ML14181A949

From kanterella
Jump to navigation Jump to search
Insp Rept 50-261/97-09 on 970720-0830.Violations Noted.Major Areas Inspected:Operations,Maint,Engineering & Plant Support
ML14181A949
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 09/26/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14181A947 List:
References
50-261-97-09, 50-261-97-9, NUDOCS 9710100035
Download: ML14181A949 (28)


See also: IR 05000261/1997009

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

50-261

License Nos:

DPR-23

Report No:

50-261/97-09

Licensee:

Carolina Power & Light (CP&L)

Facility:

H. B. Robinson Unit 2

Location:

3581 West Entrance Road

Hartsville, SC 29550

Dates:

July 20 - August 30, 1997

Inspectors:

B. Desai, Senior Resident Inspector

J. Zeiler, Resident Inspector

J. Wiseman, Region II Inspector

Approved by:

M. Shymlock, Chief, Projects Branch 4

Division of Reactor Projects

Enclosure 2

9710100035 970926

PDR

ADOCK 05000261

PDR

EXECUTIVE SUMMARY

H. B. Robinson Power Plant, Unit 2

NRC Inspection Report 50-261/97-09

This integrated inspection included aspects of licensee operations,

maintenance, engineering, and plant support. The report covers a six-week

period of resident inspection: in addition, it includes the results of an

inspection by a Region II based reactor safety inspector.

Operations

The conduct of operations was professional and safety-conscious.

Several items were identified by either the inspector or licensee that

indicated the need for greater attention to detail by operators

conducting routine rounds. Several major projects were continuing or

nearing completion which have improved plant material and cosmetic

conditions, enhanced equipment identification, and aided personnel

safety (Section 01.1).

The licensee issued a night order when the reactor coolant system hot

leg temperature indication, TE-413, was out of service. The night order

adequately addressed steps required by operators to confirm natural

circulation cooldown in lieu of the temporary loss of post-accident

temperature indication. TE-413 was subsequently returned to service

following replacement of the failed component (Section 01.2).

The inspector discovered that the B Emergency Diesel Generator (EDG)

output breaker control switch was mispositioned. This mispositioning

resulted in the B EDG being inoperable for an extended period of time.

The licensee's initial actions in response to the mispositioning were

appropriate and timely. At the end of the report period, the licensee

had not completed their investigation into the cause and risk

significance of the mispositioning. This issue was identified as an

Unresolved Item pending completion of the NRC's review of the licensee's

investigation (Section 01.3).

The inspector concluded that all three channels of Over Power Delta

Temperature (OPDT) were not calibrated in accordance with Technical

Specification (TS) 2.3.1.2.e, causing the three channels to be

inoperable. This constituted a failure to meet the minimum channel

operability requirement of TS Table 3.5-2, Item 6. This issue was

identified as a Violation (Section 08.1).

Maintenance

In general, routine maintenance activities were performed

satisfactorily. The inspector noted good controls of housekeeping and

good supervisor oversight of work activities while performing preventive

maintenance on a condenser vacuum pump. The inspector noted good

engineering support and management involvement in addressing a Steam

Generator Power-Operated Relief Valve setpoint indication drift problem.

In general, maintenance overhaul of the Dedicated Shutdown (DS) diesel

engine was performed satisfactorily, however, the inspector noted that

2

maintenance personnel were inexperienced resulting in strong reliance on

vendor support and potentially longer DS system outage time (Section

M1.1).

The waste gas analyzer continued to experience problems, indicating a

need for the licensee to adequately address the root cause. Rapid

response team support to address these problems was noteworthy (Section

M1.2).

The inspector concluded that the new Work Management Process procedure

appropriately detailed the changes that were recently updated. The

training plan associated with the new process was also considered good,

as it relied on numerous examples of what constitutes tool pouch work

(Section M1.3).

Engineering

A Non-Cited Violation (NCV) was identified for failure to meet the

requirements of 10 CFR 50.59 regarding an old design installation error

involving the failure to install a restricting orifice in the

containment airlock interlock (Section E8.1).

A NCV was identified for failure to meet the requirements of 10 CFR

50.71(e) regarding inaccuracies identified in the Updated Final Safety

Analysis Report (UFSAR) description of the spent fuel pool cooling

system (Section E8.2).

Plant Support

One instance was identified by the inspector where an untimely hourly

fire watch was performed during the implementation of fire protection

compensatory measures in the B EDG room. The problem resulted from

weaknesses in fire protection controls (Section F1.1).

The number of outstanding work requests related to the fire protection

systems was low and there was no backlog. Corrective maintenance on

degraded fire protection systems was being accomplished in a timely

manner. Appropriate Corrective Action Program assessments of fire

protection program implementation have been conducted (Section F2.1).

Appropriate surveillances and tests were being performed on the fire

protection features and systems. The surveillance and tests of the fire

protection systems and features met the requirements specified in the

UFSAR (Section F2.2).

The licensee has developed engineering evaluations in accordance with

the provisions of NRC Generic Letter 86-10 to justify variations of

in-plant installations from tested configurations for pyrocrete fire

barrier walls, penetration seals, fire doors, fire dampers

(Section F2.3).

3

The fire protection program implementing procedures met the intent of

the NRC guidelines and requirements. Implementation of the fire

protection and prevention procedures .and the general housekeeping for

control of combustibles within the plant were satisfactory

(Section.F3.1).

The performance by the fire brigade to a drill during this inspection

was good. The brigade exhibited good command and control, fire ground

tactics, and recovery operations. The actions by the fire brigade met

the established drill objectives (Section F5.1).

Licensee performance during several emergency preparedness drills

adequately demonstrated the capability of the emergency response

organization and facilities. Drill critiques were aggressive in

identifying areas for improvement (Section P1.1).

The inspectors concluded that radiation control and security practices

were proper (Section R1.1 and S1.1).

Summary of Plant Status

Robinson Unit 2 operated at full power for the entire report period. As of

the end of the report period, the unit had been continuously on-line for 313

days.

I. Operations

01

Conduct of Operations

01.1 General Comments (71707)

The inspectors conducted frequent control room tours to verify proper

staffing, operator attentiveness and communications, and adherence to

approved procedures. The inspectors attended daily operation turnovers,

management reviews, and plan-of-the-day meetings to maintain awareness

of overall plant operations. Operator logs were reviewed to verify

operational safety and compliance with Technical Specifications (TSs).

Instrumentation, computer indications, and safety system lineups were

periodically reviewed from the Control Room to assess operability.

Frequent plant tours were conducted to observe equipment status and

housekeeping. Condition Reports (CRs) were routinely reviewed to assure

that potential safety concerns and equipment problems were reported and

resolved.

In general, the conduct of operations was professional and safety

conscious. However, the inspector noted several items during this

report period that indicated the need for greater operator attention to

detail during the conduct of rounds. For example, during a routine

plant walkdown, the inspector discovered an emergency diesel generator

output breaker control switch mispositioned. This mispositioning, most

likely, had existed over numerous shifts. During another walkdown, the

inspector observed rainwater leaking through the roof of the Dedicated

Shutdown (DS) Diesel Generator cubicle wetting areas on the generator

side of the engine. The rainwater stains present indicated that this

condition had gone undetected and not corrected for a considerable

period of time. In addition, a Shift Technical Advisor (STA) identified

that the setpoints on the local positioners for the Steam Generator

Power-Operated Relief Valves (PORVs) had drifted significantly. While

the identification of this problem by the STA was good, and the setpoint

drift did not impact valve operability, the condition had existed for a

considerable time.

Good plant equipment material conditions and housekeeping continued to

be observed throughout the report period. The licensee was continuing

with or nearing completion of several major projects designed to improve

plant material and cosmetic conditions, provide easier and efficient

equipment identification, and promote greater personnel safety. These

projects included: painting equipment and plant structures, color-coding

safety equipment, installing new and improved equipment identification

tags, re-insulating piping, and re-surfacing heavily traveled areas,

2

both inside the auxiliary building and in and around the turbine

building.

01.2 Reactor Coolant System (RCS) Loop 1 Hot Leg Temperature Instrument

Failure

a. Inspection Scope (71707)

The inspector assessed the impact associated with the failure of the RCS

loop 1 hot leg wide range temperature element (TE-413). TE-413 failed

due to a problem with an electronic repeater module.

b. Observations and Findings

TE-413 provides indication of RCS loop 1 hot leg wide range temperature

in the control room, as well as locally in the charging pump room and at

the secondary control panel in the turbine building. TE-413 is powered

from the Appendix R/Safe-Shutdown power supply PP-50 and its use

includes confirmation of natural circulation in Dedicated Shutdown

Procedure (DSP), DSP-002, Hot shutdown using the Dedicated/Alternate

Shutdown System, as well as DSP-007, Cold Shutdown using the

Dedicated/Alternate Shutdown System. DSP-002 and -007 are utilized to

shutdown the plant from the secondary control panel following an event

that requires control room evacuation. While redundant RCS hot leg

temperature monitoring is available in the control room, TE-413 is the

only RCS hot leg temperature monitoring instrument available at the

secondary control panel. With TE-413 inoperable, the inspector

questioned the licensee if additional guidance was needed to confirm

natural circulation while in procedure DSP-002 and DSP-007.

The licensee assessed the condition and issued Night Order 97-031, which

provided guidance to the operators to utilize other available

information, e.g., RCS cold leg temperature and steam pressure.

c. Conclusions

The licensee issued a night order when TE-413 was out of service. The

night order adequately addressed steps required by operators to confirm

natural circulation cooldown.. TE-413 was subsequently returned to

service following replacement of the failed component.

01.3 Emergency Diesel Generator Output Breaker Control Switch Mispositioning

a. Inspection Scope (71707)

On August 20, 1997, the inspector discovered the B train Emergency

Diesel Generator (EDG) output breaker control switch in the TRIP

position rather than the NEUTRAL (i.e., normal) position. This

mispositioning rendered the B EDG inoperable. The inspector monitored

the licensee's investigation to determine the cause of the switch

mispositioning, plant risk significance, and corrective actions.

b. Observations and Findings

At approximately 11:15 a.m., on August 20, during a routine walkdown of

equipment readiness for operation in the B EDG room, the inspector

discovered the B EDG output breaker control switch, located on the

generator control panel, to be in (what appeared to be) the TRIP

position. The switch is normally in the neutral position, mid-way

between the TRIP and OPEN position indication. The inspector observed

no alarms present on the EDG control panel that indicated a problem with

the switch position. After verifying that a similar switch

configuration problem did not exist on the A EDG, the inspector alerted

operations personnel to the problem. The licensee immediately initiated

an operability determination to determine whether the as-found switch

position impacted operability of the EDG.

Following review of the output breaker control circuitry, licensee

engineering personnel determined that, with the switch in the TRIP

position, the B EDG output breaker would have immediately reopened

following closure on an E-2 Emergency Bus undervoltage condition. As a

result, the B EDG would have been incapable of automatically energizing

the E-2 Emergency Bus,.and was therefore, inoperable. At 3:44 p.m.,

plant management directed the switch to be returned to its normal

position. At that time, it was discovered that the switch was in the

TRIP and partial PULL OUT (i.e., pull-to-lock) position. In this

configuration, the EDG output breaker would have responded similarly to

the switch being held in the TRIP position.

The licensee determined that between 11:15 a.m. and 3:44 p.m., the plant

had been in the action requirements of TS 3.0 as a result of having the

A train Safety Injection (SI) Pump and Containment Spray (CS) Pump

inoperable concurrent with the B EDG inoperability. The A train SI and

CS pumps had previously been declared inoperable for scheduled

maintenance earlier that morning on HVH-6A, the safety-related A train

SI pump room cooler. HVH-6A is required to be operable to support

cooling the A ECCS pumps in the SI pump room and HVH-6B is necessary for

cooling B train ECCS pumps. Due to the potential for the B EDG to have

been inoperable greater than the outage time allowed by TS, the licensee

made a one-hour non-emergency report to the NRC in accordance with 10

CFR 50.72 for a condition outside design basis. Later that night, the B

EDG was started and operated to verify that the output breaker control

switch functioned properly. No problems were identified with either the

switch or EDG operation.

The output breaker control switch is a Westinghouse Type W-2. four

position, spring return to normal, T-handle switch. The four positions

include CLOSE, NEUTRAL, TRIP, and PULL-OUT. The NEUTRAL, i.e., normal

position, has the T-handle oriented vertically facing the 12 o-clock

position. When manipulated in the TRIP or CLOSE direction, the switch

spring returns to NEUTRAL upon release of the handle. By moving the

switch first to TRIP, then pulling the handle outward from the switch

face and moving it counter-clockwise, the switch can be placed in PULL

OUT.

4

The switch is manipulated quarterly during routine TS surveillance

testing. During this testing, the switch is turned to the CLOSE

position to connect the EDG to its E-2 Emergency Bus and later turned to

the TRIP position to disconnect from the emergency bus. The last time

this test was performed, as well as the last time the switch was known

to have been operated, was July 28, 1997.

The licensee initiated an Event Review Team to investigate the cause of

the switch mispositioning, the risk significance, and recommend

corrective actions. The team investigated three possible scenarios that

could have resulted in the switch being mispositioned. These scenarios

included (1)

the potential for the switch to have been left in the

partial PULL-OUT position when it was manipulated during the July 28,

1997 EDG testing, (2) the switch being inadvertently manipulated, e.g.,

bumped, and (3)

the switch being deliberately placed in the incorrect

position. At the end of the report period, the Event Review Team had

not completed its review of the incident. The inspector planned to

review the results of the licensee's evaluation upon completion. This

will be tracked as Unresolved Item (URI) 50-261/97-09-01:

Review

Licensee Evaluation of EDG Output Breaker Control Switch Mispositioning.

c. Conclusions

The inspector determined that the licensee's initial actions taken in

response to the discovery of the mispositioned B EDG output breaker

control switch were appropriate and timely. At the end of the report

period, the licensee had not completed their investigation into the

cause and risk significance of the mispositioning. This issue was

identified as an URI pending completion of the NRC's review of the

licensee's investigation.

07

Quality Assurance In Operations

07.1 Plant Nuclear Safety Committee and Nuclear Assessment Section Oversight

a. Inspection Scope (40500)

The inspector evaluated certain activities of the Plant Nuclear Safety

Committee (PNSC) and Nuclear Assessment Section (NAS) to determine

whether the onsite review functions were conducted in accordance with TS

and other regulatory requirements.

b. Observations and Findings

The inspector periodically attended PNSC meetings during the report

period. The presentations were thorough and the presenters readily

responded to all questions. The committee members asked probing

questions and were well prepared. The committee members displayed

understanding of the issues and potential risks. Further, the inspector

reviewed NAS audits and concluded that they were appropriately focused

to identify and enhance safety.

5

c. Conclusions

The inspector concluded that the onsite review functions of the PNSC

were conducted in accordance with TSs. The PNSC meetings attended by

the inspector were well coordinated and meetings topics were thoroughly

discussed and evaluated. NAS continued to provide strong oversight of

licensee activities.

08

Miscellaneous Operations Issues (92901)

08.1 (Closed) URI 50-261/97-08-01, Failure to Properly Calibrate the Low

Limit Value Affecting Reactor Trip Setpoint:

and,

(Closed) Licensee Event Report (LER) 50-261/97-07-00, Condition Outside

Design Basis Due to Inoperable OPDT Channels:

Background

This issue involved the identification by the licensee of non

conservative setting of the Over Power Delta Temperature (OPDT) reactor

trip setpoints affecting all three Limiting Safety System Settings

(LSSS) channels. The non-conservative setting only affected the OPDT

reactor trip setpoints at reactor power below 100 percent. The problem

was attributed to an inadequate calibration procedure that did not

specify appropriate low limit setpoints. The low limit is an adjustable

setpoint and is set during routine calibration of the loop at refueling

outage intervals. If no limits are specified on the calibration data

sheets, the limits are turned to the lowest setting so they do not

interfere with the calibration module. The licensee determined that the

condition had potentially existed since 1979 and was introduced during a

calibration data sheet revision.

Licensee corrective actions (planned and completed) included changes to

Loop Calibration Procedures (LP)-001, -002, and -003, OPDT Protection

Channels I, II, and III, respectively. The event was to be reviewed by

appropriate Maintenance and Operations personnel, and if determined

necessary, the Reactor Protection System (RPS) was to be revised to

determine which summators require high and low limits to be set. The

licensee submitted LER 50-261/97-07-00 on July 9, 1997, pursuant to 10

CFR 50.73 (a)(2)(i). The licensee had not identified any other

calibration procedures with similar errors.

Significance

The OPDT reactor trip setpoint, though an LSSS setting, is not taken

credit for in the accident analysis. Notwithstanding, the inspector

assessed the safety significance, including review of analysis performed

by Siemens Corporation (fuel supplier and core designer), as well as

discussed several potential scenarios with the reactor engineer. The

Siemens analysis performed a calculation assuming a rod withdrawal

6

accident starting at 100 percent and terminating at 118 percent combined

with a limiting axial flux difference of -20.0 and concluded that margin

existed to prevent reaching fuel centerline melt. This conservative

analysis enveloped the non-conservative trip setpoint that would

manifest only at power levels below 100 percent. Additionally, the

inspector confirmed through discussion with the reactor engineer, that

the local and average kilowatt/foot limits would not be exceeded for the

probable scenarios. Thus, the overall safety significance of the

condition was low. Additionally, the identification of the condition by

the Control Room Shift Supervisor (CRSS) was considered an example of

good attention to detail in the monitoring of control room indications.

However, the NRC is concerned about the length of time the condition had

existed since the periodic loop calibrations performed after 1979 failed

to identify the non-conservative setpoints as a result of not

appropriately prescribing the low limit values.

Conclusions

TS 2.3.1.2.e, LSSS, Protective Instrumentation, Core Protection,

requires that the OPDT reactor trip setpoint, for all three channels, be

calibrated commensurate with the formula specified. TS Table 3.5-2,

Item 6, requires that a total of three channels of OPDT be operable when

the reactor is critical.

The inspector concluded that all three channels of OPDT were not

calibrated in accordance with TS 2.3.1.2.e, causing the three channels

to be inoperable. This constituted a failure to meet the minimum

channel operability requirement of TS Table 3.5-2, Item 6. This issue

is identified as Violation (VIO) 50-261/97-09-02:

Failure to Properly

Calibrate OPDT Channels.

II.

Maintenance

M1

Conduct of Maintenance

M1.1 General Comments

a. Inspection Scope (61726 and 62707)

The inspector reviewed/observed all or portions of the following

maintenance related work requests/job orders (WRs/JOs) and/or

surveillances and reviewed the associated documentation:

WR/JO 97-ADBP1

RPS Relay Replacement (Rack 54)

WR/JO 97-ADBS1

RPS Relay Replacement (Rack 56)

WR/JO 97-ADBR1

RPS Relay Replacement (Rack 55)

WR/JO 97-ADFA1

Condenser Vacuum Pump A Packing Replacement

WR/JO AAICV-005

Condenser Vacuum Pump A Cooler Cleaning

WR/JO 917-ADXB1

Recalibrate Positioner on Secondary Control

Panel for B Steam Generator PORV Setpoint

Indication

7

WR/JO AARQ-001

Seven Year Dedicated Shutdown Diesel Generator

Inspection

OST 701-4

Inservice Inspection Valve Operations

Surveillance Test (OST)

b. Observations and Findings

The inspector observed that these activities were performed by personnel

who were experienced and knowledgeable of their assigned tasks.

Procedures were present at the work location and being followed.

Procedures provided sufficient detail and guidance for the intended

activities. Activities were properly authorized and coordinated with

operations prior to starting. Test and maintenance equipment in use was

calibrated, procedure prerequisites were met, and system restoration was

completed. Other specific observations and comments for the items

listed above included the following:

The maintenance supervisor for work related to condenser vacuum pump A

(WR/JOs 97-ADFA1 and AAICV-005) was observed frequently at the job

location and providing good oversight of work activities. Good control

of area housekeeping was maintained during the work, and upon completion

of work, the area was restored to its previous condition. Repacking of

the pump was necessitated as a result of excessive packing leakage. The

inspector noted that when the old packing rings were removed from the

outboard bearing, the four packing ring separation joints were found

aligned together. Normally, packing ring joints are offset to provide

less chance of packing leakage. The inspector noted that the procedure

did not provide guidance for installing packing rings since this

activity was considered skill of the craft. The maintenance supervisor

initiated a CR to address the mis-aligned packing rings and indicated

that corrective actions would address the need for additional training

and emphasis on correct packing ring installation.

The inspector noted good engineering support and involvement in

evaluating and developing detailed work instructions for the on-line

calibration of the positioner on the Secondary Control Panel for the B

Steam Generator PORV setpoint indication (WR/JO 97-ADXB1). This work

request, along with two others for Steam Generator PORVs A and C, were

implemented to correct a significant amount of drift identified in each

PORV's local indications of lift setpoint. The work activity was well

controlled and coordinated with operations to ensure that there was no

adverse impact on the plant. Since the setpoint drift was determined to

be a recurring problem, an Engineering Service Request was initiated to

investigate the need to replace the setpoint devices.

The inspector noted good vendor support of the seven year preventive

maintenance activity on the DS diesel engine (WR/JO AARQ-001). This

maintenance overhaul of the engine was conducted round the clock and a

vendor representative was present, both on day and night shift. The

inspector noted that maintenance personnel were not experienced in many

of the critical diesel inspections, work activities, etc., resulting in

strong reliance on the vendor and potentially longer DS system outage

8

time. Formal DS engine training and personnel training qualification

requirements were not established. However, the inspector did not

identify any areas where worker inexperience caused any adverse

maintenance quality impact. The licensee's post maintenance critique

identified actions to evaluate the need for formal training

qualifications for DS engine maintenance.

c. Conclusions

The inspector concluded that routine and corrective maintenance

activities were performed satisfactorily. The inspector noted good

controls of housekeeping and good supervisor oversight of work

activities while performing preventive maintenance on a condenser vacuum

pump. The inspector roted good engineering support and management

involvement in addressing a Steam Generator PORV setpoint indication

drift problem. In general, maintenance overhaul of the DS diesel engine

was performed satisfactorily, however, the inspector noted that

maintenance personnel were inexperienced resulting in strong reliance on

vendor support and potentially longer DS system outage time.

M1.2 Waste Gas Analyzer Problems

a. Inspection Scope (62707) (71500)

The inspector noted that the Waste Gas Analyzer continued to experience

problems in that it frequently alarmed, indicating greater than two

percent oxygen concentration in the gaseous waste disposal system.

Consequently, the inspector reviewed licensee actions related to

resolving this problem.

b. Observations and Findings

The waste gas analyzer is designed to automatically monitor oxygen and

hydrogen concentration in the waste disposal system and chemical and

volume control tanks. As discussed in Updated Final Safety Analysis

Report (UFSAR) Section 11.3.2.1, the waste disposal system is not

expected to have significant oxygen in any of the tanks. An alarm, with

a setpoint of two percent volume of oxygen, is provided to allow time to

take the required action before the combustible concentration limit is

reached. Due to problems, including oxygen inleakage, the inspector

noted that the waste gas analyzer frequently reached the two percent

alarm setpoint. Consequently, operators would remove the waste gas

analyzer from automatic sampling and place it in a manual mode, pending

resolution of the oxygen inleakage problem. Placing the waste gas

analyzer in the manual mode, resulted in the analyzer being inoperable,

and placed the unit in a 14 day reportable TS action statement per

TS 3.5.3, Table 3.5-7, Item 2, as well as requiring periodic manual

sampling of waste gas.

The inspector expressed concern to the licensee in view of the frequency

of the problems experienced with the gas analyzer. Additionally, the

inspector also noted that some of the details associated with the system

9

were not clearly understood by some members of the operating staff. The

licensee initiated several actions including, replacement of the

portions of tubing suspected of inleakage as well as promulgation of

additional guidance to the operators on operational details to minimize

reaching the alarm setpoint. Additionally, the licensee plans to

implement a modification to the alarm setpoint. The Rapid Response

Team's support associated with troubleshooting related to the system was

considered to be noteworthy. The inspector plans to review the

modification during future inspections.

The inspector also noted that the waste gas analyzer was not scoped in

the Maintenance Rule program. This issue will be further reviewed by an

upcoming NRC inspection of the licensee's Maintenance Rule program.

c. Conclusions

The waste gas analyzer continued to experience problems, indicating a

need for the licensee to adequately address the root cause. Rapid

Response Team support to address these problems was noteworthy.

M1.3 Work Control Process

a. Inspection Scope (62707) (92902)

The licensee implemented changes to the work control process. A

significant change included the addition of "tool pouch" type

maintenance. The work control process is described in Nuclear

Generation Group procedure ADM-NGGC-0104, Work Management Process.

b. Observations and Findings

The inspector reviewed procedure ADM-NGGC-0104 and discussed the process

with licensee management. The new process allows qualified individuals

to conduct corrective maintenance without a work order, written

instructions, post maintenance testing, or close-out documentation under

the tool pouch process. Tool pouch maintenance is allowed to be

conducted on safety-related equipment, provided it does not impact

system operation or availability.

The inspector reviewed the training and plans to monitor effectiveness

of this methodology during routine inspections.

c. Conclusions

The inspector concluded that the new Work Management Process procedure

appropriately detailed the changes that were recently updated. The

training plan associated with the new process was also considered good,

as it relied on numerous examples of what constitutes tool pouch work.

10

III. Engineering

E7

Quality Assurance in Engineering Activities

E7.1 Special UFSAR Review (37551)

A recent discovery of a licensee operating their facility in a manner

contrary to the UFSAR description highlighted the need for a special

focused review that compares plant practices, procedures and/or

parameters to the UFSAR descriptions. While performing the inspections

discussed in this report, the inspector reviewed the applicable portions.

of the UFSAR related to the areas inspected. The inspector verified

that for the select portions of the UFSAR reviewed, the UFSAR wording

was consistent with the observed plant practices, procedures and/or

parameters.

E8

Miscellaneous Engineering Issues (92903) (37551)

E8.1

(Closed) URI 50-261/96-04-02, Review Licensee Evaluation of UFSAR

Containment Personnel Airlock Discrepancy: This URI involved a UFSAR

discrepancy identified by the inspector associated with the containment

airlock interlock. Specifically, UFSAR Section 6.9.2.3 (Amendment 13)

stated that the Penetration Pressurization System (PPS) line that

supplies continuous air pressurization to the containment personnel

airlock seals contained a restricting orifice. The purpose of this

orifice was to assure that air consumption upon failure of the interlock

(e.g., air supply valve failed to close), would still be within the

capacity of the PPS, and would not result in loss of pressure to other

zones connected to the same PPS header. The inspector discovered that

this restricting orifice did not exist. The licensee confirmed that

this orifice, most likely, had never been installed.

The licensee initiated CR 96-00803 to address this issue. The licensee

determined that there was no safety benefit in having a restricting

orifice in this application. This was based primarily on existing

control room alarms and indications of PPS low header pressure and high

PPS header flowrates, as well as the existing capability to manually

isolate PPS to the airlock. In addition, should the interlock fail, the

PPS supply could be isolated by closing the airlock door. The inspector

reviewed CR 96-00803 and determined that the licensee had adequately

evaluated the impact of not having an orifice in this application. The

inspector also noted that during the October 1996 refueling outage (RFO

17), the licensee implemented modification Engineered Service Request

(ESR) 95-00888. This modification isolated continuous PPS air

pressurization of containment penetrations, including the containment

airlock. As a result of this modification, the airlock interlock no

longer served any function. The licensee deleted the UFSAR statement

referring to the restricting orifice with the issuance of Amendment 14

to the UFSAR, dated April 14, 1997. The inspector verified these

actions had been completed and determined that this adequately resolved

this issue.

11

The licensee indicated the reference to the restricting orifice had been

in the original plant FSAR. Since the plant had never met the

description of the airlock interlock in the FSAR, the inspector

considered this to be a defacto change from the FSAR. The inspector

determined the failure of the as-built containment airlock design to

match the description in the FSAR was a violation of the requirements of

10 CFR 50.59.

The safety significance of this violation was considered to be low

.because the lack of a restricting orifice had no adverse impact on the

operation of the PPS system. Further, the issue did not involve an

unreviewed safety question. The licensee's UFSAR Review and Upgrade

Plan was presented to the NRC in a May 30, 1996 management meeting and

was docketed in a June 10, 1996 meeting summary issued by the NRC. The

meeting summary contains information related to the scope of the UFSAR

review and examples of identified discrepancies. The initial phase of

the UFSAR review was completed on June 30, 1997. The review of UFSAR

Section 6.9.2.3 had not been completed by the licensee when this issue

was identified. The inspector considered that this issue would have

probably been identified by the licensee's UFSAR review. Regardless,

the statement referring to the orifice would have been deleted as part

of the implementation of modification ESR 95-00888.

In accordance with the "General Statement of Policy and Procedures for

Enforcement Actions" (Enforcement Policy), NUREG-1600, this violation

normally would be categorized as a Severity Level IV violation.

However, as discussed in Section VII.B.3 of the Enforcement Policy, the

NRC may refrain from issuing a Notice of Violation (Notice) for a

violation that involves a past problem, such as an old engineering,

design, or installation deficiency, provided that certain criteria are

met. After review of this violation the NRC has concluded that while a

violation did occur, enforcement discretion is warranted in this case.

Therefore, to encourage licensee efforts to identify and correct UFSAR

discrepancies, no Notice is being issued in this case. The specific

bases for this decision were (1)

the licensee's UFSAR review program, as

described in the June 10, 1996 NRC meeting summary, would likely have

identified the violation in light of the defined scope, thoroughness and

schedule; (2)

there had been no prior notice where the licensee could

have reasonably identified the violation earlier; (3)

timely and

appropriate corrective action was completed to evaluate the lack of a

restricting orifice; (4)

timely and effective long-term corrective

actions were implemented to review and identify any similar design

deficiencies; (5)

the design deficiency was considered an old design

issue in that the restricting orifice had never been installed; and, (6)

the violation was not willful.

This issue will be documented as Non

Cited Violation (NCV) 50-261/97-09-03:

Failure to Meet 10 CFR 50.59

Requirements for UFSAR Description of Containment Airlock Interlock.

E8.2 (Closed) Inspector Followub Item (IFI) 50-261/96-08-02, Review Licensee

Actions to Resolve UFSAR Inconsistencies: This IFI involved examples

where the Spent Fuel Pool (SFP) Cooling System description in the UFSAR

12

did not adequately describe the true design. The examples identified

included the following:

UFSAR Section 9.1.3.1.2 (Amendment 7) stated the design basis for

the SFP cooling capacity was to provide cooling for a full core

off-load when only one-third core already existed in the SFP.

Contrary to this, the licensee routinely conducted full core off

loads with greater than one-third core already in the SFP.

UFSAR Sections 9.1.3.1.3 (Amendment 7) and 9.1.2.3.4 (Amendment 2)

were inconsistent with regard to maximum SFP water temperatures

for one-third and full core off-loads. Section 9.1.3.1.3

indicated these SFP temperatures would be 120oF and 150 0 F,

respectively. Section 9.1.2.3.4 indicated the temperatures would

be 132oF and 166 0F, respectively.

UFSAR Section 9.1.3.3.1 (Amendment 2) discussed an alternate means

of providing SFP cooling in the event of a failure of the SFP

cooling pump by connecting a temporary pump to emergency

connections. While the capability to connect a temporary pump

still existed, the wording had not been updated following the

permanent installation of a second SFP cooling pump.

The licensee initiated CR 95-02501 to address these inaccuracies in the

SFP description in the UFSAR. The root cause was determined to be the

inadequate implementation of UFSAR description updates in 1982 when the

SFP was re-analyzed and expanded to its current storage capacity. The

inspector previously reviewed the 1982 NRC Safety Evaluation Report

(SER) and related licensee supporting analysis for the SFP expansion

project and determined that SFP cooling system was capable of performing

its design function at the current SFP storage capacity. The inspector

reviewed the latest licensee update to the UFSAR (Amendment 14),

submitted in April 1996. The inspector verified that appropriate

corrections or enhancements in the description of the SFP system had

been implemented.

10 CFR 50.71(e) requires that the FSAR be revised to include the effects

of all changes in the facility. The inspector determined that UFSAR

Sections 9.1.2.3.4, 9.1.3.1.2, 9.1.3.1.3, and 9.1.3.3.1 had contained

information that predated the SFP expansion project of 1982 that was no

longer accurate and had not been revised in a timely manner.

In accordance with the General Statement of Policy and Procedures for

Enforcement Actions" (Enforcement Policy), NUREG-1600, this violation

normally would be categorized as a Severity Level IV violation.

However, as discussed in Section VII.B.3 of the Enforcement Policy, the

NRC may refrain from issuing a Notice of Violation (Notice) for a

violation that involves a past problem, such as an old engineering,

design, or installation deficiency, provided that certain criteria are

met. After review of this violation the NRC has concluded that while a

violation did occur, enforcement discretion is warranted in this case.

Therefore, to encourage licensee efforts to identify and correct UFSAR

13

discrepancies, no Notice is being issued in this case. The specific

bases for this decision (1) the licensee's UFSAR review program, as

described in the June 10, 1996 NRC meeting summary, would likely have

identified the UFSAR inaccuracies in light of the defined scope,

thoroughness and schedule: (2) there had been no prior notice where the

licensee could have reasonably identified the violation earlier:

(3) timely and appropriate corrective action was completed to evaluate

the inaccurate SFP descriptions; (4) timely and effective long-term

corrective actions were implemented to review and identify any similar

design deficiencies in the system; (5)

the design deficiency was

considered an old design issue in that the description of the SFP had

not been adequately updated following design changes in 1982; and, (6)

the violation was not willful. This issue will be documented as NCV 50

261/97-09-04:

Failure to Update UFSAR Description of the Spent Fuel

Pool System Following Design Changes.

IV. Plant Support

F1

Control of Fire Protection Activities

F1.1 Untimely Hourly Fire Watch Performance

a. Inspection Scope (71750)

The inspector observed one instance where an hourly fire watch for the B

EDG room was not conducted in a timely manner. The inspector reviewed

fire protection procedures governing the performance of hourly fire

watches.

b. Observations and Findings

At 2:20 p.m., on August 21, the inspector noticed that an hourly fire

watch log posted at the entrance to the B EDG room had not been signed

off by the fire watch attendant for the required 2:00 p.m. log entry.

At the time, the attendant was inside the EDG room discussing the repair

of a local fire alarm manual pull station box with maintenance

personnel.

The fire watch had been implemented due to the problem with

this pull station box. After alerting the attendant to the missing log

entry, the attendant immediately initialed for the 2:00 p.m. entry.

Based on subsequent discussions with the attendant, the inspector

learned that the individual had arrived in the room at 2:15 p.m. The

attendant indicated that the previous fire watch was conducted at 1:00

p.m. This resulted in an hour and fifteen minute period for this fire

watch. The attendant indicated that hourly fire watches could be

performed anytime during the hour and not necessarily at the same time

each successive hour. While it was reasonable to allow some flexibility

in the frequency, the inspector was concerned that this understanding

allowed too much flexibility and did not meet the intent of an hourly

fire watch.

The inspector reviewed Fire Protection (FP) procedure FP-004, Duties of

a Fire Watch, Revision 7, dated June 6. 1996. The procedure did not

14

provide a clear definition of an "hourly" fire watch. The Area Fire

Watch Hourly Inspection Log (Attachment 7.1 of FP-004) provided pre-set

spaces for initialing the completion of hourly fire watch inspections on

the hour for a 24-hour period. However, the procedure did not

specifically state that the fire watch had to be performed on the hour

or at the same time each hour. The inspector discussed the untimely

fire watch in the EDG room and weaknesses identified in FP-004 with the

operations manager. The licensee initiated CR 97-01774 to address these

items. The licensee indicated that the procedure would be revised to

clearly define and document the definition and requirements for an

hourly fire watch. The inspector considered this adequate to resolve

the concerns in this area. The inspector plans to review the licensee's

corrective actions upon completion.

c. Conclusions

The inspector identified one instance where an untimely hourly fire

watch was performed during the implementation of fire protection

compensatory measures for the B EDG room. The problem resulted from

weaknesses in fire protection controls. The inspector determined that

the licensee's planned corrective actions should prevent recurrence of

this type of incident.

F2

Status of Fire Protection Facilities and Equipment

F2.1 Operability of Fire Protection Facilities and Equipment

a. Inspection Scope (64704)

The inspector reviewed open maintenance work orders, Equipment

Inoperable Records (EIRs), fire protection related CRs, fire protection

technical aid logs on the facility fire protection systems, features to

assess performance trends or material condition problems with fire

protection/safe-shutdown systems, and equipment. Walkdown inspections

were conducted of the fire protection water supply systems, Appendix R

emergency lighting, the DS diesel system, and fire barriers in safety

related plant areas, to determine the material condition of these fire

protection features.

b. Observations and Findings

As of July 31, 1997, the total number of open WR/JOs related to the fire

protection and safe-shutdown systems and features was 26. These work

requestswere grouped as follows:

Fire Barrier Door, Dampers, and Penetration Seals

10

Fire Protection Water Systems (fire Pumps/sprinklers) 7

CO Systems (EDG & Cable Vaults)

0

Haion System (Cable Spreading & Switchgear Rooms)

0

Fire Brigade Equipment

2

Dedicated Shutdown Diesel Generator System

6

Emergency Lights

1

Fire Detection System

2

Total

26

15

All except two of these work requests were issued in 1996 or 1997. The

work requests issued prior to 1996 were minor DS diesel cubical

ventilation repairs which did not affect the operability of the DS

diesel systems.

As a result of the predictive maintenance program, the licensee

identified that vibration levels on the motor driven fire pump indicated

motor degradation and a need for motor refurbishment. Special motor

vibration monitoring tests (Report No. V-6175-97-07-1) were performed on

July 14-15, 1997. The testing indicated the presence of open or loose

rotor bars in the motor. The licensee indicated that the fire pump

motor is scheduled to be removed and refurbished (WR/JO 97-AEDJ1) during

the week of August 18, 1997.

The inspector determined that the number of outstanding work requests

related to the fire protection systems was low. There was not a backlog

of open work requests.

Fire Protection System Operability:

The inspector reviewed the fire protection portion of the Equipment

Inoperable Records and the plant fire protection Technical Aid Log for

the three month period of May-July, 1997. These records indicated that

the number of fire protection impairments was relatively small and

adequately monitored to limit their duration. The inspector determined

that the identified repair impairments had been restored to service

within 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />.

The inspector conducted walkdown tours and inspected the fire protection

features to determine if the systems were operable and properly

maintained. The inspector toured the following plant fire zones/areas:

Fire doors to the Waste Evaporator Area (Fire Zone 38),

Fire barrier walls for the Component Cooling Water Surge Tank Room

(Fire Zone 36),

Unit 2 Service Water pumps and electric and diesel driven fire

pumps (Fire Zone 29),

Dedicated shutdown system indications in the 4160 VAC Switchgear

Room (Fire Zone 25E),

Dedicated Shutdown Diesel Generator (Fire Zone 25D),

Appendix R eight-hour emergency light units for the dedicated

safe-shutdown system (Fire Zone 25),

Halon 1301 and fire detection systems for the Emergency Switchgear

Room (Fire Zone 20), and,

.

Fire doors and fire detectors for the Battery Room (Fire Zone 16).

16

The inspector noted that the manual fire fighting equipment, automatic

fire detection systems, and fire zone/area walls, floors, and ceilings

of the fire zones, inspected were operational and were well maintained.

The inspector noted that the fire protection system engineer tracked

fire detection system spurious alarms and Electric Thermal Link (ETL)

fire damper resistance values for the CO2 and Halon fire suppression

systems to trend problems with detector sensitivity and automatic fire

damper operations. The inspector reviewed the system engineer trend

reports for 1997 and concluded that no adverse trends had been observed

for these systems during 1997.

Fire Protection Corrective Action Program:

The inspector reviewed a computer listing of the fire protection program

related Condition Reports issued during 1997. The number of CRs related

to the fire protection and safe-shutdown systems and features was

approximately 23. Discussions with operations fire protection personnel

indicated that while no adverse trends have been identified as part of

Corrective Action Program (CAP), the first quarter 1997 review of fire

protection program CRs had observed an increase in the number of errors

related to fire protection. This condition was identified in CR 97

01250 and was currently being reviewed by the licensee. The inspector

concluded that appropriate CAP assessments of the fire protection

program implementation had been performed.

c. Conclusions

The number of outstanding work requests related to the fire protection

.systems was low and there was no backlog. Corrective maintenance on

degraded fire protection systems was being accomplished in a timely

manner. Appropriate Corrective Action Program assessments of fire

protection program implementation had been performed.

F2.2 Surveillance of Fire Protection Features and Equipment

a. Inspection Scope (64704) (92904)

The inspector reviewed the following operations surveillance test

procedures and completed tests for various fire protection systems and

features to determine compliance with UFSAR Section 9.5.1.6, Inspection

and Testing Requirements:

OST-611, Revision 12, November 13, 1996, Low Voltage Fire

Detection and Actuation System, Zones 1&2, (Semi Annual),

OST-623, Revision 13, January 31, 1995, Fire Barrier Penetration

Seal Inspection, (18 Months),

OST-624, Revision 16, May 9, 1996, Fire Damper Inspection, (18

Months),

17

OST-625, Revision 18, November 11, 1996, Fire Door Inspection,

(Semi Annual),

OST-640, Revision 21, May 23, 1997, Self-Contained DC Emergency

Lighting System, (Semi Annual),

OST-918, Revision 5, April 9, 1996, Dedicated Shutdown

Instrumentation Check, (Monthly), and,

OST-922, Revision 9, November 21, 1995, Dedicated Shutdown

Equipment Identification Check, (Semi Annual).

b. Observations and Findings

The operability, surveillance and test requirements for the fire

protection systems and features had been removed from the Technical

Specifications and incorporated into the fire protection program as

described in UFSAR Section 9.5.1.6. These requirements met the

requirements for the fire protection features which were formerly in the

Technical Specifications. The completed surveillance tests of the fire

protection systems reviewed by the inspector were appropriately

completed and met the acceptance criteria. However, the inspector noted

that the test acceptance criteria and compensatory action requirements

of OST-640 for the 10 CFR Part 50, Appendix R, eight-hour DC emergency

light units for the dedicated safe-shutdown system were not addressed

within the.scope of administrative Fire Protection Procedure FPP-012,

Fire Protection Systems Minimum Equipment and Compensatory Actions. The

licensee stated that this issue was previously identified as a 1996 NAS

audit identified weakness and was being evaluated in the scope of

corrective actions for CRs 96-00733 and 96-00735 related to the problems

with the administrative and technical content of Fire Protection

Procedures not meeting management standards. NRC review of the status

of these issues is addressed in Section F3.1 of this report.

c. Conclusions

Appropriate surveillances and tests were being performed on fire

protection features and systems. The surveillance and tests of fire

protection systems and features met the requirements specified by UFSAR

Section 9.5.1.6.

F2.3 Design Basis for Fire Barrier Features and Components

a. Inspection Scope (64704)

Fire barriers include penetration seals, wraps, walls, structural member

fire resistant coatings, doors, dampers, etc. Fire barriers are used to

prevent the spread of fire and to protect redundant safe shutdown

equipment. Laboratory testing of fire barrier materials is done only on

a limited range of test.assemblies. However, in-plant installations can

vary from the tested configurations. Under the provisions of Generic

Letter (GL) 86-10, licensees are permitted to develop engineering

18

evaluations justifying such deviations. The inspector reviewed the

scope of the licensee's engineering evaluations associated with various

fire barrier features and components to confirm that the licensee had

established an adequate design basis for those fire barriers used to

separate safe shutdown functions.

b. Observations and Findings

In 1990, the licensee conducted a fire barrier inspection program which

identified fire barrier components which were not installed in

conformance with all NRC requirements for fire rated barriers. As a

result, the licensee generated a number of Engineering Evaluations (EEs)

to justify those deviations and address the adequacy of the installed

fire barriers for safety-related shutdown interior fire zones within the

plant. The EEs for the plant specific fire zones include EE 90-105

through EE 90-129. In addition, EE 90-104 listed fire doors and fire

dampers which do not conform to the respective National Fire Protection

Association requirements, as well as addressed generic deviations.

Nonconforming fire barrier penetration seal blockout designs were

addressed generically in EEs90-071 and 90-025.

During an NRC inspection (Inspection Report 50-261/96-12) conducted in

1996, configuration discrepancies were identified with the pyrocrete

fire barrier walls installed between fire zones 3 and 7, and between

fire zones 4 and 12. The licensee indicated that an engineering

evaluation that evaluated the wall configurations for acceptability of

the design in accordance with the provisions of GL 86-10 had been

developed for approval and identified in Engineering Service Request No.

97-00405. These engineering evaluations will be reviewed during future

NRC inspections.

c. Conclusions

The licensee has developed engineering evaluations in accordance with

the provisions of NRC GL 86-10 to justify variations of in-plant

installations from tested configurations for pyrocrete fire barrier

walls, penetration seals, fire doors, fire dampers.

F3

Fire Protection Procedures and Documentation

F3.1 Review of Fire Protection Program Procedures

a. Inspection Scope (64704)

The following Station Administration Procedures and Fire Protection

Procedures were reviewed for compliance with NRC requirements and

guidelines:

FP-001, Revision 29, Fire Emergency,

FP-002, Revision 5, Fire Report,

19

FP-003, Revision 9, Control of Transient Combustibles,

FP-009, Revision 6, Surveillance of Fire Protection Activities,

FP-010, Revision 6, Housekeeping Controls, and,

FP-012, Revision 4, Fire Protection Systems Minimum Equipment and

Compensatory Actions.

Plant tours were performed to determine procedure compliance.

b. Observations and Findings

The above procedures established the administrative guidance used to

implement the fire protection program at Robinson and included the

requirements for the control of combustibles, ignition sources and fire

brigade organization and training. The procedures met the intent of the

NRC requirements. Corrective actions of NAS audit weakness items R-FP

96-01, Weakness Nos. 1 ana 2, and CRs 96-00733 and 96-00735, addressing

the fire protection program administrative procedural problems, were not

yet completed. These items were scheduled for completion during the

fourth quarter 1997.

The inspector performed plant tours and noted that the control of

combustible and flammable materials, liquids and gases, and general

housekeeping were satisfactory.

c. Conclusions

The fire protection program implementing procedures met the intent of

NRC guidelines and requirements. Implementation of the fire protection

and prevention procedures and the general housekeeping for control of

combustibles within the plant were satisfactory.

F5

Fire Protection Staff Training and Qualification

F5.1 Fire Brigade Drill

a. Inspection Scope (64704)

The inspector witnessed a fire brigade drill and training for compliance

with the facility's fire protection program and NRC guidelines and

requirements.

b. Observations and Findings

On July 28, the inspector observed a fire brigade drill involving a

simulated fire at the outage radiation control access processing

building in the plant yard area. The fire brigade team leader and four

fire brigade members responded with the plant fire equipment carts in

full fire fighting turnout gear. An offensive fire attack was mounted

utilizing a 1 1/2-inch attack fire hose line from the first floor of the

20

building up the stairs to the second floor, followed by additional fire

hose line deployment practice in the yard area. A building search was

conducted by the brigade members and a practice search object was

successfully retrieved. The fire brigade team leader properly deployed

the fire brigade personnel, established a command post and effectively

used radio communications. The actions by the brigade met the

established drill objectives. A drill critique was conducted with the

fire brigade members following the drill to discuss the drill,

participants performance and recommendations for improvements. Several

areas of improvement were identified and were being addressed by the

fire protection and fire brigade training staffs.

c. Conclusions

During observation of a fire drill, the brigade exhibited good command

and control, fire ground tactics, and recovery operations. The ' tions

by the fire brigade met the established drill objectives.

P1

Conduct of Emergency Preparedness Activities

P1.1 Emergency Preparedness Drills (71750)

a. Inspection Scope

On July 29 and August 5, the inspector observed portions of the

licensee's emergency response drills conducted with Emergency Response

Organization Team "C" and "D", respectively. The drills were conducted

from the training simulator and included Technical Support Center (TSC),

Operations Support Center (OSC), Emergency Operations Facility (EOF),

and Joint Information Center activation with limited participation by

offsite organizations.

b. Observations and Findings

The inspector observed activities in the simulator control room, TSC,

and EOF. Activities were conducted in a professional manner and

personnel treated the exercises as if they were real.

The licensee

determined that all drill objectives were met. The inspector observed

the licensee's critique for the August 5 drill and noted that the

licensee was aggressive in identifying areas for improvement.

Strengths, deficiencies, and comments identified were appropriately

characterized, and where applicable, were entered into the corrective

action tracking program. The drill was also evaluated by NAS personnel

who provided meaningful comments on the effectiveness of the drills.

c. Conclusions

The licensee's performance during the two emergency preparedness drills

were adequate and drill critiques were aggressive in identifying areas

for improvement.

21

R1

Radiological Protection and Chemistry Controls

R1.1 General Comments (71750)

The inspector periodically toured the Radiological Control Area (RCA)

during the inspection period. Radiological control practices were

observed and discussed with radiological control personnel including RCA

entry and exit, survey postings, locked high radiation areas, and

radiological area material conditions. The inspector concluded that

radiation control practices were proper.

S1

Conduct of Security and Safeguards Activities

S1.1 General Comments (71750)

During the period, the inspector toured the protected area and noted

that the perimeter fence was intact and not compromised by erosion nor

disrepair. Isolation zones were maintained on both sides of the barrier

and were free of objects which could shield or conceal an individual.

The inspector periodically observed personnel, packages, and vehicles

entering the protected area and verified that necessary searches,

visitor escorting, and special purpose detectors were used as applicable

prior to entry. Lighting of the perimeter and of the protected area was

acceptable and met illumination requirements.

V. Management Meetings

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee

management at the conclusion of the inspection on September 10, 1997.

No proprietary information was identified.

22

PARTIAL LIST OF PERSONS CONTACTED

Licensee

J. Boska, Manager, Operations

H. Chernoff, Supervisor, Licensing/Regulatory Programs

T. Cleary, Manager, Maintenance

J. Clements, Manager, Site Support Services

D. Crook, Senior Specialist, Licensing/Regulatory Compliance

J. Keenan, Vice President, Robinson Nuclear Plant

R. Duncan, Manager, Robinson Engineering Support Services

R. Moore, Manager, Outage Management

J. Moyer, Manager, Robinson Plant

D. Stoddard, Manager, Operating Experience Assessment

R. Warden, Manager, Nuclear Assessment Section

T. Wilkerson, Manager, Regulatory Affairs

D. Young, Director, Site Operations

NRC

B. Desai, Senior Resident Inspector

J. Zeiler, Resident Inspector

M. Shymlock, Branch Chief, Region II

23

INSPECTION PROCEDURES USED

IP 37551:

Onsite Engineering

IP 40500:

Effectiveness of Licensee Controls in Identifying, Resolving, and

Preventing Problems

IP 61726:

Surveillance Observations

IP 62707:

Maintenance Observation

IP 64704:

Fire Protection Program

IP 71500:

Balance of Plant Inspection

IP 71707:

Plant Operations

IP 71750:

Plant Support Activities

IP 92901:

Followup - Operations

IP 92902:

Followup - Maintenance

IP 92903:

Followup - Engineering

IP 92904:

Followup - Plant Support

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

!Me Item Number

Status

Description and Reference

URI

50-261/97-09-01

Open

Review Licensee Evaluation of EDG Output

Breaker Control Switch Mispositioning

(Section 01.3)

VIO

50-261/97-09-02

Open

Failure to Properly Calibrate OPDT

Channels (Section 08.1)

NCV

50-261/97-09-03

Open

Failure to Meet 10 CFR 50.59 Requirements

for UFSAR Description of Containment

Airlock Interlock (Section E8.1)

NCV

50-261/97-09-04

Open

Failure to Update UFSAR Description of the

Spent Fuel Pool System Following Design

Changes (Section E8.2)

Closed

TNe Item Number

Status

Description and Reference

URI

50-261/97-08-01

Closed

Failure to Properly Calibrate the Low

Limit Value Affecting Reactor Trip

Setpoint (Section 08.1)

LER

50-261/97-07-00

Closed

Condition Outside Design Basis Due to

Inoperable OPDT Channels (Section 08.1)

URI

50-261/96-04-02

Closed

Review Licensee Evaluation of UFSAR

Containment Personnel Airlock Discrepancy

(Section E8.1)

24

NCV

50-261/97-09-03

Closed

Failure to Meet 10 CFR 50.59 Requirements

for UFSAR Description of Containment

Airlock Interlock (Section E8.1)

IFI

50-261/96-08-02

Closed

Review Licensee Actions to Resolve UFSAR

Inconsistencies (Section E8.2)

NCV

50-261/97-09-04

Closed

Failure to Update UFSAR Description of the

Spent Fuel Pool System Following Design

Changes (Section E8.2)