ML071640143

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IR 05000456-07-007 and 05000457-07-007; on 03/12/2007 - 05/01/2007; Braidwood Station, Units 1 and 2; Identification and Resolution of Problems
ML071640143
Person / Time
Site: Braidwood  Constellation icon.png
Issue date: 06/12/2007
From: Richard Skokowski
NRC/RGN-III/DRP/RPB3
To: Crane C
Exelon Generation Co, Exelon Nuclear
References
FOIA/PA-2010-0209 IR-07-007
Download: ML071640143 (36)


See also: IR 05000456/2007007

Text

June 12, 2007

Mr. Christopher M. Crane

President and Chief Nuclear Officer

Exelon Nuclear

Exelon Generation Company, LLC

4300 Winfield Road

Warrenville, IL 60555

SUBJECT: BRAIDWOOD STATION, UNITS 1 AND 2

NRC PROBLEM IDENTIFICATION AND RESOLUTION

INSPECTION REPORT 05000456/2007007 AND 05000457/2007007

Dear Mr. Crane:

On May 1, 2007, the U.S. Nuclear Regulatory Commission (NRC) completed a team inspection

of problem identification and resolution at your Braidwood Station, Units 1 and 2. The enclosed

inspection report documents the inspection findings which were discussed on March 30, 2007,

Mr. M. Smith and other members of your staff, and subsequently on May 1, 2007, with

Mr. D. Ambler and other members of your staff.

This inspection was an examination of activities conducted under your license as they

relate to the identification and resolution of problems, compliance with the Commissions

rules and regulations, and with the conditions of your operating license. Within these areas,

the inspection involved selected examination of procedures and representative records,

observations of activities, and interviews with personnel.

On the basis of the sample selected for review, the team concluded that, in general, problems

were properly identified, evaluated, and corrected. However, the inspectors identified two

findings during the inspection. One finding of very low safety significance (Green) was

identified for the licensees failure to perform an adequate extent of condition review for safety

related valves that had not been included in and tested in accordance with the inservice test

program. The second finding involved the licensees failure to maintain an adequate operations

procedure that had the potential to secure the only remaining residual heat removal pump while

in the recirculation mode of operation. Both findings were violations of NRC requirements.

However, because each finding was of very low safety significance and because the findings

were entered into your corrective action program, the NRC is treating these findings as non-

cited violations (NCVs), in accordance with Section VI.A.1 of the NRCs Enforcement Policy.

C. Crane -2-

If you contest the subject or severity of a non-cited violation, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington, DC 20555-0001; with a copy to the Regional Administrator, U.S. Nuclear

Regulatory Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL

60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission,

Washington, DC 20555-0001; and the Resident Inspector Office at the Braidwood Station.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and

its enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of NRC's document system

(ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html

(the Public Electronic Reading Room).

Sincerely,

/RA/

Richard A. Skokowski, Chief

Branch 3

Division of Reactor Projects

Docket Nos. 50-456; 50-457

License Nos. NPF-72; NPF-77

Enclosure: Inspection Report No. 05000456/2007007 and 05000457/2007007

w/Attachment: Supplemental Information

cc w/encl: Site Vice President - Braidwood Station

Plant Manager - Braidwood Station

Regulatory Assurance Manager - Braidwood Station

Chief Operating Officer

Senior Vice President - Nuclear Services

Vice President - Operations Support

Vice President - Licensing and Regulatory Affairs

Director Licensing

Manager Licensing - Braidwood and Byron

Senior Counsel, Nuclear, Mid-West Regional

Operating Group

Document Control Desk - Licensing

Assistant Attorney General

Illinois Emergency Management Agency

State Liaison Officer

Chairman, Illinois Commerce Commission

C. Crane -2-

If you contest the subject or severity of a non-cited violation, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington, DC 20555-0001; with a copy to the Regional Administrator, U.S. Nuclear

Regulatory Commission - Region III, 2443 Warrenville Road, Suite 210, Lisle, IL

60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission,

Washington, DC 20555-0001; and the Resident Inspector Office at the Braidwood Station.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and

its enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of NRC's document system

(ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html

(the Public Electronic Reading Room).

Sincerely,

Richard A. Skokowski, Chief

Branch 3

Division of Reactor Projects

Docket Nos. 50-456; 50-457

License Nos. NPF-72; NPF-77

Enclosure: Inspection Report No. 05000456/2007007 and 05000457/2007007

w/Attachment: Supplemental Information

cc w/encl: Site Vice President - Braidwood Station

Plant Manager - Braidwood Station

Regulatory Assurance Manager - Braidwood Station

Chief Operating Officer

Senior Vice President - Nuclear Services

Vice President - Operations Support

Vice President - Licensing and Regulatory Affairs

Director Licensing

Manager Licensing - Braidwood and Byron

Senior Counsel, Nuclear, Mid-West Regional

Operating Group

Document Control Desk - Licensing

Assistant Attorney General

Illinois Emergency Management Agency

State Liaison Officer

Chairman, Illinois Commerce Commission

DOCUMENT NAME: C:\FileNet\ML071640143.wpd

G Publicly Available G Non-Publicly Available G Sensitive G Non-Sensitive

To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" = Copy with attach/encl "N" = No copy

OFFICE RIII RIII

NAME DSmith:dtp RSkokowski

DATE 06/12/2007 06/12/2007

OFFICIAL RECORD COPY

Letter to Christopher M. Crane from Richard A. Skokowski dated June 12, 2007

SUBJECT: BRAIDWOOD STATION, UNITS 1 AND 2

NRC PROBLEM IDENTIFICATION AND RESOLUTION

INSPECTION REPORT 05000456/2007007; 05000457/2007007

DISTRIBUTION:

RAG1

TEB

RFK

RidsNrrDirsIrib

GEG

KGO

RML2

SAM9

SRI Braidwood

DRPIII

DRSIII

CAA1

LSL (electronic IRs only)

C. Pederson, DRS (hard copy - IRs only)

PLB1

TXN

ROPreports@nrc.gov (inspection reports, final SDP letters, any letter with an IR number)

U. S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos: 50-456; 50-457

License Nos: NPF-72; NPF-77

Report No: 05000456/2007007 and 05000457/2007007

Licensee: Exelon Nuclear

Facility: Braidwood Station, Units 1 and 2

Location: Braceville, Illinois

Dates: March 12 through May 1, 2007

Inspectors: D. Smith, Project Engineer - Team Lead

N. Valos, Senior Operations Engineer

D. Jones, Reactor Engineer

M. Perry, Illinois Emergency Management Agency

Approved by: R. Skokowski, Chief

Branch 3

Division of Reactor Projects

Enclosure

SUMMARY OF FINDINGS

IR05000456/2007007, 05000457/2007007; 03/12/2007 - 05/01/2007; Braidwood Station,

Units 1 and 2. Identification and Resolution of Problems.

This report covers an approximate 16 week period of inspection by a project engineer, two

regional specialists, and an Illinois Emergency Management Agency inspector. Two Green

findings, which were both Non-cited violations, were identified by the inspectors. The

significance of most findings is indicated by their color (Green, White, Yellow, Red) using

Inspection Manual Chapter 0609, Significance Determination Process (SDP). Findings for

which the SDP does not apply may be Green or be assigned a severity level after NRC

management review. The NRCs program for overseeing the safe operation of commercial

nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3,

dated July 2000.

Identification and Resolution of Problems

In summary, the inspectors determined that the stations corrective action program was

effectively implemented as evidenced by the identification of plant issues through various

methods including departmental assessments and nuclear oversight audits. Plant issues

were documented in the stations corrective action program in a timely manner, and the

licensee generally implemented effective corrective actions to address plant issues and

events. The station has been effectively utilizing operating experience to prevent events

and improve performance at the station. However, an example of an inadequately performed

extent of condition review resulted in a Non-Cited violation during this inspection. A similar

problem with the licensees extent of condition reviews was also identified during the

October 2005 Problem Identification and Resolution Inspection.

The presence of a challenging nuclear oversight organization was apparent at the station.

This organization as well as other internal and external groups, have noted continuing

deficiencies in supervisory oversight. This issue with supervisory oversight was evident in the

licensees ability to sustain improved performance in several struggling areas, such as, the

control of transient combustibles, maintenance of personnel qualifications, and events related

to the bumping of plant equipment. The inspectors noted good communications of and

execution of the stations employee concern program. Additionally, the results from interviews,

conducted by the inspectors, reflected a safety conscious work environment at the station.

A. NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

"Procedures," for the licensees failure to provide an adequate procedure to

ensure the continued operation of the "A" residual heat removal pump, during

cold leg recirculation mode of operation, during conditions when the "B" residual

heat removal pump was not available. The licensee initiated an issue report to

2 Enclosure

track the resolution of this finding. Subsequently, the licensee revised the

affected procedure on May 21, 2007 to ensure one residual heat removal pump

remained operable.

The licensees failure to maintain an adequate procedure to ensure the

continued operation of the A residual heat removal pump was more than minor

because the finding affected the mitigating systems cornerstone objective of

ensuring the availability and reliability of the emergency core cooling system to

respond to initiating events to prevent undesirable consequences. Specifically,

the finding was associated with the mitigating systems attribute of procedure

quality. The finding is of very low safety significance because the finding

screened as Green during the Phase 1 Significance Determination Process.

(Section 4OA2.a.1)

Appendix B, Criterion XI, "Test Control," because the licensee failed to include

several manual component cooling water system valves, that were required to

perform a safety function, in the inservice testing (IST) program and

subsequently test the valves in accordance with IST program requirements.

The finding was related to the cross-cutting area of Problem Identification and

Resolution. A cross-cutting aspect in the corrective action program was

identified because the licensee did not conduct an adequate extent of condition

review, for a previously missed IST surveillance on several essential service

water system valves. As a result, the licensee failed to identify that the

component cooling water systems valves required inclusion in and testing by

the IST program. The licensee initiated an issue report to track the corrective

actions for this finding. Subsequently, the licensee placed the valves on the

Plan-Of-The-Day Meeting Agenda to ensure testing, which was scheduled for

June 30, 2007.

The failure to account for these valves in the IST program was more than minor

because the finding affected the mitigating systems cornerstone objective of

ensuring the availability and reliability of the component cooling water and

residual heat removal systems when required to respond to initiating events to

prevent undesirable consequences. Specifically, the finding was associated with

the mitigating systems attribute of equipment performance. The finding is of

very low safety significance because the finding screened as Green during the

Phase 1 Significance Determination Process. (Section 4OA2.a.2)

B. Licensee-Identified Violations

None.

3 Enclosure

REPORT DETAILS

4OA2 Problem Identification and Resolution (PI&R) (71152B)

a. Assessment of the Corrective Action (CA) program

(1) Inspection Scope

The inspector reviewed the licensees CA program implementing procedures and

attended CA program meetings to assess the implementation of the CA program

by site personnel.

The inspectors reviewed risk and safety significant issues in the licensees CA program

since the last NRC PI&R inspection in October 2005. The selection of issues ensured

an adequate review of issues across NRC cornerstones. The inspectors used issues

identified through NRC generic communications, department self assessment, nuclear

oversight audits, operating experience reports, and NRC documented findings as

sources to select issues. Additionally, the inspectors reviewed issue reports generated

as a result of station personnels performance in daily plant activities. In addition, the

inspectors reviewed Issue Reports (IRs) and a selection of completed investigation from

the licensees various investigation methods, which included root cause, apparent

cause, equipment apparent cause, common cause, and quick human performance

investigations.

The inspectors selected four high risk systems, which included the emergency diesel

generator, circulating water, pressurizer, essential service water systems, to review in

detail. The inspectors review was to determine whether the licensee was properly

monitoring and evaluating the performance of these systems through effective

implementation of station monitoring programs. A five year review on the pressure

boundary, and essential service water systems was also undertaken to assess the

licensees efforts in monitoring for system degradation due to aging aspects. The

inspectors also performed partial system walkdowns of all the systems except for the

pressure boundary system due to the systems inaccessibility.

During the reviews, the inspectors determined whether the licensees actions were in

compliance with the stations corrective action program and 10 CFR 50, Appendix B

requirements. Specifically, the inspectors determined if station personnel was

identifying plant issues at the proper threshold, entering the plant issues into the

stations CA program in a timely manner, and assigning the appropriate prioritization for

resolution of the issues. The inspectors also determined whether the licensee assigned

the appropriate investigation method to ensure the proper determination of root,

apparent, and contributing causes. The inspectors also evaluated the timeliness and

effectiveness of corrective actions for selected IRs, completed investigations, and NRC

findings including non-cited violations.

This inspection constitutes one biennial sample of problem identification and resolution

as defined by Inspection Procedure 71152.

4 Enclosure

(2) Assessment

.1 Identification of Issues

The licensees effectiveness in implementing the stations CA program was

evidenced by the engagement of station personnel, from all departments, in

generating issue reports, documentation of findings by both internal and external

groups, number of self-identified trends, and results from the stations 2007 PI&R

Focused Area Self Assessment (FASA). Generally, department assessments and

nuclear oversight audits properly characterized issues as deficiencies when the

requirements of a CA program element were not met. Concurrently, documented

issues, meeting CA program element requirements, were appropriately specified as

recommendations to further improve station performance. However, the inspectors

did note one instance where a Nuclear Oversight (NOS) audit mischaracterized the

corrective action to revise a plant support procedure, to improve its quality, as a

recommendation. The audits characterization should have been specified as a

deficiency because the procedure could not be performed as written. This

inadequate procedure was not a violation of NRC requirements.

Based on the wide range of plant deficiencies and enhancements noted in IRs, the

inspectors determined that station personnel utilized the appropriate threshold level for

entering plant issues in the CA program. Additionally, maintenance rule, system health,

surveillance, and boric acid station program owners were appropriately generating issue

reports when program requirements were not met or upon the identification of adverse

trends. During, the inspectors reviewed control room logs from March 16 through

March 19, 2007, they noted, as did the sites PI&R FASA, that the control room

operators had not consistently generated IRs from documented operational issues or

equipment failures described in the logs. The licensee issued Operations Memo 1-07,

in January 2006, describing that such log entries warranted an issue report. In addition,

there were a few instances where the licensee did not generate timely issue reports

based on the inspectors observations. For example, a radiation area warning gate was

found blocking a painted warning sign on the floor warning personnel that radio use in

the area was prohibited. The licensees failure to ensure warning signs were not

blocked was considered minor as there were no adverse safety consequences as a

result of this failure. The gate was moved but the licensee did not generate an issue

report until several requests were made by the inspectors. Although the licensees had

not fully implemented the corrective actions from the PI&R FASA deficiency, the

inspectors considered the licensees progress slow to ensure IRs were consistently

generated.

The inspectors determined that the station implemented effective corrective actions to

address the causes of maintenance department personnels lack of involvement in

writing issue reports; this issue was identified during the 2005 NRC PI&R Inspection

(05000456/2005012; 05000457/2005012). The CA Program Manager conducted

presentations on the IR initiation process to ensure the maintenance staff understood

the process and computers were located in the maintenance shop for ease of access.

The results from the partial system walkdowns, conducted by the inspectors, indicated

that systems were well maintained and that identified deficiencies, such as oil and water

leaks, were entered into the CA program. During the walkdown, the inspectors did

5 Enclosure

identify a couple of deficiencies that had not been entered into the CA program,

however these deficiencies were minor in nature and did not adversely impact system

operability.

Findings and Observations

Inadequate Procedure to Ensure the Continued Operation of the "A" Residual Heat

Removal (RHR) Pump While in the Cold Leg Recirculation Mode of Operation

Introduction: The inspectors identified a finding of very low safety significance and

associated Non Cited Violation (NCV) of Technical Specification 5.4.1, "Procedures,"

for the licensees failure to provide an adequate procedure to ensure the continued

operation of the "A" RHR Pump, while in the cold leg recirculation mode of operation,

when the "B" RHR Pump was not available.

Description: On March 22, 2007, the inspectors identified that Braidwood Normal

Operating System Procedure, BwOP CC-8, "Isolation of CC Between Units 1 and 2,"

Revision 18, was inadequate. This procedure was used to support actions in the

Braidwood Emergency Operating Procedures (EOP), 1BwEP ES-1.3, "Transfer to

Cold Leg Recirculation Unit 1," Revision 104, and 2BwEP ES-1.3, "Transfer to Cold

Leg Recirculation Unit 2," Revision 104. The inspectors concluded that procedure

BwOP CC-8 was inadequate because the procedure would not ensure continued

operation of the safety injection and the centrifugal charging pumps when the

"B" RHR pump was not available.

Specifically, operators would use Procedure BwOP CC-8 for an event that required

the transfer of the emergency core cooling system to the recirculation mode due to

low-low refueling water storage tank level. Each unit specific EOP (1BwEP ES-1.3

and 2BwEP ES-1.3) specified the actions to complete the transfer to the recirculation

mode. Once in the recirculation mode, the centrifugal charging pumps and the safety

injection pump pumps were started using steps 1 through 6 of either EOP. Step 10.c,

of each EOP, specified aligning component cooling water system for post-loss of cooling

accident recovery using BwOP CC-14, "Post Loss of Cooling Accident [LOCA]

Alignment of the Component Cooling [CC] System, Revision 14. Procedure BwOP

CC-14 required the use of BwOP CC-8, "Isolation of Component Cooling [CC] Between

Units 1 and 2," for completing this task.

Procedure BwOP CC-8 was used to separate Unit 1 component cooling water system

flow from Unit 2 CCW flow during both normal and accident conditions. Therefore, if the

common (CC) heat exchanger was initially aligned to the unit experiencing a LOCA, the

operators were directed to secure the A RHR pumps. Steps to secure the pump were

specified by BwOP CC-8, Step F.1.c.6 for Unit 1 and Step F.2.c.7 for Unit 2, while the

RHR pumps were providing the water source supply to the safety injection and

centrifugal charging pumps (Piggyback Mode). The pump would be secured based on

the execution of either step, while manipulating several component cooling system

valves, during the time to align the common CC heat exchanger to the unit with the

LOCA. As a result of securing the only running residual heat removal pump

BwOP CC-8, while in the "piggy back" mode of operation, irreversible pump

damage could occur to the safety injection and both centrifugal charging pumps.

6 Enclosure

Upon the identification of this issue by the inspectors, the licensee initiated IR 00611024

to track this finding for resolution.

Analysis: The inspectors determined that the failure to provide an adequate procedure

to ensure the continued operation of the "A" residual heat removal pump, while in the

cold leg recirculation mode of operation, when the "B" RHR Pump was not available was

a performance deficiency warranting a significance evaluation. The inspectors reviewed

this issue against the guidance contained in Appendix B, "Issue Dispositioning

Screening," of Inspection Manual Chapter (IMC) 0612, "Power Reactor Inspection

Reports." The inspectors determined that the finding was more than minor in

accordance with IMC 0612, Appendix B, "Issue Disposition Screening," because the

finding affected the mitigating systems cornerstone objective of ensuring the availability

and reliability of the ECCS to respond to initiating events to prevent undesirable

consequences. Specifically, the finding was associated with the mitigating systems

attribute of procedure quality.

The inspectors evaluated the finding using IMC 0609, Significance Determination

Process,@ Appendix A, Significance Determination of Reactor Inspection Findings for

At-Power Situations,@ Attachment 1, dated March 23, 2007. The inspectors answered

No to all five questions under the Mitigating System Cornerstone column of

Attachment 1. The finding was not a design or qualification deficiency confirmed not to

result in loss of function per Generic Letter 91-18; did not represent a loss of system

safety function; did not represent an actual loss of safety function of a single train for

greater than its Technical Specification allowed outage time; did not represent an actual

loss of safety function of one or more non-Technical Specification trains of equipment

designated as risk-significant per 10 CFR 50.65 for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />; did not

screen as potentially risk significant due to a seismic, flooding, or severe weather

initiating event.

Also, the finding did not affect the safety function of the high pressure recirculation

system unless one train of the residual heat removal system was initially failed or

unavailable due to maintenance. The unavailability of one safety system train was

inherently accounted for in the SDP. Therefore, when the operators would have

secured the residual heat removal pump per procedure, the loss of this train would have

been accounted for in the SDP. In addition, the regional Senior Reactor Analyst (SRA)

performed a confirmatory analysis to assess the risk of the finding using the site-specific

Braidwood Standardized Plant Analysis Risk Model, Revision 3.21. The SRA assumed

that if one train of residual heat removal system was unavailable that the high pressure

recirculation function would be failed because of the inadequate procedure. Using this

assumption, the SRA determined that the change in core damage frequency due to the

finding was less than 1.0E-6/yr, which was considered to be of very low safety

significance (Green).

Enforcement: Technical Specification 5.4.1, "Procedures," required, in part, that

written procedures be established, implemented, and maintained covering the

emergency operating procedures (EOPs) required to implement the requirements of

NUREG-0737, "Clarification of TMI Action Plan Requirements," and NUREG-0737,

Supplement 1. Item I.C.1 of NUREG-0737 and NUREG-0737, Supplement 1, Section 7,

required, in part, the development of EOPs to cover transients and accidents including

7 Enclosure

an event that required transfer of the emergency core cooling system to the cold leg

recirculation mode of operation.

Contrary to this requirement, on March 22, 2007, the inspectors discovered that

Braidwood Normal Operating Procedure, BwOP CC-8, "Isolation of CC Between Units 1

and 2," Revision 18, was inadequate. This procedure was used to support actions in

each unit specific Emergency Operating Procedure, 1BwEP ES-1.3, "Transfer to Cold

Leg Recirculation Unit 1" Revision 104, and 2BwEP ES-1.3, "Transfer to Cold Leg

Recirculation Unit 2," Revision 104. A procedural step failed to ensure the continued

operation of the safety injection and centrifugal charging pumps, while in the cold leg

recirculation mode of operation, when the "B" residual heat removal system pump was

not available. The licensee generated an issue report to followed up on the corrective

actions for this finding. Subsequently, the licensee revised BwOP CC-8 on

May 21, 2007, to ensure a RHR pump remained operable.

Because the finding is of very low safety significance and it was entered into the

licensees corrective action program (IR Number 00610994), the finding is being

treated as a NCV consistent with Section VI.A.1 of the NRC Enforcement Policy.

(05000455/2007007-01;05000456/2007007-01)

.2 Prioritization and Evaluation of Issues

The inspectors concluded that the licensee had properly prioritized issues based on

the safety significance of issues, and that issues were generally well evaluated. The

inspectors did not identify any issue reports that were not properly prioritized. In

addition, the inspectors observed several station ownership committee (SOC) and

management review board committee (MRC) meetings, and concluded that both

committees generally ensured the proper prioritization and appropriate investigation

assignments for plant issues. However, the inspectors did note several instances

where the oversight provided by both committees was not thorough. The sites 2007

PI&R FASA documented issue with the performance of the MRC. The inspectors

observed that the licensee had initiated the appropriate subsequent actions to evaluate

adverse trends. Due to the effective trending at the station, the inspectors did not

identify any adverse trends that had not been previously captured in the CA program

through department self-identification, NOS activities, quarterly nuclear safety review

board site visits, and the efforts of the sites PI&R FASA team.

The inspectors determined that the licensees selection of investigation methods, in

addressing site issues in all areas of plant operations, was appropriate and

commensurate with the safety significance of the issue or event. Also, the inspectors

determined that during extent of condition reviews, for plant issues, the licensees

reviews were generally adequate. However, this inspection as well as October 2005

NRC PI&R inspection identified shortcomings in the licensees extent of condition

reviews. The 2005 PI&R documented that a root cause evaluation, which was

associated with the precipitation of calcium carbonate in the ultimate heat sink

(IR199206), was too narrowly focused and failed to identified all the potentially affected

equipment. During this inspection, the licensee was again too narrow in umbrelling the

8 Enclosure

potentially affected components. In this case, the licensees extent of condition review

failed to identify that several component cooling water valves had not been included in

and tested in accordance with the requirement of the inservice testing (IST) program.

Regarding the licensees review of equipment operability, the inspectors determined,

that in general, they were appropriate with some shortcomings noted. The sites PI&R

FASA as well as the inspectors identified that some operability evaluations did not

discuss the affect on system operability for component failures identified when the

system was not required to be operable. An example noted by the inspectors, where

the operability basis was lacking, involved issue report Number 552355, "Relief valve

removed from 2SI8848 failed final seat leakage." The evaluation only documented that

an active leak was noted last cycle when the relief valve was installed. However, the

evaluation did not discuss how the system would have been affected if the valve had

lifted and subsequently experienced excessive seat leakage. Additionally, the residents

had been identifying similar examples during inspections and discussed these issues at

prior exit meetings with the licensee. The licensee generated IRs as a result of their

own FASA, the NRC PI&R inspection, and concerns from the resident inspectors in this

area.

Both the sites 2007 PI&R FASA and the inspectors, noted a few isolated instances,

where the licensees performance did not meet the requirements of several of these

CA program elements. The issues identified by the inspectors are documented below.

Findings and Observations

Component Cooling Water (CCW) System Valves not Included in the IST Program

Introduction: The inspectors identified a Green finding involving a Non-Cited Violation of

10 CFR Part 50, Appendix B, Criterion XI, Test Control, for the licensees failure to test

several manual component cooling water system valves, that required manipulation to

support the stations safety analysis, as specified by the inservice testing program.

Description: On March 18, 2007, the inspectors assessed the licensees extent

of condition review that had been performed for Inspection Report (IR)

Number 00522178. The IR was associated with the licensees failure to include

certain essential service water system valves in the IST program; the licensee

completed an apparent cause evaluation for this issue on August 21, 2006. In

assessing the quality of the extent of condition review, the inspectors identified that

certain manual CCW valves, which required manipulation during the transfer of the

emergency core cooling system to the recirculation mode, were not included in and

tested by the IST program.

Section 4.4.3, Manual Valves, of NUREG-1482, Guidelines for Inservice Testing

at Nuclear Power Plants, Revision 1, January 2005, specified that manual valves

credited in the licensees safety analysis to perform a specific safety function in

shutting down the reactor to a safe shutdown condition, maintaining the safe

shutdown condition, or mitigating the consequences of an accident be included in

the IST program. The inspectors identified that Braidwood Emergency Operating

Procedures, for both units, 1BwEP ES-1.3, Transfer to Cold Leg Recirculation Unit 1,"

9 Enclosure

Revision 104, and 2BwEP ES-1.3, Transfer to Cold Leg Recirculation Unit 2,"

Revision 104, specified eight manual CCW system valves in each procedure.

Operators were required to manipulate these valves, to meet the safety analysis

CC W water flow of 5000 gallons per minute (gpm) for the residual heat removal

heat exchangers, after an accident. Therefore, these CCW valves required testing

in accordance with the IST program; however, the licensee did not test the valves

because the valves were not included in the program. The licensees corrective

action for this issue included generating issue report Number 00610994 and placing

the valves, at least 16 valves between both units, on the Plan-Of-The-Day Meeting

Agenda to ensure the testing which, was scheduled for June 30, 2007.

Analysis: The inspectors concluded that the licensees failure to include the

component cooling water system valves in the IST program and subsequently

test the valves per IST program requirements was a performance deficiency

warranting a significance evaluation. The inspectors reviewed this finding

against the guidance contained in Inspection Manual Chapter (IMC) 0612,

Power Reactor Inspection Reports, Appendix B, Issue Dispositioning

Screening, dated November 2, 2006. The inspectors determined that the

licensees failure to test the component cooling water system valves in

accordance with the IST program was more than minor because the finding

affected the mitigating systems cornerstone objective of ensuring the availability

and reliability of the component cooling and residual heat removal systems.

Specifically, the finding was associated with the mitigating systems attribute of

equipment performance.

The inspectors evaluated the finding using Inspection Manual Chapter 0609,

Significance Determination Process,@ Appendix A, Significance Determination

of Reactor Inspection Findings for At-Power Situations,@ Attachment 1, dated

March 23, 2007. The inspectors answered No to all five questions under the

Mitigating System Cornerstone column of Attachment 1. The finding was not a

design or qualification deficiency confirmed not to result in loss of function per

Generic Letter 91-18; did not represent a loss of system safety function; did not

represent an actual loss of safety function of a single train for greater than its

Technical Specification allowed outage time; did not represent an actual loss of

safety function of one or more non-Technical Specification trains of equipment

designated as risk-significant per 10 CFR 50.65 for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />; did not

screen as potentially risk significant due to a seismic, flooding, or severe weather

initiating event. Therefore, the issue screened as having very low safety significance

(Green). The finding was related to the cross-cutting area of Problem Identification

and Resolution and had the cross-cutting aspect of corrective action because during

the extent of condition review for IR Number 00522178, the licensee failed to identify

that at least 16 CCW system valves required inclusion in and testing by the

IST program.

Enforcement: Part 50 of 10 CFR, Appendix B, Criterion XI, "Test Control," states,

in part, that a test program shall be established to assure that all testing required to

demonstrate that safety-related structures, systems, and components will perform

satisfactorily in service is identified and performed in accordance with written test

procedures.

10 Enclosure

Contrary to this, on August 21, 2006, the licensees test program failed to ensure testing

of at least 16 safety-related component cooling water system valves, to demonstrate

that the valves would perform satisfactorily in service. This was due to an inadvertent

omission of these valves in the inservice test program. The licensees corrective action

for this issue included generating an issue report and placing the valves on the plan-of-

the-day meeting agenda to ensure testing of the valves.

Because the finding is of the very low safety significance and it was entered into the

licensees corrective action program (IR 00610994), the finding is being treated as a

non-cited violation (NCV) consistent with Section VI.A.1 of the NRC Enforcement Policy.

(NCV 05000455/2007007-02; 05000456/2007007-02)

LACK OF THOROUGHNESS BY THE MANAGEMENT REVIEW COMMITTEE

(1) IR Number 00496552 and IR Number 00507945, 1B First Stage Reheater

Drain Tank Hi-2 Alarm Failed to Reset During Reheater Valve/Intercept

Valve Surveillance

On June 1, 2005, IR Number 00496552 was written to identify a reactor power

excursion to 100.4 percent during the performance of Braidwood Operations

Surveillance Procedure, 1BwOS Technical Requirement Manual [TRM] 3.3.g.3,

Unit 1 Turbine Overspeed Protection Systems Valve Stem Freedom Check

(RV-IV Cycling). The power excursion occurred because the 1B First Stage

Reheater Drain Tank Hi-2 level alarm failed to reset, during the performance of

the monthly surveillance. When this failure occurred, increased steam flow was

routed to the condenser as a result of the emergency level control valve opening

to the condenser.

On July 10, 2005, IR Number 00507945 documented the occurrence of another

reactor power excursion event. The power excursion was due to the same

cause, failure of the 1B First Stage Reheater Drain Tank Hi-2 level alarm to reset

during the performance of the surveillance, as the June 2005 event. During the

second power excursion event, reactor power rose to 100.36 percent.

In response to these two events, the licensee closed the first event

(IR Number 00496552) to work order 900832 to repair and calibrate the

Hi-2 level switch during the next refueling outage (A1R13). Also, the licensee

performed a Quick Human Performance Investigation for the second event

(IR Number 00507945) and identified that both the station ownership committee

and the management review committee failed to realize that the first event was a

reactivity management event. The inspectors review also determined that the

Quick Human Performance Investigation failed to identify that the station

ownership committee and the management review committee did not identify the

need for timely interim correction action following the first event. Therefore,

appropriate actions were not taken, but could have been taken to prevent the

July 2005 power excursion event. The failure to take corrective actions to

prevent recurrence in this case was not required by NRC regulations, so no

violation occurred.

11 Enclosure

(2) Delayed Removal of Transient Combustibles

The inspectors attended the management review committee meeting on

March 13, 2007. Issue report Number 601183, Transient combustibles stored

at lake screen house without required permit, was reviewed by the committee

members. The issue report documented that the fire marshall was contacted for

this issue on March 6, 2007, and indicated that the quantify of transient

combustibles may be considered minor and that a permit may be required per

OP-AA-201-009, Control of Transient Combustible Materials, Revision 5.

The IR further documented that the transient combustibles would be removed

the following date. The inspectors were particularly concerned with the

disposition of this issue report due to recent and repeat transient combustibles

problems experienced at the station (see Section 4OA2.a.3 of this report). The

inspectors were concerned because the issue report did not document whether

the quantity of material was actually minor, a permit was required and had been

initiated to allow storage of the combustible, or other interim compensatory

measures had been established to allow the transient combustibles to remain at

the location.

During followup discussions with the licensee, the inspectors were informed that

significant followup discussions had taken place at the plan-of-the-day meeting

for this issue. The discussions indicated that the quantity of material was

exempt from procedural requirements; therefore, the licensee was in compliance

with the requirements of OP-AA-201-009. The inspectors were satisfied that the

licensee had appropriately recognized and assessed this issue, but, the

inspectors were concerned that the followup information was not subsequently

captured in the issue report. The omission of this information resulted in the

inability, of an independent review, to reach the same conclusion as the MRC

because of the missing information.

(3) Supervisor not held Accountability for Inadequate Radiological Briefing

The inspectors reviewed issue report Number 499359 which involved a worker

receiving an unexpected dose rate alarm. The inspectors review of the issue

report revealed that the duty supervisor was aware that the workers alarm may

alarm while performing a resin sluice evolution. However, the issue report did

not document that the duty supervisor involved with the briefing was held

accountable for conducting an inadequate briefing. The licensees failure to

address the specific performance of the supervisor was considered minor

violation since all radiation protection personnel was briefed on the issue. The

licensees corrective actions for this event was to brief all radiation protection

staff on this issue and the potential of a dose alarm for sluice activities.

(4) Cover Contamination Should have been Identified

The inspectors reviewed issue report Number 497545 which was associated with

a contamination event. The inspectors questioned the radiation protection

manager on why the contamination which had been discovered on the underside

12 Enclosure

cover plug on June 6, 2006, was not previously identified as a result of radiation

surveys. The radiation protection manager informed the inspectors that this

issue was a human performance issue. The licensees failure to have previously

identified the contamination was considered minor as the spread of

contamination was limited.

New Issue Report not Written for Expanded Scope of Deficient Supervisory

Performance In the Closure of Corrective Action Assignments

In IR Number 584820, the licensee documented that supervisory performance

with respect to corrective actions to prevent recurrence (CAPR) closure did not

meet procedural requirements. The licensee subsequently identified, through an

extent of condition review (EOC), that supervisory performance was not only

deficient for CAPR closure but also for other CA assignments closures that were,

associated with EACEs, CCA. The supervisors had also failed to provide

electronic approval for these types of CA assignment prior to the closure.

Although this new expanded deficiency of supervisory performance was part of

the EOC review, this information was captured in IR Number 584820. But, this

IR was limited to the inadequate closure of CAPRs assignments only.

The inspectors determined that the new information identified by the licensee

during the EOC review indicated that the deficient aspect of supervisory

oversight was of a larger magnitude than previously identified and documented

in the 2007 PI&R FASA. Therefore, it would have been prudent for the licensee

to have generated a new issue report at the time it was identified. However, the

licensee later recognized this issue as a missed opportunity during the FASA

and then the issue was captured in the CA program. Corrective actions taken by

the licensee included rerouting the CAPR to the department managers for

electronic approval. With respect to the other CA assignment types, the licensee

determined that department managers had approved all of the investigation type

assignments, therefore, the licensee determined not to obtain the electronic

approval for these assignments. Additionally, the licensee implemented interim

corrective actions to address these issues by inserting electronic route lists for all

open investigations, CAPR assignments, and EFR assignments through

March 31, 2007.

.3 Effectiveness of Corrective Action

The inspectors concluded that the licensee generally implemented corrective

actions that were effective in addressing plant issues. The licensees 2007 PI&R

FASA documented, isolated cases, where the requirements of this CA element

were not met. The licensee initiated issue reports for the specific PI&R FASA

deficiencies. The inspectors also noted minor examples where deficiencies were

noted in this CA element.

In general, the inspectors determined that the licensee had been identifying and

implementing corrective actions to arrest deficient plant performance.

Specifically, in January 2007, the licensee conducted a common cause analysis

(CCA), IR540986, as a result of an adverse trend in human performance errors

13 Enclosure

which had resulted in a number of station clock resets. The CCA identified two

common causes: 1) individuals were failing to detect and prevent human errors

through the use of basic human performance and technical human performance

error reduction tools; and 2) Management, including field supervision, was failing

to properly engage workers in the use of human performance and technical

human performance error reduction tools. The licensee developed a number of

corrective actions, some of which had been completed, which appeared

appropriate to address the common causes identified in the CCA.

Additionally, NOS and the nuclear safety review board noted that supervisory

oversight had been less than adequate in many instances. The licensee has

recognized that challenges, in a number of areas such as out-of-service errors,

qualification of site personnel, contractor injuries, control of transient

combustibles, and repetitive consequential bumping events. Specifically,

corrective actions associated with inadequate control of combustible materials

resulted in several repeat events. Ineffective corrective actions for a root cause

report in 2003 led to the NRC identification, in June 2006, of an NCV for

the failure to implement the licensee's procedure for control of combustible

materials. In February of 2007, the licensee again found that the root cause

evaluation initiated in 2006 was not timely and that interim actions were

ineffective at sustaining performance. Several mispositioning events have

occurred, during the last five years, due to plant personnel inadvertently bumping

plant equipment. These bumping incidents have affected safety or Technical

Specification systems and directly or indirectly caused unanticipated power

changes. The licensee has not characterized any of the events as a significant

condition adverse to quality; therefore, the licensee did not have to prevent the

occurrence of the events. In each event, the corrective actions were either

narrowly focused only on the particular system or limited to easily accessible

valves. An example of the licensees narrow corrective action involved the

mispostioning of a valve, on the day tank, for the 1B emergency diesel generator

system. The licensee had previously decided against altering this valve, to

address an earlier bumping event, on the basis that the valves location would

prevent inadvertent bumping on the valve. However, the licensee subsequently

removed the valves handle as corrective actions to this March event. Although

the licensee has implemented corrective actions to improve performance in

these struggling areas, the inspectors were concerned with the stations ability to

sustain performance in these areas.

Findings and Observations

Inadequate Response to the PI&R FASA Finding

The sites 2007 PI&R FASA documented that a corrective action assignment

from a root cause report was closed to a management assignment request

MREQ. These types of management assignments were not used as a corrective

action assignment type. The MREQ assignment action was to perform a

walkdown, in the plant, to identify equipment that may be susceptible to bumping

or other inadvertent manipulations. The inspectors reviewed the licensees

response to the documented FASA deficiency and concluded that the response

14 Enclosure

was inadequate because the licensees response specified that the use of an

MREQ assignment was acceptable because another CA assignment (IR526093-

59) was tracking the same MREQ assignment actions. Although, the licensees

response was not consistent with CA program requirements, the failure to use

the proper tracking assignment was considered minor since the issue was

captured in the CA program.

Inadequate Corrective Actions

The sites 2007 PI&R FASA documented that individuals (direct report to

managers) and managers did not properly close corrective action to prevent

recurrence (CAPRs) assignments. A supervisory review, was required by

procedure, prior to the supervisors direct reports closing the CAPRs. Although

the direct reports were to send their supervisors or managers the electronic

CAPR for approval, the supervisors failed to ensure the receipt of the electronic

CAPR. The inspectors concluded that the supervisors failure to implement this

procedural requirement was not addressed by the licensee. Specifically, the

licensees corrective action included documenting a Fundamental Management

Systems entry for the individuals, but the supervisors or managers did not

receive any Fundamental Management System entries. The inspectors

considered this corrective action narrowly focused and partially ineffective.

The inspectors determined that these corrective actions did not ensure that

supervisors and managers were held to the same level of accountability as

their direct reports even though both parties were responsible for the proper

closure of the CAPRs. Subsequently, the licensee made Fundamental

Management System entries for the supervisors.

Inappropriate Corrective Action Assignment

The inspectors reviewed two issues where the licensee assigned corrective

actions that did not appear appropriate. Specifically, cases where issues should

have been assigned as CA assignments, but were instead assigned as action

tracking item (ACIT). The ACIT assignments, as specified by procedural

guidance, track the completion of general actions required to address non-quality

related issues. Two examples of CAs for quality-related issues being tracked as

ACITs were noted. One issue was associated with the potential to adversely

impact safety related equipment, and the second issue could have resulted in not

meeting radiological posting requirements or labeling requirements, which are

necessary to inform workers of radiological hazards. The licensees failure to

use the proper CA program tracking assignment for these two issues were

considered minor because there were no adverse safety impacts as a result of

the use of the incorrect CA program assignment.

In the first case, the inspectors reviewed an item associated with a station worker

inappropriately modifying the plant that had the potential to render safety related

equipment inoperable. The licensee immediately removed the unauthorized

modification and determined that the modification did not adversely affect the

equipment while the unauthorized alteration was in place. The licensee initiated

appropriate corrective actions that entailed revising material utilized by the

15 Enclosure

worker and other in the same department. This material would be referenced in

the future when considering modifications to the plant. Also, the issue was

tailgated to the affected departments.

In the second case, the inspectors reviewed IR Number 499656 which was

associated with a NOS finding. The IR documented that NOS identified several

deficient radiological ropes, posting, and radioactive material labels. The RP

Manager generated an IR to understand why the issue had not been classified

as a CA assignment. The IR further documented that preventive maintenance

task, which was to have identified these types of issues, was inconsistently

implemented by radiation protection personnel. The corrective action specified,

was to ensure the preventive maintenance task addressed these issues and

address problems with label and rope degradation.

b. Assessment of the Use of Operating Experience (OE)

(1) Inspection Scope

The inspectors reviewed the licensees implementation of the station operating

experience program. Specifically, the inspectors reviewed implementing operating

experience program procedures, attended CA program meetings to observe the use

of OE information, completed evaluations of OE issues and events, and selected

2006 and 2007 monthly assessments of the OE composite performance indicators.

The inspectors review would determine whether the licensee was effectively integrating

OE experience in the performance of daily activities, evaluations of issues were proper

and conducted by qualified personnel, prevention of industry events, and use of

departmental assessments and NOS audits. The inspectors also assessed if corrective

actions, as a result of OE experience, were identified and effectively and timely

implemented.

(2) Assessment

The inspectors did not identify any findings of significance in this area. The inspectors'

review of operating experience reports identified that the licensee was appropriately

including the issues into the CA program and effectively implementing operating

experience at the station. During licensee staff interviews, the inspectors identified

that the use operating experience was considered during daily activities.

c. Assessment of Self-Assessments and Audits

(1) Inspection Scope

The inspectors assessed the stations ability to identify and enter issues into the station

CA program, prioritize and evaluate issues, and implement effective corrective actions,

through efforts from departmental assessments and NOS audits.

16 Enclosure

(2) Assessment

The inspectors concluded that the licensees departmental assessments and nuclear

oversight audits were effective at identifying plant deficiencies and enhancement

opportunities at an appropriate threshold level. Assessments and audits were thorough

and probing. The auditing and assessing teams were comprised on personnel with

appropriate skills, abilities, knowledge, and expertise, which resulted in the identification

of plant deficiencies, plant improvement recommendations, and plant strengths.

Assessments and audits properly characterized issues, and identified issues were

subsequently placed into the CA. One exception was noted as discussed under the

identification of issues section of this report. Also, the inspectors concluded that 2007

PI&R FASA was a very good effort that resulted in a quality product.

The 2007 PI&R FASA properly assessed each CA program element of the CA program

and determined that the stations CA program was effective. However, the PI&R FASA

documented that the requirements for various CA program elements, for a number of

isolated cases, were not met. The sites PI&R FASA noted that, although trending was

effective at the station, further improvement was needed with the performance of the

department CA program coordinators. As a result, the Site CA program Manager

increased the meeting frequency, with the department CA program coordinators from

once every two to three months to every two weeks. During these meetings, the Site

CA program Manager reviewed selected CA closure reviews for lessons learned and

departmental CA program trend boards/data for site improvements. The site CA

program Manager indicated that these efforts had resulted in improving the performance

of the department CA program coordinators during this short time period. Additionally,

the Site CA program Manager and the department CA program coordinators planned to

develop a CA program coordinators improvement action plan.

The inspectors assessment of the stations CA program was consistent with the results

documented in the site PI&R FASA. Primarily, the team identified additional examples

of the types of deficiencies, in the various CA program elements, that had been

identified during the stations PI&R FASA. In addition to similar minor issues identified

by the FASA and the NRC inspection teams, two more significant issues were identified

by the inspectors as evident by two NRC-identified violations and other observations

documented in the inspection report.

The inspectors held discussions with the station NOS manager to obtain a better

understanding of NOS activities with respect the underlying attribute of supervisory

oversight as a challenge to several problem areas and repeat issues. The NOS

manager indicated that the number one concern at the site was operations leadership in

driving performance at the station. As a result, configuration control and safety were

elements that the Operations Department was not setting the appropriate standards for

personnel performance; therefore, problems were occurring as a result of deficient

personnel performance. In addressing these issues, the licensee held a Site Wide

Standdown in February 2006, and performed a common cause analysis, for human

performance errors, which was reviewed by the inspectors.

17 Enclosure

d. Assessment of Safety Conscious Work Environment

(1) Inspection Scope

The inspectors assessed the stations safety conscious work environment through

the reviews of the stations employee concern program implementing procedures,

discussions with coordinators of the employee concern program, interviews with

personnel from various station departments, and reviews of issue reports. The

inspectors also reviewed the results from a Safety Culture Survey and the Braidwood

Occupation Safety and Heath Administration (OSHA) Voluntary Protection Program

survey.

(2) Assessment

The NRC 2005 PI&R had documented that a number of plant workers did not

understand the purpose of the stations Employee Concern Program (ECP).

Some workers were unaware that safety concerns could be raised through the ECP,

and other workers indicated that personal problems were addressed through the ECP.

The inspectors determined that the licensee appeared to have addressed this issue as

reflected by a very integrated ECP into station activities. The ECP coordinators were

very active in ensuring station awareness and understanding of the ECP. The

coordinators discussed the ECP at maintenance personnel alignment meetings and to

new station workers as they were hired at the plant. The results from the interviews of

plant staff conducted by the inspectors, it was evident that station personnel understood

the purpose of the ECP. Based on discussions with the site and backup ECP

Coordinators, the inspectors did not have any concerns with the implementation of the

ECP. The ECP Coordinators were properly implementing the site program by ensuring

workers identify were not revealed and properly monitoring the sites corrective action

program for issues which would be considered ECP concerns. Additionally, the

coordinator properly followed up on issues to ensure a chilled environment did not exist

at the station.

The results of the interview with station personnel indicated that plant workers were

knowledgeable about the tools available to them for raising nuclear safety concerns.

The inspectors did not receive any comments that indicated workers would be hesitant

about raising concerns. Furthermore, the workers communicated that station

supervision greatly supported the workers efforts in raising issues. None of the workers

indicated that they themselves or their co-workers had been retaliated against for raising

safety concerns.

The inspectors reviewed the licensees Midcycle Safety Culture Questionnaire

completed in December 2006. The results of the questionnaire indicated that a safety

conscious work environment was in existence at the station. The survey results were

consistent with comments made in the OSHA Voluntary Protection Program Survey

Results and by the Nuclear Safety Review Board (NSRB). The aspect of supervisory

oversight in the field was noted in the survey as an area needing improvement, and this

was consistent with the stations focused attention on supervisory oversight.

18 Enclosure

The inspectors also reviewed the OSHA Voluntary Protection Program Survey Results.

This survey was administered in August/September 2006 and sampled 100 percent of

station personnel. The inspectors review of the results indicated that station workers

primary concerns regarding personnel safety were that it appeared that personnel safety

took a backseat to outages and high workload times, supervisors did not spend enough

time in the plant, and personnel safety issues were not always resolved in a timely

manner. The licensee analyzed the comments and subsequently developed a list of

focus areas to address the concerns noted by the survey results.

4OA6 Meetings

.1 Exit Meeting

The inspectors presented the inspection results to Mr. D. Ambler and other members

of licensee management at the conclusion of the inspection on May 1, 2007. The

inspectors asked the licensee whether any materials examined during the inspection

should be considered proprietary. No proprietary information was identified.

An interim exit meeting was conducted on March 30, 2007, to discuss the

preliminary findings of the inspection with Mr. M. Smith and other members

of licensee management. No proprietary information was identified.

4OA7 Licensee-Identified Violations

No findings of significance were identified.

ATTACHMENT: SUPPLEMENTAL INFORMATION

19 Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

K. Aleshire, Emergency Preparedness Manager

D. Ambler, Regulatory Assurance Manager

D. Burton, Licensed Operator Requalification Training Lead Instructor

M. Cichon, Licensing Engineer

L. Coyle, Maintenance Director

C. Dunn, Site Training Director

G. Golwitler, Site Corrective Action Program Manager

R. Leasure, Radiation Protection Technical Manager

J. Moser, Radiation Protection Manager

J. Petty, Regulatory Assurance

B. Schipiour, Work Control Director

M. Smith, Engineering Director

P. Summers, Nuclear Oversight Manager

T. Tierney, Chemistry, Environmental, and Radioactive Waste Manager

C. Walrath, Operations Shift Operations Supervisor

R. Wolen, Design Engineering Manager

Nuclear Regulatory Commission

R. Skokowski, Chief, Reactor Projects Branch 3

L. Kozak, Senior Reactor Analyst

Illinois Emergency Management Agency

C. Cecil, Head Resident Inspection, Nuclear Facility Safety Illinois Emergency Management

Agency

1 Attachment

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

Opened

05000451/2007007-01; NCV The licensees failure to maintain a procedure adequate

05000452/2007007-01 could have resulted in securing the only remaining residual

heat removal pump (Section 4.OA.2.a.1)

Closed

05000451/2007007-02; NCV Inadequate extent of condition review which failed to

05000452/2007007-02 identify that IST testing was not performed for component

cooling water systems valves (Section 4.OA.2.a.2)

Discussed

None

2 Attachment

LIST OF DOCUMENTS REVIEWED

ISSUE REPORTS GENERATED DUE TO THE INSPECTION

Walkdown

00606529; Minor Oil Leak on 1B SX Pump (1SX01PB); March 20, 2007

00606470; Small Shaft Packing Leak on 2B SX Strainer (2SX01FB); March 20, 2007

CAP

00609112; NRC PI&R IDD - Concern with MRC/SOC Response to IR 601183; March 26, 2007

00610562; PI&R IDD - RP Did not Write IR for IEMA Issues; March 29, 2007

00610161; NRC PI&R IDD Concerns with IR Operability Bases Statements; March 28, 2007

00610159; NRC PI&R IDD - CAS for M&TE Trend not Effective; March 28, 2007

00610259; PI&R IDD - Operating Log Entries not Referencing IR; March 28, 2007

00610497; NRC PI&R IDD - No CA to Address Inadequate Brief By RP supervisor;

March 29, 2007

00610499; NRC PI&R IDD - ACIT that Should Have Been a CA Assign (RP); March 29, 2007

00610507; NRC PI&R IDD - RP Accountability not Addressed for Survey; March 29, 2007

00606470; Small Shaft Packing Leak on 2B SX Strainer (2SX01FB); March 20, 2007

00607571; PI&R IDD - Enhancement Opportunity for BwOP CC-8; March 22, 2007

00609263; NRC Questions Why CC Valves in EOP are Not in IST Program; March 27, 2007

00610437; IST Bases Document Requires Revision; March 29, 2007

00610514; NRC PI&R IDD - OE Not Used/Reference in Operations ACE; March 29, 2007

00610994; NRC Potential Green NCV - Manual CC Valves Not in IST Program;

March 30, 2007

00611024; NRC Potential TBD Finding - Procedure BwOP CC-8 Inadequate; March 30, 2007

00610051; PI&R IDD - Typographical Errors in Completed CCA; March 27, 2007

OE

00610514; NRC PI&R IDD - OE Not Used/Referenced in Operations ACE; March 29, 2007

ISSUE REPORTS REVIEWED DURING INSPECTION

Operations

00186275; Repeat Maintenance - 2CC9486 Failed Second LLRT (First Rework);

November 13, 2003

00353841; Procedure Needed for Swapping U-O CC Heat Exchanger; July 16, 2005

00367473; Potential Enhancements to Strainer Backwash Response; August 27, 2005

00383463; Evaluation of 1RY8028 LLRT Results; October 7, 2005

00434456; Recommendations from 2005 Reactivity Management FASA;

December 15, 2005

00435424; FASA Identified Procedure Change OP-AA-300 / WC-AA-105; December 19, 2005

00441759; Operations Reactivity Management FASA 2006; January 13, 2006

00441919; Braidwood FASA - In-Service Testing (IST); January 13, 2006

00445423; Large Number of Consequential Configuration Control Events; January 24, 2006

00446241; OPEX Review - Lesson Learned from Byron IR 444685/444975; January 26, 2006

00446244; OPEX Review - Lesson Learned from Byron IR 444975/444499; January 26, 2006

3 Attachment

00452245; Unplanned LCO Entry on 2A DG Due to Low Temperature; February 10, 2006

00457480; Unit 2 RWST Level Slowly Decreasing; February 23, 2006

00479478; Unplanned LCO Entry into 3.4.12; April 17, 2006

00484683; 1RY8028 Body to Bonnet Steam Leak; April 29, 2006

00485871; A1R12 LL 16 percent Level Drop in 1A SI Accum During BwVSR 3.4.14.1;

May 2, 2006

00496552; 1B First Stage RDT HI-2 Alarm Failed to Reset During RV/IV SRV; June 5, 2006

00526168; Potential Unplanned LCO Due to Missed Technical Specification Surveillance;

August 31, 2006

00537802; Potential Trend in the In-Service Testing Program (IST); September 29, 2006

00507945; 1B First Stage RDT HI-2 Alarm Failed to Reset During RV/IV SRV; July 10, 2006

00523372; Unplanned LCO - Procedure Problem with 1B SSPS Bi-Monthly; August 24, 2006

00534719; Potential Missed Tech Spec Surveillance; September 22, 2006

00546312; 2CC9486 Fails Its A2R12 As Found Local Leak Rate Test; October 19, 2006

00547003; Valve Disc for 2CC9486 (A2R12 Outage); October 20, 2006

0554857; 2HD005A Acting Erratic; November 7, 2006

00555147; U-2 Reactor Power Effects During 2HD005A Restoration; November 18, 2006

00561698; NRC Concerns Identified During U-1 ECCS Vent and Valve Surveillance;

November 24, 2006

00568853; NRC IDD Concern with Past Operability of 2CC9486; December 13, 2006

00574749; Reactivity Management FASA - Standards Deficiency; January 3, 2007

00584642; PI&R FASA IDD - Concern with Response to SX Strainer Finding; January 29, 2007

00585093; PI&R FASA IDD - Concern with RCR Quality on 1CV243 Bump Event;

January 30, 2007

00585839; PI&R FASA IDD - Concern with FME Not Wholly Addressed in EACE;

January 31, 2007

00594356; Unit 1 Reactor Power Effects During 1MS040D Clearance Order; February 21, 2007

00468506; 1DO2006B Found Out of Normal Position; March 20, 2006

00330826; Valve 2RE004B Inadvertently Bumped; May 2, 2005

00472884; 1FW076 Failed Open Due to 1IA1234 Found 90 percent Closed; March 30, 2006

00095256; Unplanned Entry Into AAR 2BwOS PR-1a For Failure of 2RR08J; February 14, 2002

Operations log entries

Operator logs from 3/16/2007 through 3/18/2007

Operations department memorandum 1-07;Issue Generation and Log Keeping Clarifications;

February 20, 2007

00582356; PI&R FASA ID'd Operations Log Entries Without Log Entries; January 23, 2007

00607368; TLDs Were Put Thru X Ray Machine; March 22, 2007

Radiation Protection

IR485357; Contract Employee Exited PA after Alarming Rad Monitor; May 1, 2006

IR589515; Unacceptable RAD Shipping Practices; February 9, 2007

IR546010; Unexpected ED Alarm 377' IMB Near R24; October 19, 2006

IR528711; Shielding Blankets Need Adjustment to Shield Hot Spot; September 8, 2006

IR528700; RP Source Control Check-in Deficiency; September 5, 2006

IR517975; RAD Source found in Warehouse 15 (Good catch); August 8, 2006

IR515674; Extra RAD Exposure Taken due to Computer EPN Problem; August 1, 2006

IR486492; Relief Valve 1SD016 Isotopically Contaminated; May 4, 2006

4 Attachment

IR484195; A1R12 LL ALARA/Shielding Issues w/Westinghouse CRDM Equipment;

April, 28, 2006

499359; Unexpected Electronic Dosimeter Dose Rate Alarm; June 12, 2006

497545; Level 2 Personnel Contamination Event; June 6, 2006

499656; NOS ID: Several Outdoor Radiological Postings Found Unsat; June 13, 2006

547064; Unit 2 reactor Head New O-rings Damaged; October 20, 2006

589845; NOS ID: Negative Trend in the Lack of Rad-Waste Shipments; February 9, 2007

482383; Level 3 PCE (Westinghouse); April 22, 2006

518432; VCT Valve Aisle Contaminated During Fill and Vent; August 9, 2006

532256; Seavan Number 14 and 27 in degraded Condition; September 2007

528670; Pipe Requires Flush Flushing to Eliminate Hot Spot Number 59; September 8, 2006

528681; Pipe Requires Flush flushing to Eliminate Hot Spot Number 54; September 8, 2006

539072; Pipe Requires flush To Eliminate Rad Hot Spots; October 2, 2006

481427; A1R12 LL - RP Air Samples are not being Properly Prepared; April 20, 2006

536685; Elevated Dose Rates on U2 CV Letdown Piping; September 27, 2006

490604; Increasing Trend In Personnel Contamination Events PCE; May 16, 2006

523419; Possible Unmonitored Vent Path and Water Leakage U-2 CWA; August 24, 2006

243310; LHRA Left Unlocked and Unguarded-Tech Spec Violation; August 10, 2004

Maintenance

Safety relief valves

262233; 1SI8853B Failed to Repeat Required Lift Pressure; October 11, 2004

278269; Relief Valve Failed to Lift; December 1, 2004

329172; Valve Removed From 2SI8853B Failed Seat Leak & Lift Test; April 27, 2005

332762; IST Relief Valve 2SI8851 Failed Pressure Test; May 6, 2005

454898; Need WR For Contingency Work Order for 2SI8853A; February 16, 2006

459085; Spare Relief Valve From 1SI8853B Failed Testing; February 27, 2006

507260; Pre-Outage Task for 2SI8858 Performed Three Months Early; July 7, 2006

534034; Boron Identified on 1SI8851 During U01 ECCS Vent & Valve; September 24, 2006

546046; 2SI8851 Relief Valve Failed Initial Lift Test Low"; October 19, 2006

552355; Relief Valve Removed From 2SI8858 Failed Final Seat Leakage; November 2, 2006

553376; Relief Valve Removed From 2SI8842 Failed Initial Testing; November 4, 2006

554657; Safety Relief Valve Product Advisory"; November 7, 2006

565162; Relief Valve S/N N56877-00-0147 Failed Testing; December 4, 2006

576883; IST Relief Valve 1CS08MB Failed As Found Testing; January 9, 2007

102884; Pressurizer Safety Valves Test Out of Tolerance; April 8, 2002

Maintenance Adverse Trends

554034; Safety - Contractor Adverse OSHA Recordable Trend; November 6, 2006

476197; Safety Issue - Potential Negative Trend; April 7, 2006

385495; Trend - Unsafe work Practices with Working at Heights; October 13, 2006

584806; PI&R FASA IDD - Potential Adverse Trend With Safety; January 26, 2007

546473; A2R12 - Adverse Injury Trend; October 19, 2006

445525; Potential Adverse Trend in Safety; January 24, 2006

388537; Potential Trend: Safety Work Practices in Maintenance; October 21, 2005

540986; CCA, Potential Adverse Trend - Braidwood station Human Performance;

January 12, 2007

5 Attachment

Lost M&TE

448780; "M&TE Lost in 2005"; June 26, 2006

484738; "M&TE Being Declared Lost (EMD)"; April 29, 2006

484741; "M&TE Being Declared Lost (IMD)"; April 29, 2006

484742; "M&TE Being Declared Lost (MMD)"; April 29, 2006

484745; "M&TE Being Declared Lost (Venture)"; April 29, 2006

484757; "M&TE Being Declared Lost (Unknown work group)"; April 29, 2006

509129; "M&TE Being Declared Lost (MMD)"; July 13, 2006

509438; "M&TE Being Declared Lost (Unknown work group)"; July 14, 2006

509485; "M&TE Being Declared Lost (Operations)"; July 13, 20064

548931; "M&TE Being Declared Lost (EMD)"; October 25, 2006

548948; "M&TE Being Declared Lost (IMD)"; October 25, 2006

548979; "M&TE Being Declared Lost (MMD)"; October 25, 2006

548987; "M&TE Being Declared Lost (Venture)"; October 25, 2006

550954; "Potential Trend-Lost M&TE (Maintenance)", October 30, 2006

551583; "M&TE Being Declared Lost (Venture)"; October 31, 2006

551590; "M&TE Being Declared Lost (EMD)"; October 31, 2006

595587; "M&TE Being Declared Lost (Venture)"; February 24, 2007

595589; "M&TE Being Declared Lost (EMD)"; February 24, 2007

595591; "M&TE Being Declared Lost (Reactor Services)"; February 24, 2007

595592; "M&TE Being Declared Lost (Engineering Programs)"; February 24, 2007

595596; "M&TE Being Declared Lost (Engineering Work Group)"; February 24, 2007

Assessments and Audits/NOS/NSRB

595565; NOS ID PDR - Clearance and Tagging Program; February 24, 2007

394859; NOS PDR - Maintenance Unsafe Work Practices; November 4, 2005

496580; NOS IDD PDR Maintenance Performance; June 2, 2006

552654; NOS IDD Clearance and Tagging PDR; November 2, 2006

545330; NOS IDD Unchocked Cart in Turbine Building (venture); October 17, 2006

481167; NOS Identified an Adverse Trend on Control of Carts; April 20, 2006

196476-05; Source Accountability and Control Check-In Self Assessment; September 5, 2006

593726; NOS Elevation Notice Transient Combustible Material Control; February 28, 2007

574353; NOS ID FLS Qualification Documentation; February 2, 2007

560730; PI&R FAS; February 8, 2007

Braidwood Nuclear Safety Review Board Meeting; January 16 and 17, 2007

Braidwood Nuclear Safety Review Board Meeting; September 7 and 8, 2006

Braidwood Nuclear Safety Review Board Meeting; May 17 and 18, 2006

Braidwood Nuclear Safety Review Board Meeting; January 25 and 26, 2006

Braidwood Nuclear Safety Review Board Meeting; October 18 and 19, 2005

Braidwood Station Post Outage Review (A2R12); December 15, 2006

A1R12 Post Outage Review

Braidwood NOS Site Status Report; March 26, 2007

Braidwood NOS Site Status Report; December 18, 2006

Corrective Action Program

380114; EFR Determined CA 267878-08 to be Ineffective; September 30, 2005

463049; Missed Scheduled Training - Plant Engineering; March 7, 2006

432350; Missed ERO Training (Project Management); December 7, 2005

381339; 10/5/05 FLS Training Session Cancelled; October 2, 2005

6 Attachment

457631; Trend Identified in RP Department Clock Resets; February 23, 2006

588941; PI&R FASA IDD - Deficiency with Inadequate Closures of CAs; February 7, 2007

591311; NSO Reactivation Guide Contained Omissions; February 13, 2007

584820; Pi&R FASA IDD - CAPRs Closed Without Dept Mgr Approval; January 26, 2007

585093; PI&R FASA IDD - Concern w/RCR Quality on 1CV243 Bump Event; January 26, 2007

526093; NRC Potential NCV - Unplanned LCO entry Due to 1CV243 Bumped; August 31, 2006

584990; PI&R FASA IDD - Inadequate Closed CAPR for Procedure Rev.; January 26, 2007

604938; Outboard Bearing Housing Leaks on 2B SX Pump; March 13, 2007

502360; U-2 SAC has Hi Vibes; June 21. 2006

501537; U-2 SAC Tripped on Hi Oil Temp; June 19, 2006

397297; CAP Trend Code Application Deficiency; November 10, 2006

585860; PI&R FASA IDD - Trend with Failures on OLIS-CF084; January 26, 2007

585325; PI&R FASA IDD - Trend with U-2 SAC Emergent Problems; January 26, 2007

585778; PI&R FASA IDD - No CA Initiated for Common Cause (ops); January 26, 2007

394664; DC Bus 111 Ground Alarm Toggling; November 2005

586507; PI&R FASA IDD, Issues w/operability & Reportability Reviews; February 1, 2007

601183; Transient Combustibles Stored at LSH

560730; FASA Report for PI&R Pre-NRC Inspection; February 02, 2007

563100; NRC Identified NCV Issued-Control of Combustible Materials; November 29, 2006

399061; EP Drive-In Drill Failures; November 15, 2005

526093; NRC Potential NCV-Unplanned LCO Entry Due to 1CV243 Bumped; October 13, 2006

556692; Braidwood Unit 2 in Chemistry Action Level 2 for I131; November 11, 2006

426461; Increasing Trend in EFRS that are Collectively Ineffective; November 21, 2005

0116242; NRC Identified Issues in SX Pump Rooms; July 18, 2002

0154441; Potential 1RY456 Diaphragm Leak; April 13, 2003

0156624; Enhancements to PORV Accumulator Test - BwOSR 3.4.11.3; April 30, 2003

0324246; NRC Observations Noted on 2A SX Pump (2SX01PA); April 13, 2005

BRW MRC Agenda for Tuesday, March 13, 2007

BRW MRC Agenda for Wednesday, March 14, 2007

BRW SOC Agenda for Tuesday, March 13, 2007

Braidwood; A Day In The Plant Observation; January 10, 2007

Braidwood; A Day In The Plant Observation; November 14, 2006

Braidwood; A Day In The Plant Observation; August 1, 2006

Braidwood; A Day In The Plant Observation; June 27, 2006

Braidwood; A Day In The Plant Observation; February 2, 2006

586509; PI&R FASA IDD - Deficiency w/department CAPCO performance; February 1, 2007

Department CAPCO Indoctrination Guide

BwHS 4002-097; Surveillance of Air Duct Smoke Detectors 1/2XY-VT001; Revision 2

MA-BR-723-002; Smoke Detector Testing; Revision 2

Investigations

445423; Complete CCA for 2005 Configuration Control Events; March 31, 2006

148014; Common Cause Identified for FP Sensitive Issues; February 20, 2004

053104; Corrective Actions From CCA 77614; December 28, 2001

585093; PI&R FASA-Concern W/ RCR quality on 1CV243 Bump Event; January 30, 2007

583763; RCR-574353; TQ-AA-210-4303 Rev 1 not Implemented; January 26, 2007

591458; Root Cause Report Identified Poor Actions to NCV Finding; February 14, 2007

547064; Quick Human Performance Investigation Template; Unit 2 Reactor Head New O-Rings

Damaged

7 Attachment

Other

490604; Increasing Trend in Personnel Contamination events PCE; May 16, 2006

00184989; 2CC9486; (CC Supply to RCP Inside CIV) Failed LLRT; November 6, 2003

00265910; Inadvertent TRM LCOAR 3.4.C Entry Due to Excessive PZR C/D; October 21, 2004

00291106; Unplanned LCOAR Entry - 2B DG Jacket Water Circ Pump Trips; January 15, 2005

00306938; Unplanned LCO/Risk Change During ACB 1424 Trip Checks; March 1, 2005

00370649; 1FW039A Failed 1BwOSR 3.6.3.5.FW-3; September 6, 2005

03935515; Adverse Trend - Consequential Procedure Change Errors; November 2, 2005

00437222; Unplanned LCO Entry Due to OB VC Chiller Trip; December 28, 2005

00522178; Unplanned LCO Entry - Missed Surveillance Requirement; August 21, 2006

434566; Maintenance Audit, Maintenance Functional Area; March 17, 2006

308084; Bumping of Hi-2 Level Switch Causes Heater Isolation; March 3, 2005

321000; High and Hi-2 Level in 27A Heater; April 4, 2005

328487; Wrong Valve Body Installed for 2RH8427A in 2AR11; April 25, 2005

329241; Reactive Load Transients on 2B DG During PMT; April 27, 2005

454883; Shortfalls in Implementation of M&TE Program; March 30, 2006

474360; EMD Respirator Qualifications Below 50 percent; April 3, 2006

559573; Potential Adverse Trend-Braidwood Station Procedure Adherence; February 6, 2007

591444; Historical-Improperly Closed Action Items From 2003 RCR; February 14, 2007

00274721; HI-2 Isolation of 15-17 Heaters Causing OPDT Runback; November 18, 2004

00526093; NRC Potential NCV - Unplanned LCO Entry Due to 1CV243 Bumped;

August 31, 2006

00601545; Need WR to Disassemble and Inspect Valve 1CW018; March 9, 2007

DRAWINGS

M-66 Sheet 2; Diagram of Component Cooling Unit 1; Revision AO

M-66 Sheet 3A; Diagram of Component Cooling Units 1 and 2; Revision AU

M-66 Sheet 4D; Diagram of Component Cooling Units 1 and 2; Revision BC

M-139 Sheet 2; Diagram of Component Cooling Unit 2; Revision AI

REFERENCES

LS-AA-115; Operating Experience; Revision 10

LS-AA-120, Issue Identification and Screening Process, Revision 6

LS-AA-125, Corrective Action Program (CAP) Procedure, Revision 11

LS-AA-125-1001; Root Cause Analysis Manual; Revision 6

LS-AA-125-1002; Common Cause Analysis Manual; Revision 5

LS-AA-125-1003; Apparent Cause Evaluation Manual; Revision 7

LS-AA-125-1004; Effectiveness Review Manual; Revision 2

LS-AA-125-1005, Coding and Analysis Manual, Revision 5

LS-AA-126; Self-Assessment Program; Revision 5

LS-AA-126-1001; Focused Area Self-Assessments; Revision 4

LS-AA-126-1005, Check-In Self Assessments, Revision 3

LS-AA-126-1006, Benchmarking Program, Revision 1

EI-AA-1; Employee Issues; Revision 1

EI-AA-101; Employee Concerns Program; Revision 6

EI-AA-100-1003; Employee Issues Advisory Committee Notification; Revision 0

EI-AA-101-1002; Employee Concerns Program Trending Tool; Revision 3

MA-AA-716-017, Equipment Readiness and Reliability, Revision 1

Employee issues; E1-AA-1; Revision 1

8 Attachment

Employee Concerns Program; EI-AA-101; Revision 6

Employee Concerns Program Trending Tool; Revision 3; EI-AA-101-1002

EI-AA-101-1001; Employee Concerns Program Process; Revision 4

NOS Objective Evidence Report; May 9, 2006 - June 16, 2006

Nuclear Oversight Quarterly Report, NOSPA-BW-06-4Q; January 24, 2007

NO-AA-200-002-1002; Nuclear Oversight Audit Templates; Revision 6

NO-AA-200-002; Nuclear Oversight Regulatory Audit Procedure; Revision 10

TQ-AA-1018; Trainee Conduct Standards; Revision 1

BwAP 340-1; Use of Procedures for Operating Department; Revision 20

1BwEP ES-1.3; Transfer to Cold Leg Recirculation Unit 1; Revision 104

2BwEP ES-1.3; Transfer to Cold Leg Recirculation Unit 2; Revision 104

1BwGP 100-5; Plant Shutdown and Cooldown; Revision 33

BwOP CC-8; Isolation of CC Between Units 1 and 2; Revision 18

BwOP CC-14; Post LOCA Alignment of the CC System; Revision 11

OP-AA-106-101-1006; Operational and Technical Decision Making Process; Revision 4 Memo

No. BR-40, Expectations for Extending Issue Report Cause Investigations and Corrective

Action Due Dates, Revision 1

Procedure BwMP 3305-109; "IST and Non-IST Safety / Relief Valve testing; November 8, 2006

Procedure MA-AA-716-040; "Control of Portable Measurement and Test Equipment Program";

January 26, 2007

NRC Information Notice 2006-24; "Recent Operating Experience Associated With Pressure and

Main Steam Safety/Relief Valve Lift Setpoints; November 14, 2006

Memo No. BR-059, Day In The Plant Observation Program, Revision 1

Memo No. BR-055, Expectations for Root Cause Report Quality of Preparation, Oversight, and

Timeliness, Revision 0

NUREG-1482; Guidelines for Inservice Testing at Nuclear Power Plants; Revision 1

WCAP-12232; Commonwealth Edison Company - Byron/Braidwood Plants - Component

Cooling Water System; Revision 0

WCAP-13588, Operating Strategies for Mitigating Pressurizer Insurge and Outsurge

Transients; March 1993

Engineering

599516; OVA09FB - Carbon Sample Failed the Test; March 5, 2007

374437; Inaccurate ECC Calculation; September 16, 2005

465719; FRAC Tank Berm Collapse; March 13, 2006

480489; Boric Acid Accumulation at Bottom of PZR; April 19, 2006

484671; 1FW039 Repack Caused Decrease in 1D S/G Lvl; April 29, 2006

428868; Elevated Tritium Levels in On-Site Monitors; November 30, 2005

504769; 2CS01PA Seal Leakage During RTS; June 29, 2006

324966; Increased RCS Leakage Identified-Mispositioning of 2PR5045; April 15, 2005

523419; Possible Unmonitored Vent Path and water Leakage U-2 CWA; August 24, 2007

Security

IRs generated from June 2006 through March 9, 2007 in security

Miscellaneous

369873; Training Evaluation Methodology Deficiency; September 3, 2005

582168; CMO Group PQD Revision Issues"; January 23, 2007

583451; Chemistry ID'd Qualification Issue During Qual Reviews; January 25, 2007

9 Attachment

583465; Engineering Qualification Review Results; January 25, 2007

583480; Chemistry ID'd Missing Qualifications in PQD; January 25, 2007

583477; Chemistry Training Qualification Review; January 25, 2007

583484; Incomplete Training Documentation; January 25, 2007

585938; HR Identified Gaps In Quals In PQD; January 31, 2007

Operations Department Memorandum 06-6 "Inadvertent Contact Devices; September 26, 2006

10 Attachment

LIST OF ACRONYMS USED

ACIT Action Tracking Item

ADAMS Agency-Wide Document Access and Management System

CA Corrective Action

CAPR Corrective Action to Prevent Recurrence

CCA Common Cause Analysis

CC Component Cooling

CCW Component Cooling Water

CFR Code of Federal Regulation

EACE Equipment Apparent Cause Evaluation

ECP Employee Concern Program

EOP Emergency Operating Procedure

FASA Focused Area Self Assessment

DRS Division of Reactor Safety

EOC Extent of Condition

GPM Gallons Per Minute

IMC Inspection Manual Chapter

IR Issue Report

IST Inservice Testing

LOCA Loss of Coolant Accident

MRC Management Review Committee

NCV Non-Cited Violation

NOS Nuclear Oversight

NRC United States Nuclear Regulatory Commission

OE Operating Experience

OSHA Occupation Safety and Health Administration

PI&R Problem Identification and Resolution

QHPI Quick Human Performance Investigation

RCA Root Cause Analysis

RHR Residual Heat Removal

SDP Significance Determination Process

SOC Station Ownership Committee

SRA Senior Reactor Analyst

TRM Technical Requirement Manual

11 Attachment