ML14178A194

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Insp Rept 50-261/92-02 on 920114-0207.Violation Noted.Major Areas Inspected:Operational Safety Verification,Surveillance Observation,Maint Observation & self-assessment
ML14178A194
Person / Time
Site: Robinson 
Issue date: 02/25/1992
From: Christensen H, Garner L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14178A192 List:
References
50-261-92-02, 50-261-92-2, IEB-80-11, NUDOCS 9203100039
Download: ML14178A194 (13)


See also: IR 05000261/1992002

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION-II

<

101 MARIETTA STREET,N.WV.

ATLANTA, GEORGIA 30323

Report No.:

50-261/92-02

Licensee:

Carolina Power and Light Company

P. 0. Box 1551

Raleigh, NC 27602

Docket No.:

50-261

License No.: DPR-23

Facility Name: H. B. Robinson

Inspection Conducted:

January 14, 1992 -

February 7, 1992

Lead Inspector:

L'.

. Gar er, Senior Resident kfispector

Date Signed

Other Inspector: M. . Hunt, Reactor Engineer

K. . Jury, Resident Inspector

)

Approved

v:

. 0. hristensen, Section Chief*

Da e igned

Divisi n of Reactor Projects

SUMMARY

Scope:

This routine, announced inspection was conducted in the areas of operational

safety verification, surveillance observation, maintenance observation,

self-assessment, and follow-up.

Results:

A violation was identified for failure to adequately perform stroke timing of

two containment isolation valves in the manner required by the test procedure

(paragraph 3).

A non-cited violation was identified involving the failure of existing

procedures to contain adequate instructi.ons to completely test the motor

driven auxiliary feedwater subsystem initiation circuitry as required by

Technical Specification 4.8.5 and Table 4.8-1 (paragraph 3).

920a3100039 920225

PDR

ADOCK 05000261

PDR

2

Preliminary Individual Plant Examination results identified two scenarios as

contributing approximately 71 percent of the plant's 1.7E-03 total core damage

frequency.

The scenarios were a reactor coolant pump seal loss of coolant

accident (LOCA)

induced by the loss of all component cooling water pumps and

an inter-system LOCA initiated by leakage from the primary system into the

residual heat removal system (paragraph 2).

Two lower pistons were replaced in the emergency diesel generator A's engine

after the vendor notified the licensee via a 10 CFR Part 21 notification that

the pistons could contain a manufacturing flaw (paragraph 2).

A Nuclear Assessment Department audit of the Environmental

and Radiation

Control Unit identified poor radiological work practices and an ineffective

self-audit program as potential issues (paragraph 2).

In 1991 the site experienced the lowest person-rem site exposure, smallest

quantity of radwaste shipped, and smallest contaminated area since these items

have been trended (paragraph 2).

Design Basis Documentation discrepancies were being adequately evaluated and

appropriately addressed (paragraph 2).

Addressing corrective actions to preclude recurrence on non-significant

Nuclear Engineering Department

(NED)

Adverse Condition Reports (ACR)

was a

good practice. However,

an 1991 third quarter NED ACR trend report indicated

that procedures and methods may not establish conditions that effectively

prevent the occurrence of an adverse condition (paragraph 5).

REPORT DETAILS

1. Persons Contacted

  • R. Barnett, Manager, Outages and Modifications
  • D. Bauer, Regulatory Compliance Coordinator, Regulatory Compliance
  • R. Chambers, Plant General Manager, Robinson Nuclear Project

D. Crook, Senior Specialist, Regulatory Compliance.

J. Curley, Manager, HBR Engineering Support Section, Nuclear Engineering

Department

  • C. Dietz, Vice President, Robinson Nuclear Project
  • J. Dobbs, Manager, Nuclear Assessment Department Site Unit

R. Femal, Shift Supervisor, Operations

  • W. Flanagan, Jr., Manager, Operations
  • W. Gainey, Manager, Plant Support
  • J. Kloosterman, Manager, Regulatory Compliance

D. Knight, Shift Supervisor, Operations

A. McCauley, Manager -

Electrical Systems, Technical Support

R. Moore, Shift Supervisor, Operations

  • M. Olinger, Senior Engineer, Nuclear Engineering Department Site Unit

R. Oliver, Manager - Risk Assessment, Nuclear Engineering Department

A. Padgett, Manager, Environmental and Radiation Control

M. Page, Manager, Technical Support

D. Seagle, Shift Supervisor, Operations

M. Scott, Manager - Support Systems, Technical Support

  • R. Smith, Manager, Maintenance

W. Stover, Shift Supervisor, Operations

D. Winters, Shift Supervisor, Operations

Other licensee employees contacted included technicians, operators,

engineers, mechanics, security force members, and office personnel.

  • Attended exit interview on February 12, 1992.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2. Operational Safety Verification (71707)

The inspectors evaluated licensee activities to confirm that the facility

was

being operated safely and in conformance with regulatory

requirements.

These activities were confirmed by direct observation,

facility tours, interviews and discussions with licensee personnel and

management, verification of safety system status, and review of facility

records.

2

To verify equipment operability and compliance with TS,

the inspectors

reviewed shift logs, Operation's records, data sheets, instrument traces,

and records of equipment malfunctions.

Through work observations and

discussions with Operations staff members,

the inspectors verified the

staff was knowledgeable of plant conditions, responded properly to

alarms,

adhered to procedures and applicable administrative controls

except as discussed below, cognizant of in-progress surveillance and

maintenance activities, and aware of inoperable equipment status.

The

inspectors performed channel verifications and reviewed component status

and safety-related parameters to verify conformance with TS.

Shift

changes were observed,

verifying that system status continuity was

maintained and that proper control room staffing existed.

Access to the

control room was controlled and operations personnel carried out their

assigned duties in an effective manner.

Control room demeanor and

communications were appropriate.

Plant tours and perimeter walkdowns were conducted to verify equipment

operability, assess the general condition of plant: equipment,

and to

verify that radiological controls, fire protection controls, physical

protection controls,

and equipment tagging procedures were properly

implemented.

Preliminary IPE Results

On January 13,

1992, the licensee informed Region II of preliminary IPE

results which indicated a total CDF of 1.7E-03 per reactor year.

On

January 14,

the licensee reviewed these preliminary results in more

detail with NRR and Region II. Two scenarios, transient-induced LOCA and

interfacing system LOCA, account for 76.4 percent of the total CDF.

The major contributor to the transient-induced LOCA CDF was a common mode

failure of the CCW pumps which cascades into a loss of RCP seals and a

loss of ECCS. A loss of CCW would result in the direct loss of cooling

to the RCP thermal barrier coolers and loss of cooling to the charging

pump coupling oil coolers.

The failure of the charging pumps would

result in the loss of RCP seal injection cooling water, i. e., a loss of

all cooling to the

RCP

seals resulting in RCP

seal

failures.

Simultaneously CCW cooling to the SI and RHR seal coolers would also be

interrupted causing failure of the ECCS pumps.

This slow moving daisy

chain of events could be stopped by manually supplying cooling water to

the charging pump coupling oil cooler.

Temporary instructions were

issued on January 15,

1992,

to provide procedural steps for connecting

fire water from a nearby hose station to the existing couplings on the

charging pump coupling oil coolers.

The inspectors verified that'these

temporary instructions were adequate,

had been disseminated to the

operating shifts, and all the equipment necessary for the temporary

cooling connection had been pre-staged.

3

  • The primary contributor to the interfacing system LOCA was leakage

through the normally closed RHR-750 and 751 valves, the RHR system

suction valves from the RCS hot leg, which initiates an unisolable LOCA

in the low pressure RHR system.

This coolant leakage could also steam

bind the ECCS pumps thus preventing the them from performing their safety

function.

The relative large contributor of this scenario to the CDF

resulted from the probability of the valves' double disk gate failures

due to not periodically leak testing these valves.

Leak testing every

refueling interval would result in the calculated interfacing system LOCA

contribution to the total CDF being reduced by approximately two orders

of magnitude. The licensee plans to leak test these valves during RO 14

which is scheduled to begin on March 27, 1992.

The inspectors verified

that at the end of the report period the outage schedule was being

modified to include RHR-750 and 751 valve leak testing.

Implementation of the above described procedure change and leak testing

of the RHR-750 and 751 valves will reduce the total CDF from 1.7E-03 to

4.9E-04 per reactor year.

The inspectors will continue to follow-up on

the proposed actions as part of the routine inspection program.

B Inverter Malfunction

On January 23,

1992,

the B inverter which supplies power to protection

and control circuits on instrument busses #3 and #8 was observed to have

an erratic output voltage, i. e. indicated

voltage swings of

approximately 15 volts.

Operations declared the inverter inoperable and

placed the instrument busses on their alternate supply. The inverter was

repaired by replacing the capacitors on one of the inverter's circuit

cards.

The inverter was then placed back in operation and observed for

approximately one hour prior to returning it to service.

The inspectors

observed the inverter's removal from service, troubleshooting activities,

and its return to service.

The inspectors observed that operating

personnel

took prudent precautionary measures

such

as placing the

feedwater control system in manual during the time the instrumentation

busses were being transferred.

Part 21 Involving Pistons With Manufacturing Flaws

On January 29,

1992, Coltec Industries Inc. notified the licensee that a

Part 21 report was being issued concerning the potential for piston

cracking due to a manufacturing defect.

The Part 21 Report was

apparently only applicable to HBR since vendor records indicated that HBR

is the only nuclear plant which has a Fairbanks Morse EDG with rotating

pistons. The vendor recently determined that circumferential cracking of

diesel generator pistons in and immediately below the piston ring grooves

was traceable to one foundry which had supplied castings to Coltec

Industries Inc..

The foundry has now corrected the manufacturing process

problem.

Review of records revealed that four lower pistons supplied for

HBR's EDGs in 1989 and 1991 may have come from the suspect castings. The

licensee determined that two of the suspect pistons were stored in the

warehouse; however, the other two pistons had been installed during the

-4

last refueling outage in cylinders #2 and #8 of the A EDG

.

Further

review of records was unable to determine if

these pistons had been

manufactured from the suspect castings.

Thus, on February 3, 1992, the

licensee determined that it was prudent to replace the two pistons in the

A EDG.

The inspectors observed the piston replacement on that day.

Visual inspection of the removed pistons, as well as, the two pistons in

the warehouse revealed no indications of cracking. The licensee plans to

return all four potentially suspect pistons to the vendor for testing.

Containment Isolation Valve Leakage

On January 13,

1992,

primary sample valve PS-956F,

a normally closed

outboard CIV from RCS loops 2 and 3,.failed to meet its stroke time test

requirement of 10 seconds.

This test was being conducted following

maintenance on the valve's'position indicating lights.

The penetration

was apparently isolated as required by TS 3.6.3 by closing and removing

power to the PS-956E valve, which is the inboard CIV.

During repair

efforts on January 14, it

was determined that valve PS-956E had not fully

closed and was leaking at the 'rate of approximately 830 cc/min with RCS

system pressure at 2235 psig. It was also determined that valve PS-956F

was leaking and while not measured, its leakage rate appeared to be less

than the 830 cc/min through valve PS-956E. These two valves have IVSW

injected between them.-to-,enha.nce ,the.i.r contai-nment .i.solation..,ability.

Since the valve acceptance leak rate per EST-004,

Isolation Valve Seal

Water, is at 46 psig, the determination of whether or not the valve was

exceeding its allowable leak rate based upon the 2235 psig leak rate

could not be determined by the SS.

As a result the SS initiated an

Expert Operability Determination.request-at--5:00 p.m. on-January 14.

On January 15, the actuator spring for PS-956E was adjusted in an effort

to reduce the leak rate to allow work on PS-956F.

This evolution

ultimately reduced.the leak rate to 13 cc/min at 2235 psig at 11:00 a.m..

Subsequent attempts

to. adjust the spring actuator on

PS-956F was

unsuccessful in further reducing the leak rate.

On January 16

calculation 92-C-0001 was generated by Technical Support to correlate the

leakage at 2235 psig to-46 -psig-to determine the-.signific-ance of the leak

and penetration operabilit y.- -The -c-al culation demonsvtrated that -the .13

cc/min leakage rate was low enough to meet operability requirements;

however,

it

concluded that from 5:00 p.m.

on January 14 through 11:00

a.m.

on January 15, -"the observed leakage- was -such that -the. -penetration

could not be considered -operable...".

This condition was reported as

required by 10 CFR 50.73 (a) (z) (ii) in LER 92-001.

While reviewing the history associated with. the valve failures, the

inspectors determined that problems with primary sample valve stroking

had occurred in December 1991.

At that time,

it

was identified that

valves PS-956F and 956G coul-d not be successfully timed from the local

panel

due to dual indication while closing and the loss of closed

indication, respectively.

The operators then locally timed the valves'

stem travel. as remote-timing was -not possible.

Discussions with the SS

which managed the evolution revealed that Operations felt local timing of

5

valve stem travel

was

adequate to comply with their procedural

requirements.

However, OST-701, Inservice Inspection Valve Test, section

6.3, required that. the valve stroke times be measured from control switch

actuation (or other actuating signal) to the time the valve reaches the

required position as determined by the valve position indicating lights.

This methodology is utilized by the licensee to meet ASME Section XI

stroke testing requirements and to demonstrate valve operability.

By

only timing valve stem travel, the licensee did not verify necessary.

valve disk movement via an approved or accepted methodology.

Failure to

follow the requirements of OST-701 in testi.ng these sample valves is a

violation: Failure To Test Primary Sample Valves In Accordance With

Procedures, 92-02-01.

Several concerns resulted from this evolution. The first deals with the

SS and operators being unaware what effect the December 1991 testing

methodology utilized had on assuring valve operability.

The second

concern is that while indication of inadequate CIV operation was

available (i. e.,

dual indication for PS-956F),

operations did not take

the proper actions to verify that the valve could perform its containment

isolation function nor was analysis performed to determine the cause of

the dual indication

(WR

initiation was the only action taken).

Additionally,

after the concern with the testing methodology was

identified on ACR 92-009, the timing methodology to be utilized during

future valve stroke tests and what actions to take if

a test anomaly

occurs,

was not formally nor uniformly disseminated to all operating

shifts. These concerns were discussed with the Operations Manager.

The licensee intends to leave the penetration in the configuration of

PS-956E and 956F closed with power removed until RO 14,

at which time

repairs can be performed.

Other sample points are being utilized for

monitoring purposes.

The inspectors reviewed the licensee's actions,

Operability Determination, and LER,

and do not have significant technical

concerns with the actions taken

nor

the penetration's current

configuration.

E&RC Performance

In January 1992,

NAD completed an E&RC assessment.

The draft report

identified several potential findings, the most significant of which

involved field observations of poor radiological work practices and an

ineffective self-audit program.

At the end of the report period, site

management was in the process of determining the scope of the potential

issues such that corrective actions could be implemented.

Inspection of

the licensee's response to the potential issues will be conducted by both

the residents and regional specialists as part of the routine inspection

program.

6

Review of E&RC goals for 1991 revealed a continuing improving trend in

certain key performance indicators.

Of specific note were three items

which indicated the best performance on record.

These were: 1) the

lowest site exposure,

193 person-rem;

2) the smallest quantity of

radwaste shipped,

2289 cubic feet; and 3) the smallest amount of

contaminated floor space excluding the CV, 1340 square feet.

DBD Status

The inspectors reviewed the status of the DBD effort. The licensee plans

to complete the initial DBD writing effort by the spring of this year.

The inspectors reviewed DBD discrepancies to verify that they had been

evaluated for operability concerns and completed and proposed resolutions

were adequate.

The inspectors verified that there were not operability

concerns in the open DBD discrepancies and that documentation was

generally sufficient to verify that

the discrepancy was

being

satisfactorily resolved.

In those instances in which the documentation

was not sufficient, the inspectors were supplied additional information

to demonstrate that the item was being satisfactorily addressed.

All DBD

discrepancies should be resolved by the end of the year; however,

implementation of these resolutions may take several years. As they were

identified, the most significant resolutions were being scheduled.

The

licensee had no plans to incorporate references to the resolutions in

their revised DBDs.

Since these documents contain valuable information,

the inspectors noted that including resolution references would be

beneficial.

The licensee indicated that they would consider the benefits

of providing this information in the DBDs.

M-1087 10 CFR 50.59 Review

The inspectors review the 10 CFR 50.59 safety review package for M-1087,

RHR Minimum Flow Recirculation.

The inspectors observed that the

modification package, which was still in approval routing, indicated that

no unreviewed safety question existed. However, on page C42, the safety

review package stated that "Avoiding an Unreviewed Safety Question is

contingent upon a successful Large Break LOCA calculation by our fuel

vendor that accommodates the change in delivered LHSI."

The inspectors

discussed with

the NED HBR

Engineering Support Manager

the

appropriateness

of signing the modification approval

sheet as no

unreviewed safety question existed when the safety analysis contained a

contingency.

Further discussion with the author of the safety analysis

and cognizant engineer revealed that sufficient preliminary results had

been obtained from their Fuel Section to justify that an unreviewed

safety question did not exist and that the wording in the analysis had

been poor.

The engineering manager indicated that it

was not their

practice to sign-off unreviewed safety question determinations which

contained contingencies.

The inspectors had

no further concerns

regarding the reviewed documentation.

One violation was identified.

7

I0

3. Monthly Surveillance Observation (61726)

The inspectors observed certain safety-related surveillance activities on

systems and components to ascertain that these activities were conducted

in accordance with license requirements.

For the surveillance test

procedures listed below, the inspectors determined that precautions and

LCOs were. adhered to, the required administrative approvals and tagouts

were obtained prior to test initiation, testing was accomplished by

qualified personnel in accordance with an approved test procedure, the

tests were completed at the required frequency,

and that the tests

conformed to TS requirements.

Upon test completion,

the inspectors

verified the recorded test data was complete,

accurate,

and met TS

requirements, test discrepancies were properly documented and rectified,

and that the systems were properly returned to service.

Specifically,

the

inspectors witnessed/reviewed portions of the following test

activities:

OST-207

Motor Driven Auxiliary Feedwater Pump Flow Test

OST-401

Emergency Diesels.(Slow Speed Start)

Inadequate AFW Test Procedures

On January 28, 1992, the licensee identified that existing surveillance

test procedures did not completely verify that MDAFW

pump actuation

circuitry would function properly.

Specifically, testing one set of

normally closed contacts and associated interconnecting wiring in each of

the MDAFW pump actuation circuits had not been incorporated in the test

procedures.

These contacts must remain closed and the wiring integrity

must be maintained for the MDAFW

pumps to automatically start when

low-low S/G water level or tripping of the main feedwater pumps is

detected.

TS 4.8.5 and TS Table 4.8-1 items a and e. requires periodic

testing to verify that these conditions will automatically start the

MDAFW pumps.

In addition, the untested portion of the circuitry also

included the ATWS AFW actuation feature; however, testing of this feature

is not required by TS.

This testing deficiency resulted from inadequate

overlap of tests which were performed during plant shutdowns when

portions of the actuation circuitry is normally bypassed.

Review of

plant records revealed that both MDAFW pumps had successfully started on

August 30,

1991 when a low-low S/G water level condition had occurred

after a condensate pump shaft failure resulted in reduced feedwater flow

(see

IR 91-19).

This event was sufficient to demonstrate within the

required TS frequency (refueling interval) that the untested portion of

the circuitry would function properly.

The licensee plans to implement

revised test procedures during RO 14 to fully test the MDAFW actuation

circuitry.

Similar deficiencies in TS required surveillance activities

have been previously identified.

As discussed in their responses dated

July 9, 1990,

and April 3, 1991, to Notice of Violations, a review of the

programmatic and procedural adequacy of the TS surveillance program will

be completed during 1992.

This violation will not be. subject to

enforcement action because the licensee's efforts in identifying and

8

correcting the violation meet the criteria specified in Section V.G. of

the Enforcement Policy.

This item is identified as NCV: Failure To

Provide Adequate Procedures For Performing TS Required AFW Surveillance

Activities, 92-02-02.

One NCV was identified.

4. Monthly Maintenance Observation (62703)

The inspectors observed safety-related maintenance activities on systems

and components to ascertain that these activities were conducted in

accordance with TS,

approved procedures,

and appropriate industry codes

and standards.

The inspectors determined that these activities did not

violate LCOs and that required redundant components were operable.

The

inspectors verified that required administrative, material,

testing,

radiological,

and fire prevention controls were adhered to.

In

particular, the inspectors observed/reviewed the following maintenance

activities:

PIC-002

D/P Electronic Transmitter (4-20ma)

CM-610

Emergency Diesel Piston, Ring Main Bearing And

Crankshaft Overhaul

CM-615

Emergency Diesel Generator A And B Injector

Nozzle And Injector Nozzle Adapter

WR/JO 92-ABBZ1

B Inverter Repair

WR/JO 92-ABJI1

EDG A Cylinder #2 And #8 Lower Piston

Replacement

During performance of CM-610

the inspectors observed that the lower

piston retainer plate to grove clearance was recorded as 0.00015, whereas

the measured value was 0.0015.

The correct value was subsequently

entered into the procedure.

The measured value met the 0.002 maximum

allowed clearance.

During performance of CM-615,

the inspectors noted that the procedure

which had been revised on January 15,

1992 as part of the maintenance.

procedure upgrade program contained a human factor weakness.

The

weakness involved placement of acceptance criteria in caution notes

without repeating the information in the subsequent procedure steps or on

data sheets.

Examples included the caution notes on page 16 of the

procedure which provided a +/- 25 degree acceptance criteria for

positioning the injector nozzle adapter collar studs and a requirement

that the injector nozzle holder be positioned with the word TOP in the up

position.

This item was discussed with the appropriate maintenance

personnel.

No violations or deviations were identified.

9

5. Self-Assessment (45000)

The inspectors reviewed the corporate NED corrective action program as it

pertained to HBR.

The inspection consisted of a review of all the 1991

ACRs associated with the HBR engineering project. The inspectors verified

that the ACRs

had been properly classified as significant or non

significant, were being addressed in a timely manner,

and corrective

actions appeared to be appropriate.

The inspectors noted that most

non-significant ACRs,

through not required by procedures, had corrective

actions specified to preclude recurrence.

This was considered to be a

good practice.

However, the 1991 Third Quarter Trend Report For Adverse

Condition Reports Generated By NED,

the latest report available involving

all three nuclear sites, identified a management attention item, i. e.,

"Evaluation of causal factors indicates that NED procedures and methods

may not establish conditions that effectively prevent the occurrence of

an adverse condition."

In response to this potential item, a committee

had been formed to perform a detailed review of the ACRs' casual factors

and determine what corrective actions,

if

any,

are required.

The

inspectors will follow-up on this item as part of the routine inspection

program.

No violations or deviations were identified.

6. Follow-up (92700, 92701, 92702)

(Open) URI 50-261/89-26-02, Cable Submergence Qualification. The

licensee discovered in 1989 that several

EQ cables would

become

submerged,

but felt that if the cables met the LOCA submergence testing

they were qualified.

The NRC staff did not accept this submergence

testing as meeting the intent of NUREG-0588,

paragraph 2.2(5).

The

licensee then chose to await further industry testing.

In May of 1991,

NUREG/CR-5655 was published which documented the testing of 12 different

cable products.

The licensee's list of cables that would be submerged contained 3

brand/types that were not identical or similar to those tested.

These

were identified during this inspection.

Later, discussions with the

licensee were held and the licensee is to submit additional data to the

NRC for acceptability studies.

This item remains open.

(Closed) IFI 90-19-01,

Evaluate Licensee's Inspection Program

For

Openings In Reinforced Concrete Walls With Respect To Appendix "R" and

IEB 80-11 Reinforcements.

The inspector reviewed Operations Surveillance

Test Procedure OST-623, Fire Barrier Penetration

Seal

Inspection

(Refueling) which was completed January 26,

1991.

This inspection was

performed over a period of time from April until December of 1991,. and

identified 50 fire barrier penetration which by procedure were declared

inoperable.

The inspector reviewed the Final Report for Supplemental

Response to IE Bulletin 80-11,

dated March 1991 which documented the

inspections and verification or justification for the fill-in materials

for the block out configuration of the 50 questionable fire barrier

10

penetrations originally identified by OST-623.

The fill-in material for

these penetration was determined and evaluated.

External loading affects

were considered and evaluated for the walls containing these penetrations.

Additional rework was required for five HVAC penetration which contained

only one row of brick and twenty-four attachments.

After correction of

these 5 penetrations the analysis and evaluation confirmed that existing

brick in-fill penetration conform to the requirement of IEB 80-11.

Engineering evaluations90-104, Generic Evaluation of HVAC Fire Damper and

Fire Door Installation Discrepancies and 90-129,

Evaluation of Fire

Barrier Penetration Seals in Fire Zone 27 were reviewed by the inspector.

The purpose of these evaluations was to determine the adequacy of the

existing fire dampers and doors and the adequacy of the fire barrier

penetrations seals in fire zone 27.

There were no concerns identified by

the inspector. This item is closed.

No violations or deviations were identified.

7.

Exit Interview (30703)

The inspection scope and findings were summarized on February 12,

1992,

with those persons indicated'in paragraph 1. The inspectors described the

areas inspected and discussed in detail the inspection findings listed

below and in the summary. Dissenting comments were not received from the

licensee.

The licensee did not identify as proprietary any of the

materials provided to or reviewed by the inspectors during this

inspection.

Item Number

Description/Reference Paragraph

92-02-01

VIO -

Failure To Test Primary Sample Valves In

Accordance With Procedures (paragraph 2).

92-02-02

NCV -

Failure To Provide Adequate Procedures For

Performing

TS

Required

AFW

Surveillance

Activities (paragraph 3).

8.

List of Acronyms and Initialisms

a.m.

Ante Meridiem

ACR

Adverse Condition Report

AFW

Auxiliary Feedwater

ASME

American Society of Mechanical Engineers

ATWS

Anticipated Transient Without Scram

cc/min

cubic centimeters/minute

CCW

Component Cooling Water

CDF

Core Damage Frequency

CFR

Code of Federal Regulations

ontainment Isolation Valve

CM

corrective Maintenance

CCopnnColnWae

CV

Containment Vessel

DBD

.

Design Basis Documentation

D/P

Differential Pressure.

E&RC

Environmental and Radiation Control

ECCS

Emergency Core Cooling System

EDG

Emergency Diesel Generator

EQ

Environmental Qualifications

EST

Engineering Surveillance Test

HBR

H. B. Robinson

HVAC

Heating Ventilation Air Conditioning

ie.

That is

IE

Inspection and Enforcement

IEB

Inspection and Enforcement Bulletin

IFI

Inspector Follow-up Item

IR

Inspection Report

IPE

Individual Plant Evaluation

IVSW

Isolation Valve Seal Water

LCO

Limiting Condition for Operation

LER

Licensee Event Report

LOCA

Loss of Coolant Accident

LHSI

Low Head Safety Injection

M

Modification

MDAFW

Motor Driven Auxiliary Feed Water

NAD

Nuclear Assessment Department

NCV

Non-cited Violation

NED

Nuclear Engineering Department

NRR

Nuclear Reactor Regulation

OST

Operations Surveillance Test

p.m.

Post Meridiem

PIC

Process Instrument Calibration

PS

Primary Sample

Psig

Pounds per square inch

gage

RCP

Reactor Coolant Pump

RCS

Reactor Coolant System

rem

Roentgen Equivalent Man

RHR

Residual Heat Removal

RO

Refueling Outage

S/G

Steam Generator

SI

Safety Injection

SS

Shift Supervisor

TS

Technical Specification

URI

Unresolved Item*

VIO

Violation

WR

Work Request

WR/JO

Work Request/Job Order

  • Unresolved items are matters about which more information is required to

determine whether they are acceptable or may involve violations or

deviations.