ML060460211

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PNO-III-06-004, Tritium Leakage
ML060460211
Person / Time
Site: Dresden, Byron  Constellation icon.png
Issue date: 02/15/2006
From: Matthew Mitchell, Orth S K
NRC/RGN-III
To:
References
FOIA/PA-2006-0130, FOIA/PA-2010-0209 PNO-III-06-004
Download: ML060460211 (2)


Text

February 15, 2006PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE -- PNO-RIII-06-004This preliminary notification constitutes EARLY notice of events of POSSIBLE safety or publicinterest significance. The information is as initially received without verification or evaluation, and is basically all that is known by the Region III staff on this date.FacilityDresden 2 and 3Exelon Generation Co.

Morris, Illinois Docket: 50-237 and 50-249 License: DPR-19; DPR-25 Byron 1 and 2 Exelon Generation Co.

Byron, Illinois Docket: 50-454 and 50-455 License: NPF-37; NPF-66Licensee Emergency Classification Notification of Unusual Event Alert Site Area Emergency General Emergency X Not Applicable

SUBJECT:

TRITIUM LEAKAGEDESCRIPTION:

On February 10, 2006, Exelon's Dresden Station informed the resident inspectors and Region III (Chicago) that elevated levels of tritium (the radioactive isotope of hydrogen) hadbeen measured in a monitoring well located near underground piping. The piping in the area goes from the condensate storage tank (CST) to the High Pressure Coolant Injection (HPCI) system. The pipe is located onsite.In 2004, leakage was discovered in the CST to HPCI supply line pipe. The pipe is 175 feetlong; the licensee replaced approximately 75 feet of piping where leaks had been identified in 2004. The licensee suspects that the current leak is in the 100 feet of piping that was notreplaced at that time.The sample result on February 11, 2006, was 486,000 picocuries per liter (pCi/L), on February 12, 2006, was 529,000 pCi/L, on February 13, 2006, was 680,000 pCi/L, and onFebruary 14, 2006, was 540,000 pCi/L.The pipe was isolated on February 11, 2006. The licensee plans to drain the pipe. Thelicensee had planned to replace the pipe in June 2006, but is considering an adjustment to the schedule for replacement.Also, on February 10, 2006, Exelon's Byron Station informed the resident inspectors andRegion III (Chicago) that elevated levels of tritium in water had been identified in severalvacuum breaker vaults located along the discharge piping. CONTACTS:

Mark MitchellSteven Orth630/829-9855630/829-9827 PNO-RIII-06-004-2-This piping is on plant property. The piping is approximately 2.5 miles long normally carryingnon-radioactive circulating water to the Rock River. The discharge pipe is also used for planned liquid radioactive effluent releases with effluent mixing with the discharge water. The licensee is pursuing installation of monitoring wells adjacent to the piping to determine if tritium has migrated from the vaults. The licensee sampled water in 5 vaults along the pipeline. The tritium concentrations rangedfrom 256 pCi/L to 86,000 pCi/L. Resident inspectors and Region III staff are monitoring the licensee's activities. Based oncurrent information, the effects of the leakage are localized to the immediate area.The licensee is issuing a news release regarding the tritium issues at Braidwood, Byron, andDresden and announcing program for tritium assessment at all 10 of the Exelon Nuclear Generating sites.The State of Illinois has been notified. The information in this preliminary notification has beenreviewed with licensee management and is current as of 9 a.m. on February 15, 2006.