ML043620071

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Comment (13) of Louis Zeller on Implementation of the Reactor Oversight Process
ML043620071
Person / Time
Site: Catawba  Duke Energy icon.png
Issue date: 12/16/2004
From: Zeller L
Blue Ridge Environmental Defense League
To: Lesar M
NRC/ADM/DAS/RDB
References
69FR63411 00013
Download: ML043620071 (9)


Text

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__i tFHN IbU0-Ul -I Page 1 1 From: Louis Zeller <BREDL skybest.com>

To: <nrcrep@nrc.gov>

Date: Thu, Dec 16, 2004 6:57 PM

Subject:

Implementation of the Reactor Oversight Process, FRN 7590-01-P BLUE RIDGE ENVIRONMENTAL DEFENSE LEAGUE 6 Sip<?

www.BREDL.org - PO Box 88 Glendale Springs, North Carolina 28629 - Phone (336) 982-2691 - Fax (336) 982-2954 - BREDL~skybest.com

/3 December 16, 2004 Michael T. Lesar Chief, Rules and Directives Branch Office of Administration (Mail Stop: T6-D59)

Nuclear Regulatory Commission Washington, DC 20555-0001 Re: Implementation of the Reactor Oversight Process, FRN 7590-01-P

Dear Mr. Lesar:

On behalf of the Blue Ridge Environmental Defense League, I write to comment on the Implementation of the Reactor Oversight Process, noticed in the Federal Register on 25 October 2004 [FRN 7590-01 -P].

First, I will comment as you requested on the 19 questions for Initial ROP/Current ROP:

1) 4/5
2) 3/3
3) 3/3
4) 3/3
5) 2/2
6) 3/3
7) 5/5
8) 3/4
9) 4/5
10) 5/5
11) 2/4
12) 5/5
13) 4/5
14) 4/5
15) 4/5

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~~SJRCREP SCRP- r-ide atonof the Reactor Oversiight Process, FRN 7590~1P -1P -~-Pg

16) 5/5
17) 3/3
18) 3/3
19) 4/5
20) Additional comments:

On October 23, 2003 the NRC issued an inspection report for Catawba Nuclear Station, Units 1 and 2 (IR 05000413/2003-004, IR 05000414/2003-004; 612912003-9/2712003). Under NRC-identified findings, the report stated that barrier integrity was GREEN. However, the non-cited violation involved Duke's failure to comply with 10 CFR 50 Appendix B, Criterion 3, Design Control, "due to inadequate design measures." At issue were relief valves which were too small to prevent excess water pressure in the event of reactor pump thermal barrier rupture. Why has this been deemed "green"?

On September 27, 2004 the NRC held a conference call with Duke Energy regarding steam generator tube inspections. At issue were cracks in the Westinghouse Model D5 steam generator tubes. Catawba Unit 2 has four such steam generator units and each unit contains 4570 tubes with diameters of 0.75 inches and nominal wall thicknesses of 0.043 inches. Overexpansion in some of the tubes resulted in "circumferential indications," that is, cracks. The "indication" in the tack roll segment was 330 degrees in circumference, i.e., nearly all way round, and 100% "through-wall," i.e., broken. If the licensee plans to plug the damaged tube, there was no indication of when this might happen. This looks like an accident waiting to happen which would be compounded by the inadequate relief valves cited in the NRC's October 23rd inspection report.

On December 6, 2004 Catawba Unit 1 suffered an automatic turbine trip which caused a reactor trip (Event No. 41246). The event report stated, "All emergency Core Cooling Systems.are fully operable if needed." This would seem to be contradicted by the non-cited violation cited on October 23, 2003 for inadequate "relief valve sizing to prevent exceeding the design pressure of the component cooling water (KC) piping in the event of a reactor coolant pump (RCP) thermal barrier rupture." (IR 05000413/2003-004, IR 05000414/2003-004; 6/29/2003-9/27/2003) and cracks in steam generator units at Catawba Unit 2 which was simultaneously "operating at 100% power."

Meanwhile, Duke Energy seeks to extend the time between checking Actuation System slave relays from 92 days to 18 months, six times as long between inspections. NRC has requested additional information regarding the greatly reduced surveillance regime for this safety system. But one must ask why would the agency even consider such an extension in an aging plant with the aforementioned weak points in critical systems?

The reactor oversight process must not allow event reports and inspection reports to simply serve as by-standers in the operation of nuclear power plants. The litany of non-cited violations and exemptions from requirements is a path to certain failure. I have attached a list of such reports to these comments.

Why in the world would NRC not cite a violation of the regulations? Citations and fines would censure licensees and prompt better operations. Nuclear utilities seem to enjoy a privileged place in the sight of the agency empowered to write and enforce safety regulations. During hearings before the Atomic Safety and Licensing Board, the NRC staff counsel parrot utility opinions. We who have brought cases are outnumbered two to one, with industry and NRC counsel acting as if they are playing on the same team instead of as opponent and referee.

Someone at the agency has got to recognize the inherent danger of such a system.

Respectfully submitted,

NRCREP - the 01rtcjoo R-eaictor.Overs~ight Proess FRN 7590-01f-P _

Louis Zeller Attachment U.S. Nuclear Regulatory Commission http:l/www.nrc.gov/NRR/OVERSIGHT/ASSESS/CAT2/cat2-pim.html Last modified: March 01, 2002 Catawba 2 Initiating Events IE3rdIE Significance:G Sep 23, 2000 Identified By: Licensee Item Type: FIN Finding Reactor Trip Caused by Moisture Intrusion into Main Feedwater Pump 2B Speed Control Circuitry Poor workmanship and inadequate oversight of turbine building roof repairs, coupled with inadequately constructed roof drainage systems, resulted in a June 5, 2000, Unit 2 reactor trip. Water from heavy rains that day could not be properly drained from the turbine building roof, partially due to debris and other roofing material that had collected in the drainage system. Water overflowed from the roof and into the turbine building, and leaked into the 2B main feedwater pump turbine speed control cabinet. A secondary plant transient resulted, which ultimately led to a turbine trip/reactor trip. This issue was determined to be of very low safety significance because it did not affect the ability of mitigating systems to perform their safety functions (Section 40A3.1).

Inspection Report# : (pdf)

Mitigating Systems Significance:G Dec 22, 2001 Identified By: Licensee Item Type: NCV NonCited Violation Violation of TS 3.6.9 due to Inoperable Hydrogen Ignition System Inoperable Ignitors on Both Trains of the Hydrogen Ignition System Due to a Common Cause Failure Mode on Non-Safety Related Equipment Resulting in Inoperable Hydrogen Ignition System and a Violation of TS 3.6.9.

Inspection Report# : (pdf)

Significance:G Sep 22, 2001 Identified By: NRC Item Type: NCV NonCited Violation Failure to Implement Effective Corrective Actions Associated With the Unit 2 FWST Level Channels Failures The inspectors identified a failure to implement effective corrective actions for the Unit 2 Refueling Water Storage Tank (FWST) level channels 1 and 3 that was dispositioned as a non-cited violation. Specifically, portions of the instrument cables experience conduit temperatures of 275 degrees Fahrenheit which exceed the cable design rating of 194 degrees. This condition was identified in 1996 but was not promptly evaluated nor has the problem been fully resolved. The failure was determined to be of very low safety significance because all mitigation systems remained operable, the ability to manually swap the emergency core cooling system suction source from the FWST to containment sump was still available, and the channel failures did not render the system unavailable to perform its function. (Section 1R1 2.2)

Inspection Report# : (pdf)

NRCREP - Implementation of the Reactor Oversight Process, FRN 7590-01 -P Paqe 41 NRCREP: Implementation of the Reactor OversightProcess, FRN 7590-01-P Page 41 Significance:G Sep 22, 2001 Identified By: Licensee Item Type: NCV NonCited Violation Failure to Identify A Condition Adverse to Quality that Rendered the "A"Chiller Inoperable Operations personnel failed to identify a condition adverse to quality which contributed to not recognizing that the N"A Train of the Control Room Area Chilled Water System (CRACWS) was inoperable. The successful start of the "A"chiller was the basis for calling 'A' Train CRACWS operable. However, the fact that maintenance personnel assisted in the chiller start and unreliable operation of the chiller pressure switch was exhibited in earlier testing was not factored into the operability decision. This was dispositioned as a non-cited violation. The failure was determined to be of very low safety significance because the "A" Train CRACWS f unctioned properly while "B"Train CRACWS was being restored to service. Also during subsequent tests, the "A"chiller operated satisfactorily. Additional information on this finding is provided in NRC letter to Duke Energy Corporation dated January 9, 2002. (Section 40A3)

Inspection Report# : (pdf)

MS4th Significance:G Mar 30, 2001 Identified By: NRC Item Type: NCV NonCited Violation Failure to Adequately Perform TS SR 3.4.9.3 for Pressurizer Heaters A non-cited violation was identified regarding the licensees failure to properly perform Technical Specification Surveillance Requirement 3.4.9.3, which verifies that pressurizer heaters can be automatically transferred from their normal power supplies to their emergency power supplies. Once identified, the portion of the automatic circuit that had been omitted from the test was properly tested on February 5, 2001, and was verified to be functional. This finding had a credible impact on safety because the licensee had never demonstrated the full automatic capability of the power supply transfer circuitry for the pressurizer heaters, which are important for maintaining pressurizer pressure control during a loss of offsite power event. The finding was also the latest in a number of missed surveillance requirements identified at Catawba over the last two to three years. This finding was of very low safety significance because the circuit was functional when tested and because of provisions in the licensee's emergency procedures for manually aligning the heaters to their emergency power source had the automatic transfer failed during a loss of normal power event (Section 1R22).

Inspection Report# :(pdf)

Significance:G Mar 30, 2001 Identified By: NRC Item Type: FIN Finding Failed to Demonstrate Performance of the Station Drinking Water System as Backup Cooling Water to the Unit 1 and 2 A Train Charging Pumps The licensee failed to demonstrate that the performance or condition of the station drinking water system, a risk-important system that provides backup cooling water to the Unit 1and 2 A train charging pump motors and bearing oil coolers, was being effectively controlled through the performance of appropriate preventive maintenance (including surveillance activities). This resulted in a failure to recognize and correct a degraded systemn pressure condition, until it was identified by the inspectors. The degraded pressure condition was determined to be of very low safety significance because an analysis performed by the licensee demonstrated that the backup function to cool the charging pumps and motors would have been provided at the degraded pressure (Section 1R12.2).

Inspection Report# : (pdf)

Significance: N/A Mar 30, 2001 Identified By: NRC Item Type: FIN Finding Failure to Identify Two Maintenance Preventable Functional Failures Affecting the Unit 2 Auxiliary Feedwater SystemI The inspectors identified a failure to identify two maintenance preventable functional failures (MPFFs)

NRCREP ImplementationoftheReactorOversightProcessiF-RN7590-01--P- Page 5 3 NRCREP Implementation of the Reactor Oversight Process FRN 7590-01-P Pacie5 y affecting the Unit 2 auxiliary feedwater system, one involving the turbine-driven auxiliary feedwater pump, the other involving the A motor-driven pump. Both of these occurred on October 5, 2000, following an inadvertent transfer of pump control to a local control panel. Although the finding did not involve a violation of the maintenance rule, it represented a recurring performance problem in this area as the latest of several missed maintenance preventable functional failure determinations involving different safety systems over the last year and a half. This finding was of very low safety significance because the failure to identify these MPFFs did not directly affect the ability of the auxiliary feedwater system to perform its safety function (Section 1R1 2.1).

Inspection Report# : (pdf)

Significance:G Jun 24, 2000 Identified By: Licensee Item Type: NCV NonCited Violation Failure to Provide Adequate Procedures for Performing Maintenance on Safety-Related Sump Pump Level Switches Residual heat removal and containment spray pump room sump level alarm function was lost for several months up to February 2000 due to inadequate maintenance procedures associated with sump level switch calibrations. This issue was characterized as a non-cited violation of Technical Specification 5.4.1 and was determined to be of very low safety significance due to the availability of other emergency core cooling system leak detection methods (Section 40A3.2).

Inspection Report#: (pdf)

Significance:G Jun 24, 2000 Identified By: NRC Item Type: NCV NonCited Violation Failure to Scope an Accident Mitigating Function Associated with ECCS Leak Detection in the Maintenance Rule The licensee failed to include in its maintenance rule scope an accident mitigating function for a control room alarm associated with emergency core cooling system post-accident leak detection capability. The alarm was tied to residual heat removal and containment spray pump room sump levels and was identified in 1998 as a mitigating function, as described in the Catawba Updated Final Safety Analysis Report. As a result, two functional failures were not properly classified in February 2000. This issue was characterized as a non-cited violation of 10 CFR 50.65 (b)(2) and was determined to have very low safety significance because the licensee's scoping and functional failure determination errors did not directly result in additional unavailability of the alarm function (Section 1R12.2).

Inspection Report# : (pdf)

Significance:G Jun 24, 2000 Identified By: NRC Item Type: FIN Finding Failure to properly classify a maintenace rule functional failure of the Unit 2 A steam generator power operated relief valve (2SV-1 9)

The licensee failed to properly classify a maintenace rule functional failure of the Unit 2 A steam generator power operated relief valve (2SV-1 9) when it failed to open on April 15, 2000. The licensee incorrectly assumed that the valve's failure was not a functional failure because other redundant valves were available at the time. This issue was determined to have very low safety significance because the licensee's error did not result in additional equipment unavailability (Section 1R1 2.1).

Inspection Report# : (pdf)

Significance:G Jun 24, 2000 Identified By: Licensee Item Type: FIN Finding Steam generator power operated relief valve 2SV-1 9 failed to open on April 15, 2000, due to mispostioned nitrogen pressure regulators Steam generator power operated relief valve 2SV-1 9 failed to open on April 15, 2000, due to mispostioned nitrogen pressure regulators, which are required to function during a design basis event involving the loss

qRCREP - Implementation of the Reactor Oyersight Process, FRN7590-0 -Pagebq of normally available instrument air. The licensee determined the mispositioned regulators to be a human performance issue, but were not able to pinpoint when the actual mispositioning took place. This issue was determined to have very low safety significance due to the availability of other steam generator power operated relief valves and diverse means of cooling the secondary plant (Section 1R22.2).

Inspection Report# : (pdf)

Barrier Integrity BI3rdBI Significance:G Jun 24, 2000 Identified By: NRC Item Type: FIN Finding Failure to properly evaluate plant risk associated with emergent work for the Unit 2 hydrogen ignition system on April 27, 2000.

The licensee did not properly evaluate plant risk associated with emergent work for the Unit 2 hydrogen ignition system on April 27, 2000. As a result, the unit was in an unevaluated increased risk condition while planned work associated with the containment spray system was ongoing. This condition was allowed by Technical Specifications and plant procedures, but plant procedures required that a written contingency plan be developed prior to the work commencing, which was not done. This issue was of very low safety significance due to the availability of diverse and redundant systems designed to accomplish the hydrogen mitigation and containment pressure control functions (Section 1R13).

Inspection Report# : (pdf)

Emergency Preparedness EP3rdOR1 st Occupational Radiation Safety OR3rdOR Significance:G Jun 24, 2000 Identified By Licensee Item Type: NCV NonCited Violation Failure to Prevent the Release of Radioactive Byproduct Material from the Radiological Control Area and Plant Site A non-cited violation was identified for the failure to comply with the requirements of 10 CFR 20.1802.

Specifically, on April 7, 2000, the licensee failed to prevent the release of radioactive byproduct material (e.g., a radioactive particle on a contract employee's lanyard) from the radiological control area and plant site. Based on the activity of the particle and the resulting occupational dose assessment for the affected contract employee, this finding was determined to be of very low significance (Sections OS2, 2PS3).

Inspection Report# : (pdf)

Public Radiation Safety PR3rdPP1 st Physical Protection

NRCREP -ImTplementation of the Reactor Overight Process, FRN 7590-01 -P Pa Paqe 710 PP3rdPP Significance:G Jun 24, 2000 Identified By: Licensee Item Type: NOV NonCited Violation Failure to Secure Two Vital Area Openings Exceeding 96 Square Inches in February 1999 A non-cited violation of the Physical Security Plan was identified for the licensee's failure to secure two vital area openings exceeding 96 square inches in February 1999. This issue was determined to have very little significance, given the non-predictable basis of the failures and the fact that there was no evidence that the vulnerabilities had been exploited (Section 3PP2).

Inspection Report# : (pdf)

Miscellaneous Significance: G Jun 23, 2001 Identified By: Licensee Item Type: NOV NonCited Violation Failure to Develop Appropriate Written Procedures or Documented Instructions for Maintenance Activities Performed on the A train YC Chiller as Described in PIP C-01 -01 994 Technical Specification 5.4.1 .a,and Regulatory Guide 1.33, Section 9, Procedures for Performing Maintenance, required that maintenance that can affect the performance of safety related equipment should be properly planned and performed in accordance with written procedures and documented instructions. Contrary to this, on May 3, 2001, the licensee failed to develop appropriate written procedures or documented instructions for maintenance activities performed on the A train YC chiller as described in PIP C-01 -01 994.

Inspection Report# : (pdf)

Significance:G Jun 23, 2001 Identified By: Licensee Item Type: NOV NonCited Violation Failed to Perform Adequate Testing Following Replacement of the Evaporator Differential Pressure Switch for the A train YC Chiller as Described in PIP 0-01 -01 333 10 CFR Part 50, Appendix B, Criteria Xi, Test Control, requires that a test program be established to assure that all testing required to demonstrate that SSCs will perform satisfactorily in service is identified and performed in accordance with written test procedures. Contrary to this, on March 13, 2001, the licensee failed to perform adequate testing following replacement of the evaporator differential pressure switch for the A train YC chiller as described in PIP 0-01 -01 333.

Inspection Report# : (pdf)

Significance: N/A Feb 16, 2001 Identified By: NRC Item Type: FIN Finding Identification and Resolution of Problems Overall, the licensee's corrective action program was effective at identifying, evaluating, and correcting problems. The threshold for entering problems into the corrective action program was sufficiently low.

Reviews of operating experience information were comprehensive. In general, the licensee properly prioritized items (by Action Category) in its corrective action program database, which ensured that timely resolution and appropriate causal factor analyses were employed commensurate with safety significance.

Some exceptions were noted in the area of problem identification, where all relevant issues of problems were not identified and equipment performance was adversely affected. The inspection identified three exceptions in the area of prioritization and evaluation of issues, where more comprehensive root cause determinations would have provided more effective evaluations and corrective actions. Inthe area of effectiveness of corrective actions, it was noted that the corrective action program was not timely in resolving various documentation deficiencies with Technical Specification (TS) surveillances, Updated

NRCREP - Impleentatio of the Reactor Oversight Process, FRN 75-90-01-P Page 8 R NRCREP-lmplementation of the Reactor Oversight Process, ERN 7590-01-P

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_ . . . ., t Final Safety Analysis Report changes and TS bases changes. Previous non-compliance issues documented as non-cited violations were properly tracked and resolved via the corrective action program.

The results of the last comprehensive corrective action program audit conducted by the licensee (September 1999) were properly entered and dispositioned in the corrective action program. Based on discussions with plant personnel and the apparently low threshold for items entered in the corrective action program database, the inspectors concluded that workers at the site generally felt free to raise safety concerns to their management.

Inspection Report#: (pdf)

Significance: N/A Dec 23, 2000 Identified By: Licensee Item Type: NCV NonCited Violation Technical Specification 5.4.1 and Regulatory Guide 1.33, Section 7, for failing to have adequate procedures to control the release of radioactive material during a pressurizer gas space venting evolut Technical Specification 5.4.1 and Regulatory Guide 1.33, Section 7, for failing to have adequate procedures to control the release of radioactive material during a pressurizer gas space venting evolution on October 14, 2000, as described in the licensee's corrective action program. Reference PIPs C-00-04914 and 05241.

Inspection Report# : (pdf)

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Subject:

Implementation of the Reactor Oversight Process, FRN 7590-01-P Creation Date: Thu, Dec 16, 2004 6:53 PM From: Louis Zeller <BREDL@skybest.com>

Created By: BREDL@skvbest.com Recipients nrc.gov twf2_po.TWFNDO NRCREP Post Office Route twf2_po.TWFNDO nrc.gov Files Size Date & Time MESSAGE 21508 Thursday, December 16, 2004 6:53 PM TEXT.htm 24720 Mime.822 50064.

Options Expiration Date: None Priority: Standard Reply Requested: No Return Notification: None Concealed

Subject:

No Security: Standard