches by the scheduled August, 1988, refueling outage were

radiographed during January 11 -

15,

1988.

Weld 4-SCH-3, associated

with containment fan cooler unit HVH-4,

was found to have exceeded

the structural limit of 10.19 inches.

The fan unit was declared

inoperable, the weld was sleeved and HVH-4 returned to service on

January 20, 1988.

During January 22

-

February 8, 1988, all welds in the auxiliary

building service water system which are considered susceptible to MIC

and which were unsleeved were radiographed.

One additional weld on

HVH-4 was found to have slightly exceeded the structural limit and

was sleeved. Other welds which exceeded the administrative criteria

for sleeving, e.g.

one half the structural limit or which might

exceed the structural limit by the upcoming refueling outage, were

also sleeved. Thus,

of the 272 original welds in the auxiliary

building, 144 welds are now sleeved. Service water pipe welds inside

containment are already sleeved.

The December 1986 radiographic examination indicated that sleeved

welds exhibited growth in the sleeve-to-pipe fillet weld heat

affected zone.

A sampling of such weld joints revealed that growth

is continuing in these joints.

Based

upon this fact and the

increased growth rate, the licensee is considering changes to the MIC

surveillance program. A new program with increased emphasis on both

the unsleeved welds in the auxiliary building and the fillet weld

heat affected zones inside containment

as well

as a revised

examination frequency is under evaluation.

A revised program should

be ready for implementation by early Spring,

1988.

The resident

inspectors and/or Region II inspectors will review the program when

available.

b. NRC Information Notice No. 88-01, Safety Injection Pipe Failure

The inspectors reviewed the subject document to ascertain whether or

not the document is relevant to the plant's SI design.

The three

positive displacement charging pumps are not part of the SI system.

The three SI pumps which would inject through the BIT into the cold

legs have a shutoff head of 1700 psig. This shutoff head is well

below the normal RCS operating pressure of 2235 psig. Hence, leaking

into the RCS via leaking valves with the associated thermal cycling

of piping is not considered a feasible event for this design.

No violations or deviations were identified within the areas inspected.

4

5. Operational Safety Verification (71707)

The inspectors observed licensee activities to confirm that the facility

was being operated safely and in conformance with regulatory requirements,

and that the licensee management control system was effectively dis

charging its responsibilities for continued safe operation. These activi

ties were confirmed,

by direct observations,

tours of the facility,

interviews and discussions with licensee management and personnel,

independent verifications of safety system status and limiting conditions

for operation, and reviews of facility records.

Periodically, the inspectors reviewed shift logs, operations records, data

sheets, instrument traces, and records of equipment malfunctions. Specific

items reviewed include control room logs, maintenance work requests,.

auxiliary logs,

operating orders,

standing orders,

jumper logs,

and

equipment tagout records. The inspectors routinely observed shift changes

to verify that continuity of system status was maintained and that proper

control room staffing existed. The inspectors also observed 'that access

to the control room was controlled and operations personnel were carrying

out their assigned duties in an attentive and professional manner.

The

control room was observed to be free of unnecessary distractions. The

inspectors performed channel checks, reviewed component status and safety

related parameters, including SPDS information, to verify conformance with

the TS.

During this reporting interval, the inspectors verified compliance with

selected limiting conditions for operation.

This verification was

accomplished by direct observation of monitoring instrumentation, valve

positions, switch positions, and review of completed logs and records.

The inspectors verified the axial flux difference was within the values

required by the TS.

Plant tours were routinely conducted to assess the operability of standby

equipment and general plant/equipment conditions, such as the existence of

unusual fluid leaks, excessive pipe vibrations, pipe hanger and seismic

restraint abnormalities,

various valve and circuit breaker positions,

equipment clearance tags,

component status verifications, instrument

calibrations, operability of fire fighting equipment including fire

alarms, suppression equipment, and emergency lighting equipment.

The inspectors determined the following:

plant personnel

including

operation staff members were knowledgeable of plant conditions including

equipment out of service and maintenance activities, that appropriate

radiation controls were properly established and implemented,

and that

fire hazards and combustible materials were properly controlled. The

.

inspectors also selectively examined radiation protection instrumentation

such as area monitors, friskers, and portal monitors to verify operability

and adherence to calibration frequency requirements.

Plant housekeeping

and contamination control were observed to be adequate.

5

On

February 2,

1988 the inspectors toured containment.

In general,

conditions of equipment were adequate.

Some deficiencies which did not

effect operability were observed and reported to the

licensee for

appropriate action.

No violations or deviations were identified within the areas inspected.

6. Physical Protection (71707)

In the course of the monthly activities, the inspectors included a review

of the licensee's physical security program.

The inspectors verified by

general observation,

perimeter walkdowns and interviews that measures

taken to assure the physical protection of the facility met current

requirements. The inspectors visited the central and secondary alarm

stations at various times during the reporting period to ensure that they

were properly staffed and operational.

The performance of various shifts of the security force was observed to

verify that daily activities were conducted in accordance with the

requirements of the

security plan.

Activities inspected included

protected and vital areas,

access controls,

searching of personnel,

packages and vehicles, badge

issuance and retrieval,

escorting of

visitors, patrols, and compensatory measures. In addition, the inspectors

routinely observed protected and vital area lighting and barrier

integrity.

During this inspection period a Regional QA effectiveness inspection team

identified that two security audits, QAA/0020-86-01 and QAA/0020-87-01,

contained audit checklist items which potentially specified safeguards

information.

The concern was identified to the appropriate regional

personnel.

Followup action by Region II security specialists is currently

planned.

No violations or deviations were identified within the areas inspected.

7. Monthly Surveillance Observation (61726)

The inspectors observed certain surveillance related activities of

safety-related systems and components to ascertain that these activities

were conducted in accordance with license requirements.

The inspectors

determined that the surveillance test procedures listed below conformed to

TS requirements, that all precautions and LCO's were met,

and that the

surveillance test was completed at the required frequency. The inspectors

also verified that the required administrative approvals and tagouts were

obtained prior to initiating the test, that the testing was accomplished

by qualified personnel in accordance with an approved test procedure and

that the required test instrumentation was properly calibrated.

Upon

completion of the testing, the inspector observed that the recorded test

data was accurate, complete and met TS requirements; ensured that test

discrepancies were properly rectified; and independently verified that the

6

systems were properly returned to service.

Specifically, the inspectors

witnessed/reviewed portions of the following test activities:

a. OST-611 (revision 6) Low Voltage Fire Detection and Actuation System

Zones 1,2,3,4,5,6 and 7

The purpose of this semi-annual test is to provide an operational

verification of the detection capability of the pyrotronics fire

detection system as required by TS Section 4.14.1.1.b.

During the

conduct of this test several discrepancies were identified including

the failure of detector 1B2 to operate. The inspectors determined

that appropriate compensatory

measures were taken including the

posting of a fire watch within one hour and that corrective actions

were initiated to repair the subject deficiencies.

The inspectors

will continue to monitor this activity during subsequent inspections.

b. OST-905 (revision 9) Radiation Monitoring System

This test is conducted daily in order to verify the operability and

response of the radiation monitoring system as stipulated in TS Sections 4.1.1, 4.19.1,

and 4.19.2.

Specifically, the inspectors

determined that all operable radiation monitors had power available,

that the required

monitors

and their associated pumps

were

functioning, and that the source check values were properly recorded.

No deficiencies were identified during the conduct of this test.

c. OST-007 (revision 4) Nuclear Instrumentation Comparator Channel

The inspector- witnessed the operational verification of the alarm

setpoints of the power range channels. In particular, the inspectors

determined that subject channels and their associated comparitor

bistables were within the required setpoint tolerance of two plus or

minus 0.5 of their full scale value by comparing the deviation

between the power range channel being tested and lowest power range

channel not being tested. The inspectors confirmed that the required

control room annunicators responded correctly to the test conditions

and that over power differential temperature and over temperature

differential temperature reactor trip bistables were reset to the

normal mode.

No deficiencies were identified during the conduct of

this test.

d. OST-001

(revision

18)

Nuclear Instrumentation Source Range,

Intermediate Range, Power Range Weekly.

This test performs surveillances required by TS Table 4.1-1, items 1

through 3.

On January 20,

1988,

OST-001 was being performed in

preparation for startup. The inspectors observed that the operator

had recorded a value for an intermediate range monitor which exceeded

the acceptance criteria without noting the exception.

The operator

stated that they are not required by procedure to flag any out of

tolerance value and the acceptance criteria would be reviewed by the

7

shift foreman prior to final signoff.

The inspectors observed that

the operator continued with the procedure and did not report the out

of tolerance value to the shift foreman until shift turnover,

approximately an hour after the condition was found.

Technical

Specification

requirements

were

not

exceeded

because

the

instrumentation was not required to operable in that mode.

No violations or deviations were identified within the areas inspected.

8. Monthly Maintenance Observation and.Maintenance Program Evaluation

(62703, 62704, 62705)

The

inspectors observed several maintenance related activities of

safety-related systems and components to ascertain that these activities

were conducted in accordance with approved procedures, TS and appropriate

industry codes and

standards.

The inspectors determined that these

activities were not violating LCO's and that redundant components were

operable. The inspectors also determined that the procedures used were

adequate to control the activity, that QC hold points were established

where required, that required administrative approvals and tagouts were

obtained prior to work initiation, that proper radiological controls were

adhered to, that appropriate ignition and fire prevention controls were

implemented,

and that replacement parts and materials used were properly

certified.

The

inspectors confirmed that these

activities were

accomplished by qualified personnel using approved procedures, and that

the effected equipment was properly tested before being returned to

service.

In particular the inspectors observed/reviewed the following

maintenance activities:

a. MST-552 (revision 3) Turbine Redundant Overspeed Trip System Testing

This test is conducted monthly in accordance with TS requirements in

Table 4.1-1. The inspectors observed that the following surveillance

test acceptance criteria were satisfied:

Voltages were within the specified tolerance

Overspeed test potentiometer setting

remained within the

specified allowable ranges

Proper indications were observed on the test and

failure lamps

Required operation of the overspeed trip system logic occurred

as verified by

the correct operation of all

test light

indications.

b.

MST-014 (revision

14)

Steam Generator Pressure Protection Channel

Testing

This test. confirms operability of the steam generator pressure

protection channels II, III, and IV.

The successful completion of

8

this surveillance test satisfies the requirements of TS table 4.1-1,

item 24.

For those portions of the surveillance test observed, the

inspectors confirmed that the annunciators gave the proper status,

that the associated alarms responded

as required,

and that the

specified test voltages were within the

required tolerance.

Subsequent to this maintenance activity, the inspectors determined

that the required processing points for the ERFIS computer were

correctly returned to service.

c. MST-021 (revision 1) Reactor Protection Logic Train "B" at Power

The inspectors observed the adequacy of communications between the

reactor protection logic panel and the control room as well as the

conduct of the individuals involved in the surveillance test.

The

inspectors determined that the logic network de-energized the under

voltage coil for the B reactor trip breaker for

each logic

combination specified in the test procedure and that the appropriate

annunciator lights and alarms were received on the reactor turbine

generator board.

The inspectors also reviewed several outstanding work requests and the

licensee's automated maintenance management tracking system to determine

that the licensee was giving priority to safety-related maintenance and

that a backlog which might affect performance was not developing.

No violations or deviations were identified within the areas inspected.

9.

ESF System Walkdown and Monthly Surveillance Observation (71710,61726)

The inspectors verified the operability of an engineered safety features

system by performing a walkdown of the accessible portions of the SI

system.

The inspectors confirmed that the system lineup procedures

matched plant drawings and the as-built configuration.

The inspectors

verified the absence of equipment conditions and items that might degrade

performance such as loose pipe supports, the presence of debris or loose

materials,

and unauthorized jumpers

or evidence of rodents inside

electrical and instrumentation cabinets. Valves were verified to be in

the proper position with power available and locked as appropriate. Local

and remote indications were verified to be consistent.

The inspection also included observation of the successful completion of

OST-151, Safety Injection System Component Test, revision 22, for SI pumps

B and C. The inspectors verified that the differential pressure and pump

bearing vibration amplitude met acceptance criteria, that all components

associated with the subject SI pumps appeared to functioning as designed,

and the system was properly returned to service.

No violations or deviations were identified within the areas inspected.

9

10.

Onsite Followup of Events at Operating Power Reactors (93702, 37701,

92700)

a. Potentially Non-conservative OT Delta T Trip Setpoint

On December 12,

1987, the licensee determined that an error existed

in the safety analysis used to determine the OT Delta T trip setpoint

for the present core load (cycle 12).

The analysis performed by

Advanced Nuclear Fuels improperly utilized information contained in

FSAR Table 15.0.7-1. Advanced-Nuclear.Fuels had incorrectly assumed

that the table's OT Delta T nominal time delay of 2.3 seconds was the

total time for transport of fluid from the manifold scoops to the

RTD's,

response of the RTD's and signal processing time till

the

reactor trip breakers open. The 2.3 seconds represent only a portion

of this total time. The total value should be approximately 4.5

seconds.

The licensee is in the process of determining the exact

value.

Completion is expected by early March.

In the interim, the

licensee, after consulting with Westinghouse and Advanced Nuclear

Fuels, determined the maximum upper limit on the desired delay time

is 6 seconds.

Using 6 seconds, a new value for K1,

a constant used

in the OT Delta T trip setpoint equation,

was calculated. . The

revised K1 constant was implemented on December 12,

1987,

by plant

modification M-950.

Use of too small of a time delay would result in the analysis

indicating that an event terminated by the OT Delta T trip would end

earlier and potentially with less consequences than it

might in

actuality. The incorrect time delay was used in accident analysis

for the following events; 1) loss of external load, 2) uncontrolled

rod withdrawal and 3) rod drop with turbine runback. The licensee is

in the process of determining if

the error resulted in operation

outside the safety analysis described in the FSAR.

This item is considered as an unresolved item: Review OT Delta T

Safety Analysis Results (50-261/88-03-01).

b. Turbine Trip/Reactor Trip

Due

to Failed Component in Turbine

Electro-Hydraulic Control System

On January 19,

1988, Unit 2 experienced a turbine trip/reactor trip

from approximately

66% power as a result of low autostop oil

pressure.

Reactor power

had been reduced to test the turbine

overspeed trip feature of the turbine electro-hydraulic control

system in accordance with a monthly operations surveillance test

OST-551. All safety systems operated as designed including auxiliary

feed water which was

secured following normalization of steam

generator levels. As determined in the post trip review the combined

effects of a leaking relief valve (LO-57) and the lifting of a second

relief valve (LO-58)

during the pressure transient that accompanies

reseting of the turbine trip caused low autostop oil pressure to the

interface valve. This allowed the interface valve to open (venting

the governor hydraulic fluid) which by design caused all of the

turbine steam control, stop, intercept, and reheat valves to close.

10

Following this event both of the original autostop oil pressure

relief valves,

LO-57 and LO-58,

were replaced and OST-551

was

performed to provide post maintenance verification of the repair.

The inspectors witnessed the performance of this surveillance test

and determined that the overspeed trip valve operated properly and

the autostop oil pressure was within the expected range.

Subsequent to this testing the inspectors witnessed the unit startup

from hot shutdown at no-load T-avg to critical,

as controlled by

general procedure GP-003 (revision 15), Normal Plant Startup From Hot

Shutdown to Critical.

The inspectors determined that all required

procedural prerequsites had been performed and that the expected

critical boron concentration was within the allowable difference

between the estimated critical position and the actual critical

position. The unit was synchronized to the grid on January 19, 1988.

C. Single Failure Design Deficiency

On January 28,

1988, during development of a response to an NRC to

licensee letter, subject, Request for Additional Information Safety

Injection Pump B Auto Transfer Scheme,

dated January

14,

1988,

engineering personnel determined that a single failure of either

battery could result in only one SI pump being available to mitigate

a design basis event (see

scenario 1 below).

A PNSC

review

determined at 5:00 p.m.

that an unanalyzed condition existed.

A

plant shutdown at 10% per hour was initiated at this time such that

the plant could be in hot shutdown in 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> as required by TS

action statement 3.0. One hour notification was made pursuant to 10

CFR 50.72.b.1.ii.A at 5:49 p.m.

Review of the normal

breaker

configuration for powering the B SI

pump from either of the two

emergency buses revealed that realignment of the normal

breaker

configuration would prevent the problem.

A procedure change was

made, the breakers were realigned, and the shutdown was terminated at

40% of full power at 11:43 p.m. Full power operation was resumed at

5:35 a.m. on January 29.

As a result of a subsequent review by the NRC on January 29, the

licensee was verbally requested by the Senior Resident Inspector at

approximately 11:00 a.m.

to provide information concerning plant

response to certain other types of faults in the-electrical system

which could also have a potential for resulting in automatically

starting only one SI pump.

One of the questions dealt with what

effect a loss of the A battery bus would have on EDG A after having

successfully loaded, i.e. SI pumps A and B, sequenced onto it. While

preparing an answer to this and other questions, another single

failure was identified which, with the normal plant configuration,

would also result in only one SI pump being automatically available

(see

scenario 4 below).

At that time plant management decided that

another procedure fix, though available, was unacceptable and elected

to shut the unit down until a comprehensive single failure review

could be performed and appropriate corrective actions taken.

TS

11.

Action Statement 3.0 was re-entered at 1:25 p.m.

and the unit was

placed in hot shutdown at 8:46 p.m.

The NRC was notified at 2:10

p.m.

in accordance with 10 CFR 50.72.b.l.ii.A.

At the end of the

report period the unit was in cold shutdown.

By the end of the report period four scenarios had been identified

which required plant procedure or equipment changes.

Two additional

items were also being evaluated, which included tie bus breaker

coordination and the effect of a diesel generator voltage regulator

failure. Resolution of the latter items will be discussed in a

subsequent inspection report.

A brief description of the four

confirmed scenarios follows:

1. Breaker Misalignment El-E2 Bus Cross Tie

The loss of the A battery bus would result in El not being

powered (EDG A would not start). Also no control power would be

available to open the normally closed El to El-E2 breaker.

Thus,

the El to El-E2 breaker interlock to the E2 to E1-E2

breaker would

prevent

E2

from

powering

the

El-E2 bus.

Therefore, both SI pumps A and B would be inoperable.

The loss

of the B battery bus would result in E2 not being powered (EDG

B would not start) and control power would not be available to

close the normally open B SI pump breaker.

Consequently, SI

pumps B and C would be inoperable.

2. Train A Safeguards Sequence Interlock with Train B Safeguards

Sequencer

Normally, the B SI pump which is powered from the El-E2 bus is

preferrentially selected to El by a relay in the A train which

prohibits the B train from closing the E2 to E1-E2 breaker if A

train has been actuated. This interlock relay is in parallel

with the sequencing relay which initiates closure of the A SI

pump and El to El-E2 bus breakers.

Thus a failure of the

sequencing relay would result in A SI pump not starting and the

absence of power to El-E2 from El.

At the same time, the

interlock relay would actuate, thereby, locking out the B train

from powering El-E2 from the other bus,

E2.

Similarly two SI

pumps, A and B, would not auto start.

4.

Loss of EDG Field Flash Circuitry During LOOP with SI Conditions

After successful completion of sequencing of loads onto El due

to an SI coincident with a LOOP,

the equipment has aligned

itself in the same configuration as described in scenario 1

except that it

is being powered by the EDG's.

The loss of

battery bus A would then result in loss of excitation to EDG A.

The loss of EDG A would cause a similar situation as described

in scenario 1.

12

5.

Loss of DC Control Power to El or E2 Emergency Buses

DC control power to the El and

E2 bus breaker are separate

circuits from the respective train A and B safeguard circuits.

The loss of DC control power during the sequencing onto El or E2

would result in the safeguard train interlocks responding as

though the loads had properly

sequenced onto El

and

E2.

However,

since DC control power must be available to close

breakers, the loads would not have sequenced onto the effected

bus.

The result is similar to the sequencer relay failure

discussed in scenario 2. Since loss of DC control power is a

detectable

occurrence, this

scenario

is feasible

only

immediately preceding an SI or within the first 20 seconds after

an SI.

After 20 seconds,

two SI pumps would already have

sequenced onto the emergency bus and loss of breaker control

power would not result in breakers tripping.

The above scenario numbers and titles are from a licensee to NRC

letter dated February 12,

1988,

subject,

Commitments to Resolve

Concerns Regarding Safety Injection System Operability.

Scenario 3

described in the February 12,

1988,

letter was determined not to

exist because of the way in which wiring was terminated to power

sources.

The time the plant has operated in the configuration

described by scenario 1 has not been determined in that scenario 1.

did not involve hardware changes. However,

scenarios 2, 4, and 5

have existed since initial licensing of the plant.

At

the end of the report period,

Modification-947,

SI

Pump

Availability Upgrade, had been,installed and tested per Special

Procedure-796, Verification of SI Pump Availablility and Safeguards

Sequencer Functions, to correct the design deficiencies identified by

the above scenarios.

Two regional

inspectors assisted by the

resident

inspectors

witnessed

the

performance

of

Special

Procedure-796.

The

review of the technical

adequacy of this

procedure

and

corresponding

observations

made

during

its

implementation are documented in Inspection Report No. 50-261/88-05.

Manual initiation of a second SI pump,

e.g.

SI pump B, for the

postulated four scenarios is available in the El-E2 bus room, located

immediately below the control room. The Westinghouse style DB-50 and

DB-75 breakers,

the SI

pump B breaker and the El-E2 bus supply

breakers respectively, can be tripped by actuating a mechanical trip

button located on the breaker and can be closed by inserting a bar

into a slot on the front of the breaker and pushing the contacts into

the latched position. Thus, for the four scenarios, the ability of

the operating crew to potentially mitigate the accident was never

lost. However, because of the uncertainty associated with whether or

not operator actions would or could be timely, existing safety

analysis does not take credit for operator actions.

13

As described above,

the four scenarios (Nos.

1, 2, 4 and 5)

constitute conditions in which a single failure would result in only

one SI pump automatically starting to mitigate the consequences of an

accident. Operations with only one SI pump is outside the design

basis of the plant and thus the SI system would not.meet the ECCS

criteria of 10 CFR 50.46.

FSAR Table 6.3.2-8, Single Failure

Analysis -

Safety Injection

System,

states that the

safety

evaluations are based

on operation of two SI pumps.

The four

scenarios constitute four examples of a violation: Failure to Operate

Plant Within the Design Basis (50-261/88-03-04).

Furthermore,

the failure to identify the additional three single

failure scenarios (Nos.

2, 4 and 5) after entering

TS Action

Statement 3.0 on January 28,

1988 is a violation of 10 CFR 50,

Appendix B, Criterion XVI.

Failure to Promptly Identify Conditions

Adverse to Quality (50-261/88-03-05).

Two violations were found within the areas inspected.

11.

Onsite Review Committee (40700)

The inspectors evaluated certain activities of the plant nuclear safety

committee to determine whether the onsite review functions were conducted

in accordance with TS and other regulatory requirements.

In particular,

the inspectors attended the special PNSC meeting held on January 19, 1988,

concerning the turbine trip/reactor trip which occurred while plant

personnel were performing OST-551. It was ascertained that provisions of

the TS dealing with membership, review process, frequency, qualifications,

etc., were satisfied, and that the previous meeting minutes were reviewed

to confirm that decisions and recommendations were accurately reflected in

the minutes.

The inspectors also followed up on selected previously

identified

PNSC

activities to independently confirm that corrective

actions were progressing satisfactorily.

No violations or deviations were identified within the areas inspected.

12.

Natural Circulation Cooldown (25586)

During this inspection period, the licensee's actions to implement Generic

Letter 81-21,

Natural Circulation Cooldown were reviewed.

This review

included the following documents:

TI-200 Rev 22 Plant Operator Requalification Program

TI-201 Rev 18 Plant Operator Replacement Training Program

TI-203 Rev 11 Senior Reactor Operator Replacement Training Program

TI-301 Rev 19 Training Documentation

TI-303 Rev 14 Dissemination of Information

TI-902 Rev 5 Instructor Requalification Program

TI-906 Rev 11 Training Records

14

EOP Lesson Plan for EPP-5

EOP Lesson Plan for EPP-6

EPP-5 Rev 1 Natural Circulation Cooldown

EPP-6 Rev 1 Natural Circulation Cooldown with Steam Void in Vessel

WOG ES-0.2 LP-Rev 1 Natural Circulation Cooldown

WOG ES-0.4 LP-Rev 1 Natural Circulation Cooldown with Steam Void in

Vessel

WOG Background Information for ES-0.2 LP-Rev 1

WOG Background Information for ES-0.4 LP-Rev 1

WOG Emergence Response Guidelines-Executive Volume Rev 1

RO Training Records

SRO Training Records

The inspectors determined from their review of the training records, that

the training includes both classroom and simulator training on natural

circulation cooldown.

The above training is included in RO and SRO

certification

training

and in the operator retraining programs.

Additionally, the procedures were reviewed to ensure they followed the WOG

guidelines with respect to step content, specific plant parameters

had been added, cooldown rates, subcooling temperature limitations, hold

points for reducing head temperatures, and step deviations are documented.

During the review the inspectors noted that the Procedure Generation

Package forwarded by the licensee on July 2,1984, contains in Section

II.E.

Conversion Method Documentation,

a statement that an

ERG/EOP

Transition Document was created to document and track the conversion

process from ERG to EOP.

This document was to contain a list of the

differences between the ERG LP reference plant and HBR,

step deviation

forms and derivations for the instrument values used in HBR EOP's.

The

step deviations forms were to be used to explain any variance between a

HBR step and a WOG step.

At the time of this inspection, the step

deviation documents were not available for review and interviews with

personnel indicated that not all had been generated.

This will be an

inspector followup item: Review the Transition Document and the Step

Deviation Forms (50-261/88-03-02).

It was also noted that a deviation from the WOG was contained in EPP-5

step 22 in that 190 degrees of subcooling is called for vice the 200

degrees in the WOG and the soak time was 11 hours1.273148e-4 days <br />0.00306 hours <br />1.818783e-5 weeks <br />4.1855e-6 months <br /> vice the 9 hours1.041667e-4 days <br />0.0025 hours <br />1.488095e-5 weeks <br />3.4245e-6 months <br /> in the

WOG. Additionally, an earlier SER dated Sept 27,

1983 indicated a soak

time of 20 hours2.314815e-4 days <br />0.00556 hours <br />3.306878e-5 weeks <br />7.61e-6 months <br /> and 200 degrees of subcooling was required. This will be

an inspector followup item: Review the Step Deviation Forms for Plant

Specific Soak Time and Subcooling Margin. (50-261/88-03-03)

EPP-5 and EPP-6 appear to be almost verbatim rewrites of the WOG with very

little plant specific information other than temperatures,

pressures,

levels and operating procedure references.

No specific plant information

was included for several steps in these procedures. Additionally, step 9

of EPP-5 requires pressure less than 1950 psig and step 11 requires

pressure at 1950 psig.

Steps 5 and 6 of EPP-6 contain

similar

inconsistencies. Steps 7, 13, and 17 of EPP-6 do not contain instructions

to place the charging and letdown controls in manual although these

15

instruction are recommended in the WOG. The need for enhancements in this

area was discussed with the Training Manager.

No violations or deviations were identified in this area.

13.

List of Abbreviations

AFW

Auxiliary Feedwater System

AVG

Average

BIT

Boron Injection Tank.

CCW

Component Cooling Water System

CFR

Code of Federal Regulations

DC

Direct Current

ECCS

Emergency Core Cooling System

EDG

Emergency Diesel Generator

EOP

Emergency Operation Procedures

EPP

End Path Procedures

ERFIS

Emergency Response Facility Information System

ERG

Emergency Response Guidelines

FSAR

Final Safety Analysis Report

GL

Generic Letter

HBR

H. B. Robinson

HP

Health Physics

IE

Inspection and Enforcement

,IFI

Inspector Followup Items

LCO.

Limiting Conditions for Operations

LOCA

Loss of Coolant Accident

LOOP

Loss of Offsite Power

LP

Lesson Plan

MIC

Microbiologically Induced Corrosion

MST

Maintenance Surveillance Test

NRC

Nuclear Regulatory Commission

OST

Operations Surveillance Test

OT Delta T

Overtemperature Delta Temperature

PRZR

Pressurizer

RCP

Reactor Coolant Pump

RCS

Reactor Coolant System

REV

Revision

RO

Reactor Operator

SALP

Systematic Assessment of Licensee Performance

SBLOCA

Small break Loss of Collant Accident

SER

Safety Evaluation Report

SI

Safety Injection

SPOS

Safety.Parameter Displays Systems

SRO

Senior Reactor Operator

SW

Service Water System

TI

Training Instruction

TS

Technical Specification

mUNR

Unresolved Item

WOG

Westinghouse Owners Group