ML13324A547

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Plant Vent Stack Flow Measurement Calibr Test
ML13324A547
Person / Time
Site: San Onofre Southern California Edison icon.png
Issue date: 01/16/1985
From:
Southern California Edison Co
To:
Shared Package
ML13324A546 List:
References
SO1-CT-82-240, SO1-CT-82-240-0, SO1-CT-82-240-01-R00, SO1-CT-82-240-1-R, TAC-56339, NUDOCS 8501180406
Download: ML13324A547 (2)


Text

/ENCLOSURE 1

TEST

SUMMARY

SO1-CT-82-240-01, REV.0 (wP#82-240)

PLANT VENT STACK FLOW MEASUREMENT CALIBRATION TEST SAFETY RELATED The objective of this test was to verify the Plant Vent Stack Wide Range Gas Monitor (WRGM), RT-1254, properly calculates stack flow.

This test was performed to satisfy the disposition of NCR #so1-F-2222, REV. 2, attached to this summary for information.

The test method was to traverse the plant vent stack with an accurate, calibrated velocity probe and compare the empirical data obtained for three different fan combinations with the WRGI! process flow indication.

Beginning with two fan operation, the values were required to agree within +/- 107.

The deviation for two fans was 20.4% (with the WRGI indicating low), and the procedure allowed a new data base constant calculation based on the results.

Once the new constant was entered into the WRGM computer, the WRGM indicated flow was 99.9% of the emptrical value.

Testing continued with single fan operation, and the deviation was 22.1% (with the WRGM once again indicating low).

Three far. operation eilded a 35.3% deviation (WRGM indicating high).

TER-01 was generated to document the out of +/- 10 deviation tolerance WRGX indication for single fan operation.

NCRiSOI-F-3049 was generated and retest P01 was performed to calculate a new constant to bring single fan operation into tolerance.

The retest resulted in proper indication for single fan operation and conservative indication for two fan operation (as compared to empirical data which was obtained again for both fan combinations).

TER-02 was generated to document the 35.3% deviation for three fan operation.

The resolution to this TER was "Accept as is" per the disposition of NCRSO1-F-30 4 9.

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TEST

SUMMARY

TER-03 was generated due to step 9.4 not being performed.

This step required a TCN to be written to surveillance procedure SO1-II-1.14 if the RT-1254 data base constant (process flow conversion factor) was recalculated during the performance of the test.

The TER resolution was "Accept as is " since this step was to be performed in Retest #01 after a new calculation was made.

Retest #01 was performed satisfactorily and NCR SOl-F-3049 has been closed.

Two TCN'S were generated as follows:

TCN 01: This was a scope/intent change to Retest #01 to enable the test method specified by NCR #SO1-F-3049.

TCN 02: This corrected a constant in the data base calculation for single fan operation in Retest #01 and was not a scope/intent change.

No further TCN's were generated.

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