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MONTHYEARW3F1-2011-0067, License Amendment Request, Proposed Change to Technical Specification 3/4.7.4 Table 3.7-3, Ultimate Heat Sink Minimum Fan Requirements Per Train.2011-10-13013 October 2011 License Amendment Request, Proposed Change to Technical Specification 3/4.7.4 Table 3.7-3, Ultimate Heat Sink Minimum Fan Requirements Per Train. Project stage: Request ML1131204702011-11-0808 November 2011 Email, Supplemental Information Request for Acceptance Review, License Amendment Request to Revise Technical Specification 3/4.7.4 Table 3.7-3, Ultimate Heat Sink Minimum Fan Requirements Per Train. Project stage: Acceptance Review W3F1-2011-0082, Supplement to License Amendment Request Proposed Change to Technical Specification 3/4.7.4 Table 3.7-3, Ultimate Heat Sink Minimum Fan Requirements Per Train.2011-11-25025 November 2011 Supplement to License Amendment Request Proposed Change to Technical Specification 3/4.7.4 Table 3.7-3, Ultimate Heat Sink Minimum Fan Requirements Per Train. Project stage: Supplement ML12023A0802012-01-18018 January 2012 Calculations Requested for License Amendment Request, Proposed Change to Technical Specification 3/4.7.4 Table 3.7-3, Ultimate Heat Sink Minimum Fan Requirements Per Train Project stage: Request ML1202303452012-01-23023 January 2012 Acceptance Review Following Supplement Email, License Amendment Request to Revise Technical Specification 3/4.7.4 Table 3.7-3, Ultimate Heat Sink Minimum Fan Requirements Per Train Project stage: Acceptance Review ML1205807382012-02-27027 February 2012 Request for Additional Information License Amendment Request for Proposed Change to Technical Specification 3/4.7.4 Table 3.7-3, Ultimate Heat Sink Minimum Fan Requirements Per Train Project stage: RAI ML1205807292012-02-27027 February 2012 Email, Request for Additonal Information License Amendment Request for Proposed Change to Technical Specification 3/4.7.4 Table 3.7-3, Ultimate Heat Sink Minimum Fan Requirements Per Train Project stage: Other W3F1-2012-0019, Response to Request for Additional Information, License Amendment Request to Revise Technical Specification 3/4.7.4 Table 3.7-3, Ultimate Heat Sink Minimum Fan Requirements Per Train2012-04-0303 April 2012 Response to Request for Additional Information, License Amendment Request to Revise Technical Specification 3/4.7.4 Table 3.7-3, Ultimate Heat Sink Minimum Fan Requirements Per Train Project stage: Response to RAI W3F1-2012-0028, Supplement 2 of License Amendment Request to Revise Technical Specification 3/4.7.4 Table 3.7-3, Ultimate Heat Sink Minimum Fan Requirements Per Train2012-05-22022 May 2012 Supplement 2 of License Amendment Request to Revise Technical Specification 3/4.7.4 Table 3.7-3, Ultimate Heat Sink Minimum Fan Requirements Per Train Project stage: Supplement ML1217105922012-06-19019 June 2012 Email, Request for Additional Information, Round 2, License Amendment Request for Proposed Change to Technical Specification 3/4.7.4 Table 3.7-3, Ultimate Heat Sink Minimum Fan Requirements Per Train Project stage: RAI W3F1-2012-0053, Response to a Request for Additional Information Regarding License Amendment Request to Revise Technical Specification 3/4.7.4 Table 3.7-3, Ultimate Heat Sink Minimum Fan Requirements Per Train.2012-07-17017 July 2012 Response to a Request for Additional Information Regarding License Amendment Request to Revise Technical Specification 3/4.7.4 Table 3.7-3, Ultimate Heat Sink Minimum Fan Requirements Per Train. Project stage: Response to RAI ML12250A4352012-10-31031 October 2012 Issuance of Amendment No. 237, Revise Technical Specification 3/4.7.4 Table 3.7-3, Ultimate Heat Sink Minimum Fan Requirements Per Train Project stage: Approval 2012-10-31
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Category:Letter type:W
MONTHYEARW3F1-2024-0049, Notification of Readiness for Supplemental Inspection2024-10-21021 October 2024 Notification of Readiness for Supplemental Inspection W3F1-2024-0042, License Amendment Request to Extend Allowable Outage Times for One or More Control Room Air Conditioning Units Inoperable2024-10-16016 October 2024 License Amendment Request to Extend Allowable Outage Times for One or More Control Room Air Conditioning Units Inoperable W3F1-2024-0038, Response to Request for Additional Information - Proposed Alternative WF3-RR-24-01 for Examinations of Pressurizer Circumferential and Longitudinal Shell-to-Head Welds and Nozzle-to-Vessel Welds2024-09-24024 September 2024 Response to Request for Additional Information - Proposed Alternative WF3-RR-24-01 for Examinations of Pressurizer Circumferential and Longitudinal Shell-to-Head Welds and Nozzle-to-Vessel Welds W3F1-2024-0039, Response to Request for Additional Information - Proposed Alternative WF3-RR-24-02 for Examinations of Steam Generator Pressure-Retaining Welds and Full Penetration Welded Nozzles2024-09-24024 September 2024 Response to Request for Additional Information - Proposed Alternative WF3-RR-24-02 for Examinations of Steam Generator Pressure-Retaining Welds and Full Penetration Welded Nozzles W3F1-2024-0041, Reply to a Notice of Violation, EA-24-0522024-09-19019 September 2024 Reply to a Notice of Violation, EA-24-052 W3F1-2024-0040, Special Report SR 2024-001-00 Radiation Monitor Inoperable Greater than 7 Days2024-09-0303 September 2024 Special Report SR 2024-001-00 Radiation Monitor Inoperable Greater than 7 Days W3F1-2024-0019, (Waterford 3) - Steam Generator Tube Inspection Report for the 25th Rf Inspection Performed During Operating Cycle 25 / Refuel 252024-07-22022 July 2024 (Waterford 3) - Steam Generator Tube Inspection Report for the 25th Rf Inspection Performed During Operating Cycle 25 / Refuel 25 W3F1-2024-0032, Completion of License Renewal Activities Prior to Entering the Period of Extended Operation2024-07-17017 July 2024 Completion of License Renewal Activities Prior to Entering the Period of Extended Operation W3F1-2024-0025, Automatic EFAS Actuation During Surveillance Test2024-07-10010 July 2024 Automatic EFAS Actuation During Surveillance Test W3F1-2024-0024, Special Report SR 2023-004-02 Radiation Monitor Inoperable Greater than 7 Days2024-06-17017 June 2024 Special Report SR 2023-004-02 Radiation Monitor Inoperable Greater than 7 Days W3F1-2024-0013, Manual Reactor Trip Due to Engineered Safety Features Actuation System Relay Failure2024-05-15015 May 2024 Manual Reactor Trip Due to Engineered Safety Features Actuation System Relay Failure W3F1-2024-0011, Licensee Amendment Request to Modify Surveillance Requirements in Support of Surveillance Frequency Control Program2024-05-0808 May 2024 Licensee Amendment Request to Modify Surveillance Requirements in Support of Surveillance Frequency Control Program W3F1-2024-0018, Submittal of Owners Activity Report Form for Inservice Inspection Performed During Operating Cycle 25 / Refuel 252024-05-0101 May 2024 Submittal of Owners Activity Report Form for Inservice Inspection Performed During Operating Cycle 25 / Refuel 25 W3F1-2024-0014, Report of Facility Changes, Tests, and Experiments and Commitment Changes for Two Year Period Ending April 28, 20242024-04-29029 April 2024 Report of Facility Changes, Tests, and Experiments and Commitment Changes for Two Year Period Ending April 28, 2024 W3F1-2024-0015, Annual Radioactive Effluent Release Report (ARERR) 2023 with Revised ODCM and Revised Process Control Program Procedure2024-04-24024 April 2024 Annual Radioactive Effluent Release Report (ARERR) 2023 with Revised ODCM and Revised Process Control Program Procedure W3F1-2024-0016, Annual Radiological Environmental Operating Report (AREOR) - 20232024-04-24024 April 2024 Annual Radiological Environmental Operating Report (AREOR) - 2023 W3F1-2024-0017, Annual Report of Individual Monitoring of Radiation Exposure for 2023 Per 10 CFR 20.22062024-04-23023 April 2024 Annual Report of Individual Monitoring of Radiation Exposure for 2023 Per 10 CFR 20.2206 W3F1-2024-0020, Annual Report on Westinghouse Electric Company LLC Combustion Engineering Emergency Core Cooling System Performance Evaluation Models for Calendar Year 20232024-04-11011 April 2024 Annual Report on Westinghouse Electric Company LLC Combustion Engineering Emergency Core Cooling System Performance Evaluation Models for Calendar Year 2023 W3F1-2024-0008, Proposed Alternative WF3-RR-24-01 for Examinations of Pressurizer Circumferential and Longitudinal Shell-to-Head Welds and Nozzle-to-Vessel Welds2024-03-18018 March 2024 Proposed Alternative WF3-RR-24-01 for Examinations of Pressurizer Circumferential and Longitudinal Shell-to-Head Welds and Nozzle-to-Vessel Welds W3F1-2024-0009, Proposed Alternative WF3-RR-24-02 for Examinations of Steam Generator Pressure-Retaining Welds and Full Penetration Welded Nozzles2024-03-18018 March 2024 Proposed Alternative WF3-RR-24-02 for Examinations of Steam Generator Pressure-Retaining Welds and Full Penetration Welded Nozzles W3F1-2024-0012, Response to NRC Integrated Inspection Report 05000382/20230042024-03-11011 March 2024 Response to NRC Integrated Inspection Report 05000382/2023004 W3F1-2024-0006, Special Report SR-2023-004-01, Radiation Monitor Inoperable Greater than 7 Days2024-02-28028 February 2024 Special Report SR-2023-004-01, Radiation Monitor Inoperable Greater than 7 Days W3F1-2023-0056, Owners Activity Report Form for Inservice Inspection Performed During Operating Cycle 24 / Refuel 242023-12-19019 December 2023 Owners Activity Report Form for Inservice Inspection Performed During Operating Cycle 24 / Refuel 24 W3F1-2023-0055, Reply to a Notice of Violation2023-12-14014 December 2023 Reply to a Notice of Violation W3F1-2023-0052, Core Operating Limits Report (COLR) - Cycle 26, Revision O2023-11-0707 November 2023 Core Operating Limits Report (COLR) - Cycle 26, Revision O W3F1-2023-0049, Revise Technical Specification 3/4.3.2 to Remove Exemption from Testing Certain Relays at Power to Support Elimination of Potential Single Point Vulnerability - Withdrawal2023-09-28028 September 2023 Revise Technical Specification 3/4.3.2 to Remove Exemption from Testing Certain Relays at Power to Support Elimination of Potential Single Point Vulnerability - Withdrawal W3F1-2023-0048, Special Report SR 2023-004-00 for Waterford Steam Electric Station, Unit 3, Radiation Monitor Inoperable Greater than 7 Days2023-09-25025 September 2023 Special Report SR 2023-004-00 for Waterford Steam Electric Station, Unit 3, Radiation Monitor Inoperable Greater than 7 Days W3F1-2023-0035, Application for Technical Specification Change to Revise Surveillance Requirements Included in the Surveillance Frequency Control Program2023-07-26026 July 2023 Application for Technical Specification Change to Revise Surveillance Requirements Included in the Surveillance Frequency Control Program W3F1-2023-0036, Special Report SR-2023-003-01 for Waterford Steam Electric Station, Unit 3, Radiation Monitor Inoperable Greater than 7 Days2023-05-0404 May 2023 Special Report SR-2023-003-01 for Waterford Steam Electric Station, Unit 3, Radiation Monitor Inoperable Greater than 7 Days W3F1-2023-0032, Annual Radioactive Effluent Release Report (ARERR) 20222023-04-27027 April 2023 Annual Radioactive Effluent Release Report (ARERR) 2022 W3F1-2023-0033, Submittal of Annual Radiological Environmental Operating Report - 20222023-04-27027 April 2023 Submittal of Annual Radiological Environmental Operating Report - 2022 W3F1-2023-0025, Annual Report of Individual Monitoring of Radiation Exposure for 2022 Per 10 CFR 20.22062023-04-11011 April 2023 Annual Report of Individual Monitoring of Radiation Exposure for 2022 Per 10 CFR 20.2206 W3F1-2023-0018, Updated Final Supplemental Response to NRC Generic Letter 2004-022023-03-30030 March 2023 Updated Final Supplemental Response to NRC Generic Letter 2004-02 W3F1-2023-0022, Registration of Dry Fuel Storage Cask Use2023-03-22022 March 2023 Registration of Dry Fuel Storage Cask Use W3F1-2023-0021, Submittal of Special Report SR 2023-003-00 Radiation Monitor Inoperable Greater than 7 Days2023-03-17017 March 2023 Submittal of Special Report SR 2023-003-00 Radiation Monitor Inoperable Greater than 7 Days W3F1-2023-0016, Registration of Dry Fuel Storage Cask Use2023-03-0303 March 2023 Registration of Dry Fuel Storage Cask Use W3F1-2023-0014, Reply to a Notice of Violation; EA-22-1192023-02-20020 February 2023 Reply to a Notice of Violation; EA-22-119 W3F1-2023-0013, Notification of Readiness for Supplemental Inspection2023-02-15015 February 2023 Notification of Readiness for Supplemental Inspection W3F1-2023-0007, Registration of Dry Fuel Storage Cask Use2023-02-0606 February 2023 Registration of Dry Fuel Storage Cask Use W3F1-2023-0010, Special Report SR 2023-002-00, Radiation Monitor Inoperable Greater than 7 Days2023-01-25025 January 2023 Special Report SR 2023-002-00, Radiation Monitor Inoperable Greater than 7 Days W3F1-2023-0002, SR 2023-001-00 for Waterford Steam Electric Station, Unit 3, Radiation Monitor Inoperable Greater than 30 Days2023-01-0505 January 2023 SR 2023-001-00 for Waterford Steam Electric Station, Unit 3, Radiation Monitor Inoperable Greater than 30 Days W3F1-2022-0067, Commitment Change Notification for Generic Safety Issue 191 and Generic Letter 2004-022022-12-20020 December 2022 Commitment Change Notification for Generic Safety Issue 191 and Generic Letter 2004-02 W3F1-2022-0054, Revise Technical Specification 3/4.3.2 to Remove Exemption from Testing Certain Relays at Power to Support Elimination of Potential Single Point Vulnerability2022-11-0101 November 2022 Revise Technical Specification 3/4.3.2 to Remove Exemption from Testing Certain Relays at Power to Support Elimination of Potential Single Point Vulnerability W3F1-2022-0063, Submittal of Emergency Preparedness Documents. Includes EP-001-001, Revision 372022-10-27027 October 2022 Submittal of Emergency Preparedness Documents. Includes EP-001-001, Revision 37 W3F1-2022-0059, Response to Clarification Questions Concerning Supplement to License Amendment Request to Adopt TSTF-5052022-10-13013 October 2022 Response to Clarification Questions Concerning Supplement to License Amendment Request to Adopt TSTF-505 W3F1-2022-0058, Reply to a Notice of Violation; EA-22-0332022-10-12012 October 2022 Reply to a Notice of Violation; EA-22-033 W3F1-2022-0049, Response to Request for Additional Information Regarding License Amendment Requests to Adopt 10 CFR 50.69 and TSTF-5052022-08-19019 August 2022 Response to Request for Additional Information Regarding License Amendment Requests to Adopt 10 CFR 50.69 and TSTF-505 W3F1-2022-0037, Submittal of Owner'S Activity Report Form for Inservice Inspection Performed During Operating Cycle 24 / Refuel 242022-08-0808 August 2022 Submittal of Owner'S Activity Report Form for Inservice Inspection Performed During Operating Cycle 24 / Refuel 24 W3F1-2022-0044, SR-2022-004-00 for Waterford Steam Electric Station, Unit 3, Radiation Monitor Inoperable Greater than 7 Days2022-07-0606 July 2022 SR-2022-004-00 for Waterford Steam Electric Station, Unit 3, Radiation Monitor Inoperable Greater than 7 Days W3F1-2022-0042, SR-22-003-00 for Waterford Steam Electric Station, Unit 3, Radiation Monitor Inoperable Greater than 7 Days2022-06-27027 June 2022 SR-22-003-00 for Waterford Steam Electric Station, Unit 3, Radiation Monitor Inoperable Greater than 7 Days 2024-09-03
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Entergy Nuclear South Entergy Operations, Inc.
17265 River Road Killona, LA 70057-3093 Tel 504 739 6660 Fax 504 739 6678 SEntergy Djacob2@entergy.com Donna Jacobs Vice President, Operations Waterford 3 W3F1-2012-0019 April 3, 2012 U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555-0001
SUBJECT:
Response to Request for Additional Information, License Amendment Request to revise Technical Specification 3/4.7.4 Table 3.7-3, "Ultimate Heat Sink Minimum Fan Requirements per Train" Waterford Steam Electric Station, Unit 3 Docket No. 50-382 License No. NPF-38
References:
- 1. Waterford 3 Letter W3F1 -2011-0067, License Amendment Request, Proposed Change to Technical Specification 3/4.7.4 Table 3.7-3, "Ultimate Heat Sink Minimum Fan Requirements per Train" (ADAMS Accession No. ML11290A009) dated September 21, 2011.
- 2. Waterford 3 Letter W3F1-2011-0082, Supplement to License Amendment Request, Proposed Change to Technical Specification 3/4.7.4 Table 3.7-3, "Ultimate Heat Sink Minimum Fan Requirements per Train" (ADAMS Accession No. ML113290070) dated November 25, 2011.
- 3. Waterford 3 Letter W3F1-2012-0004, Calculations Requested for License Amendment Request, Proposed Change to Technical Specification 3/4.7.4 Table 3.7-3, "Ultimate Heat Sink Minimum Fan Requirements per Train" (ADAMS Accession No. ML12023A080) dated January 18, 2012.
- 4. NRC E-mail Correspondence, Request for Additional Information, Kaly Kalyanam (Project Manager) to William J. Steelman (Licensing Manager)
Waterford, Unit 3, (ADAMS Accession Nos. ML120580729 and ML120580738) dated February 28, 2012.
Dear Sir or Madam:
By letter dated October 13, 2011, as supplemented by letters dated November 25, 2011, and January 18, 2012 (References 1, 2, and 3), Entergy Operations, Inc. (Entergy) made application to amend the Technical Specifications (TS) 3/4.7.4 Table 3.7-3, "Ultimate Heat Sink Minimum Fan Requirements Per Train." of the Waterford Steam Electric Station, Unit 3 (Waterford 3).
W3F17-2012-0019 Page 2 In Reference 4, the NRC staff made a Request for Additional Information (RAI) to answer a question they had regarding the validity of an equation used in a calculation that had been provided in Reference 3.
While considering the response to the RAI regarding the proposed change to Technical Specification Table 3.7-3, Waterford 3 obtained the services of a cooling tower expert to review the NRC question and provide an independent analysis. The cooling tower expert has preliminarily confirmed that the original calculation ECM95-009 method of determining the impact of taking wet cooling tower fans out-of-service uses a Cooling Tower Institute (CTI) equation that is not intended for that purpose. The equation correlates cooling tower performance to the cube root of the ratio of actual fan horsepower to design fan horsepower.
The cooling tower industry expert confirmed that the equation is intended to be used for comparing design performance to test performance where small changes in fan horsepower were measured. It was not intended to predict tower performance where total fan horsepower is reduced by large amounts.
Waterford 3 has entered this condition into the corrective action process (Condition Report CR-WF3-2012-1395) to identify the misapplication of the CTI equation. For the current configuration with all 8 wet cooling tower fans operable, the wet cooling towers are capable of performing their design basis function. The CTI equation misapplication only impacts the calculated performance capacity of the wet cooling tower with fans out-of-service.
Waterford 3 will provide a supplement to Reference 1 to ensure a conservative revised specification within the next 30 days. The corrective action program will be utilized to correct the Waterford 3 calculations and determine if additional actions are needed.
This submittal contains one new commitment as summarized in Attachment 1.
Please contact William Steelman, Licensing Manager, at 504-739-6685 if there are any comments regarding this response I declare under penalty of perjury that the foregoing is true and correct. Executed on April 3, 2012.
Sincerely, DJ/RJA
Attachment:
- 1. Regulatory Commitment
W3F1-2012-0019 Page 3 cc: Mr. Elmo E. Collins, Jr. RidsRgn4MailCenter@nrc.gov Regional Administrator U. S. Nuclear Regulatory Commission Region IV 1600 E. Lamar Blvd.
Arlington, TX 76011-4125 NRC Senior Resident Inspector Marlone.Davis@nrc.gov Waterford Steam Electric Station Unit 3 Dean. Overland@nrc.gov P.O. Box 822 Killona, LA 70057-0751 U. S. Nuclear Regulatory Commission Kaly.Kalyanam@nrc.gov Attn: Mr. N. Kalyanam Mail Stop O-07D1 Washington, DC 20555-0001 Louisiana Department of Environmental Ji.Wiley@LA.gov Quality Office of Environmental Compliance Emergency and Radiological Services Division P. 0. Box 4312 Baton Rouge, LA 70821-4312
Attachment 1 To W3F1-2012-0019 Regulatory Commitment to W3F1-2012-0019 Page 1 of 1 Regulatory Commitment The following table identifies those actions committed to by Entergy in this document. Any other statements in this submittal are provided for information purposes and are not considered to be regulatory commitments.
TYPE (Check one) SCHEDULED ONE- CONTINUING COMPLETION COMMITMENT TIME COMPLIANCE DATE (If ACTION Required)
Waterford 3 will provide a supplement to Reference X May 2, 2012 1 to ensure a conservative revised specification with the next 30 days.