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Category:Letter type:HNP
MONTHYEARHNP-18-050, Request to Extend Reactor Vessel Surveillance Capsule Report Submission Date2018-09-17017 September 2018 Request to Extend Reactor Vessel Surveillance Capsule Report Submission Date HNP-18-004, License Amendment Request to Change Shearon Harris Nuclear Power Plant, Unit 1, Emergency Plan Emergency Action Level Scheme2018-08-13013 August 2018 License Amendment Request to Change Shearon Harris Nuclear Power Plant, Unit 1, Emergency Plan Emergency Action Level Scheme HNP-18-035, Relief Request I3R-18, Alternative Repair and Replacement Testing Requirements for the Containment Building Equipment Hatch Sleeve Weld, Lnservice Inspection Program for Containment, Third Ten-Year Interval2018-06-0404 June 2018 Relief Request I3R-18, Alternative Repair and Replacement Testing Requirements for the Containment Building Equipment Hatch Sleeve Weld, Lnservice Inspection Program for Containment, Third Ten-Year Interval HNP-18-049, Submittal of 1 0 CFR 50.54(q) Evaluation Form of Changes to Procedure EMP-420, Emergency Program Maintenance, Revision 192018-05-0303 May 2018 Submittal of 1 0 CFR 50.54(q) Evaluation Form of Changes to Procedure EMP-420, Emergency Program Maintenance, Revision 19 HNP-18-023, Report of Changes Pursuant to 10 CFR 50.59 and Summary of Commitment Changes2018-05-0202 May 2018 Report of Changes Pursuant to 10 CFR 50.59 and Summary of Commitment Changes HNP-18-042, Annual Environmental (Non-radiological) Operating Report2018-04-30030 April 2018 Annual Environmental (Non-radiological) Operating Report HNP-18-032, Annual Radiological Environmental Operating Report2018-04-25025 April 2018 Annual Radiological Environmental Operating Report HNP-18-031, Annual Radioactive Effluent Release Report2018-04-25025 April 2018 Annual Radioactive Effluent Release Report HNP-18-047, Relief Request I4R-18, Reactor Vessel Closure Head Nozzle Repair Technique, Inservice Inspection Program, Fourth Ten-Year Interval, Non-Proprietary Version of Calculation2018-04-20020 April 2018 Relief Request I4R-18, Reactor Vessel Closure Head Nozzle Repair Technique, Inservice Inspection Program, Fourth Ten-Year Interval, Non-Proprietary Version of Calculation HNP-18-045, Submittal of Relief Request I4R-18, Reactor Vessel Closure Head Nozzle Repair Technique, Inservice Inspection Program, Fourth Ten-Year Interval2018-04-18018 April 2018 Submittal of Relief Request I4R-18, Reactor Vessel Closure Head Nozzle Repair Technique, Inservice Inspection Program, Fourth Ten-Year Interval HNP-18-044, Cycle 22 Core Operating Limits Report, Revision O2018-04-16016 April 2018 Cycle 22 Core Operating Limits Report, Revision O HNP-18-039, Supplement to License Amendment Request Regarding Spent Fuel Storage Pool Criticality Analyses2018-04-13013 April 2018 Supplement to License Amendment Request Regarding Spent Fuel Storage Pool Criticality Analyses HNP-18-021, Annual Report in Accordance with Technical Specification 6.9.1.22018-02-19019 February 2018 Annual Report in Accordance with Technical Specification 6.9.1.2 HNP-18-020, Supplement to Response to Request for Additional Information Regarding License Amendment Request for Spent Fuel Storage Pool Criticality Analyses2018-02-16016 February 2018 Supplement to Response to Request for Additional Information Regarding License Amendment Request for Spent Fuel Storage Pool Criticality Analyses HNP-18-019, Cycle 21 Core Operating Limits Report, Revision 12018-02-14014 February 2018 Cycle 21 Core Operating Limits Report, Revision 1 HNP-18-017, CFR 50.54(q) Evaluations2018-02-0505 February 2018 CFR 50.54(q) Evaluations HNP-18-001, Application to Adopt 10 CFR 50.69, Risk-Informed Categorization and Treatment of Structures, Systems, and Components (Sscs) for Nuclear Power Reactors.2018-02-0101 February 2018 Application to Adopt 10 CFR 50.69, Risk-Informed Categorization and Treatment of Structures, Systems, and Components (Sscs) for Nuclear Power Reactors. HNP-18-002, Response to Request for Additional Information Regarding a License Amendment Request Proposing Changes to Emergency Diesel Generator Technical Specifications Surveillance Requirements2018-01-22022 January 2018 Response to Request for Additional Information Regarding a License Amendment Request Proposing Changes to Emergency Diesel Generator Technical Specifications Surveillance Requirements HNP-18-003, Response to Request for Additional Information Regarding License Amendment Request for Spent Fuel Storage Pool Criticality Analyses2018-01-18018 January 2018 Response to Request for Additional Information Regarding License Amendment Request for Spent Fuel Storage Pool Criticality Analyses HNP-18-007, License Amendment Request to Incorporate Tornado Missile Risk Evaluator Into Licensing Basis - Supplement Regarding De Minimis Penetrations2018-01-11011 January 2018 License Amendment Request to Incorporate Tornado Missile Risk Evaluator Into Licensing Basis - Supplement Regarding De Minimis Penetrations HNP-18-006, Submittal of 14-Day Special Report for Accident Radiation Monitors2018-01-0404 January 2018 Submittal of 14-Day Special Report for Accident Radiation Monitors HNP-17-093, Supplement to License Amendment Request Proposing a New Set of Fission Gap Release Fractions for High Burnup Fuel Rods That Exceed the Linear Heat Generation Rate Limit Detailed in Regulatory Guide 1.183, Table 32017-11-29029 November 2017 Supplement to License Amendment Request Proposing a New Set of Fission Gap Release Fractions for High Burnup Fuel Rods That Exceed the Linear Heat Generation Rate Limit Detailed in Regulatory Guide 1.183, Table 3 HNP-17-078, Response to Request for Additional Information Regarding a License Amendment Request Proposing Changes to Emergency Diesel Generator Technical Specifications Surveillance Requirements2017-11-27027 November 2017 Response to Request for Additional Information Regarding a License Amendment Request Proposing Changes to Emergency Diesel Generator Technical Specifications Surveillance Requirements HNP-17-082, Response to Request for Additional Information Regarding License Amendment Request Proposing a New Set of Fission Gas Gap Release Fractions for High Burnup Fuel Rods That Exceed the Linear Heat Generation Limit Detailed In..2017-10-30030 October 2017 Response to Request for Additional Information Regarding License Amendment Request Proposing a New Set of Fission Gas Gap Release Fractions for High Burnup Fuel Rods That Exceed the Linear Heat Generation Limit Detailed In.. HNP-17-084, Response to Request for Additional Information Regarding a License Amendment Request Proposing Changes to Emergency Diesel Generator Technical Specifications Surveillance Requirements2017-10-30030 October 2017 Response to Request for Additional Information Regarding a License Amendment Request Proposing Changes to Emergency Diesel Generator Technical Specifications Surveillance Requirements HNP-17-025, Fourth Interval Lnservice Inspection Plan, Third Interval Containment Lnservice Inspection Plan, and Fourth Interval Lnservice Inspection Pressure Test Plan2017-10-23023 October 2017 Fourth Interval Lnservice Inspection Plan, Third Interval Containment Lnservice Inspection Plan, and Fourth Interval Lnservice Inspection Pressure Test Plan HNP-17-072, License Amendment Request to Incorporate Tornado Missile Risk Evaluator Into Licensing Basis2017-10-19019 October 2017 License Amendment Request to Incorporate Tornado Missile Risk Evaluator Into Licensing Basis HNP-17-077, License Amendment Request Regarding Rod Control Movable Assemblies Technical Specifications2017-10-10010 October 2017 License Amendment Request Regarding Rod Control Movable Assemblies Technical Specifications HNP-17-076, Supplement to License Amendment Request to Relocate Technical Specification Cycle-Specific Parameters to the Core Operating Limits Report, Delete Reference to Plant Procedure PLP-106, and Delete Duplicate Reporting Requirements.2017-10-0202 October 2017 Supplement to License Amendment Request to Relocate Technical Specification Cycle-Specific Parameters to the Core Operating Limits Report, Delete Reference to Plant Procedure PLP-106, and Delete Duplicate Reporting Requirements. HNP-17-073, Supplemental Information for License Amendment Request Regarding Spent Fuel Storage Pool Criticality Analyses2017-09-14014 September 2017 Supplemental Information for License Amendment Request Regarding Spent Fuel Storage Pool Criticality Analyses HNP-17-062, Response to March 12, 2012, Request for Information Enclosure 2, Recommendation 2.1, Flooding, Required Response 3, Flooding Focused Evaluation Summary Submittal2017-09-13013 September 2017 Response to March 12, 2012, Request for Information Enclosure 2, Recommendation 2.1, Flooding, Required Response 3, Flooding Focused Evaluation Summary Submittal HNP-17-061, Supplement to License Amendment Request Regarding Spent Fuel Storage Pool Criticality Analyses2017-07-20020 July 2017 Supplement to License Amendment Request Regarding Spent Fuel Storage Pool Criticality Analyses HNP-17-008, License Amendment Request Regarding Spent Fuel Storage Pool Criticality Analyses2017-06-28028 June 2017 License Amendment Request Regarding Spent Fuel Storage Pool Criticality Analyses HNP-17-003, License Amendment Request for Emergency Diesel Generator Surveillance Requirements Regarding Voltage and Frequency Limits and the Voltage Limit for Emergency Diesel Generator Load Rejection2017-06-0505 June 2017 License Amendment Request for Emergency Diesel Generator Surveillance Requirements Regarding Voltage and Frequency Limits and the Voltage Limit for Emergency Diesel Generator Load Rejection HNP-17-040, Snubber Program Plan2017-06-0101 June 2017 Snubber Program Plan HNP-17-051, 10 CFR 50.54(q) Evaluation2017-05-24024 May 2017 10 CFR 50.54(q) Evaluation HNP-17-050, Transmittal of 10 CFR 50.54(q) Evaluation for Revision 21 to PEP-250, Activation and Operation of the Joint Information Center2017-05-24024 May 2017 Transmittal of 10 CFR 50.54(q) Evaluation for Revision 21 to PEP-250, Activation and Operation of the Joint Information Center HNP-17-041, Response to Request for Additional Information Regarding License Amendment Request to Relocate Technical Specification Cycle-Specific Parameters to the Core Operating Limits Report, Delete Reference to Plant Procedure PLP-106, and Delete2017-05-22022 May 2017 Response to Request for Additional Information Regarding License Amendment Request to Relocate Technical Specification Cycle-Specific Parameters to the Core Operating Limits Report, Delete Reference to Plant Procedure PLP-106, and Delete Du HNP-17-033, License Amendment Request Proposing a New Set of Fission Gas Gap Release Fractions for High Burnup Fuel Rods That Exceed the Linear Heat Generation Rate Limit Detailed in Regulatory Guide 1.183, Table 3, Footnote 112017-05-22022 May 2017 License Amendment Request Proposing a New Set of Fission Gas Gap Release Fractions for High Burnup Fuel Rods That Exceed the Linear Heat Generation Rate Limit Detailed in Regulatory Guide 1.183, Table 3, Footnote 11 HNP-17-049, Transmittal of 10 CFR 50.54(q) Evaluation and Revision 26 to PEP-110, Emergency Classification and Protective Action Recommendations.2017-05-18018 May 2017 Transmittal of 10 CFR 50.54(q) Evaluation and Revision 26 to PEP-110, Emergency Classification and Protective Action Recommendations. HNP-17-047, 10 CFR 50.54(q) Evaluation2017-05-18018 May 2017 10 CFR 50.54(q) Evaluation HNP-17-048, Transmittal of 10 CFR 50.54(q) Evaluation and Revision 28 to PEP-230, Control Room Operations.2017-05-18018 May 2017 Transmittal of 10 CFR 50.54(q) Evaluation and Revision 28 to PEP-230, Control Room Operations. HNP-17-046, 10 CFR 50.54(q) Evaluation2017-05-18018 May 2017 10 CFR 50.54(q) Evaluation HNP-17-024, Annual Environmental (Nonradiological) Operating Report2017-04-28028 April 2017 Annual Environmental (Nonradiological) Operating Report HNP-17-023, Annual Radioactive Effluent Release Report2017-04-28028 April 2017 Annual Radioactive Effluent Release Report HNP-17-034, Response to Request for Additional Information Regarding License Amendment Request to Relocate Technical Specification Cycle-Specific Parameters to the Core Operating Limits Report, Delete Reference to Plant Procedure PLP-106..2017-04-25025 April 2017 Response to Request for Additional Information Regarding License Amendment Request to Relocate Technical Specification Cycle-Specific Parameters to the Core Operating Limits Report, Delete Reference to Plant Procedure PLP-106.. HNP-17-035, Request for Pilot Plant Status and Fee Waiver to Implement Tornado Missile Risk Evaluator2017-04-12012 April 2017 Request for Pilot Plant Status and Fee Waiver to Implement Tornado Missile Risk Evaluator HNP-17-045, 10 CFR 50.54(q) Evaluation of Change in Emergency Plan Implementation Procedure PEP-241, Revision 7, Technical Support Center (TSC) Emergency Ventilation System Operation2017-03-30030 March 2017 10 CFR 50.54(q) Evaluation of Change in Emergency Plan Implementation Procedure PEP-241, Revision 7, Technical Support Center (TSC) Emergency Ventilation System Operation HNP-17-014, Annual Report in Accordance with Technical Specifications, Section 6.9.1.22017-02-16016 February 2017 Annual Report in Accordance with Technical Specifications, Section 6.9.1.2 HNP-17-015, Summary of 10 CFR 50.54(q) Evaluation2017-02-15015 February 2017 Summary of 10 CFR 50.54(q) Evaluation 2018-09-17
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Progress Energy 10 CFR 50.4 September 22, 2011 Serial: HNP-11-089 Document Control Desk U. S. Nuclear Regulatory Commission Washington, DC 20555-0001 Shearon Harris Nuclear Power Plant / Unit I Docket No. 50-400 / Renewed License No. NPF-63
Subject:
Response to Request for Clarification regarding 180-day Steam Generator Tube Inspection Report
References:
- 1. Letter from D. Corlett to the Nuclear Regulatory Commission, Serial HNP-1 1-045, "Shearon Harris Nuclear Power Plant, Unit 1, Docket No. 50-400 / Renewed License No. NPF-63, 180-day Steam Generator Tube Inspection Report" dated May 5, 2011.
- 2. Email from B. Mozafari, USNRC, to J. Caves "Shearon Harris Unit I SG Inspection Report (TAC No. ME635 8)" dated August 23, 2011.
Ladies and Gentlemen:
By letter dated May 5, 2011, identified as Reference I above, Carolina Power & Light Company, doing business as Progress Energy Carolinas, Inc., submitted the 180-Day Steam Generator Tube Inspection Report for the Shearon Harris Nuclear Power Plant (HNP).
On August 23, 2011, HNP received a request for clarification of three points in the report, transmitted as Reference 2. HNP's response to the request for clarification is attached as an enclosure to this letter.
This document contains no new regulatory commitments.
Progress Energy Carolinas, Inc.
Harris Nuclear Plant AOO P. 0. Box 165 New Hill, NC27562
U. S. Nuclear Regulatory Commission Page 2 HNP-1 1-089 If there are any questions or if additional information is needed, please contact me at 919.362.3137.
Dave Corlett Supervisor, Licensing/Regulatory Programs Harris Nuclear Plant
Enclosure:
Response to Request for Clarification regarding Shearon Harris Unit I Steam Generator Inspection Report cc: Mr. J. D. Austin, NRC Sr. Resident Inspector, HNP Mr. V. M. McCree, NRC Regional Administrator, Region II Mrs. B. L. Mozafari, NRC Project Manager, HNP
U. S. Nuclear Regulatory Commission Page 3 HNP-1 1-089 bcc:
Mr. D. T. Conley Mr. J. W. Donahue Mr. J. D. Dufner Mr. S. D. Ebneter Mr. D. G. Eisenhut Mr. D. Griffith Mr. R. K. Holbrook Mr. W. Jefferson Jr.
Mr. E. J. Kapopoulos Jr.
Mr. C. W. Kornegay Mr. B. C. McCabe Mr. H. J. Miller Mr. G. D. Miller Mr. G. Peterson Mr. J. Scarola Mr. M. S. Tuckman Mr. J. C. Warner HNP NOS NTA Licensing Files (2 copies)
Nuclear Records
U. S. Nuclear Regulatory Commission Page lof2 HNP-1 1-089 Enclosure Response to Request for Clarification regarding 180-day Steam Generator Tube Inspection Report Question 1: For each refueling outage and SG tube inspection outage since installationof the replacement SGs, provide the cumulative effective full power months that the SGs have operated.
Response 1:
Outage Number Year Cumulative Outage Type EFPM ROW1 Fall 2001 0.0 S/G Replacement ROl1 Spring 2003 15.4 S/G tube inspection/Refueling Mid Cycle 12 Spring 2004 26.6 Unplanned S/G tube inspection following leak R012 Fall 2004 31.4 Refueling R013 Spring 2006 47.9 S/G tube inspection/Refueling R014 Fall 2007 64.1 Refueling RO15 Spring 2009 81.5 Refueling R016 Fall 2010 98.0 S/G tube inspection/Refueling Question 2: During the 2006 SG inspections, a restrictionwas identified approximately 22 inchesfrom the cold-leg tube end in SG B. Discuss what inspections, if any, were performed on this tube in the fall 2010 refueling outage. In addition, discuss the results of these inspections.
Response 2: The restriction identified during the 2006 inspection was located at row 23, column 26.
During this inspection, the full size .560 Bobbin Probe (Zetec EC-560-LLMC) was unable to complete the full length exam. The probe was inserted from tube end hot and met the restriction at tube sheet cold.
A .520 RPC Zetec probe was then inserted from tube end cold and through the restriction at tube sheet cold. No degradation was detected. The restriction was believed to be caused by the .560 Bobbin Probe itself and not by a defect in the tube. In 2010, the tube was inspected with a similar .560 Bobbin Probe (Zetec LLMC-EC-.560-110-36). This probe completed a full length exam without restriction. No detectable degradation was discovered on this tube during the 2010 inspection.
U. S, Nuclear Regulatory Commission Page 2of 2 HNP- 11-089 Enclosure Question 3: Provide any observations on whether any new dents/dings were identified during the fall 2010 inspectionsand whether the dents identified duringthe 2006 inspections (at the 8th and 9th tube supportplates in SG C) have changed If either new dents were identified or the previous dents have changed in size, provide details regardingthe cause of the new/changing indications.
Response 3: There were 12 new dents in S/G A, 2 new dents in S/G B, and 0 new dents in S/G C identified during the fall 2010 inspections. There was a slight difference in the voltage of previous dents (including those at the 8th and 9th tube support plates in S/G C) where some went up and others went down. The differences can be attributed to a change in probe type and also the orientation of the probe by the dent. The change in voltage was not deemed significant.
Although the scope of the 2010 inspection was roughly 50% of the 2006 inspection, the number of new dents discovered during the 2010 inspection has shown a marked decrease.
New Dents New Dents 2010 2006 S/G A 12 222 S/G B 2 12 S/G C 0 174