ML070120256

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PNO-III-07-001: Monticello Reactor Shutdown Due to Turbine Control Valve Failure (Event Notification EN 43088)
ML070120256
Person / Time
Site: Monticello Xcel Energy icon.png
Issue date: 01/12/2007
From:
NRC/RGN-III
To:
References
EN 43088 PNO-III-07-001
Download: ML070120256 (2)


Text

January 12, 2007PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE -- PNO-III-07-001This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or publicinterest significance. The information is as initially received without verification or evaluation, andis basically all that is known by the Region III staff on this date.FacilityMonticelloNuclear Management Co.Monticello, MNDocket: 50-263License: DPR-22Licensee Emergency Classification Notification of Unusual Event Alert Site Area Emergency General Emergency X Not Applicable

SUBJECT:

MONTICELLO REACTOR SHUTDOWN DUE TO TURBINE CONTROL VALVEFAILURE (EVENT NOTIFICATION EN 43088)DESCRIPTION:

At 3:28 p.m. CDT on January 10, 2007, the reactor shut down automatically after all four turbinecontrol valves unexpectedly opened subsequent to turbine control valve testing. Prior to thetrip, the reactor was at 90 percent power and stable. The open control valves caused adecrease in main steam line pressure which eventually led to the automatic scram. All safetysystems functioned as designed during the reactor scram. Because of the decrease in main steam line pressure when the control valves opened, the mainsteam isolation valves automatically closed; preventing the use of the main condenser fordecay heat removal. Cooldown and depressurization was accomplished using a combination ofmanual manipulation of the safety relief valves, and the High Pressure Coolant Injection andReactor Core Isolation Systems. The reactor is currently stable and in the cold shutdowncondition, with the residual heat removal system being used for decay heat removal. During the initial investigation of the cause of the scram, the licensee identified that the turbinecontrol valve actuator box was displaced by 8-12 inches, as a result of damage to the weldsthat connected the actuator platform to the support I-beams. Plant staff and the residentinspectors are investigating the cause of the weld damage and the turbine valve closure, aswell as whether the two problems are connected.The plant will remain shut down until the root causes for the two issues are identified and theturbine control valve problems are repaired.NRC resident inspectors are monitoring the situation. Additional NRC inspections will augmentthe resident inspectors to assist in gathering information concerning the apparent structuralfailures that resulted in the displacement of the turbine control valve actuator box. The State of Minnesota has been informed.

The event was reported to the NRC at 7:46 EDT on January 11, 2007. This information hasbeen discussed with licensed management and is current as of 10:00 a.m. CDT on January 12, 2007.

This preliminary notification will be updated as close to plant restart as possible.CONTACTS:

Nick ShahBruce Burgess630/829-9821630/829-9629