ML13329A178

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Insp Repts 50-206/92-20,50-361/92-20 & 50-362/92-20 on 920604-0716.Violation Noted.Major Areas Inspected: Operational Safety Verification,Radiological Protection, Security & Evaluation of Plant Trips & Events
ML13329A178
Person / Time
Site: San Onofre  Southern California Edison icon.png
Issue date: 08/13/1992
From: Wong H
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML13329A176 List:
References
50-206-92-20, 50-361-92-20, 50-362-92-20, NUDOCS 9208310305
Download: ML13329A178 (24)


See also: IR 05000206/1992020

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION V

Report Nos.

50-206/92-20, 50-361/92-20, 50-362/92-20

Docket Nos.

50-206, 50-361, 50-362

License Nos.

DPR-13, NPF-10, NPF-15

Licensee:

Southern California Edison Company

Irvine Operations Center

23 Parker Street

Irvine, California 92718

Facility Name:

San Onofre Units 1, 2 and 3

Inspection at:

San Onofre, San Clemente, California

Inspection conducted: June 4, 1992 through July 16, 1992

Inspectors:

C. W. Caldwell, Senior Resident Inspector

D. L. Solorio, Resident Inspector

C. D. Townsend, Resident Inspector

T. Sundsmo, Project

spector

Approved By:

-_<ZJ_ e

___

_____8

H. J. Wong, Cief

Date Signed

Reactor Projects Section 2

Inspection Summary

Inspection on June 4. 1992 through July 16, 1992 (Report Nos. 50-206/92-20,

50-361/92-20, 50-362/92-20).

Areas Inspected:

Routine resident inspection of Units 1, 2 and 3 Operations

Program including the following areas: operational safety verification,

radiological protection, security, evaluation of plant trips and events,

monthly surveillance activities, monthly maintenance activities, independent

inspection, licensee event report review, electrical maintenance, design basis

document review, emergency preparedness drill, training, and followup of

previously identified items and items of non-compliance. Inspection

procedures 37700, 41701, 60710, 61726, 62703, 62705, 71707, 71710, 82301,

90712, 92700, 92701, 92702 and 93702 were utilized.

Safety Issues Management System (SIMS) Items:

None

9208310305 920813

PDR

ADOCK 05000206

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PDR

III2

Results:

General Conclusions and Specific Findings:

Strengths

A new site record of 236 days of continuous operation was set by Unit 1 on

July 12, 1992. The inspector considered that this record was achieved

through the diligence and attention to detail on the part of all personnel

involved with the operation and maintenance of the Unit (Paragraph 2).

The inspector considered that the licensee's efforts to understand and

propose corrective actions for weaknesses in the maintenance process, and to

reduce the backlog of maintenance items to be extensive. The implementation

and effectiveness of these efforts will be reviewed further as part of the

routine inspection effort (Paragraph 9.d).

Weaknesses

The inspector noted two events that were indicative of a weakness in the

interface between Station Technical and Operations to maintain configuration

control of plant equipment during surveillance activities.

In the first instance, the inspector observed that Station Technical (STEC)

personnel did not obtain approval from the Senior Reactor Operator (SRO)

Operations Superintendent to perform an inservice test of a Unit 2 auxiliary

feedwater pump. As a result, the SRO was not involved to the level required

by both Operations and Engineering procedures (Paragraph 5.b).

In the second instance, a Unit 2 salt water cooling (SWC) pump became

inoperable due to a misaligned valve. The event was detailed in licensee

event report (LER) 2-92-009. In that case, Operations personnel failed to

recognize that the Engineering procedure did not comply with procedural

requirements to provide for an Operations sign-off and an independent

verification of equipment manipulation. Thus, proper configuration control

was not maintained.

As a result of these two events, the inspector was concerned that additional

licensee attention was necessary to strengthen the STEC/Operations interface.

Significant Safety Matters:

Summary of Violations:

One violation concerning the failure of Station Technical personnel to obtain

approval to perform a surveillance on an auxiliary feedwater pump from the

SRO Operations Supervisor was identified (Paragraph 5.b).

Open Items Summary:

During this report period, four new followup items were opened and 12 were

closed; one was examined and left open.

DETAILS

1. Persons Contacted

Southern California Edison Company

H. Ray, Senior Vice President, Nuclear

  • H. Morgan, Vice President and Site Manager
  • R. Krieger, Station Manager

J. Reilly, Manager, Nuclear Engineering & Construction

B. Katz, Manager, Nuclear Oversight

  • R. Rosenblum, Manager, Nuclear Regulatory Affairs
  • K. Slagle, Deputy Station Manager
  • R. Waldo, Operations Manager
  • L. Cash, Maintenance Manager
  • M. Short, Manager, Station Technical

M. Wharton, Manager, Nuclear Design Engineering

P. Knapp, Manager, Health Physics

W. Zintl, Manager, Emergency Preparedness

D. Herbst, Manager, Quality Assurance

C. Chiu, Manager, Quality Engineering

  • J. Schramm, Plant Superintendent, Unit 1

V. Fisher, Plant Superintendent, Units 2/3

  • D. Brevig, Supervisor, Onsite Nuclear Licensing
  • G. Hammond, Supervisor, Onsite Nuclear Licensing

J. Reeder, Manager, Nuclear Training

H. Newton, Manager, Site Support Services

  • R. Plappert, Manager, Technical Support and Compliance
  • J. Jamerson, Lead Engineer, Onsite Nuclear Licensing
  • D. Axline, Engineer, Onsite Nuclear Licensing
  • W. Marsh, Assistant Manager, Operations
  • S. Paranandi, Supervisor, Quality Assurance
  • N. Maringas, Supervisor, Quality Assurance
  • J. Rainsberry, Plant Licensing Manager
  • J. Fee, Assistant Manager, Health Physics
  • S. Hetrick, Supervisor, Computer Engineering, Station Technical
  • N. Quigley, Engineering Supervisor, Station Technical
  • D. Roberts, Safety Injection Cognitive Engineer
  • W. Conklin, Compliance Engineer, Station Technical
  • R. Nielsen, Cognitive Engineer, Station Technical

San Diego Gas and Electric Company

  • R. Lacy, Manager, Nuclear Department
  • R. Erickson, Site Representative
  • Denotes those attending the exit meeting on July 16, 1992.

The inspectors also contacted other licensee employees during the course

of the inspection, including operations shift superintendents, control

room supervisors, control room operators, QA and QC engineers, compliance

engineers, maintenance craftsmen, and health physics engineers and

technicians.

2

2. Plant Status

Unit I

Unit 1 operated at power the entire inspection period and established a

new site record (236) days for continuous operation on July 12, 1992.

Unit 2

Unit 2 operated at power for the entire inspection period.

Unit 3

Unit 3 operated at power for the entire inspection period.

3. Operational Safety Verification (71707)

The inspectors performed several plant tours and verified the operability

of selected emergency systems, reviewed the tag out log and verified

proper return to service of affected components. Particular attention

was given to housekeeping, examination for potential fire hazards, fluid

leaks, excessive vibration, and verification that maintenance requests

had been initiated for equipment in need of maintenance. The inspectors

also observed selected activities by licensee radiological protection and

security personnel to confirm proper implementation of and conformance

with facility policies and procedures in these areas.

Several minor discrepancies were noted and discussed with the Shift

Superintendents for resolution. In addition, the following issue was

noted as discussed below.

Unit 1 Turbine Building

On June 4, 1992, the inspector noted that a pipe draining into a floor

drain was splashing water onto the floor around the drain in the Unit 1

Turbine Building. Because the drain was labeled potentially

contaminated, the inspector contacted health physics (HP) supervision to

determine if the water splashing onto the floor was spreading

contamination.

In response to the inspector's question, HP performed a survey of the

drain and the floor around it. Contamination was found in the drain, but

not on the surrounding floor. The draining pipe provided waste drainage

from the secondary plant chemistry lab. Initially, HP installed one end

of a plastic wrap around the pipe and the other end to the floor around

the drain. This was done to prevent water from splashing out from the

drain onto the surrounding floor. However, with the plastic secured to

the floor, it was not clear to the inspector that the drain would have

functioned properly.

3

The inspector questioned HP management as to whether they were defeating

the purpose of the drain by this modification. HP management responded

that they did not know but would find out. A few days later the

inspector observed that the plastic had been removed from the floor

around the drain. In fact, the plastic had been re-secured to the inside

of the drain.

The inspector noted that the drain in question was located near the 4160

VAC (4KV) and 480V switchgear rooms. The inspector observed other floor

drains in the same area, but was unable to determine if they were

functioning properly. The inspector will evaluate the consequences and

significance of the temporary drain modification as part of the routine

inspection effort.

4. Evaluation of Plant Trips and Events (93702)

a. Temporary Waiver of Compliance From Technical Specification 3.3.1

For Safety Injection Valve HV852B - Unit 1

On May 18, 1992, the licensee was granted a Temporary Waiver of

Compliance (TWOC) from TS 3.3.1, "Safety Injection and Containment

Spray Systems Operating Status," to allow repairs of safety

injection (SI) hydraulic valve (HV) HV852B. The duration of the

TWOC was for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> and was initiated on May 19, 1992. At 11:09

p.m. on May 19, 1992, HV852B was restored to service, establishing

compliance with TS 3.3.1.

The waiver was requested to allow for the replacement of the HV852B

accumulator nitrogen addition valves (schrader valves), which had

been identified to be leaking nitrogen. The nitrogen leakage had

resulted in a recharging frequency of the accumulators of

approximately once every three days.

Hydraulic valve 852B is opened with a pneumatic-hydraulic pump, and

closed by two nitrogen-hydraulic fluid accumulators connected at

their hydraulic discharge to the valve actuator. The nitrogen in

the accumulators is separated from the hydraulic fluid by a piston

with seal rings. The nitrogen in the accumulators provides the

motive force necessary to displace the hydraulic fluid from the

accumulator which is used to move the valve to its closed SI

position. Nitrogen is added to the accumulators by connecting a

nitrogen high pressure cylinder to accumulator schrader valves with

a charging manifold.

On May 19, 1992, HV852B was removed from service to replace the

schrader valves on both accumulators.

Initially the accumulators

were ultrasonically tested to determine the locations of the

pistons. However, measurements of piston positions were

indeterminate. Upon removal of the schrader valves from the top of

the accumulators, the position of the pistons were measured visually

using reach rods. The pistons were found to be misaligned. One

accumulator piston was found at its uppermost possible location with

II

4

the maximum volume of hydraulic fluid and minimum volume of nitrogen

gas. The other piston was found at its lowest possible location

with the minimum volume of hydraulic fluid and maximum volume of

nitrogen gas.

As corrective action, the schrader valves were replaced, the

accumulators were recharged with nitrogen, and the pistons were

evenly aligned. After measuring the piston locations with the rods,

STEC considered the operability of the valve to be indeterminate and

initiated an evaluation after completion of the corrective

maintenance.

On June 17, 1992, a nonconformance report (NCR) was issued to

document the degraded condition of HV852B as found on May 19, 1992.

Station compliance determined that the degraded condition of HV852B

was reportable under 10 CFR Part 50.73, which required SCE to submit

a licensee event report (LER) within 30 days. On June 23, 1992, the

valve vendor and STEC concluded that HV852B had been inoperable

prior to its repair on May 19, 1992.

Based on the events associated with HV852B, the inspector had the

following concerns:

o

The accumulators were modified in 1986 to use the pistons to

isolate the hydraulic fluid from the nitrogen. Up to two weeks

prior to replacement of the schrader valves, it was not

recognized that leaks from the accumulators could result in

piston misalignment. (The most severe consequence of the

misalignment was the valve becoming inoperable).

Evidence of

this is supported by the absence of a program to monitor the

piston locations concurrent with or independent of accumulator

recharging evolutions.

o

Ultrasonic testing of the other HV accumulators following the

discovery of HV852B piston misalignment would have identified

the ongoing degradation of HV851A prior to June 17, 1992 when

the licensee requested a TWOC (reference section 4.b for

discussion).

o

The NCR documenting the inoperable condition of HV852B was

initiated approximately one month after the valve was found in

its inoperable condition.

This is an unresolved item pending review of the licensee's assessment of

the condition as documented in their LER (50-206/92-20-01).

b. Temporary Waiver of Compliance From Technical Specification 3.3.1

For Safety Injection Valve HV851A - Unit 1

On June 17, 1992, the licensee requested a TWOC from the

requirements of sections A(1) and A(3) of Technical Specification (TS) 3.3.1, "Safety Injection System - Containment Spray Systems -

II

5

Operating Status."

This was necessary for a period of 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> in

order to facilitate repairs to safety injection (SI) valve HV851A.

This request was granted verbally by the NRC on June 17, 1992 and

formally documented in a June 18, 1992 letter to the NRC. At 11:48

a.m. on June 18, 1992, HV851A was restored to service, establishing

compliance with TS 3.3.1.

The SI valve, HV851A, is a double disc gate valve, with a pneumatic

hydraulic actuator which is similar in configuration to HV852B as

discussed above. The only major difference is that HV851A has one

accumulator instead of two.

The actuator associated with SI discharge isolation valve HV851A

experienced minor hydraulic fluid leakage on the accumulator side.

The leakage had been monitored by STEC. The licensee assumed that a

significant loss of hydraulic fluid could limit the capability of

the valve to stroke to the fully open position upon demand. An

evaluation was initiated, which included the use of ultrasonic

testing (UT) to determine the position of the accumulator piston.

The conclusion from the evaluation was that a loss of hydraulic

fluid had occurred which would prevent the valve from opening beyond

approximately 85% of full stroke. The licensee stated that in this

condition the valve would still perform its required safety function

since analyses had recently been completed which demonstrated that

the required SI flow would occur with HV851A 50% open. However, the

licensee requested the TWOC to remove HV851A from service to

recharge the accumulator hydraulic side in order to regain the full

stroke capability of the valve.

Because the accumulator oil leak was not repaired, (repairs would

have required valve disassembly), the licensee committed to

implement measures that would assure continued operability of

HV851A. Those measures were to trend the frequency of accumulator

nitrogen recharging and perform periodic piston location

measurements using the UT method developed previously.

Because there were questions as to the positions of the other HV

accumulator pistons, the licensee committed to perform UT

measurements on them (with the exception of HV852B, which had been

ultrasonically tested approximately two weeks prior and left with

pistons in their optimum position).

On July 1, 1992, the remaining HVs (8518, 8548, 853B, 852A, 853A,

854A) were ultrasonically tested. All of the HVs were found to be

in an optimum condition except for HV854A. The accumulator pistons

for HV854A were found to be misaligned greater than the V/"

limit

that station engineering had determined was the optimum

configuration for dual accumulator valves. However, the valve was

determined to be operable. The licensee subsequently realigned the

pistons by recharging the accumulators with nitrogen.

6

No violations or deviations were identified.

5. Bi-Monthly Surveillance Activities (61726)

During this report period, the inspectors observed or conducted

inspection of the following surveillance activities:

a. Observation of Routine Surveillance Activities (Unit 1)

SO1-V-2.14.1

"Auxiliary Feedwater Pump, S1-AFW-G1O, Inservice

Pump Test."

S01-II-1.6.20

"Surveillance Requirement Intermediate Range

Channels NIY-1203 and NIY-1204 Neutron Flux

Channel Test."

501-12.4-2

"Operations In-Service Valve Testing."

SO1-II-1.1.2

"Surveillance Requirement Pressurizer Level and

Pressurizer Pressure Channel Test."

SO1-V-3.9

"Isothermal Temperature Coefficient."

b. Observation of Routine Surveillance Activities (Unit 2)

5023-1-2.72

"Fire Detection-Surveillance Testing Of

Actuation Detectors Outside Unit 2 Containment."

S023-V-3.4.1

"Auxiliary Feedwater Inservice Pump Test Monthly

Surveillance 2P140."

On July 1, 1992, the inspector observed surveillance testing on the

Unit 2 and Unit 3 auxiliary feedwater (AFW) pumps, 2P140 and 3Pl41,

required by surveillance procedure S023-V-3.4.1. During the Unit 2

surveillance of 2P140, the inspector noticed that approval to

conduct the test had been received from the Control Operator (CO),

but the procedure directed that approval be from the SRO Operations

Superintendent. The inspector discussed this observation with the

on-shift SRO and determined that he knew the test would be performed

that day, but had not actually discussed it with engineering

personnel.

Step 3.2 of S023-V-3.4.1 stated; "Obtain the SRO Operations

Supervisor approval to conduct the test. Operations should release

pump 2(3)1305MP140 to the Cognizant Engineer for testing at this

point under a verbal approval."

The inspector noted that the

signature block allowed the engineer to document who was informed

including the date and time the individual was contacted. The

engineer had filled the signature block indicating approval from the

CO. When this was discussed with the engineers involved, they

indicated that it was appropriate to gain approval from the CO and

had utilized the CO for approvals previously. However, their

II7

supervisor indicated that the procedure should be adhered to and

that the SRO should have reviewed the scope of the surveillance

before it was performed.

Further inspection revealed that section 6.11, "Plant Manipulations

Using Other Division Procedures" of operations procedure 50123-0-20,

"Use Of Procedures," stated, in part, that it is acceptable to use

other division procedures to manipulate the plant provided the

procedure is reviewed and approved by a SRO Operations Supervisor

(prior to performing work). The procedure also stated that the

Control Room Supervisor is responsible for overall plant safety and

can suspend test activities at any time.

The inspector discussed this issue with licensee management who

agreed that the surveillance procedure was not properly followed.

It is important to consider that there was little safety

significance to this issue as the plant was operating at steady

state with no other related safety equipment out of service and the

surveillance was run successfully and in accordance with other

procedures. However, as shown by the missed procedural requirements

(as identified above), there appeared to be a weakness in

configuration control since the SRO operations supervisor was not

involved to the level required by both the operations and

engineering procedures. Failure to follow procedures S023-V-3.4.1

and S0123-0-20 is a violation, (50-361/92-20-02).

The inspector was concerned with the interface between Operations

and STEC and the impact on configuration control of plant equipment

during the performance of STEC procedures. In addition to the

concern identified above, a Unit 2 salt water cooling (SWC) pump

became inoperable in May 1992, due to a misaligned emergency seal

water supply valve. The event was detailed in LER 2-92-009. In

that case, the Station Technical surveillance procedure, S023-V

3.5.4, "Inservice Testing Of Check Valves," was used to perform a

quarterly test of SWC check valves. A step in the procedure was

signed by the test engineer indicating that he had requested

Operations to open the emergency seal water supply valve. However,

flow data suggest that the valve may have been inadvertently left

closed following the check valve test. Operations personnel failed

to recognize that Engineering procedure S023-V-3.5.4 did not comply

with the requirements in Operations procedure S0123-0-20 prior to

authorizing the test engineer to perform the check valve test. In

particular, the requirements for an Operations sign-off and

independent verification of equipment manipulation were not

contained in the Engineering procedure.

As a result of these two events, the inspector was concerned that

additional licensee attention was necessary to resolve

STEC/Operations interface weaknesses to ensure that plant

configuration control is properly maintained.

8

c. Observation of Routine Surveillance Activities (Unit 3)

5023-1-2.73

"Fire Detection Surveillance Testing Of

Actuation Detectors Outside Unit 3 Containment."

S023-V-3.4.1

"Auxiliary Feedwater Inservice Pump Test Monthly

Surveillance 3P141."

5023-3-3.27.2

"Weekly Electrical Bus Surveillance."

One violation was identified in this area.

6. Monthly Maintenance Activities (62703)

During this report period, the inspectors observed or conducted

inspection of the following maintenance activities:

a. Observation of Routine Maintenance Activities (Unit 1)

92051545000

"Intermediate Range Drawer Channel 1203, SL-NIS-NIY

1203, Channel Test."

92060339001

"Several Relays Have Caused The 'Start Up Rate

Reactor Trips Active' Permissive To Illuminate Upon

Relay Failure."

92061088000

"Bank A Instrument Air/N2 Header Relief Valve, S1

GNI-PSV-301, Is Leaking Through, Resulting In

Lowering Pressure On The Backup Nitrogen Banks For

HV851A."

92061958000

"Readjustment of the Dual Accumulator Pistons. East

Accumulator Piston Is At A Higher Level Than The West

Accumulator Piston."

92061860000

"Support STEC/QC In UT Inspection Of The Accumulator

For HV-851B."

92061867000

"Support STEC/QC In UT Inspection Of The Accumulator

For HV-854B."

92061964000

"Excessive Leakage On Outboard Seal of North

Component Cooling Water Pump. A Small Stream

Approximately 12 Ounces Per Minute."

b. Observation of Routine Maintenance Activities (Unit 2)

92060333000

"Main Steam Relief Valve To Atmosphere, 2P5V8407,

Water Leak Where Relief Valves Downstream Piping

Connects to the Stand Pipe."

9

92060334000

"Main Steam Relief Valve To Atmosphere, 2P5V8408, 30

Drips A Minute Leak Where Relief Valve Downstream

Piping Connects To The Stand Pipe."

92060019000

"Steam Generator, 2E088, Blowdown Vent Valve,

S21301MR800, Has Body Leak Of Steam That Is Getting

Worse."

92010602000

"Diesel Generator, 2G002, Fire Protection Pre-Action

Actuating Detector Surveillance Testing."

90050432000

"High Pressure Safety Injection Pump, S21204MP019,

Train B - P3 -

Inspect Each Cyclone Separator To

Ensure Their 0-Rings Are In Place. If The 0-Rings

Are Missing Replace With Qualified In-Kind Parts."

c. Observation of Routine Maintenance Activities (Unit 3)

92051337000

"Diesel Generator, 3G002, Fire Protection Pre-Action

Actuating Detector Surveillance Testing."

92070060001

"General Isolation PH Bus Potential Transformer,

S31802EPXP1, Cross-tie Generator Potential

Transformer Channel B To A To Provide For Voltage

Regulating, Per TFM 3-92-MAA-002, Revision 0."

92070942000

"125VDC Station Battery 301, S31806E6007, Cell #14

Voltage is 2.066 VDC, Allowable Limit Is 2.07 VDC.

Jumper Out Cell #14, Jumper In Cell #53."

92060813000

"125VDC Station Battery 3D1, S31806EB007, Perform A

Bank Equalize Charge."

92070965000

"125VDC Station Battery 3D1, S31806EB007, Perform

Single Cell Charge On Cell #53, Cell Voltage Is

1.208VDC."

The inspector observed the licensee's actions to jumper out failed

cell #14 and replace it with cell #53 in battery 301.

Failure of

cell #14 resulted in the Unit entering a 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> Technical

Specification (TS) action statement to restore the battery to

operable status or to shut down the Unit. As a result of the

licensee's activities, the inspector had a number of questions

related to the performance of the surveillance test that identified

the failed cell and the adequacy of the replacement cell.

The

inspector will further evaluate the licensee's actions related to

this matter as followup item (50-362/92-20-03).

No violations or deviations were identified.

III_

_10

7. Independent Inspection (62705, 37700, 41701, 82301)

a. Electrical Maintenance (62705)

The inspector observed that cell 58 of Class 1E battery 3D3, was

being charged by a non-Class 1E portable single cell battery

charger.

The inspector noted that the use of non-Class 1E individual cell

chargers to charge Class 1E batteries has generally been accepted

when a licensee has demonstrated that adequate equalization of cell

voltages cannot be maintained using a full capacity charger and when

administrative controls have been maintained. Administrative

controls would be required to preclude the masking of data which

would indicate a potentially failing cell. These administrative

controls would typically limit any cell to the following:

o

Perform only one individual cell equalization charge a

year.

o

Limit the equalization charge rate to the battery

manufacturer's limits.

o

Recheck cell parameters two weeks after the charge.

o

Ensure that a 10 CFR 50.59 evaluation had been

accomplished to verify that a fault on the non-1E charger

would not degrade the 1E battery.

o

Provide criteria to demonstrate that adequate equalization

of cell voltages could not be maintained using a full

capacity charger.

The inspector reviewed the following licensee documents concerning

the batteries:

o

Procedure S0123-1-9.301, Revision 1, Temporary Change 6,

"Battery - Spare and Single Battery Cell Inspection and

Testing"

o

S0123-I-2.3, Revision 1, "Quarterly Battery Inspection"

o

A June 11, 1992, 10 CFR 50.59 evaluation for use of the

individual battery charger

o

Current and previous data for cell 58 and for battery 3D3

As a result of the review of the data for the cell 58, the inspector

concluded that cell 58 was not continually failing surveillances and

being individually recharged. Based on this data, the inspector

concluded that there was no immediate operability question for cell

58 in battery 3D3.

However, based on a review of Procedure 50123-1-9.301, the inspector

concluded that administrative controls for individual cell charging

were not in place to preclude use of the individual cell charger to

mask a failing cell.

In response to the inspector's concern, the licensee stated that

maintenance supervisors make the decision on when an individual cell

charge will be performed based on the number of cells which require

charging. The licensee stated that engineering personnel review

Class 1E cell data outside the normal performance characteristics.

As a result of these controls, the licensee stated that no changes

to add additional administrative controls for individual Class 1E

cell charging were planned.

In addition, based on a review of Procedures S0123-1-9.301 and

50123-1-2.3, the inspector concluded that the licensee's battery

procedures did not contain a method for demonstrating that they only

use the single cell charger if the licensee can't maintain voltage

using the full capacity charger.

The inspector noted that the June 11, 1992, 10 CFR 50.59 evaluation

for use of the individual battery charger concluded that the charger

was an isolation device as defined in IEEE STANDARD 384, "Criteria

for Independence of Class 1E Equipment and Circuits," because it was

a current limiting device. The evaluation was based on a Ratelco

Constant Voltage Charger, Type FF8504, Model 102-3617.00. The

evaluation concluded that the charging rate was limited to 80 amps,

based on output fuses in the charger. The evaluation also concluded

that an 89 amp charging rate would not damage the battery.

Based on a review of the licensee's 10 CFR 50.59 evaluation and

Procedure 50123-1-9.301, the inspector concluded that the licensee's

individual cell charger 10 CFR 50.59 evaluation was inconsistent

with Procedure S0123-I-9.301. A charging current limit of 80 amps

assumed in the 50.59 evaluation was not contained in the procedure.

In fact, a note after Step 6.3.7, Procedure S0123-1-9.301, directed

that the craft person performing the charge monitor the charging

operation hourly for charging currents over 100 amps. The inspector

also concluded that the licensee's evaluation that a battery charger

was a current limiting device was generally acceptable in accordance

with IEEE STD 384.

The inspector provided the conclusions discussed above to the

licensee. The licensee agreed that the note after Step 6.3.7 did

not match the 10 CFR 50.59 evaluation. As a result, the licensee

committed to revise the note to match the 10 CFR 50.59 review and

the actual equipment being used.

In addition to the concerns discussed above, the inspector also

questioned the effect of using the single cell charger on the

12

seismic qualification of the vital batteries. The inspector will

further evaluate the licensee's controls for use of the single cell

charger as followup item (50-362/92-20-04).

b. Design Bases Documentation Review (37700)

A Region V inspector performed an informal review of the licensee's

design bases documentation (DBD) program during the weeks of May 18

to 21 and June 8 to 11, 1992. This review primarily focused on

inspection of plant systems to ensure that these systems actually

exhibited selected safety significant design characteristics

documented by the DBD program. The inspector reviewed each system's

DBD, identified several verifiable safety significant

characteristics for each system, and then inspected each system to

verify the characteristics. The inspection was conducted in Unit 2,

and included the following systems:

SYSTEM

DBD DOCUMENT NO.

Class 1E 125 Volt DC

DBD-S023-140, Revision 0

Component Cooling Water

DBD-S023-400, Revision 0

Saltwater Cooling

DBD-S023-410, Revision 0

Instrument Air/Dedicated

Backup Nitrogen

DBD-SO23-540, Revision 0

Emergency Chilled Water

DBD-S023-800, Revision 0

Results of the plant system DBDs inspected during this review

indicated that these documents appeared adequate. Inspection of

additional plant systems will periodically be conducted by Region V

and documented in inspections reports as additional DBD documents

are developed by the licensee.

c. Observation of Emergency Preparedness Drill (41701, 82301)

On June 10, 1992, the inspectors observed an emergency preparedness

(EP) drill being conducted by the licensee for training purposes.

The drill involved a steam generator tube rupture (SGTR) and a

sequential loss of all feedwater on Unit 2. These events required

the operators to perform emergency operating instructions (EOIs) for

reactor trip, SGTR, and finally transition into the functional

recovery procedures (FRPs).

During the drill, the inspector had the following observations:

1) Control room evaluators (controllers) were not prepared to

evaluate operator actions during the drill. The prepared

13

scenario summary emphasized EP actions, but excluded operator

actions except for event classifications. For example, an

inspector informed the lead control room evaluator (operations

department) that the operators were performing actions that

were not contained in the EOI that was being performed

(functional recovery success path HR-2).

The evaluator stated

that he had not reviewed this procedure lately and wasn't sure

if it prescribed the observed operator actions or not. Because

the evaluators were not conscious of required operator actions,

they were not objectively critical of those actions.

The inspector considered that emergency drills are a good

opportunity to perform operator evaluations. This was

discussed with the licensee who indicated that they would

evaluate the inspector's observation.

2) Operators used the E0Is as guidance in certain instances,

rather than as procedures for the scenario given. In

particular, actions taken by the operators to cross-connect

Unit 3 condensate to Unit 2 were not directed by the E0Is;

these actions were improvised on the spot by the operators

without identification that they were deviating from the

prescribed course of action in the EOIs. However, the EOIs

directed use of the (Unit 2) condensate transfer system. Even

though the operator's actions had merit, there was no

indication that the course of action prescribed by the EOIs

would have been unsuccessful when the operators decided to

deviate from the EOIs. The operators continued with prescribed

EOI actions when the improvised actions were unsuccessful.

The inspector noted that the EOIs do not incorporate directions

to cross-connect systems between units in order to mitigate an

accident. The observed drill identified the need for cross

connecting condensate upon a loss of all feedwater event, and

the lack of a procedure to implement it.

The-ability to cross-connect Unit 2 and Unit 3 systems during

an emergency was discussed with the licensee after the drill.

The licensee indicated that they had a "desk top" procedure for

cross-connecting electrical systems between Units 2 and 3, but

did not have an emergency procedure to cross-connect condensate

systems. They indicated that the "desk top" procedure was not

an official procedure since it could not pass a 10 CFR 50.59

evaluation. However, the licensee indicated that this would

only be used when they were in an accident scenario that was

beyond the design basis event and not adequately covered by the

FRPs. In addition, it would be a conscious management decision

to implement it.

The inspector will review use of this "desk top" procedure further.

In particular, the inspector questioned if the "desk top" procedure

should undergo the formal review and approval process, and if it was

I

14

consistent with current methodology for complementing the E0I.

Followup item (50-361/92-20-05).

No violations or deviations were identified.

8. Review of Licensee Event Reports (90712, 92700)

Through direct observations, discussion with licensee personnel, or

review of the records, the following Licensee Event Reports (LERs) were

closed:

Unit 1

91-07, Revision 0

"Large Break LOCA Analysis Nonconservative Due

To Incorrect RCS Volumes."

91-07, Revision 1

"Large Break LOCA Analysis Nonconservative Due

To Incorrect RCS Volumes."

On March 28, 1991, with Unit 1 operating at 20% reactor power, it was

determined that the value for the reactor vessel refill volume used in

the Large Break Loss of Coolant Accident (LBLOCA) analysis performed by

Westinghouse was underestimated by approximately 182 cubic feet. A

supplement to this LER providing a complete discussion of the event,

causes, corrective actions, and safety assessment was to be submitted by

May 10, 1991.

LER 91-07, Revision 1, was issued on June 14, 1991. This LER contained a

discussion of the event, causes, corrective actions, and safety

assessment associated with the volume underestimation in the LBLOCA

analysis performed by Westinghouse.

Immediate corrective actions as stated in LER 91-07, Revision 1,

included:

1) immediately restricting reactor power level to 75%, and

2) administratively restricting Incore Axial Offset (IAO) to allow

for full power operation.

Planned Corrective Actions were to submit an amendment application to the

NRC by June 18, 1991. The amendment was to request a change to Technical

Specification (TS) 3.11, "Continuous Power Distribution Monitoring,"

reflecting the current administratively imposed IAO values and also to

change the basis of TS 3.5.2, "Control Rod Insertion Limits," for the new

values of specific power and peaking factors.

On June 18, 1991, the licensee submitted Amendment Application No. 196,

which consisted of the Proposed Change No. 245, to the Provisional

Operating License, DPR-13, for SONGS, Unit 1. Proposed Change No. 245

was a request to revise Appendix A, TS Section 3.5.2, "Control Rod

Insertion Limits," and Section 3.11, "Continuous Power Distribution

15

Monitoring." The proposed change was to impose more restrictive limits

on core axial offset than those specified in the current Technical

Specifications.

On July 8, 1992 the licensee requested that the NRC postpone issuance of

Proposed Change No. 245 and make it contingent on Unit 1 operating beyond

its current cycle, Cycle XI. Currently, Unit 1 is scheduled to be

decommissioned at the end of Cycle XI.

The inspector verified the implementation of administrative controls

restricting IAO to allow for full power operation and also changes to the

values of specific power and peaking factors as identified in LER 91-07,

Revision 1. These administrative controls were implemented by reactor

engineering procedures S01-V-1.6, "Incore Flux Mapping", and SO1-V-1.16,

"Axial Offset Correlation." The inspector concluded that no further

followup action is required. This item is closed.

Unit 2 92-006, Revision 0

"Reactor Shutdown To Test Safety Injection Pump

Miniflows."

No violations or deviations were identified.

9. Follow-Up of Previously Identified Items (92701)

a. (Open) Followup Item (50-361-362/91-29-02). "IN-88-73, 'Direction

Dependent Leak Characteristics of Containment Purge Valves.'"

Paragraph 4 of Inspection Report 91-29, dated November 6, 1991,

concerned a followup to NRC Information Notice (IN) 88-73,

"Direction-Dependent Leak Characteristics of Containment Purge

Valves." The IN provided guidance regarding the testing of Fisher

Model 9200 valves used for containment isolation. In particular, it

had been observed that these valves, which have tapered seats, had a

direction-dependent leakage characteristic. The valves could seal

in both directions but a test in the preferred direction did not

always verify sealing in the non-preferred direction.

The licensee's Independent Safety Engineering Group (ISEG) completed

a review of IN 88-73 in October 1988, as documented in report 88

ISEG-152. The ISEG review determined that Southern California

Edison's (SCE) containment penetration testing practices were

acceptable. However, the inspector learned from the ISEG Supervisor

that 88-ISEG-152 was not accurate. A design change, in response to

IN 88-73 had occurred, reversing the seating direction of the Units

2 and 3 inside-containment 8-inch purge valves. Further, the

licensee had committed to review other plant valves which had

leakage limits, to determine if the recommendations of Information

Notice 88-73 also applied. In addition, the licensee also committed

to revise 88-ISEG-152 to include this information.

II16

For followup, on May 28, 1992, "Request for Action: NRC Information

Notice 88-73 (Amended Evaluation), 'Direction-Dependent Leak

Characteristics of Containment Purge Valves' RCTS No. 9205022" was

prepared by the ISEG Supervisor with the action request to

"determine administrative or design changes necessary to resolve

direction-dependent leakage of Fisher Series 9200 valves". On June

5, 1992, a Regulatory Commitment Tracking System (RCTS) E-mail

commitment was received by the ISEG Supervisor accepting these

commitments and proposing a due date of June 1, 1993.

The inspector will monitor the licensee's efforts to resolve this

issue. Therefore, this item will remain open.

b. (Closed) Followup Item (50-206/91-13-03). "NCR Not Written For

Failed Sequencer Test."

Following a monthly surveillance test, troubleshooting and a retest

of the Unit 1 sequencer were performed as a result of varying and

conflicting results. The inspector questioned why an NCR had not

been generated for the test failure. At the time there was some

difference of opinion as to whether or not NCR procedure S0123-XV-5,

"Nonconforming Material, Parts, or Components," was clear in its

direction to generate an NCR for the failed surveillance. The

licensee agreed to review the procedure and make enhancements where

necessary as a result of the inspector's concern.

For followup to this issue, the licensee revised procedure S0123-XV

5 on January 29, 1992, to give more detailed information as to when

an NCR would be required. This revision included specific details

that indicated that when results of a surveillance test fail to meet

acceptance criteria, an NCR shall be written. The procedure also

indicated that an NCR shall be written when a component is

determined to have a failure rate significantly higher than the

industry average as determined by existing programs. Based on these

revisions, the inspector considered that the licensee's actions were

appropriate. Therefore, this item is closed.

c. (Closed) Followup Item (50-206/91-13-04). "Maintenance Program

Implementation For Corroded Fasteners."

The inspector observed several components in the plant with

fasteners which were corroded to some degree (as discussed in

inspection report 206/91-13) and also noted that there was no

program to specifically evaluate the condition of fasteners in many

systems. As a result of the inspector's concern, the licensee

stated that they would evaluate the need for a program to inspect

fasteners. In order to do this they would have to gather data

during the Unit 2 refueling outage in the fall of 1991.

As a result of the licensee's assessment on this matter, it was

determined that levels of fastener degradation, resulting from

corrosion, varied from cosmetic to severe. However, most findings

17

were cosmetic in nature and of the large sample taken (536

maintenance orders), only 32 maintenance orders (MOs) were

identified as having potentially corroded fasteners. And of those,

six MOs were found to have corroded fasteners warranting further

inspection.

The licensee tested fifteen fasteners from the six MOs and one

failure was found. The licensee therefore concluded that although

the number of failures was small, more attention should be given to

routine inspection and preservation of fasteners in plant systems.

The licensee has planned a number of actions with regard to this

matter. For example the licensee would do the following:

o

Enhance training for personnel who walk down systems

o

Include fastener corrosion identification in the SONGS

preservation program

o

Include incidents observed of fastener corrosion with the

weekly active leak report

o

Expand the thermography program to cover insulated high energy

systems on a sampling basis

o

Develop a procedure for inspection and further corrective

actions as warranted

The inspector considered that the licensee's efforts and planned

corrective actions appeared adequate. However, the inspector will

continue to monitor the licensee's implantation of corrective

actions as part of the routine inspection effort. This item is

closed.

d. (Closed) Followup Item (50-361/91-13-02). "Material Condition Of The

Units - MO Backlog."

As discussed in inspection report 50-361/91-13, the inspector noted

numerous deficiency tags on equipment in all three units. Although

most of the items appeared to be of relatively low safety

significance, many dated back a few years (to 1987 or 1988).

It was

noted that the backlog of outstanding maintenance items appeared to

have been increasing in recent months, with most items being low

priority (non-safety related). (A backlog is considered as

corrective maintenance items that are safety or non-safety related

that have been in existence for more than 120 days that are awaiting

work that can be done on-line.)

The inspector had noted the slowly

increasing backlog of items awaiting repair and questioned whether

they were being properly prioritized and effectively dealt with.

Discussions with the licensee revealed that they were aware of the

18

backlog and had provided a method of tracking and trending these

items. The licensee also indicated that a Work Authorization Task

Force (WATF) had been formed to review the situation and recommend a

course of action.

The inspector reviewed the licensee's WATF efforts and noted that a

number of recommendations were made. Recommendations included the

implementation of work window managers, a dedicated operator to

interface between Maintenance and Operations for the issuance of

work orders, and a revised prioritization scheme. The inspector

also noted that the licensee's Nuclear Oversight Department (NOD)

also performed an organizational assessment that introduced a number

of recommendations.

The inspector noted that the licensee was in the process of

implementing a Work Process Management Team consisting of the

Operations and Maintenance Superintendents in Units 2 and 3. They

will be responsible for setting a charter and a schedule to further

enhance the maintenance process and implement remaining WATF and NOD

recommendations. The licensee also was very close to implementing

procedures that streamline and enhance the maintenance process by

incorporating all work group responsibilities into a single set of

procedures.

With regard to the maintenance order backlog, the licensee just

recently dedicated significant resources to reduce it. The

inspector noted that some progress has been made, although there was

a long way to go. Discussions with the licensee indicated that they

believed the backlog reduction rate would increase as maintenance

efforts get fully implemented.

The goals for maintenance items were less than 500 items per unit in

Units 2 and 3. Discussions with the Maintenance Manager indicated

that Unit 1 currently met the backlog goal.

However for Units 2 and

3, the level of items was approximately 650 items per unit at the

end of the inspection period.

The inspector noted that some maintenance items were being resolved

by the minor maintenance effort. This process as defined in

procedure S0123-XX-3, "Minor Maintenance Program," consisted of less

paperwork and planning needed to execute the work activity. Minor

maintenance is done on equipment if it meets a number of

requirements (e.g., it is within the skill of the craft, no written

work plan is necessary, it does not involve the disposition of an

NCR, and it does not require any operability testing).

The

procedure also provided examples of work activities that would fit

in the minor maintenance category.

The inspector considered the licensee's efforts to understand and

correct weaknesses in the maintenance process to be extensive. The

effectiveness of these actions and the licensee's efforts to reduce

the backlog of maintenance items including work performed under

19

minor maintenance procedures, will be reviewed as part of the

routine inspection effort. This item is closed.

e. (Closed) Information Notice (50-206/IN-86-99), Supplement 1,

"'Degradation Of Steel Containments' - Inspector Followup On

Licensee ISEG Evaluation For Potential Applicability To Unit 1."

NRC IN 86-99, Supplement 1, "Degradation Of Steel Containments," was

issued in response to the discovery of significant corrosion on the

external surface of the carbon steel drywell in the sand bed region

of the Oyster Creek plant.

On August 26, 1991, the licensee's ISEG organization issued its

evaluation of NRC IN 86-99. The inspector noted that the evaluation

stated that the SONGS Unit I containment is a 140 ft. diameter steel

sphere which extends 40 ft. below grade. It is continuously

supported by a concrete cradle between the steel shell and the

undisturbed soil.

The free-standing steel shell contains a concrete

structure which provides support and shielding for the equipment.

Loads from this structure are transmitted through the sphere shell

and the exterior concrete cradle to the soil.

The exterior surface

of the sphere, below grade, is protected from corrosion by an epoxy

coating and by cathodic protection. The cathodic protection system

is the impressed current type.

The method of verification for containment integrity is an

Integrated Leak Rate Test (ILRT) per 10 CFR 50, Appendix J. The

licensee stated that, as of the date of the ISEG evaluation, no ILRT

data had been obtained that would indicate that containment

integrity had deteriorated.

The inspector considered the evaluation adequate and that no further

followup action is required. Therefore, this item is closed.

f. (Closed) Information Notice (50-361, 362/IN-91-13). "Inadequate

Testing Of EDGs - Applies To 2nd And 3rd Units At Multi-Unit Sites."

This IN was intended to alert licensees to inadequacies in the

testing of emergency diesel generators (EDGs) at nuclear power

plants. In particular, some EDG testing had not adequately verified

the capability of the EDG to carry its maximum expected loads and

other tests had failed to properly verify the operation of the load

shedding logic for the EDG. More specifically, it was noted that

there was no requirement to test the EDG at its reactive load limit

or to compensate for ambient temperature effects.

The inspector reviewed the licensee's evaluation of the conditions

as applicable to SONGS. The inspector noted that the licensee

concluded, after discussions with the vendor, that a requirement to

compensate for ambient temperature variations was not necessary

since the EDG would only be affected by temperatures well above the

design maximum of 100 degrees in the diesel generator buildings.

20

The inspector also noted that the licensee revised procedure S023-3

3.12, "Diesel Generator Monthly Test," to include testing the EDGs

at reactive loads of 3000 to 3200 KVAR which is greater than the

worst case reactive load calculated at 2614 KVAR.

The inspector considered that the licensee's evaluation of this IN

was adequate. Therefore, this item is closed.

No violations or deviations were identified.

10. Follow-Up On Items Of Non-Compliance (92702)

a. (Closed) Violation (206/91-36-01). "Inoperable Halon System In The

4KV Switchqear Room."

This item identified that the Unit 1 4160 VAC (4KV) room Halon

system was inoperable without a continuous fire watch being

available for certain periods of time as required by Technical

Specifications (TS).

The licensee implemented a number of corrective actions following

the inoperability of this event. Those actions included properly

configuring the Halon system, revising procedures to include

drawings and instructions for the system actuation lines, and plans

to provide specific training on proper configuration of the Halon

system. The inspector considered the licensee's actions (both

implemented and planned) to be appropriate. Therefore, this item is

closed.

b. (Closed) Violation (206/91-36-02). "Inadequate Licensee Report

Concerning The Inoperable Halon System In The 4KV Switchgear Room."

This item identified a statement in an LER which was inaccurate.

The inaccurate statement was that a design basis fire in the 4KV

room would not have prevented the Unit from achieving and

maintaining safe shutdown.

For corrective actions on this issue, the licensee revised the LER

to properly reflect plant conditions at the time of the event,

discussed with LER writers the need to ensure that safety

assessments consider all plant conditions, and had all management

personnel review the response to the NOV to ensure that they were

aware of the need for LERs to be complete and accurate. Based upon

these actions, this item is closed.

c. (Closed) Violation (206/91-36-03). "Inadequate Halon System

Testing."

This item identified that the licensee's test program did not

include testing to demonstrate operability of the Halon bottle slave

cylinders.

21

For corrective actions to this item, the licensee revised the Halon

bottle surveillance procedures to include drawings of the system

actuation configuration and to include the fire protection system

manuals in the Vendor Interface Program to ensure that vendor

information is properly incorporated into fire protection

procedures. The inspector considered the licensee's actions

appropriate. This item is closed.

d. (Closed) Violation (50-361/91-13-04). "Followup Of Corrective

Actions Described In Licensee Civil Penalty Response Dated 2/2/91."

As discussed in inspection report 50-361/91-13, three corrective

actions remained to be completed concerning two violations first

referenced in inspection report 50-361/90-37. These violations

involved an auxiliary feedwater pump being inoperable due to a

misaligned steam trap (Unit 2), and the ECCS and containment spray

subsystem being inoperable due to a misaligned emergency sump outlet

valve (Unit 3).

The corrective actions that remained to be implemented from the

licensee's February 2, 1991, response to the Notice of Violation

were the following:

"

Install audible annunciator for engineered safety feature (ESF)

valves when in abnormal positions.

"

Review the administrative workload assigned to operators to

reduce non-operational duties.

o

Perform an AFW pump/turbine overspeed trip analysis to

determine optimum setting.

As of this inspection period, the licensee completed a review of the

administrative workload assigned to the operators. This resulted in

a number of changes to reduce the administrative burdens including

the assignment of a designated operator to interface with

maintenance in the preparation of work authorizations.

The inspector noted that the licensee formulated a work schedule to

install the audible annunciator for ESF valves during the Cycle VIII

refueling outages for Units 2 and 3. This commitment was entered in

the licensee's regulatory commitment tracking system (RCTS) to

ensure completion of the commitment.

The inspector noted that the licensee formulated a schedule to

perform the AFW pump turbine overspeed trip analysis during the

upcoming Cycle VII refueling outages for Units 2 and 3. This action

was also entered in the licensee's RCTS system to ensure completion

of the required action.

The inspector considered that the licensee's proposed and completed

I

22

corrective actions were conservative measures and appeared adequate

to minimize the potential for similar errors. Implementation of

remaining actions will be reviewed as part of the routine inspection

effort. Therefore, this item is closed.

No violations or deviations were identified.

11.

Unresolved Items

Unresolved items are matters about which more information is required to

determine whether they are acceptable items, violations or deviations.

An unresolved item addressed during this inspection is discussed in

paragraph 4 of this report.

12.

Exit Meeting

On July 16, 1992, an exit meeting was conducted with the licensee

representatives identified in Paragraph 1. The inspectors summarized the

inspection scope and findings as described in the Results section of this

report.

The licensee acknowledged the inspection findings and noted that

appropriate corrective actions would be implemented where warranted. The

.licensee

did not identify as proprietary any of the information provided

to or reviewed by the inspectors during this inspection.