ML14181A729

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Insp Rept 50-261/95-19 on 950514-0617.Violations Noted.Major Areas Inspected:Plant Operations,Maint Activities, Engineering Efforts & Plant Support Functions
ML14181A729
Person / Time
Site: Robinson 
Issue date: 07/17/1995
From: William Orders, Verrelli D
NRC Office of Inspection & Enforcement (IE Region II)
To:
Carolina Power & Light Co
Shared Package
ML14181A726 List:
References
50-261-95-19, NUDOCS 9507240360
Download: ML14181A729 (20)


See also: IR 05000261/1995019

Text

pf REGUo

UNITED STATES

o

NUCLEAR REGULATORY COMMISSION

REGION II

4 7

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report No.:

50-261/95-19

Licensee:

Carolina Power and Light Company

P. 0. Box 1551

Raleigh, NC 27602

Docket No.:

50-261

License No.:

DPR-23

Facility Name: H. B. Robinson Unit 2

Inspection Conducted:

May 14 - June 17, 1995

Lead Inspector:

7-f 7___ 5_

T

T. Orders, Senior Resident Inspector

Date Signed

Other Inspectors: C. R. Ogle, Resident Inspector

P. J. Fillion, Reactor Inspector

W. Garne , Project Engineer

Approved by:

_

d__

___'____--_

__7-/7-9_

Dav'd M. Vefelli, Chief

Date Signed

Rea tor Projects Branch 1A

Division of Reactor Projects

SUMMARY

SCOPE:

This routine, resident inspection was conducted in the areas of plant

operations, maintenance activities, engineering efforts, and plant support

functions. The inspection effort included reviews of activities during non

regular work hours on May 14, 17, 21, 23, 30 and June 1, 2, 3, 4, 8, 14, and

17, 1995.

RESULTS:

Plant Operations [Paragraph 3]:

A violation was identified involving multiple examples of configuration

control events.

An unresolved item was identified involving racking-in of an SI pump breaker

with LTOPP in service.

A second unresolved item was identified involving loose paint in containment.

An improving trend in the material condition of components and structures in

the Auxiliary Building was noted.

9507240360 950717

PDR ADOCK 05000261

Q

PDR

2

Maintenance [Paragraph 4]:

A violation was identified involving an inadvertent RHR pump start during

maintenance.

A non-cited violation was identified involving personnel not following a FMEA

procedure.

Engineering [Paragraph 5]:

A non-cited violation was identified involving the licensee's failure to

incorporate load sequencing timer settings into appropriate design documents.

In the main, the licensee's performance in implementing the control room human

factors enhancement modification was good. However, the safety evaluation for

the modification did not accurately describe the effects of deletion of two

non-safety-related annunciator points from the control room. This fact

represents a weakness in the design control process.

The failure to identify a potentially intermittent abnormal auxiliary

feedwater pump sequencing response during surveillance testing was considered

a weakness.

REPORT DETAILS

1.

PERSONS CONTACTED

Licensee Employees:

W. Brand, Supervisor, Environmental and Radiation Control

  • M. Brown, Manager, Design Engineering
  • P. Cafarella, Superintendent, Mechanical Systems
  • A. Carley, Manager, Site Communications
  • B. Clark, Manager, Maintenance

D. Crook, Licensing/Regulatory Compliance

  • A. Garrou, Acting Manager, Licensing/Regulatory Programs

D. Gudger, Senior Specialist, Licensing/Regulatory Programs

  • M. Herrel, Manager, Training
  • C. Hinnant, Vice President, Robinson Nuclear Project

P. Jenny, Manager, Emergency Preparedness

  • K. Jensen, Supervisor, Reactor Systems
  • M. Knacszck, Superintendent, Projects

J. Kozyra, Licensing/Regulatory Programs

  • R. Krich, Manager, Regulatory Affairs

E. Martin, Manager, Document Services

  • B. Meyer, Manager, Operations
  • G. Miller, Manager, Robinson Engineering Support Section
  • J* Moyer, Manager, Nuclear Assessment Section
  • P. Musser, Manager, Plant Operations Assessment

W. Randlett, Manager, Security

B. Steele, Manager, Shift Operations

  • R. Stewart, Robinson Engineering Support Section
  • W. Stover, Manager, Operations Procedures

D. Taylor, Plant Controller

G. Walters, Manager, Support Training

R. Wardern, Manager, Plant Support Nuclear Assessment Section

W. Whelan, Industrial Health and Safety Representative

  • D. Whitehead, Manager, Plant Support Services

T. Wilkerson, Manager, Environmental Control

L. Woods, Manager, Technical Support

  • D. Young, Plant General Manager

Other licensee employees contacted included technicians, operators,

engineers, mechanics, security force members, and office personnel.

NRC Personnel:

  • W. Orders, Senior Resident Inspector
  • C. Ogle, Resident Inspector
  • P. Fillion, Reactor Inspector
  • L. Garner, Project Engineer
  • Attended one or more of the three exit interviews conducted for this

report necessitated by visiting RH inspectors.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2. PLANT STATUS AND ACTIVITIES

a.

Operating Status

The report period began with the unit in day 16 of refueling

outage 16.

Following the completion of planned outage work, with

the unit at normal operating temperature and pressure, an RCS leak

was identified on the main flange area of the C reactor coolant

pump. This forced a plant cooldown to conduct repairs. Following

these repairs, an orderly transition was made through plant fill,

heatup, and startup. The unit output breakers were shut on

June 21, 1995, day 54 of the outage.

b.

Other NRC Inspections and Meetings

P. Fillion, a Region II Reactor Inspector, was on site during the

week of May 22 - 26, 1995, to conduct an inspection of

modifications to the control room. Results of this inspection are

contained in this report.

L. Garner, a Region II Project Engineer, was on site during the

week of June 12 - 16, 1995, to conduct an inspection of station

modifications and major surveillance testing. Results of this

inspection are contained in this report.

3. OPERATIONS

a.

Plant Operations (71707)

The inspectors evaluated licensee activities to determine if the

facility was being operated safely and in conformance with

regulatory requirements. These activities were assessed through

direct observation, facility tours, discussions with licensee

personnel, as well as, management, evaluation of equipment system

status, and review of facility records.

Routine plant tours were conducted to evaluate equipment

operability, assess the general condition of plant equipment, and

to verify that radiological controls, fire protection controls,

physical protection controls, and equipment tagging procedures

were properly implemented. During routine inspections of the

Auxiliary Building by a Region II inspector, it was noted that the

external material condition of plant equipment had improved as

compared to that observed approximately two years ago. This

observation was based upon fewer components, such as valves, with

boron acid buildup due to leaks; leak catch container.usage has

become infrequent; and equipment and structural coatings (paint)

have been improved.

3

Clearance Procedure Error, Valve SI-883R

On May 26, 1995, the licensee experienced difficulties filling the

safety injection accumulators. The licensee determined that valve

SI-883R was shut with a clearance tag attached. This valve

isolates the accumulator fill header from the SI pump discharge

flowpath and is normally open. The tag was removed, the valve was

restored to the proper position, and a condition report was

generated. The inspectors were informed that the clearance tag

hanging on the valve was from a local clearance and test request

which had been canceled on May 2, 1995.

The inspectors interviewed the Operations personnel involved in

the disposition of the clearance tag found hanging on SI-883R,

reviewed all clearances identified as having been on the valve

during the current refueling outage, and reviewed licensee

procedures: Operations Management Manual Procedures, OMM-005,

Clearance and Test Request; OMM-001, Operations - Conduct of

Operations; and Plant Program Procedure, PLP-30, Independent

Verification.

The inspectors determined that an auxiliary operator and an

independent verifier initialled the clearance on May 2, 1995,

indicating that the valve was open and the tag removed.

Subsequently, a licensed senior reactor operator signed the

clearance attesting that all tags listed in the clearance were

accounted for. In fact these activities had not been accomplished

for valve SI-883R.

The AO and independent verifier stated that on May 2, they entered

the CV to both remove and install several clearances and that

working copies of the clearances were taken into the CV to

accomplish these activities. The AO stated that SI-883R was not

repositioned when the clearance tag was removed since other

clearance tags were attached to the valve which required that it

remain shut and he thought that he denoted that fact on the

working copy of the clearance. These individuals also informed

the inspectors that upon exiting the CV, the working copies of the

clearances and the tags were discarded as potentially contaminated

material. Contrary to the requirements of OMM-005, the tags which

had been removed were not "called-in" to the clearance center for

accountability before they were disposed of. When the AO and

independent verifier returned to the work control center, they

completed the master copy of the clearance from memory indicating,

in part, that SI-883R had been opened and the tag removed.

The inspectors interviewed the SRO who signed the clearance

attesting to the fact that all tags and caps associated with it

had been accounted for. He stated that he did not recall the

specifics of the clearance in question, but speculated that the

clearance may have been removed incrementally. He stated that

when clearances are removed in this fashion, caps and tags are not

4

retained until the clearance is completely removed and hence, no

final verification of tag accountability is performed. He stated

that in this situation, the licensed operator in the clearance

center relies on the initials on the clearance as the basis for

verification of accountability.

The inspectors concluded that the individuals involved in the

restoration of SI-883R failed to comply with the requirements of

OMM-005. This is identified as one of six examples which

collectively constitute a violation, 50-261/95-19-01: Operations

Configuration Control Events Concerning RHR Pump Flow Path,

SI-883R, Steam Driven Auxiliary Feedwater, And Containment

Ventilation Unit.

HVH-2 Run With Air Flowpaths Isolated

On May 26, 1995, during a tour of containment, the inspectors

noted an abnormal noise coming from containment recirculation fan

unit, HVH-2. The unit was running but the inlet damper and intake

butterfly valve were both closed. The inspectors notified the

control room and the unit was stopped. A condition report was

generated to address this issue.

The inspectors interviewed the control room SRO and two SROs

assigned to the clearance center at the time, reviewed Local

Clearance And Test Request 95-FO476 which was in force on the HVH

unit at the time of this observation, and evaluated Operations

Management Manual Procedure, OMM-005, Clearance And Test Request.

The inspectors determined that the inlet damper to HVH-2 was

failed closed as a result of instrument air supply to the damper

activator being isolated by clearance 95-FO476. The clearance did

not alter the position of the butterfly valve or its air supply

valve. The clearance specified that a CIT be affixed to the RTGB

control switch for HVH-2 to alert operators of the clearance. The

inspectors were informed that a CIT was not on the switch when the

unit was started. From a review of the clearance paperwork, the

inspectors noted that no signature or initials were recorded to

demonstrate that the CIT had been affixed.

The inspectors concluded that the failure to affix the CIT was

contrary to the requirements of OMM-005. This example constitutes

one of six examples which collectively comprise Violation 50-261/

95-19-01, Operations Configuration Control Events Concerning RHR

Pump Flow Path, SI-883R, Steam Driven Auxiliary Feedwater, And

Containment Ventilation Unit.

5

SI Pump Breaker Racked In With LTOPP In Service

At 5:26 a.m., on the morning of May 30, 1995, the A SI pump motor

breaker was racked in to fill the SI accumulators. Approximately

one minute later, the RCS vent path to containment was isolated

when the pressurizer PORVs were unblocked and shut in preparation

for placing LTOPP in service. At 5:31 a.m., this activity was

complete and LTOPP was declared in service. This configuration

existed until 6:08 a.m., when the SI pump breaker was again

racked-out.

Having an SI pump breaker racked in with the RCS not vented

appears to be contrary to licensee procedures and TS 3.3.1.3.

Pending a review of the licensing basis associated with TS 3.3.1.3

and LTOPP, this will be tracked as an Unresolved Item,

URI 50-261/95-19-02, SI Pump Breaker Racked-In With LTOPP In

Service.

RHR Pump Operated With No Flow

On June 3, 1995, the licensee was preparing to restart the unit,

having completed refueling. Using GP-002, Cold Shutdown To Hot

Subcritical At No Load TAVG, control room operators were

performing procedure steps to depressurize and cooldown the "A"

train of the RHR system after having isolated it from the Reactor

Coolant System. This is done by recirculating the RHR train

through its associated heat exchanger until it has been cooled

down to approximately 150* F. After approximately fifteen minutes

in this alignment, the operators noticed that they had not seen

the expected temperature decrease in the system. Initially, the

control room operators dispatched an AO to increase the amount of

component cooling water being supplied to the RHR heat exchanger.

The operators still did not see the expected temperature decrease,

so they dispatched an AO to check the position of valve RHR-743

which was to have been providing the recirculation flowpath.

Recirculation flow through this path is not indicated in the

control room. Initially, the AO reported that the valve was open.

The control room operators then instructed the AO to verify flow

on local indicator FI-608. The AO reported that there was no flow

indicated. It was concluded that valve RHR-743 was closed. The

AO was instructed to open the valve. After the valve was opened,

the control room operators detected an immediate decrease in

temperature of the RHR system. By this time, the A RHR pump had

been run for approximately 66 minutes with little or no

appreciable flow.

Valve RHR-743 had been verified to be open on May 28, 1995, during

the performance of Operations Surveillance Test OST-163, Safety

Injection Test, and is required to be open as an Initial Condition

of GP-002. Ultimately, this mis-configuration resulted in the A

RHR pump being declared inoperable. This in turn forced the

6

licensee to return the unit to cold shutdown to facilitate the

disassembly and inspection of the pump.

The misalignment of valve RHR-743 constitutes one of six examples

which collectively constitute Violation 50-261/95-19-01,

Operations Configuration Control Events Concerning RHR Pump Flow

Path, SI-883R, Steam Driven Auxiliary Feedwater, And Containment

Ventilation Unit.

On June 9, 1995, after the A RHR pump had been inspected and

reassembled, control room operators were aligning the pump to

place it in service. At the time, the B RHR pump was supplying

decay heat removal in a configuration which bypassed its heat

exchanger. In this configuration, valve HCV-758, the common

discharge from both RHR trains' heat exchangers, was closed. The

operators started the A RHR pump, and stopped the B pump. They

immediately noticed that RHR flow decayed rapidly, restarted the B

pump and secured the A pump. Ultimately, the operators determined

that valve HCV-758 was closed and the A RHR pump had been started

without a flow path. The operators opened cross connect valve,

RHR-757C, restarted the A pump and successfully placed it in

service. The pump was operated for approximately two minutes with

only minimal flow afforded by the fact that valve HCV-758 leaked

by.

The inspectors concluded that procedure OP-201 was inadequate in

that it did not align the system to facilitate a flow path for the

A RHR pump before having the operator start it. This constitutes

one of six examples which collectively comprise Violation

50-261/95-19-01, Operations Configuration Control Events

Concerning RHR Pump Flow Path, SI-883R, Steam Driven Auxiliary

Feedwater, And Containment Ventilation Unit.

Reduced Inventory Operations

On June 9, 1995, the licensee initiated a draindown of the RCS in

accordance with GP-008, Draining The Reactor Coolant System, to

facilitate repairs of a leak on the main flange of RCP C. During

the repairs, RCS level was reduced to 43 inches below the main

vessel flange.

The inspectors reviewed the licensee's preparations for entry into

the reduced inventory condition on June 7, 1995. Licensee

preparations and precautions for a reduced inventory/mid-loop

operations were reviewed by the inspector. No deficiencies were

noted during this review. The inspectors witnessed portions of

the draindown on June 9; as well as, RCS level stabilization

immediately following draindown termination on June 10, 1995.

Additionally, the inspectors monitored operator performance during

routine control room tours while RCS inventory was below the

flange.

7

The inspectors concluded that appropriate sensitivity to risks

associated with operation in reduced inventory was displayed by

Operations personnel and the performance of operators during this

evolution was good.

AFW Pump Auto Start During Generator Draindown

At 5:33 p.m., on June 14, 1995, both MDAFW pumps started and the

SG blowdown isolation valves on all three SGs closed due to a low

low level in steam generator B. This occurred while draining the

steam generators in preparation for plant startup. In response to

this event, the operators defeated the AFW pump auto-start logic,

stopped the MDAFW pumps, and reopened the blowdown isolation

valves. AT 6:53 p.m. that day, the licensee made a 4-hour non

emergency report to the NRC in accordance with 10 CFR 50.72

(b)(2)(ii), ESF Actuation. A condition report was generated by

the licensee.

In response to this event, the inspectors reviewed Operating

Procedure OP-406, Steam Generator Blowdown/Wet Layup System;

Administrative Procedure AP-006, Procedure Use And Adherence; log

entries associated with the event; and Operations Management

Manual Procedure OMM-001, Conduct of Operations; reviewed the

auxiliary feedwater pump startup logic diagram, the ERFIS sequence

of events printout, the events notification worksheet, and

interviewed the AO and SRO involved in the event.

The inspectors determined that the event occurred as a result of a

failure by Operations personnel to appropriately block the SG low

and low-low level signals from the MDAFW autostart logic circuit

during the draindown of the generators. Blocking these inputs is

performed by repositioning 4 key switches in the back of the RTGB

from the "normal" to "defeat" position.

Draining of the steam generators was performed in accordance with

OP-406. This procedure requires that the 4 key switches be taken

to the "defeat" position prior to draining the generators. The

inspectors noted that although the AO initialed OP-406 as having

verified these key switches were positioned to the defeat

position, the switches were found in the "normal" position

following the event. The AO stated that while performing OP-406,

he called the SRO in the control room to request verification that

the 4 key switches were in the "defeat" position. Based on the

SRO's confirmation, the AO initialed the verification steps in the

procedure and continued.

The SRO advised the inspectors that his confirmation of the

defeated autostart circuit was based on noting the Train A and

Train B AFW Auto Initiation Defeated warning lights on the RTGB

were illuminated. This approach was flawed since these warning

lights can be illuminated without the 4 key switches specified in

OP-406 being in defeat position.

8

The inspectors concluded that the failure to adequately verify the

position of the 4 key switches prior to draining the steam

generators was contrary to the requirements of OP-406. This is

identified as one of six examples which collectively constitute

VIO 50-261/95-19-01, Operations Configuration Control Events

Concerning RHR Pump Flow Path, SI-883R, Steam Driven Auxiliary

Feedwater, And Containment Ventilation Unit.

Inadequate Containment Closeout

On June 3 and 4, 1995, the inspectors conducted inspections of

containment to verify the adequacy of the licensee's containment

closeout. This closeout was conducted in accordance with Plant

Program Procedure PLP-006, Containment Vessel Inspection/Closeout.

The areas toured by the inspectors included, but were not limited

to: all pump bays, the pressurizer cubicle, and the operating

deck. Numerous examples of loose tools, equipment and debris were

identified by the inspectors and reported to the licensee.

Additional cleanup of the CV was conducted by the licensee.

The plant startup was subsequently aborted and the RCS cooled down

to conduct repairs to RCP C. After the repairs to RCP C were

complete, the licensee commenced an RCS heatup in preparation for

reactor plant startup. Following the licensee's completion of

PLP-006, the inspectors again conducted a containment inspection

to verify the adequacy of the licensee's closeout. While the

general cleanliness had improved, the inspectors again found

numerous examples of loose equipment and debris. These were again

identified to the licensee for disposition.

Due to their size and weight, it is probable that many of the

items identified by the inspectors would not have been transported

to the ECCS sump during a LOCA. However, given the abundance, the

ease of detection, and prior inspector observations of deficient

CV closeout, the inspectors concluded that the licensee's efforts

at CV closeout were inadequate. This is identified as a weakness

in the licensee's containment closeout process.

Throughout the outage and following tours of containment, the

inspectors expressed concerns to licensee management regarding

loose paint in containment. Primarily, these concerns centered on

numerous areas of loose paint on the floor of the first level of

the CV, but the inspectors also noted areas of peeling or loose

paint on the operating deck, polar crane, and several of the HVH

units.

In response to these concerns, the licensee removed some of the

loose paint from the floors in containment and the HVH units and

provided the inspectors with documentation related to the generic

issue of loose paint in containment. This information did not

completely resolve the situation at H.B. Robinson. Pending

9

further review, this issue this is identified as an Unresolved

Item 50-261/95-19-03, Loose Paint In Containment.

b.

Followup - Operations (92901)

Inadequate Clearance For Work On Valve V1-8A

On April 17, 1995, routine preventive maintenance was to be

performed on valve V1-8A, one of three motor-operated valves which

supply motive steam to the SDAFW pump. Valve MS-20 which is

immediately upstream of V1-8A, was not closed. As a result, the

SDAFW pump started when valve V1-8A was opened.

At the end of report period for Inspection Report 95-14, the

inspectors had not completed their review of the circumstances

associated with this event. Accordingly, this issue was tracked

as Unresolved Item, 50-261/95-14-02, Inadequate Clearance For Work

On Valve V1-8A.

The inspectors reviewed the clearance, 95-00748, and reviewed

Operations Management Procedure OMM-005, Clearance And Test

Request. The clearance did not address valve MS-20. At the time

of the event, valve MS-20 was open. Accordingly, when valve V1-8A

was opened, steam was admitted to the SDAFW pump resulting in an

inadvertent start.

Procedure OMM-005, requires in part that all valves necessary to

protect personnel and equipment are properly closed or open as

necessary.

Clearance LCTR 95-00748 was inadequate in that it did not specify

a position for valve MS-20. Ultimately, this resulted in a

misconfiguration and inadvertent operation of the SDAFW pump.

It is noted that the planning of this work activity was inadequate

in that the maintenance on V1-8A did not adequately address the

operability of the SDAFW pump. When V1-8A was opened during the

event, and the "SDAFW Pump Low Discharge Pressure Trip"

annunciator was received, operations personnel questioned the

operability of the pump. Operations personnel appropriately

declared the pump inoperable and entered TS 3.4.4. until the

operability concern could be resolved.

The operability evaluation was performed by the system engineer.

Using the electrical logic and control wiring diagrams, the system

engineer concluded that the SDAFW pump would be inoperable if

V1-8A were greater than 96 percent open and the SDAFW pump had not

started, since valves V1-8B and V1-8C, the other two steam supply

valves to the SDAFW pump, would not open upon the receipt of a

valid start signal.

10

Historically, this preventative maintenance had been performed

with the unit in cold shutdown, this was the first time it had

been attempted with the unit on line. Although this activity had

been reviewed by operations and technical support personnel,

operability of the SDAFW pump had not been adequately evaluated.

During the event, annunciator APP-007-F5, "SDAFW Pump Low

Discharge Pressure Trip,"

was received. It is believed this

alarm may have been received during past performance of this

maintenance; however, operability of the pump was not questioned

at that time since the plant had been in cold shutdown during the

activity.

The technical review of this work activity was inadequate in that

the planned activity resulted in the misconfiguration and

inoperability of the SDAFW pump.

This issue constitutes one of six examples which collectively

comprise Violation 50-261/95-19-01, Operations Configuration

Control Events Concerning RHR Pump Flow Path, SI-883R, Steam

Driven Auxiliary Feedwater, And Containment Ventilation Unit.

Unresolved Item 50-261/95-14-02, Inadequate Clearance For Work On

Valve V1-8A is closed.

4.

MAINTENANCE

a.

Maintenance Observation (62703)

The inspectors observed safety-related maintenance activities on

systems and components to ascertain that these activities were

conducted in accordance with TS, approved procedures, and

appropriate industry codes and standards. The inspectors

determined that these activities did not violate LCOs and that

required redundant components were operable. The inspectors

verified that required administrative, material, testing,

radiological, and fire prevention controls were adhered to. In

particular, the inspectors observed/reviewed the following

maintenance activities detailed below:

WR/JO 94-AQYY1

Thermal Overload Testing (SI-860B)

WR/JO 95-AGGG1

Troubleshoot Cause Of Instrument Air

Compressor Breaker Fire

SP-1329

Flux Thimble Replacement

WR/JO 95-AHDB1

Troubleshoot RHR Pump Fails To Start

During OST-163

Upper Internals Installation

On May 22, 1995, the inspectors witnessed the installation of the

reactor vessel upper internals which was accomplished in

accordance with Maintenance Refueling Procedure MRP-005, Upper

Internals Removal and Installation. Overall, the internals lift

and installation were well conducted. However, the inspectors

noted that the subsequent lifting rig removal and return to the

storage stand were not as well orchestrated. During this phase of

the evolution, the inspectors observed the lifting rig impact the

manipulator crane, the wall of the refueling cavity, and an

electrical cord at the side of the cavity. None of these impacts

was particularly severe, but, this performance represented a

marked degradation below that observed by the inspectors for the

same basic activities only moments before. The inspectors

discussed these observations with the refueling coordinator and

were subsequently advised that a Condition Report would be

initiated to address this event.

FMEA Procedure Not Followed

On May 23, 1995, during a routine tour of containment, the

inspectors observed a worker in the reactor vessel head storage

area who was not logged into the area on the posted Foreign

Material Accountability Log Sheet. When questioned, the

individual acknowledged not logging into the area and attributed

his failure to not observing the warning sign posted at the

entrance to the FMEA area. The individual exited the area and a

condition report was generated. The inspectors were advised later

that the individual was counselled by licensee management on his

actions.

In response to this issue, the inspectors reviewed Plant Programs

Procedure PLP-047, Foreign Material Exclusion Area Program. The

inspectors also reviewed the condition report generated by the

licensee and interviewed the responsible supervisor. From this

review, the inspectors noted that PLP-047 established the head

storage area as a FMEA. As such, the individual was required to

log into the area and abide by other requirements to minimize the

potential of foreign material introduction into the reactor vessel

head. Overall, the inspectors concluded that the worker's failure

to log into the area was a violation of the requirements of

PLP-047. This failure constitutes a violation of minor

significance and is being treated as a non-cited violation,

consistent with Section VII of the NRC Enforcement Policy. This

is identified as NCV 50-261/95-19-04, FMEA Procedure Not Followed

In Head Storage Area.

Vessel Head Lift

On May 24, 1995, the inspectors witnessed a portion of the reactor

vessel head installation accomplished in accordance with

Maintenance Refueling Procedure, MRP-004, Reactor Vessel Head

Removal and Installation. This observation included head movement

from the storage stand to placement on the vessel.

The inspectors

12

also attended the pre-job brief. Overall, the conduct of the

evolution was good. Noteworthy strengths included lift team

coordination and communications. Strong management involvement

was also observed.

Inadvertent RHR Pump Start

On May 29, 1995, the inspectors witnessed portions of

troubleshooting performed to determine the cause of the B RHR pump

not starting during the performance of Operations Surveillance

Test OST-163, Safety Injection Test and Emergency Diesel Generator

Auto Start On Loss Of Power And Safety Injection And Emergency

Diesel Trips Defeat.

To facilitate troubleshooting, the RHR pump motor breaker was

racked to the test position. A defective relay was detected which

was removed, and taken to the I & C shop for further

troubleshooting. Subsequently, Operations racked-in the pump

motor breaker in the event RHR B pump was needed since the normal

pump starting circuitry was not affected by the aforementioned

relay. A member of the I & C troubleshooting team was informed of

the change in breaker position, but failed to advise the other

individuals involved in the repair effort.

Subsequently, a new relay was installed and when jumpers were

installed to verify its proper operation, the RHR pump motor B

started. Control room personnel immediately secured the pump.

Ultimately, the B RHR pump was successfully tested during a later

part of OST-163.

10 CFR 50, Appendix B, Criterion XIV requires that measures be

established for indicating the operating status of structures,

systems, and components, to prevent inadvertent operation. The

inspectors concluded that the licensee failed to establish

adequate measures to prevent the inadvertent start of the RHR

pump. This is contrary to the requirements of 10 CFR 50

Appendix B and is identified as a violation, VIO 50-261/95-19-05,

RHR Pump Start Due To Troubleshooting.

b.

Surveillance Observation (61726)

The inspectors observed certain safety-related surveillance

activities on systems and components to ascertain that these

activities were conducted in accordance with license requirements.

For the surveillance test procedures listed below, the inspectors

determined that precautions and LCOs were adhered to, the required

administrative approvals and tagouts were obtained prior to test

initiation, testing was accomplished by qualified personnel in

accordance with an approved test procedure, test instrumentation

was properly calibrated, the tests were completed at the required

frequency, and that the tests conformed to TS requirements. Upon

test completion, the inspectors verified the recorded test data

13

was complete, accurate, and met TS requirements, test

discrepancies were properly documented and rectified, and that the

systems were properly returned to service. Specifically, the

inspectors witnessed and/or reviewed portions of the following

test activities:

OST-163

Safety Injection Test and Emergency Diesel

Generator Auto Start On Loss Of Power And

Safety Injection And Emergency Diesel

Trips Defeat

SP-1246

Reactor Vessel Level Instrumentation

(System Calibration)

No violations or deviations were identified.

5.

ENGINEERING

Emergency Load Sequencing Timers (92903)

OST-163, Safety Injection Test And Emergency Diesel Generator Auto

Start On Loss Of Power And Safety Injection And Emergency Diesel

Trips Defeat, revision 24, included verification that emergency

loads sequenced onto the emergency buses at the appropriate times.

During two partial OST-163 performances on May 28, most of the

individual loads sequenced onto the emergency buses approximately

0.1 or 0.2 seconds outside the procedure's acceptance criteria.

Subsequent licensee investigation determined that the timing

relays had been improperly set earlier in that RFO.

The timers

were recalibrated and the applicable portion of OST-163 involving

the emergency bus load timing sequences was successfully completed

on May 29.

The inspectors reviewed the circumstances surrounding the improper

timer calibrations. Documents reviewed included: M-1035,

Emergency Load Sequencer Relay Replacement, and its field

revisions 1 and 4, that installed and initially calibrated the

digital timing relays; draft SP-1056, Time Delay Relay Calibration

Safeguards Train B, that was written but never issued to calibrate

the B train timing relays; Maintenance Procedure Revision/New

Procedure Request Form dated August 6, 1993, that requested

maintenance write calibration procedures for the timers; PIC-018

(020), Time Delay Relay Calibration Safeguards Train B (A), and

their associated document review packages and safety analyses; and

completed PIC-018 and 020 performed this RFO. In addition, the

inspectors interviewed cognizant maintenance and engineering

personnel who were either involved with the development of PIC-018

and 020 or participated in the investigation into the calibration

problem. The system engineer who developed the draft SPs and

interfaced with maintenance during M-1035 implementation and the

14

development of PIC-018 and 020 had retired from the company. The

inspectors confirmed that the licensee's investigation had

identified the contributing causes that resulted in the timers

being improperly calibrated during that RFO.

CR No. 95-01379, approved June 7, 1995, documented the causes and

proposed corrective actions to address the improper timer

calibrations. The primary cause was personnel error that resulted

in a failure to ensure design values developed for field

Revision 4 to M-1035 were properly transferred to design

documents.

For example, drawing 5379-3238 was not revised to

reflect that the actual timer set points were to be adjusted for

the times required for the logic circuits to actuate and close

their associated load breakers. A planned corrective action

identified in CR 95-01379 was to provide lessons learned from the

event to the engineering staff. Also, optimum timer settings were

to be established and associated maintenance procedures revised

accordingly. The inspectors considered that these actions were

appropriate to preclude recurrence of this event.

The failure to incorporate design information into appropriate

design documentation such that sequencing timer calibration

procedures were established with improper values was a violation

of 10 CFR 50, Appendix B, Criterion III.

The violation has

minimal safety significance, in that, the amount the timers were

outside the expected values was not sufficient to adversely

affect emergency bus loadings and the unit was never operated with

the improper settings. This licensee identified and corrected

violation is being treated as a non-cited violation consistent

with Section VII of the NRC Enforcement Policy. Thus, this item

is identified as NCV 50-261/95-19-06, Failure To Incorporate

Sequencing Timer Settings Into Appropriate Design Documents.

During the event review, the inspectors identified that during the

second test performed on May 28, the A AFW pump breaker closed

approximately 0.8 seconds later than the B AFW pump breaker.

Review of the previous three tests (two in 1993) and the

subsequent successful test on May 29, revealed that the A AFW pump

breaker typically closed within 0.1 seconds of the B AFW pump

breaker. Maintenance personnel indicated that they had taken no

action to review the occurrence since Operations had not informed

them of the abnormal reading. Further review revealed that

personnel performing the test and reviewing the test results had

failed to identify this discrepancy. Not performing a

sufficiently detailed review of OST-163 test data to identify a

potentially intermittent condition for additional review or future

monitoring was considered a weakness.

During this inspection, the inspectors noted that the calibration

frequency for the sequencing timers was every third RFO.

Comparison of the as-left timer settings from M-1035 field

revision 4 and the as-found values per calibration procedures

15

PIC-018 and 020 indicated that the timers had drifted a maximum of

0.8% (0.04 seconds) between December 1989 and May 1995. Thus, the

inspectors concluded that an every third RFO calibration interval

was acceptable.

Electrical Maintenance and Modifications (62705)

During the refueling outage, the licensee implemented

modifications to the main control room aimed at improving the

layout from the human factors viewpoint. The modification

consisted of removing a fairly large control panel, which was

greatly under utilized as a result of previous modifications.

Removal of the panel created additional space in the central area

of the control room. Operator work stations were relocated and

upgraded thus achieving improved use of space in the control room.

Plant related non-safety annunciators which had been on the

deleted control panel were relocated within the control room, and

non-safety 230 Kv breaker status lamps were replaced by ERFIS data

points. A number of safety-related cables which had been routed

through the deleted control panel were removed and rerouted using

new cable. The modification was implemented under Engineering

Services Request (ESR) No.94-882.

Due to extensive wiring changes taking place in a relatively short

time period, the NRC inspected the controls that the licensee

employed to ensure that the changes were correctly implemented.

Requirements relevant to the area of inspection were 10 CFR 50.59,

Changes, Tests and Experiments, and 10 CFR 50, Appendix B,

Criterion III, Design Control.

The inspection focused on wiring changes. Specific inspection

activities and findings were as follows:

Walkdown inspection of the equipment, raceways and cables in

the main control room, relay panels/spreading room and

control room roof involved with ESR 94-882. The inspector

concluded that the work was done according to the licensee's

installation specification, including conduit fill and

pulling points, and the quality of workmanship was good.

In relation to safety-related cables C21732C and C21732D,

which were multi-conductor cables selected at random, the

inspector verified the following attributes: wires were

landed on the correct relay panel terminals, correct size

lugs were used, and correct size crimping tool was used. In

addition, the inspector verified calibration of the crimping

tool.

The inspector reviewed the completed post-modification test

sheets for the modified circuits, and verified that the

testing was adequate and results good.

16

The inspector was told that annunciator points associated with

switchyard equipment were deleted from the control room by ESR 94-882. These points were:

OCB 52-8 [generator breaker] failure detection trouble

North 230 kV bus breaker failure lockout

North 230 kV bus differential lockout

OCB 52-9 [generator breaker] failure detection trouble

It could not be determined during the inspection what the original

basis was for having these particular four points in the main

control room. The inspector inquired as to whether important

information was lost as a result of deletion of these annunciator

points. The system engineer assigned to coordinate with the

Transmission Department stated that these four points were

repeated on an annunciator in the switchyard relay house. He also

stated the annunciator points were repeated at the transmission

system control center in Raleigh, N. C., and that the dispatcher

would notify the nuclear plant control room operator should the

annunciator go to alarm condition. The inspector indicated to the

licensee that he wanted to verify the annunciators in the

switchyard relay house. This activity was scheduled for the

following day. The following day the system engineer stated that

the two generator breaker failure detection trouble annunciators

were not at the annunciator panel in the switchyard relay house

and therefore were not repeated at the Raleigh center. Instead,

the breaker failure relays were monitored by lamps, which were

mounted on the front of the respective breaker control panels. A

supervisory lamp is considerably different than an annunciator

because an annunciator gives immediate information to system

operators whereas a lamp can only give information when operators

visit the relay house, which was reported to be about once per

month. The inspector went to the relay house and verified the

annunciator inscriptions and the breaker failure supervisory

lamps.

The safety evaluation for ESR 94-882 indicated the following: "The

switchyard annunciator APP-033 alarm lights on the 230 kV Line

Panel are removed. Alarms for four of the lights are repeated on

an annunciator in the switchyard building. The activity maintains

the alarm functions associated with APP-033." The design basis

document for ESR 94-882 indicated that: "The annunciator lights

[from APP-033] are not required since their functions are repeated

elsewhere; therefore, these lights will be deleted from the

control room."

The inspector noted that the safety evaluation and the design

basis document did not accurately describe the change because, as

stated above, two of the annunciators in question were in fact not

repeated elsewhere. The fact that these documents were not

accurate in this regard was considered significant by the

inspector. As far as could be determined through discussions with

17

licensee personnel, persons preparing the safety evaluation

misinterpreted statements made by transmission system engineers as

to the design of the annunciators at the relay house. More

significantly, apparently no attempt was made to verify the

particular description in the safety evaluation. The inspector

concluded that the safety evaluation could be revised to support

deletion of the two non-safety-related annunciators in question.

The fact that the original information was not correct represents

a weakness in the sense that, should the licensee continue to

allow unverified statements to form the basis for conclusions in

their safety evaluations, inadequate safety evaluations could

result.

Overall, the inspector concluded that the wiring changes to the

main control room performed under ESR 94-882 were well

implemented. This conclusion was based on results of walkdown

inspections, detailed verification of representative cables, the

post-modification test results, and discussions with engineers.

6.

EXIT INTERVIEW

The inspectors met with licensee representatives (denoted in paragraph

1) at the conclusion of the inspection on June 28, 1995. During this

meeting, the inspectors summarized the scope and findings of the

inspection as they are detailed in this report. The licensee

representatives acknowledged the inspector's comments and did not

identify as proprietary any of the materials provided to or reviewed by

the inspectors during this inspection. No dissenting comments from the

licensee were received.

Item Number

Status

Description

URI 95-14-02

Closed

Inadequate Clearance For Work On

Valve V1-8A.

VIO 95-19-01

Opened

Operations Configuration Control

Events Concerning RHR Pump Flow

Path, SI-883R, Steam Driven

Auxiliary Feedwater, And Containment

Ventilation.

URI 95-19-02

Opened

SI Pump Breaker Racked-In With LTOPP

In Service.

URI 95-19-03

Opened

Loose Paint In Containment.

NCV 95-19-04

Open/Closed

FMEA Procedure Not Followed In Head

Storage Area.

VIO 95-19-05

Opened

RHR Pump Start Due To

Troubleshooting.

Item Number

Status

Description

NCV 95-19-06

Opened/Closed

Failure To Incorporate Sequencing

Timer Settings Into Appropriate

Design Documents.

7.

ACRONYMS AND INITIALISMS

AFW

Auxiliary Feedwater

AO

Auxiliary Operator

CFR

Code Of Federal Regulation

CIT

Clearance Information Tag

CR

Control Room, Condition Report

CV

Containment Vessel

ECCS

Emergency Core Cooling System

ERFIS

Emergency Response Facility Information System

ESF

Engineered Safety Feature

FMEA

Foreign Material Exclusion Area

HVH

Heating Ventilation Handling

I&C

Instrumentation And Control

LCO

Limiting Condition for Operation

LOCA

Loss Of Coolant Accident

LTOPP

Low Temperature Over Pressure Protection

MDAFW

Motor Driven Auxiliary Feedwater

OMM

Operations Management Manual

PLP

Plant Program Procedure

PORV

Power Operated Relief Valve

RCP

Reactor Cooling Pump

RCS

Reactor Coolant System

RHR

Residual Heat Removal

SDAFW

Steam Driven Auxiliary Feedwater

SG

Steam Generator

SI

Safety Injection

SRO

Senior Reactor Operator

TS

Technical Specification