ML031120115
| ML031120115 | |
| Person / Time | |
|---|---|
| Site: | Arkansas Nuclear |
| Issue date: | 04/21/2003 |
| From: | Laura Smith NRC/RGN-IV/DRP |
| To: | Anderson C Entergy Operations |
| References | |
| IR-03-002 | |
| Download: ML031120115 (37) | |
See also: IR 05000313/2003002
Text
April 21, 2003
Craig G. Anderson, Vice President,
Operations
Arkansas Nuclear One
Entergy Operations, Inc.
1448 S.R. 333
Russellville, Arkansas 72801-0967
SUBJECT: ARKANSAS NUCLEAR ONE, UNITS 1 AND 2 - NRC INTEGRATED INSPECTION
REPORT 50-313/03-02; 50-368/03-02
Dear Mr. Anderson:
On March 22, 2003, the NRC completed an inspection at your Arkansas Nuclear One, Units 1
and 2, facility. The enclosed report documents the inspection findings, which were discussed
with you and other members of your staff on April 3, 2003, and as described in Section 4OA6.
The inspection examined activities conducted under your licenses as they relate to safety and
compliance with the Commissions rules and regulations and with the conditions of your
licenses. Within these areas, the inspection consisted of selected examination of procedures
and representative records, observations of activities, and interviews with personnel.
Based on the results of this inspection, the NRC has identified issues that were evaluated under
the risk significance determination process as having very low safety significance (Green) as
well as one issue that required evaluation using our traditional enforcement process. The NRC
has also determined that violations are associated with these issues. These violations are
being treated as noncited violations (NCVs), consistent with Section VI.A of the Enforcement
Policy. These NCVs are described in the subject inspection report. If you contest the violations
or significance of these NCVs, you should provide a response within 30 days of the date of this
inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,
ATTN: Document Control Desk, Washington DC 20555-0001, with copies to the Regional
Administrator, U.S. Nuclear Regulatory Commission, Region IV, 611 Ryan Plaza Drive,
Suite 400, Arlington, Texas 76011; the Director, Office of Enforcement, U.S. Nuclear
Regulatory Commission, Washington DC 20555-0001; and the NRC Resident Inspector at the
Arkansas Nuclear One facility.
In accordance with 10 CFR 2.790 of the NRCs "Rules of Practice," a copy of this letter, its
enclosure and your response (if any) will be made available electronically for public inspection
in the NRC Public Document Room or from the Publicly Available Records (PARS) component
of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Entergy Operations, Inc.
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Should you have any questions concerning this inspection, we will be pleased to discuss them
with you.
Sincerely,
/RA/
Linda Joy Smith, Chief
Project Branch D
Division of Reactor Projects
Dockets:
50-313
50-368
Licenses:
NPF-6
Enclosure:
NRC Inspection Report
50-313/03-02; 50-368/03-02
cc w/enclosure:
Executive Vice President
& Chief Operating Officer
Entergy Operations, Inc.
P.O. Box 31995
Jackson, Mississippi 39286-1995
Vice President
Operations Support
Entergy Operations, Inc.
P.O. Box 31995
Jackson, Mississippi 39286-1995
Manager, Washington Nuclear Operations
ABB Combustion Engineering Nuclear
Power
12300 Twinbrook Parkway, Suite 330
Rockville, Maryland 20852
County Judge of Pope County
Pope County Courthouse
100 West Main Street
Russellville, Arkansas 72801
Winston & Strawn
1400 L Street, N.W.
Washington, DC 20005-3502
Entergy Operations, Inc.
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Bernard Bevill
Radiation Control Team Leader
Division of Radiation Control and
Emergency Management
4815 West Markham Street, Mail Slot 30
Little Rock, Arkansas 72205-3867
Mike Schoppman
Framatome ANP, Inc.
Suite 705
1911 North Fort Myer Drive
Rosslyn, Virginia 22209
Technological Services Branch
Chief
FEMA Region VI
800 North Loop 288
Federal Regional Center
Denton, Texas 76201-3698
Entergy Operations, Inc.
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Electronic distribution by RIV:
Regional Administrator (EWM)
DRP Director (ATH)
DRS Director (DDC)
Senior Resident Inspector (RLB3)
Branch Chief, DRP/D (LJS)
Senior Project Engineer, DRP/D (JAC)
Staff Chief, DRP/TSS (PHH)
RITS Coordinator (NBH)
B. McDermott (BJM)
ANO Site Secretary (VLH)
Dale Thatcher (DFT)
Regional State Liaison Officer (WAM)
ADAMS: Yes
No Initials: ______
Publicly Available Non-Publicly Available
Sensitive
Non-Sensitive
R:\\_ANO\\2003\\AN2003-02RP-RLB.wpd
RIV:RI:DRP/D
SRI:DRP/D
PE:DRP/D
SPE:DRP/D
C:DRS/PSB
KDWeaver
RLBywater
ELCrowe
JAClark
TWPruett
T - LJSmith
T - LJSmith
E - LJSmith
E - LJSmith
MPShannon for
4/21/03
4/21/03
4/21/03
4/21/03
4/21/03
C:DRP/D
LJSmith
/RA/
4/21/03
OFFICIAL RECORD COPY
T=Telephone E=E-mail F=Fax
ENCLOSURE
U.S. NUCLEAR REGULATORY COMMISSION
REGION IV
Dockets:
50-313, 50-368
Licenses:
Report No:
50-313/03-02; 50-368/03-02
Licensee:
Entergy Operations, Inc.
Facility:
Arkansas Nuclear One, Units 1 and 2
Location:
Junction of Hwy. 64W and Hwy. 333 South
Russellville, Arkansas
Dates:
December 29, 2002, through March 22, 2003
Inspectors:
R. Bywater, P.E., Senior Resident Inspector
J. Clark, Senior Project Engineer, Project Branch D
R. Lantz, Senior Emergency Preparedness Inspector
L. Ricketson, P.E., Senior Health Physicist
K. Weaver, Resident Inspector
Approved By:
Linda Joy Smith, Chief, Project Branch D
Division of Reactor Projects
Attachment 1:
Attachment 2:
Supplemental Information
ANO Paper, "Secondary System Pressure Boundary as an Extension of
Containment Liner"
SUMMARY OF FINDINGS
Arkansas Nuclear One, Units 1 and 2
NRC Inspection Report 50-313/03-02; 50-368/03-02
IR05000313-03-02, IR05000368-03-02; Entergy Operations, Inc.; 12/29/02 - 03/22/03; Arkansas
Nuclear One, Units 1 and 2; Evaluations of Changes, Tests, or Experiments; Temporary Plant
Modifications; ALARA Planning and Controls.
The inspection was conducted by the resident inspectors, one senior project engineer, a senior
health physicist, and a senior emergency preparedness inspector. The inspection identified three
findings. The significance of most findings is indicated by their color (Green, White, Yellow, or Red)
using IMC 0609, "Significance Determination Process" (SDP). Findings for which the SDP does not
apply may be "Green" or be assigned a severity level after NRC management review. The NRCs
program for overseeing the safe operation of commercial nuclear power reactors is described in
NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000.
A.
Inspector-Identified Findings
Cornerstone: Mitigating Systems
Green. The licensee did not properly evaluate a temporary alteration that was performed
when a door separating a safety-related switchgear room from the turbine building was
removed for maintenance. As a result, the impact of a potential high energy line break on
equipment needed to mitigate the event was not identified or evaluated by an engineering
evaluation. Failure to perform an engineering evaluation to support this temporary alteration
was a violation of Unit 1 Technical Specification 5.4.1.a. This violation is being treated as a
noncited violation (NCV) consistent with Section VI.A in the Enforcement Policy.
The safety significance of this issue was determined to be very low since this issue screened
as Green during a Phase 1 SDP assessment, because the finding did not result in
equipment becoming incapable of performing its function in the case of a design basis
accident. The issue was considered to be more than minor because it affected the mitigating
systems cornerstone objective for design control and modifications because the ability to
mitigate the consequences of a high energy line break would have been affected if the
finding had affected more than one train of equipment (Section 1R23).
Cornerstone: Barrier Integrity
Severity Level IV. The inspectors identified a noncited violation of 10 CFR 50.59 because
the licensee failed to identify that changes made to the Units 1 and 2 Updated Safety
Analysis Reports required a license amendment request. These changes removed
containment isolation valve controls for secondary system containment penetrations. The
licensee initiated corrective action on March 28, 2003, to prepare a license amendment
request to obtain NRC approval of the changes to the Updated Safety Analysis Reports.
This is an item for traditional enforcement because it involves an issue not appropriate for
evaluation using the SDP. It involves a violation of 10 CFR 50.59, an issue which impacts
NRC oversight ability. The issue is more than minor because it involves a programmatic
issue affecting containment controls for all secondary system penetrations. It was
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considered to be a noncited Severity Level IV violation. Management review determined
it was greater than minor because the change should have received NRC review prior to
implementation. Redundant containment barrier (system piping) existed and the
licensee entered this issue into its corrective action program (Section 1R02).
Cornerstone: Occupational Radiation Safety
Green. The inspectors identified a noncited violation of Units 1 and 2 Technical Specifications 5.4.1.a and 6.8.1.a, respectively, because the licensee failed to follow
procedural requirements. Specifically, the licensee failed to provide the reason radiation
work permits and work activity dose estimates were revised as required by
Procedure NMM RP-105, Revision 1, Section 5.8.
The inspectors determined that this finding was associated with the Occupational
Radiation Safety Cornerstone program and process attributes (ALARA
planning/projected dose) and affected the objective of the cornerstone, which is to
protect the worker from exposure to radiation. Therefore, the finding was greater than
minor. The occurrence involved a failure to maintain or implement, to the extent
practical, procedures needed to achieve occupational doses that were ALARA, which
resulted in unplanned, unintended occupational collective dose for a work activity.
Therefore, the safety significance of the finding was evaluated using the Occupational
Radiation Safety SDP. However, because the licensees 3-year rolling average
collective dose was not greater than 135 person-rem/unit, the finding had no more than
very low safety significance.
B.
Licensee-Identified Findings
Violations of very low safety significance, which were identified by the licensee, have
been reviewed by the inspectors. Corrective actions taken or planned by the licensee
have been entered into the licensee's corrective action program. These violations and
corrective action tracking numbers are listed in Section 4OA7 of this report.
Report Details
Summary of Plant Status
Unit 1 began the inspection period at approximately 100 percent power and remained at or near
100 percent throughout the inspection period.
Unit 2 began the inspection period at 100 percent power. On February 9, 2003, Unit 2
operators reduced reactor power to approximately 70 percent in support of engineering data
collection for feedwater system testing. Unit 2 operators returned the unit to 100 percent power
the same day.
1.
REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity
[REACTOR-R]
1R01
Adverse Weather Protection (71111.01)
a.
Inspection Scope
On January 21-23, 2003, the inspectors walked down the Unit 2 safety-related battery
rooms to verify that compensatory measures were in place for the cold weather
conditions and to verify that the battery room temperature was sufficient to maintain the
electrolyte temperature above the Technical Specification 4.8.3.b.3 limit of 60°F. The
inspectors reviewed Unit 2 Procedure 2106.032, "Unit Two Freeze Protection Guide,"
Revision 9, to determine all applicable cold weather protection requirements for the
Unit 2 station batteries and verified that these measures were in place to protect the
equipment.
b.
Findings
No findings of significance were identified.
1R02
Evaluations of Changes, Tests, or Experiments (71111.02)
.1
Unit 2 Containment Isolation Valve Designation Change
a.
Inspection Scope
During a routine review of plant status for Unit 2, on or about December 21, 2001, to
January 16, 2002, the inspectors noted that Unit 2 Steam Generator B Sample
Valve 2CV-5859-2 had been de-energized in the open position and backseated due to a
packing leak, which resulted in a Unit 2 control room panel alarm of "CIAS inop." This
valve is located directly outside containment Penetration 2P7 and receives an
engineered safety feature actuation signal to close on a containment isolation actuation
signal (CIAS) on high containment pressure. With the valve de-energized open, it would
not perform its function to close on a CIAS.
The inspectors found that Technical Specification 3.6.3.1, "Containment Isolation
Valves," limiting condition for operation was not entered for this valve, while it was in the
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open position and de-energized for 26 days (December 21, 2001, to January 16, 2002).
This exceeded the action time requirements of the Technical Specifications. The
licensee stated that the valve was no longer considered a containment isolation valve.
The inspectors performed a historic review of the licensing basis for this valve to
determine why Valve 2CV-5859-2 was no longer considered a containment isolation
valve within the scope of the action requirements of Technical Specification 3.6.3.1.
b.
Findings
(1)
Introduction
As a result of an inadequate 10 CFR 50.59 screening, the licensee failed to perform a
safety evaluation for:
Changing the description of containment documented in the Updated Final
Safety Analysis Report (UFSAR)
Changing the description of General Design Criterion (GDC) 57, "Closed System
Isolation Valves," applicability documented in the UFSAR
Changing Procedure 1015.034, "Containment Penetration Administrative
Controls," Revision 1, to indicate that Unit 2 Steam Generator B Sample
Valve 2CV-5859-2 was not a containment isolation valve within the scope of
Technical Specification 3.6.3.1
Several other secondary system containment penetration valves were also included in
these changes. The failure to perform a safety evaluation for these changes to the
Unit 2 UFSAR and Procedure 1015.034 was determined to be an example of a violation
of 10 CFR 50.59.
(2)
Description
Background
As part of this historical review, the inspectors reviewed the Unit 2 Preliminary Safety
Analysis Report and the Unit 2 Final Safety Analysis Report. These documents were
used by the Commission to perform the radiological safety review with respect to a
decision concerning issuance of an operating license for Unit 2. The staffs review was
documented in NUREG-0308, "Safety Evaluation Report, Arkansas Nuclear One,
Unit 2," Supplement 1, dated November 1977. NUREG-0308, Supplement 1, states
that, "the radiological safety review with respect to a decision concerning issuance of an
operating license for ANO-2 has been based on the applicants Final Safety Analysis
Report (Amendment 20) and subsequent Amendments 21-43, all of which are available
for review at the Nuclear Regulatory Commissions Public Document Room . . . ." The
Safety Evaluation Report (SER) summarizes the results of the radiological safety review
of Unit 2 performed by the staff. The SER further states that "The conclusions reached
as a result of the evaluation of the applicants application to operate Unit 2 are presented
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in Section 22.0 of the SER." NUREG-0308, "Containment Isolation Systems,"
Supplement 1, Section 6.2.4, states that "The containment isolation system is designed
to isolate the containment atmosphere from the outside environment under accident
conditions. Double barrier protection, in the form of closed systems and isolation
valves, is provided so that no single valve or piping failure can result in loss of
containment integrity. Containment building penetration piping up to and including the
external isolation valve is designed as seismic Category I equipment and is protected
against missiles which could be generated under accident conditions. Containment
isolation will occur automatically upon receipt of a containment isolation actuation signal
of high containment pressure (5 pounds per square inch gauge.) All fluid penetrations
not required for operation of the engineered safety features equipment will be isolated.
Remotely operated isolation valves have been provided for those safety-related systems
which will not be automatically isolated . . . ."
NUREG-0308, Supplement 1, further states that "we have reviewed the containment
isolation system for conformance to General Design Criteria 54, 55, 56, and 57. We
conclude that the system meets the General Design Criteria and is, therefore,
acceptable."
As stated earlier, the staff documented in NUREG -0308, Supplement 1, that "the
radiological safety review with respect to a decision concerning issuance of an operating
license for ANO-2 has been based on the applicants Final Safety Analysis
Report (FSAR) (Amendment 20) and subsequent Amendments 21 through 43." FSAR
Section 6.2.4 through Amendment 32, dated October 31, 1975, stated that "the
containment isolation systems provide the means of isolating fluid systems that pass
through containment penetrations so as to confine to the containment any radioactivity
that may be released following a postulated accident. Unit-2 does not have a particular
system for containment isolation; however, isolation is achieved by applying common
criteria to penetrations in the various fluid systems, and by using a single parameter,
containment pressure, to actuate the appropriate valves." FSAR, "Design Bases,"
Section 6.2.4.1, states that "the Design basis for the CIS is to minimize the release of
radioactive material from the Containment by closing all fluid penetrations not serving
accident consequence limiting systems, so that the site boundary thyroid and whole
body doses from radioactive material escaping through the containment penetrations
plus the doses from other sources during any postulated accident are within the limits of
10 CFR Part 100. The containment isolation systems are designed in accordance with
10 CFR Part 50, Appendix A, General Design Criteria 54, 55, 56 and 57, and meet the
leak testing criteria of 10 CFR Part 50, Appendix J. The applicable criterion for each
penetration is shown in Table 6.2-26." FSAR Table 6.2-26 and amendments used by
the staff for the radiological safety review concerning issuance of an operating license
for Unit 2 identified Containment Penetrations 2P1, 2P2, 2P3, 2P4, 2P7(SGA),
2P7(SGB), 2P32, 2P35, 2P64, and 2P65 as meeting the GDC 57 criterion. The above
listed penetrations are all associated with the containment building secondary system
piping penetrations.
Based on review of the Unit 2 FSAR, amendments documented in NUREG-0308, and
the current UFSAR through Amendment 16, the inspectors found that Unit 2 Steam
Generator B Sample Valve 2CV-5859-2 had always been previously identified and
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documented in the FSAR as a containment isolation valve, which met 10 CFR Part 50,
Appendix A, GDC 57, until a change was made in the UFSAR in Amendment 13. In
addition, this valve had previously been identified as a containment isolation valve
required to be operable in Unit 2 Technical Specification Table 3.6-1 (referenced by
Technical Specification 3.6.3.1) with an isolation time of <20 seconds on a CIAS. The
requirement that this valve be considered a containment isolation valve remained
identified in Technical Specification Table 3.6-1 until License Amendment 154 was
implemented.
The licensee requested and was granted approval in License Amendment 154 to
remove Technical Specification Table 3.6-1 and replace Technical Specification 3.6.3.1
with the following: "Each containment isolation valve shall be OPERABLE." This was
done in accordance with the guidance of Generic Letter 91-08, "Removal of Component
Lists from Technical Specifications." The SER for Amendment 154 states that "the
licensee confirmed that with the proposed changes, the new Technical Specifications
applied to all valves classified as containment isolation valves by the plant licensing
basis." The NRC staff found that the proposed changes to the Technical Specification
were primarily an administrative change that did not alter the requirements set forth in
the Technical Specifications. The NRC staff concluded that the changes would allow
the licensee to make corrections and updates to the list of components for which the
Technical Specification requirements applied, under the provision that these changes to
plant procedures be controlled as specified in the Administrative Controls Section of the
Technical Specifications. The SER also states that the Technical Specification Bases
were amended to include reference to a new list of containment isolation valves that
would be included in Procedure 2203.005, "Loss of Containment Integrity," and that the
new list would be subject to the administrative control requirements of the Technical
Specifications and 10 CFR 50.59. The inspectors noted that the new list of containment
isolation valves was actually included in Procedure 1015.034, "Containment Penetration
Administrative Control," Revision 0.
During review of NRC Generic Letter 91-08, the inspectors noted that the generic letter
states that "Generally, the UFSAR identifies those valves that are classified as
containment isolation valves. With this Technical Specification change, the limiting
condition for operation (LCO), remedial actions, and surveillance requirements will apply
for all valves that are classified as containment isolation valves by the plant licensing
basis." The inspectors noted that Valve 2CV-5859-2 was identified as a GDC 57
containment isolation valve in the Unit 2 UFSAR, Table 6.2-26, "Containment
Penetrations," and in Procedure 1015.034 at the time when License Amendment 154
was approved and incorporated into the Unit 2 Technical Specifications.
Description of Change to the UFSAR
During review of their containment penetrations, the licensee had identified that the
licensing documents that specified containment isolation valves were not consistent and
determined that this was caused by various personnel incorrectly interpreting the
definition of the containment boundary. In 1995 and 1996, Procedure 1015.034,
"Containment Penetration Administrative Control," Revision 0, and Unit 2 UFSAR,
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Table 6.2-26, were changed with Licensing Document Change Request 2-6-2-002 for
UFSAR, Amendment 13. In this amendment, note 9 was added and the applicability of
GDC 57 was deleted for 38 valves associated with the following Unit 2 secondary
system containment penetrations:
Containment Penetration 2P1
Main Steam from S/G 2E24A - MSIS
Containment Penetration 2P2
Main Steam from S/G 2E24B - MSIS
Containment Penetration 2P3
Feedwater to S/G 2E 24A - MSIS
Containment Penetration 2P4
Feedwater to S/G 2E 24B - MSIS
Containment Penetration 2P7
S/G 2E24A Sample - CIAS
Containment Penetration 2P7
S/G 2E24B Sample - CIAS
Containment Penetration 2P32
S/G 2E24A Blow down - MSIS
Containment Penetration 2P35
Containment Penetration 2P64
S/G 2E4B Blow down - MSIS
Containment Penetration 2P65
Note 9 stated "These penetrations are associated with the secondary side of the steam
generators and are not subject to GDC 57 since the containment barrier integrity is not
breached during DBA LOCA conditions. The containment boundary or barrier against
fission product leakage to the environment is the inside surface of the steam generator
tubes, the outer surface of the lines emanating from the steam generator, and the outer
surface of the steam generator above the bottom tube sheets. Valves associated with
these penetrations are not containment isolation valves."
During discussions with the licensees staff, the inspectors were informed that this
treatment of the secondary system as part of the containment boundary had always
been the licensee's view of containment and that historical inconsistencies in the
designation of secondary system containment valves could be explained, if this was
understood. They also noted that their view was consistent with a 1972 Westinghouse
document describing the containment boundary. See Attachment 2 for additional details
regarding the licensee's perspective. The inspectors could not identify that the 1972
Westinghouse document was ever referenced in any licensing correspondence with the
NRC that was applicable to Unit 2. The inspectors were also not able to find where the
NRC staff had reviewed and accepted this alternative view of the containment boundary.
Screening Review
Approval for UFSAR, Amendment 13, was based on Engineering Report 93-R-0007-01,
"Containment Penetration Design Summary Document," Revision 0. The inspectors
reviewed Engineering Report 93-R-0007-01 and the associated 10 CFR 50.59 screening
review. The following note was included in the Basis for Change for all of the secondary
system containment penetration valves:
"ADMINISTRATIVE/EDITORIAL - Information is confusing in that it leaves the
impression that these valves are Reactor Building Isolation valves when they are not.
Deletion is consistent with note 9" (Unit 2 UFSAR, Table 6.2-26).
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Because the changes made for all of the secondary system containment penetration
valves were viewed as administrative/editorial, these changes met the licensees criteria
for changes specifically exempted from further 10 CFR 50.59 evaluation. This decision
was in accordance with Procedure 1000.131, "10 CFR 50.59 Review Program,"
Attachment 1, which was, at that time, the licensees procedure governing
10 CFR 50.59 determinations/evaluations.
The inspectors reviewed containment descriptions in other sections of the initial
FSAR and the NRC Safety Evaluation Report and did not find that the licensees view of
containment had been previously documented. The inspectors determined that the
change in definition of containment was not an administrative/editorial change because
changes in the potential for increased fission product release during a steam generator
tube rupture accident or other postulated accidents were not evaluated.
While the inspectors acknowledged that the original licensing basis for the containment
boundary was in some cases silent and sometimes inconsistent, the inspectors noted
the Unit 2 FSAR and amendments documented in NUREG-0308 included FSAR,
Table 6.2-26, Amendment 23, which identified all the above secondary system Unit 2
containment penetrations and listed all of the secondary system valves as being
GDC 57 containment isolation valves.
Based on the historical review, the inspectors concluded that on March 31, 1995, the
licensee performed an inadequate 10 CFR 50.59 screening review documented in
Evaluation FFN-95-166, which was approved by the Plant Safety Review Committee on
August 31, 1995, for proposed changes to the Unit 2 UFSAR. As a result of this
inadequate screening, the licensee had not performed a required safety evaluation.
10 CFR 50.59 was changed via publication in the "Federal Register" on October 4, 1999
(64 FR 53582). It is NRC policy to exercise enforcement discretion pursuant to
Section VII.B.6 of the Enforcement Policy and not issue citations or document noncited
violations against the old rule if the revised rule requirements were met.
Safety Evaluation Using the Revised Rule
At the inspectors' request, the licensee performed a safety evaluation of the change
using criteria of the revised 10 CFR 50.59 rule for the Unit 2 Steam Generator B sample
valve.
The licensee identified that the change would result in a very small increase in the
consequences of an accident previously evaluated. The inspectors reviewed the
guidance in Regulatory Guide 1.187, "Guidance for Implementation of 10 CFR 50.59,
Changes, Tests, and Experiments," and in NEI 96-07, "Guidelines for 10 CFR 50.59
Implementation," Revision 1, Section 4.3.3, and concluded that this increase in
consequences would be minimal and, therefore, did not require NRC review for that
reason.
The licensee did not identify that the change resulted in a small increase in the
probability of occurrence of a malfunction of equipment important to safety previously
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evaluated in the Safety Analysis Report, which should have received the NRCs approval
prior to implementation. Using the guidance in NEI 96-07, Revision 1, Section 4.3.2, by
definition, departure from GDC 57 results in more than a minimal increase in the
likelihood of occurrence of a malfunction of a component important to safety. In
addition, the probability of malfunction did increase when Valve 2CV-5859-2 was
de-energized in the open position for 26 days (December 21, 2001, through January 16,
2002).
(3)
Analysis
This finding is not suitable for evaluation using the Significance Determination
Process (SDP). The finding is determined by management to be of very low safety
significance. The inspectors reviewed an analysis performed by the licensee and found
that the expected increase in consequences will meet the minimal standard described in
NEI 96-07, Revision 1, Section 4.3.3. This finding is more than minor because the
change should have received NRCs review prior to implementation.
(4)
Enforcement
The inspectors evaluated the change in the UFSAR documented description of
containment, the change in the UFSAR list of containment isolation valves, and the
change in Procedure 1015.034 for compliance with 10 CFR 50.59. At the time that the
10 CFR 50.59 screening was performed in 1995, the rule required the licensee maintain
records of changes in procedures described in the Safety Analysis Report and these
records include a written safety evaluation which provides the basis for the
determination that the change does not involve an unreviewed safety question. The
licensee had not initially performed a safety evaluation for the change in the UFSAR
documented containment description, for the deletion of multiple valves from the UFSAR
list of containment isolation valves, and for the resultant deletion of Technical
Specification applicability for these containment isolation valves in Procedure 1015.034.
The failure to perform the safety evaluation was a violation of 10 CFR 50.59.
Under the previous 10 CFR 50.59 rule, the inadequate screening evaluation resulted in
the licensee not identifying that the change would result in a small increase in the
consequences of an accident previously evaluated and a small increase in the
probability of occurrence of a malfunction of equipment important to safety previously
evaluated in the Safety Analysis Report. This constituted an unreviewed safety question
which should have received NRC approval prior to implementation.
To evaluate conformance with the revised 10 CFR 50.59 rule, the inspectors reviewed
the change in the UFSAR documented containment description, the deletion of multiple
valves from the UFSAR list of containment isolation valves, and the resultant deletion of
the Technical Specification applicability for these containment isolation valves in
Procedure 1015.034 against the requirements of the new rule, using the guidance in
Regulatory Guide 1.187, and NEI 96-07, Revision 1.
Under the revised rule, the increase in consequences was minimal. However, departure
from GDC 57 does result in more than a minimal increase in the likelihood of occurrence
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of a malfunction of a component important to safety. Specifically, the probability of
malfunction increased more than minimally when Unit 2 Steam Generator B Sample
Valve 2CV-5859-2 was de-energized in the open position for 26 days (December 21,
2001, through January 16, 2002). Based on these findings, the inspectors concluded
that a license amendment was also required by the revised rule.
Therefore, the NRC will not exercise enforcement discretion pursuant to Section VII.B.6
of the Enforcement Policy for the 1995 failure to perform a safety evaluation as required
by 10 CFR 50.59.
The violation is not suitable for SDP evaluation, but has been reviewed by NRC
management and is determined to be a Green finding of very low significance. The
licensee entered this finding into its corrective action program as Condition
Report ANO-2003-0242. This violation is being treated as an example of a noncited
violation (50-313/0302-01; 50-368/0302-01) consistent with Section VI.A of the
.2
Unit 1 Containment Isolation Valve Designation Change
a.
Inspection Scope
During the inspectors review of the Unit 2 issue of deletion of GDC 57 requirements
from certain Unit 2 containment isolation valves, the inspectors also found that multiple
secondary system reactor building penetration valves which were previously identified
as GDC 57 reactor building isolation valves were removed from the Unit 1 UFSAR in the
same manner. The inspectors reviewed Engineering Report 93-R-0007-01, its
associated 10 CFR 50.59 determination, and the Unit 1 UFSAR, Table 5-1, to determine
if the licensee had appropriately performed these reviews.
b.
Findings
(1)
Introduction
The inspectors found that Engineering Report 93-R-007-01 and the associated
10 CFR 50.59 determination was used for changes to both the Units 1 and 2 UFSARs
and containment penetration administrative control procedures. Therefore, the issue of
the licensees departure from GDC 57 applicability for the steam generator secondary
side reactor building/containment building penetration valves (which were previously
identified as GDC 57 valves) from the Units 1 and 2 UFSARs and the Units 1 and 2
Technical Specification requirements as implemented by the respective Unit 1 and 2
containment penetration control procedures, is applicable to both Units 1 and 2.
As a result of an inadequate 10 CFR 50.59 screening, the licensee failed to perform a
safety evaluation for:
Changing the description of containment documented in the Unit 1 UFSAR
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Changing the description of GDC 57 applicability documented in the Unit 1
Several secondary system containment penetration valves were included in these
changes. The failure to perform a safety evaluation for these changes to the Unit 1
UFSAR was determined to be an example of a violation of 10 CFR 50.59.
(2)
Description
Background
As part of the inspectors' review for the Unit 1 issue, the inspectors found that a
previous violation had been cited for Unit 1 concerning the failure to lock closed two
reactor building isolation valves between the feedwater isolation valves and the
containment in accordance with Technical Specification 3.6.5. This violation was
documented in 1994 in NRC Inspection Report 50-313/94-07; 50-368/94-07. The
subject valves were secondary system reactor building penetration feedwater line vent
and drain Valves FW-1038 and FW-1049. They are located in secondary system
penetrations that were affected by the licensee's UFSAR change. The inspectors
reviewed the licensee response and corrective actions associated with the violation to
understand the licensee's interpretation of the definition of containment at that time, just
prior to the deletion of GDC 57 applicability for secondary system penetrations.
In the licensee response to the violation, dated December 16, 1994, the licensee stated:
"The identified concern is that main feedwater vent valves FW-1038 and FW-1049 were
not being maintained as locked valves. Implied in the violation is that General Design
Criterion (GDC) 57, Closed System Isolation Valves, is applicable to the manual test
connection, vent and drain valves located at the given penetrations. GDC 57 requires
manual containment isolation valves be closed and locked to maintain containment
integrity. Locking the test connection, vent and drain valves represents a level of
administrative control not previously considered to be required for these and other test
connection, vent or drain valves.
"The general design basis governing containment building isolation requirements is
leakage through all fluid penetrations, not serving accident-consequence limiting
systems, must be minimized by a double barrier so that no single, credible failure or
malfunction of an active component can result in loss of isolation or intolerable leakage.
The installed double barriers take the form of closed piping systems, both inside and
outside the containment building, and various types of isolation valves.
"Based on ANOs licensing basis and NRC regulations, no specific requirement to lock
these valves previously existed. Industry guidance indicates that test connection, vent
and drain valves should not be classified as GDC isolation valves, but as
administratively con trolled containment system barriers. ANO has procedurally
controlled these valves to ensure they are closed during power operations.
-12-
"The general design basis governing containment isolation requirements is given in
Section 5.2.5 of the current Arkansas Nuclear One- Unit 1 (ANO-1) Safety Analysis
Report. The ANO-1 Safety Analysis Report Table 5.1, Reactor Building Isolation
Valves, lists GDC 55, 56, and 57 penetrations and the applicable containment isolation
valves. There are no test connection, vent and drain valves identified in the table. The
definition of ANSI/ANS-56.2-1984, Containment Isolation Provisions for Fluid Systems,
clearly distinguish between containment isolation valves and the containment
penetration test connection, vent and drain valves by defining test connections or vents
as being provided so that containment isolation valves can be tested. Figures 1 and 2
of ANSI/ANS-56.2-1984 demonstrate the criteria for GDC 55, 56, and 57 and includes
only the main process line valves (main feedwater block valves for P-3 and P-4), and do
not demonstrate provision for test connection, vent or drain valves."
In Section 6.2.3 of the ANO-1 Safety Evaluation Report (SER), it states, in part, "the
reactor building isolation system is designed to isolate the containment atmosphere from
the outside environment under accident conditions. Double barrier protection, in the
form of closed systems and isolation valves, is provided so that no single valve or piping
failure can result loss of containment integrity." The SER further states that "the NRC
staff has reviewed the containment isolation system for conformance to GDC 55, 56,
and 57." The NRC concluded that, the containment isolation system meets the intent of
the general design criteria. From the Final Safety Analysis Report (FSAR) description of
the containment building isolation system it is evident that only the process line valves
were included as containment building isolation valves. Test connection, vent and drain
valves on these penetrations are neither depicted nor described."
The inspectors noted that the process valves that the licensee discussed in their
response to the violation are some of the valves for which the licensee now has deleted
GDC 57 applicability.
The inspectors also found during the review that, during the initial licensing process for
Unit 1, the Commission Staffs Request for Additional Information 5.83 requested
information regarding compliance with GDC 57 for the Unit 1 main feedwater lines to
each steam generator and was specifically evaluated by the Commissions Staff to
determine if the piping configuration used complied with GDC 57. In addition, Request
for Additional Information 10.1 for Unit 1 requested information concerning the turbine
stop valves serving as containment isolation valves for isolation of the unaffected steam
generator in the event of a steamline rupture accident. The licensee responded to
Question 10.1 that the main steam block valves, not the turbine stop valves, were
designed to serve as the containment isolation valves and that these valves met
Criterion 57 of 10 CFR Part 50, Appendix A. The staff also requested information
regarding how the licensee was implementing GDC 57 for penetrations containing the
steam generator sample valves for Unit 1.
-13-
Description of Change to the Unit 1 UFSAR
During review of this issue, the inspectors questioned the licensee concerning the
licensing basis for the Unit 1 steam generator secondary side reactor building
penetrations and the subsequent deletion of the GDC applicability for the following
Containment Penetration P1
Main Steam from Steam Generator E-24A to EFW
and Main Turbine
Containment Penetration P2
Main Steam from Steam Generator E-24B to EFW
and Main Turbine
Containment Penetration P3
Main Feedwater to Steam Generator E24-A
Containment Penetration P4
Main Feedwater to Steam Generator E-24B
Containment Penetration P10
Steam Generator Sampling
Containment Penetration P17
EFW to Steam Generator E-24A
Containment Penetration P65
EFW to Steam Generator E-24B
Based on the inspectors questions, the licensee performed a review of the Unit 1
design and licensing bases and developed a position paper, which is Attachment 2 to
this inspection report. In the licensees position paper, the licensee stated "The
containment boundary or barrier against fission product leakage to the environment is
the inside surface of the steam generator tubes, the outer surface of the lines
emanating from the steam generator, and the outer surface of the steam generator
between the tube sheets. This position is based on the concept of treating the
secondary system pressure boundary as an extension of the containment liner." The
licensee further stated that, although this position was not well documented, this position
has always been the understanding of plant personnel familiar with the original design
and licensing basis. The licensee further stated that this concept was based on
Westinghouse Document WCAP-7451, dated September 1972. The inspectors could
not identify that this document describing the containment boundary was ever
referenced in any licensing correspondence with the Commission that was applicable to
Unit 1.
The licensee stated that, ultimately, the concept of the secondary pressure boundary
being an extension of containment boundary was explicitly approved by the NRC in the
Safety Evaluation Report approving renewal of the Unit 1 operating license. This was
based on the NRC's Request for Additional Information 2.3.2.7-2.
The Request for Additional Information stated "In P&ID LRA-M-237, Sheet 1, the
redundant isolation valves (SS-1017B and SS-1018B) for the test connections of the
sampling system are not highlighted as being within the scope of license renewal.
However, containment isolation provisions require double isolation at the test
-14-
connections for greater assurance of containment integrity. Provide a justification as to
why the second isolation valve on each test connection is not in-scope." The licensees
response, dated August 30, 2000, stated "Please see ANO-1 Safety Analysis Report,
Table 5-1, Penetration 10, and note 8. This penetration is associated with the
secondary side of the steam generator and is not subject to GDC 57. In accordance
with the current licensing basis, the containment boundary or barrier against fission
leakage to the environment is the inside surface of the steam generator tubes, the outer
surface of the lines emanating from the steam generator, and the outer surface of the
steam generator between the tube sheets. Therefore, Valves SS-1017B and SS-1018B
do not meet the scoping criteria for license renewal."
The NRC found the licensees response acceptable. However, the inspectors noted that
the GDC 57 applicability for the secondary system penetrations had already been
deleted without prior Commission approval with the administrative change that is the
subject of this violation for the change to UFSAR, Table 5-1.
Based on the inspectors review, the inspectors concluded that on March 31, 1995, the
licensee performed an inadequate 10 CFR 50.59 screening and, as a result, the
licensee had not performed a safety evaluation as required by 10 CFR 50.59.
Screening Review for Unit 1 changes
Approval for UFSAR, Amendment 14, was based on Engineering Report 93-R-0007-01,
"Containment Penetration Design Summary Document," Revision 0. As stated in the
previous section of this inspection report, the inspectors reviewed Engineering
Report 93-R-0007-01 and the associated 10 CFR 50.59 screening review. The following
note was included in the Basis for Change for all of the secondary system containment
penetration valves:
"ADMINISTRATIVE/EDITORIAL - Information is confusing in that it leaves the
impression that these valves are Reactor Building Isolation valves when they are not.
Deletion is consistent with note 8" (Unit 1 UFSAR, Table 5-1).
Because the changes made for all of the secondary system containment penetration
valves were viewed as administrative/editorial, these changes met the licensees criteria
for changes specifically exempted from further 10 CFR 50.59 evaluation. This decision
was in accordance with Procedure 1000.131, Attachment 1, which was, at that time, the
licensees procedure governing 10 CFR 50.59 determinations/evaluations.
The inspectors determined that the change in definition of containment was not an
administrative change because changes in the potential for increased fission product
release during a steam generator tube rupture accident or other postulated accidents
were not evaluated.
-15-
(3)
Analysis
This finding is not suitable for evaluation using the SDP. The finding is determined by
management to be of very low safety significance. This finding is more than minor,
because the change should have received NRCs review prior to implementation.
(4)
Enforcement
The inspectors evaluated the change in the UFSAR documented description of
containment and the change in the updated UFSAR list of containment isolation valves.
At the time that the 10 CFR 50.59 screening was performed in 1995, the licensee did
not perform a safety evaluation for the change in the UFSAR documented containment
description or for the deletion of multiple valves from the UFSAR list of containment
isolation valves and resultant deletion of Technical Specification applicability for these
containment isolation valves. The failure to perform a safety evaluation was a violation
of 10 CFR 50.59.
Under the previous 10 CFR 50.59 rule, an inadequate screening evaluation resulted in
the licensee not identifying whether the change would result in an increase in the
consequences of an accident previously evaluated or whether there was an increase in
the probability of occurrence of a malfunction of equipment important to safety
previously evaluated in the Safety Analysis Report change should have received NRC
approval prior to implementation, because the change constituted an unreviewed safety
question.
To evaluate conformance with the current 10 CFR 50.59 rule, the inspectors reviewed
the change in the UFSAR documented containment description, deletion of multiple
valves from the UFSAR list of containment isolation valves, and the resultant deletion of
the Technical Specification applicability for these containment isolation valves against
the requirements of the new rule, using the guidance in Regulatory Guide 1.187 and
NEI 96-07, Revision 1.
An evaluation under the new rule was not performed by the licensee. However,
departure from GDC 57 does result in more than a minimal increase in the likelihood of
occurrence of a malfunction of a component important to safety. Based on these
findings, the inspectors concluded that a license amendment was also required by the
current 10 CFR 50.59 rule.
Therefore, NRC will not exercise enforcement discretion pursuant to Section VII.B.6 of
the Enforcement Policy for the 1995 failure to perform a safety evaluation as required by
The violation is not suitable for SDP evaluation, but has been reviewed by NRC
management and is determined to be a Green finding of very low significance. The
licensee entered this finding into its corrective action program as Condition
Report (CR) ANO-C-2003-0242. This violation is being treated as an example of a
noncited violation (50-313/0302-01; 50-368/0302-01) consistent with Section VI.A of the
-16-
1R04
Equipment Alignment
.1
Partial System Walkdown (71111.04)
a.
Inspection Scope
The inspectors performed a partial system walkdown of the Unit 2 service water system
while maintenance was being performed on Pump 2P-4C on February 3-5, 2003. The
inspectors verified proper component alignment and operation in accordance with
Procedure 2104.029, "Service Water System Operations," Revision 53, and system
piping and instrumentation diagrams to verify that the system was in a proper standby
lineup. The inspectors also examined component material condition.
The inspectors performed a partial system walkdown of the Unit 1 service water system
while maintenance was being performed on Pump P-4A on February 18-20, 2003. The
inspectors verified proper component alignment and operation in accordance with
Procedure 1104.029, "Service Water and Auxiliary Cooling System," Revision 55, and
system piping and instrumentation diagrams to verify that the system was in a proper
standby lineup. The inspectors also examined component material condition.
The inspectors performed a partial system walkdown of the Unit 2 vital dc electrical
system during maintenance on Battery 2D-12 on March 14-15, 2003. The inspectors
verified proper system alignment and operation in accordance with Procedure 2107.004,
"DC Electrical System Operation," Revision 20, to verify that the system was in a proper
standby lineup.
b.
Findings
No findings of significance were identified
1R05
Fire Protection
.1
Routine Inspection (71111.05Q)
a.
Inspection Scope
The inspectors referenced the Fire Hazards Analysis Report, Revision 7, during the
following inspections to ensure that conditions were consistent with the requirements of
the licensees fire protection program for fire protection systems design, control of
transient combustibles and ignition sources, fire detection and suppression capability,
fire barriers, and any related compensatory measures. Additional documents reviewed
included Procedure 2203.014, "Alternate Shutdown," Revision 14; Technical
Guideline 2203.014, "Alternate Shutdown," Revision 14; "ANO Pre-Fire Plan,"
Revision 1; Procedure 1000.047, "Control of Combustibles," Revision 15;
Procedure 2203.034, "Fire or Explosion," Revision 5; and CR ANO-2-2003-0229.
Unit 2 Battery Room 2D11, Fire Zone 2103V, conducted on February 21, 2003
-17-
Unit 1 Switchgear Room A3, Fire Zone 99M, conducted on February 19-21, 2003
Unit 1 Cable Spreading Room, Fire Zone 97R, conducted on March 5-7, 2003
Unit 1 Integrated Control System Relay Room, Fire Zone 97R on March 5-7,
2003
Unit 1 North Battery Room, Fire Zone 95-O, on March 5-7, 2003
Unit 2 Battery Room 2D12, Fire Zone 2102Y, conducted on March 11-13, 2003
Unit 2 Core Protection Calculator Room, Fire Zone 2098C, conducted on
February 10, 2003
b.
Findings
No findings of significance were identified.
1R13
Maintenance Risk Assessments and Emergent Work Control (71111.13)
a.
Inspection Scope
The inspectors evaluated and discussed with the licensee the risk assessments listed
below to verify that assessments were performed when required and appropriate
compensatory actions were taken. The inspectors reviewed these assessed risk
configurations against actual plant conditions and any inprogress evolutions or external
events to verify that the assessments were accurate, complete, and appropriate for the
conditions. In addition, the inspectors walked down the control room and plant areas to
verify that compensatory measures identified by the risk assessments were
appropriately performed.
Unit 1 Emergency Diesel Generator K4B risk assessment associated with the
system outage conducted on January 17, 2003
Unit 1 Emergency Diesel Generator K4A risk assessment associated with the
system outage conducted on January 21-22, 2003
Unit 2 Service Water Pump 2P-4C electrical power supply cable replacement
conducted on February 3-4, 2003
Unit 1 Service Water Pump P-4A electrical power supply cable replacement
conducted on February 17-20, 2003
Unit 2 Battery Cell 2D12 replacement and testing conducted January 10, 2003
Unit 2 Battery Cell 2D12 replacement and testing conducted March 14-16, 2003
-18-
Unit 1 Emergency Diesel Generator K4A maintenance activities conducted on
February 14-19, 2003
b.
Findings
No findings of significance were identified.
1R14
Personnel Performance Related to Nonroutine Plant Evolutions and
a.
Inspection Scope
The inspectors observed the following nonroutine evolutions to verify that they were
conducted in accordance with licensee procedures and Technical Specification
requirements:
On February 2, 2003, Unit 2 experienced a failure of the operating Loop 2 Service
Water Pump 2P-4C. Operators entered Abnormal Operating Procedure 2203.022,
"Loss of Service Water," Revision 8, and promptly started Standby Service Water
Pump 2P-4B to provide service water to Loop 2. The licensee initiated
CR ANO-2-2003-0178 to document the event and corrective actions. As part of an
extent of condition review, the licensee also initiated CR ANO-C-2003-0067 to review
the condition of medium-voltage underground cables at the facility. From this review,
the licensee identified that the cables for Unit 1 Service Water Pump P-4A should be
replaced as a prudent measure. The cables for Pump P-4A were replaced during the
week of February 17, 2003.
b.
Findings
No findings of significance were identified.
1R15
Operability Evaluations (71111.15)
a.
Inspection Scope
The inspectors reviewed operability determinations to assess the correctness of
evaluations, the use of compensatory measures, if needed, and compliance with the
Technical Specifications. The inspectors' review included a verification that operability
determinations were made as specified by the licensee's Procedure LI-102, "Corrective
Action Process," Revision 2, and Procedure 1000.104, "Condition Reporting and
Immediate Reportability Determinations," Revision 17. The technical adequacy of the
determinations was reviewed and compared to the Technical Specifications, Technical
Requirements Manual, UFSAR, and associated licensing-basis documentation, as
appropriate. The operability determinations that were reviewed were documented in the
following CRs:
ANO-C-2003-00067
Service water pump power supply cable evaluation
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ANO-2-2002-00644
Installation of temporary alteration for installation of
heaters to supplement local heating due to Battery
Room 2D11 temperature below 65°F
ANO-2-2003-00237
Various abnormal indications and alarms which occurred
at roughly the same time on Unit 2
ANO-2-2003-00383
Failed support rod from Hanger 2EBD-15-H2 which
provides support from main steam header to stop
Valve 2CV-0250
ANO-1-2003-00225
EDG K-4A fuel oil sight glass leakdown problem
ANO-1-2003-00193
Air entrained in the EDG 1 fuel oil return system
ANO-2-2002-02084
Low voltage on Unit 2 Battery 2D12 Cell 40
ANO-2-2003-00412
Low voltage on Unit 2 Battery 2D12 Cell 40
ANO-2-2003-00193
Unit 2 low spent fuel pool temperature
ANO-1-2003-00378
Emergency Feedwater Valve SV-2613 nameplate and
documentation errors
b.
Findings
No findings of significance were identified.
1R17
Permanent Plant Modifications
.1
Annual Review (71111.17A)
a.
Inspection Scope
The inspectors reviewed the plant modification described in Engineering
Request (ER) ANO-2000-2688-002, "Uprate L-3 Spent Fuel Crane to Handle
Capacity of 122 Tons." This modification replaced the previous Crane L-3
nonsingle-failure proof trolley, rated at 100 tons, with a new trolley of single-failure
proof design rated at 130 tons. This modification was necessary to allow the licensee to
lift spent fuel storage casks of a new, heavier design. The review included the safety
evaluation prepared to determine if the modification required a license amendment per
the requirements of 10 CFR 50.59.
b.
Findings
The licensee's 10 CFR 50.59 evaluation concluded that the proposed modification did
not require a license amendment. The licensee concluded that the upgraded crane
design met the requirements of NUREG-0554, "Single-Failure-Proof Cranes for Nuclear
-20-
Power Plants," and NUREG-0612, "Control of Heavy Loads at Nuclear Power Plants."
Therefore, the licensee concluded that the upgraded crane design was acceptable for
implementation without the need for an NRC license amendment.
The inspectors disagreed with this conclusion. The inspectors acknowledged the new
crane was intended to meet single-failure-proof design standards and utilized a trolley
design documented in a vendor topical report that was previously approved by the NRC.
However, the inspectors noted that Generic Letter 85-11, "Completion of Phase II of
Control of Heavy Loads at Nuclear Power Plants NUREG-0612," identified that
installation of a single-failure-proof crane design may reasonably be expected to
eliminate most, perhaps 90 percent, of load drop probability, meaning the failure
probability was not zero. The inspectors concluded that the increase in the maximum
critical load rating of the crane (from 100-130 tons), combined with a required load path
that would carry a loaded spent fuel storage cask over the control rooms, would require
a license amendment.
The inspectors, managers from the NRC Region IV office, and representatives of the
NRC Office of Nuclear Reactor Regulation (NRR) informed the licensee of this
conclusion in a telephone call on February 13, 2003. The inspectors also informed the
licensee that failure to submit a license amendment request for this modification was a
potential violation of 10 CFR 50.59. The licensee entered this issue into its corrective
action program as CR ANO-C-2003-0092. The licensee subsequently submitted a
license amendment request for the Crane L-3 modification to the NRC on February 24,
2003. The license amendment request was still under review by the NRR staff at the
conclusion of the inspection period. Although a potential violation of 10 CFR 50.59 was
determined to exist, the inspectors considered this issue to be an unresolved item,
pending completion of review of the license amendment request by the NRR staff and a
determination of the significance of the violation (50-313/0302-02; 50-368/0302-02).
The upgraded crane had not been used to transport a loaded spent fuel storage cask
and was under administrative controls preventing its use in this manner, pending
resolution of this issue. Therefore, this issue had no immediate safety significance.
1R19
Postmaintenance Testing (71111.19)
a.
Inspection Scope
For the maintenance activities identified below, the inspectors observed the
postmaintenance testing activities in the control room or locally and/or reviewed the test
data obtained from the field. The inspectors observed whether the tests were
performed in accordance with procedures, acceptance criteria were consistent with
Technical Specifications, and the results recorded met the test acceptance criteria. In
addition, the inspectors verified that any deficiencies were recorded and resolved.
These activities included:
Unit 1 Emergency Diesel Generator 1 testing in accordance with
Procedure 1104.036, "Emergency diesel Generator Operation," Revision 41,
conducted on January 24, 2003
-21-
Unit 1 Emergency Diesel Generator 1 testing in accordance with
Procedure 1104.036, "Emergency Diesel Generator Operation," Revision 41,
conducted on February 19, 2003
Unit 2 2D12 battery testing for Cell 40 replacement conducted on March 10-15,
2003, as described in the maintenance action plan associated with
CR ANO-2-2003-0412
b.
Findings
No findings of significance were identified.
1R22
Surveillance Testing (71111.22)
a.
Inspection Scope
The inspectors observed from either the control room or locally the performance of
and/or reviewed the documentation for the following surveillance tests. This was done
to verify that the surveillance tests were performed in accordance with approved
licensee procedures and met Technical Specification requirements. In addition, the
applicable test data was also reviewed to verify whether they met Technical
Specifications, UFSAR, and licensee procedure requirements.
Procedure 2104.036, "2DG1 Monthly Test (Slow Start)," Supplement 1B,
Revision 46, performed on January 29, 2003
Procedure 2105.009, "CEA Exercise Test," Supplement 2, Revision 21,
performed on March 21, 2003
Procedure 2403.023, "2D12 Quarterly Surveillance," Revision 14, performed on
March 17, 2003
Procedure 2403.023, "2D12 Quarterly Surveillance," Revision 14, performed on
March 19, 2003
b.
Findings
No findings of significance were identified.
1R23
Temporary Plant Modifications (71111.23)
a.
Inspection Scope
On January 28-30, 2003, the inspectors reviewed the implementation of
Procedure 2106.032, "Unit 2 Freeze Protection Guide," Revision 9, Section 8, "Battery
Room Low Temperature." This procedurally controlled temporary alteration installed a
temporary portable 15 Kw electric heater in Unit 2 Corridor 2104 to provide
supplemental heating for the safety-related battery rooms in severe wintertime
-22-
conditions. The justification for the temporary non-Q battery room heating was
evaluated and documented in ER ANO 2002-0145-000. The inspectors confirmed that
this temporary alteration was properly installed as authorized by the procedure and the
ER.
On February 3-4, 2003, the inspectors reviewed the implementation of Maintenance
Action Item (MAI) 79434, which installed a temporary alteration evaluated by
ER ANO-2003-0098-00. This temporary alteration installed a temporary power supply to
the Unit 2 Service Water Pump 2P-4C motor while its permanent power supply cables
were being replaced. The inspectors confirmed that this temporary alteration was
implemented and installed as authorized by MAI 79434 and Procedure 1000.028,
"Control of Temporary Alterations," Revision 25.
On February 19-21, 2003, the inspectors observed that Fire Door 48 had been removed
in support of the power supply cable replacement for the Unit 1 Service Water
Pump P-4A motor. The door had been removed per the instructions of MAI 80036.
During the week of March 3, 2003, the inspectors reviewed this maintenance activity to
determine whether an unevaluated temporary alteration to the facility had been
performed.
b.
Findings
A Green noncited violation was identified for performing a maintenance activity that
resulted in the implementation of an unevaluated temporary alteration. Removal of
Door 48 was not evaluated for its impact on safety-related equipment following a
potential high energy line break or for its impact on room cooling capability performance.
Door 48 is a 3-hour rated fire door separating safety-related switchgear Room A3 from
the turbine building. Located outside switchgear Room A3 are two high-pressure
feedwater heaters. The inspectors reviewed the Unit 1 UFSAR, "An Evaluation of Pipe
Breaks Outside the Reactor Building," Section A.7, Amendment 17, and noted that the
main feedwater pipe break analysis stated that steam and water from a postulated
feedwater pipe break are prevented by walls from entering into the switchgear rooms.
The inspectors concluded that this statement implied that doors in the subject walls
were also credited as barriers. The inspectors also reviewed Procedure 1104.027,
"Battery and Switchgear Emergency Cooling System," Revision 20. This procedure
identified that the emergency cooling system was designed to limit maximum room
temperature to 104°F in switchgear Room A3 with turbine building ambient air
temperatures at 122°F. The inspectors also reviewed the component database for
Door 48 and found that this door was not identified as having a design function as a
high-energy line break barrier or room temperature maintenance barrier.
Door 48 was removed per MAI 80036 on February 17, 2003, in order to support cable
replacement activities for Service Water Pump P-4A and was returned to service on
February 20, 2003. The MAI did not include an engineering evaluation for the
acceptability of removal of Door 48 nor was there one performed.
-23-
The inspector concluded that removal of Door 48 resulted in a change to the design
function of the barrier separating switchgear Room A3 and the turbine building and was
a temporary alteration. Procedure 1000.028, "Control of Temporary Alterations,"
Revision 23, requires that all temporary alterations receive an engineering review
documented in an ER.
The licensee entered this issue into its corrective action program as
CR ANO-1-2003-0258. Per UFSAR, Section A.7.3, a postulated main feedwater pipe
break outside of Door 48 was a credible event. With Door 48 removed, the resultant
harsh environment from a break would have potentially incapacitated one of the
redundant trains of equipment necessary to achieve safe shutdown conditions.
However, the remaining train of equipment would have remained unaffected. The
condition did not result in equipment being inoperable because equipment in switchgear
Room A3 was capable of performing its intended function during a design basis event
(e.g., a loss-of-coolant accident) during the time Door 48 was removed.
As part of its corrective action for this finding, the licensee surveyed all doors that
separate the turbine building from safety-related equipment areas. All doors that were
discovered to also have a design function to provide a high energy line break barrier
were identified and were provided administrative controls requiring an engineering
evaluation prior to their removal.
Unit 1 Technical Specification 5.4.1.a requires that written procedures shall be
established, implemented, and maintained, covering activities identified in Regulatory
Guide 1.33, Revision 2, Appendix A, which includes modification work.
Procedure 1000.028 required an engineering evaluation be performed to support a
temporary alteration. Failure to perform an engineering evaluation for removal of
Door 48 was a violation. The safety significance of removal of Door 48 was determined
to be very low since this issue screened as Green during a Phase 1 SDP evaluation.
The issue was considered more than minor because it affected the mitigating systems
cornerstone objective for design control and modifications, because the ability to
mitigate the consequences of a high energy line break would have been affected if the
finding had affected more than one train of equipment. This violation is being treated as
noncited violation, consistent with Section VI.A of the NRC Enforcement Policy
(NCV 50-313/0302-03).
Cornerstone: Emergency Preparedness
1EP4
Emergency Action Level and Emergency Plan Changes (71114.04)
a.
Inspection Scope
The inspectors performed an in-office review of Revision 27 to the Arkansas Nuclear
One Emergency Response Plan, received January 25, 2002, and Procedure 1903.010,
"Emergency Action Level Classification," Revision 37. The inspector compared the
current revisions with their previous revisions and 10 CFR 50.54(q) to determine if the
current revision decreased the effectiveness of the emergency plan.
-24-
b.
Findings
No findings of significance were identified.
2.
Radiation Safety
Cornerstone: Occupational Radiation Safety
2OS2 ALARA Planning and Controls (71121.02)
a.
Inspection Scope
The inspectors reviewed radiation work permits (RWPs) from Refueling Outages 2R15
and 1R17 that both accrued more than 5 rem and that had actual doses that exceeded
the initial work activity dose estimates by more than 50 percent. No high exposure jobs
or work activities in high radiation areas were performed during the inspection; however,
the inspectors observed the movement of Cooling Coil VUC1B (in accordance with
RWP 2003-1040) and the replacement of Spent Fuel Filter F4 (in accordance with
RWP 2003-1017). During the work activities, the inspectors made independent
radiation measurements and observed ALARA practices and contamination control
practices. The following specific items were reviewed and compared with regulatory
requirements:
Plant collective exposure history for the past 3 years, current exposure trends,
and 3-year rolling average dose information
ALARA program procedures
RWP 2002-1420, "Scaffolding and Insulation Activities During 1R17";
RWP 2002-1452 and RWP 2002-1515, "Reactor Head CRD Nozzle Inspection";
RWP 2002-2442, "Steam Generator Inspection and Maintenance"; and
RWP 2002-2507, "Pressurizer Heater Repair"
Radiological work planning
Use of engineering controls to achieve dose reductions
Processes used to estimate and track exposures
Selected corrective action documentation involving higher than planned
exposure levels and radiation worker practice deficiencies since the last
inspection in this area (CRs ANO-C-2001-00297, ANO-2-2002-00882,
ANO-C-2003-00034, and ANO-C-2003-00118)
b.
Findings
Introduction: The inspectors identified a Green noncited violation because the licensee
failed to provide an adequate reason for revising RWPs, as required by a Technical
Specification required procedure.
-25-
Description: During a review of RWP packages, the inspectors noted multiple examples
of the licensee adjusting work activity dose estimates without providing adequate bases.
The dose estimates were adjusted to account for failures to control work activity doses
and failed to implement additional means to control dose.
For example, RWP 2002-1420, "Scaffolding and Insulation Activities During 1R17,"
Revision 4, increased the work activity dose estimate from 15.578-16.578 rem. The
documented reason stated, "The dose estimate would have been exceeded in the next
shift. Additional dose was added to complete work." The licensee provided no other
justification for the work activity dose estimate adjustment. RWP 2002-1452,
Revision 2, increased the work activity dose estimate from 4.2-7.9 rem. The
documented reason stated, "Made corrections to EAD setpoints in the special instruction
to match the ERIMS trigger on the RWP." While this was a legitimate reason for a RWP
revision, it did not address the basis for the adjustment of the work activity dose
estimate. In the most significant example with regard to actual dose exceeding the
legitimate work activity estimate, RWP 2002-2507, Revision 2, increased the work
activity dose estimate from 4.6-6.893 rem. The reasons cited for the revision were:
(1) vendor equipment did not machine correctly, (2) workers were less efficient because
of heat stress conditions, and (3) mockup facilities used for training were inconsistent
with actual plant components. RWP 2002-2507, Revision 3, increased the work activity
dose estimate from 6.893-7.0 rem. The reasons cited for the revision were: (1) the
current projection was insufficient to cover the work on two remaining mechanical nozzle
sealing assembly clamps and (2) additional management was in the field to provide
oversight for inexperienced workers.
With respect to RWP 2002-2507, the inspectors found that equipment ineffectiveness
was a legitimate reason in some cases for revising dose estimates. However, the
licensee had previously cited equipment ineffectiveness as a basis for Revision 1 of the
RWP, in which the work activity dose estimate was increased from 3.660-4.600 rem. No
additional justification was provided to support the use of equipment ineffectiveness a
second time to justify an increase to the dose estimate. Licensee representatives stated
that similar environmental conditions existed in previous refueling outages. Therefore,
containment environmental conditions should have been anticipated. The inconsistent
mockup facility resulted from plant drawing discrepancies and, according to licensee
personnel, was not a recent development. Therefore, the licensee had sufficient
opportunity to identify and correct the situation before the refueling outage. The
inspectors determined through interviews with licensee personnel that the work on all
mechanical nozzle sealing assembly clamps was considered in the original dose
estimate and the number of clamps did not increase. The use of inexperienced workers
did not begin at this stage of the work and should have been considered from the start
and addressed through additional training. The inspectors, after consultation with NRR,
concluded that the bases for the work activity dose estimate adjustments in
RWP 2002-2507, Revisions 2 and 3, were invalid because there were inadequate
justifications for the adjustments. Consequently, the actual dose for this work activity
(RWP 2002-2507) exceeded 5 rem (7.165) and exceeded the legitimate dose estimate
(4.6 rem) by more than 50 percent.
-26-
Analysis: The inspectors determined that this finding was associated with the
Occupational Radiation Safety Cornerstone program and process attributes (ALARA
planning/projected dose) and affected the objective of the cornerstone, which is to
protect the worker from exposure to radiation. Therefore, the finding was greater than
minor. The occurrence involved a failure to maintain or implement, to the extent
practical, procedures needed to achieve occupational doses that were ALARA, which
resulted in unplanned, unintended occupational collective dose for a work activity.
Therefore, the safety significance of the finding was evaluated using the Occupational
Radiation Safety SDP. However, because the licensees 3-year rolling average
collective dose was not greater than 135 person-rem/unit, the finding had no more than
very low safety significance.
Enforcement: Unit 1 Technical Specification 5.4.1.a and Unit 2 Technical Specification 6.8.1.a require that procedures be established, implemented, and
maintained covering the applicable procedures in Appendix A of Regulatory Guide 1.33,
Revision 2, February 1978. Regulatory Guide 1.33, Appendix A, Section 7.e.1, includes
procedures for an RWP program. Procedure NMM RP-105, "Radiation Work Permits,"
Revision 1, implements this requirement. Procedure NMM RP-105, Section 5.8.3,
requires that the reason for a revision be recorded on the RWP Revision/Edit form.
However, the licensee failed to record the reason for the revision of RWPs when it
adjusted work activity dose estimates without providing an adequate bases. Because
the failure to record the reasons for RWP revisions was of very low safety significance
and has been entered into the corrective action program as CR ANO-C-2003-0031, this
violation is being treated as a noncited violation, consistent with Section VI.A of the NRC
Enforcement Policy (NCV 50-313/0302-04; 50-368/0302-04).
4.
Other Activities [OA]
4OA2 Identification and Resolution of Problems
.1
Cross-Reference to Problem Identification and Resolution Findings Documented
Elsewhere
Section 2OS2 describes a problem involving the lack of justification for adjusting work
activity dose estimates. The NRC identified a previous example of this problem in
May 2001. The problem resulted in a noncited violation, which was documented in NRC
Inspection Report 50-313/2001-02; 50-368/2001-02. The licensee initiated
CR ANO-C-2001-00297 to document the problem and track the corrective actions. This
CR was closed in February 2002 after the corrective actions were implemented. The
corrective actions proved ineffective to prevent the recurrence of the problem.
4OA3 Event Followup (71153)
.1
(Open) Licensee Event Report (LER) 50-368/2002-002-00: Automatic actuation of the
reactor protection system caused by a main turbine trip due to failure of the main
generator reverse power relay resulted in a reactor trip.
-27-
This LER was issued during this inspection period for an event that occurred on
December 19, 2002. Continued evaluation of the root cause and significance will be
performed and documented in a future inspection report.
.2
(Closed) LER 50-368/2001-001-00: Crediting a designated operator for manual action
during surveillance tests affected operability of the emergency feedwater system if
condensate pumps had been lost during the tests.
In May 2001, an NRC inspection identified that the licensees method of surveillance
testing of the Unit 2 emergency feedwater system resulted in inappropriately crediting
operator actions and resulted in operation prohibited by Technical Specifications. The
method of testing employed using the startup and blowdown demineralizer system as a
source of emergency feedwater suction. If a loss of condensate pumps occurred, both
trains of the emergency feedwater system were potentially incapable of performing their
intended function. The NRC documented the finding, enforcement, and safety
significance in NRC Inspection Report 50-313/2001-02; 50-368/2001-02. The licensee
initiated CR ANO-2001-0349 to address the issue and corrective actions. The licensee
reported this condition of using the startup and blowdown demineralizer system as a
source of emergency feedwater pump suction and inappropriately crediting manual
actions during surveillance testing in the LER.
The inspectors reviewed the LER and concluded that the licensees root cause
determination was adequate and the completed and proposed corrective actions were
appropriate. This LER is closed.
.3
(Closed) LER 50-313/2001-003-00: Control room emergency ventilation system
radiation monitors were inoperable due to an inadequate procedure change caused by
training and system knowledge deficiencies.
On April 17, 2001, the licensee identified that maintenance was performed on auxiliary
building ventilation supply fans while the normal control room ventilation dampers were
closed and neither of the control room emergency ventilation supply fans was running.
The licensee determined that both trains of control room emergency ventilation system
radiation monitors were inoperable. With the normal ventilation dampers closed, the
ability of these detectors to generate a radiation signal for control room emergency
ventilation initiation would be significantly degraded without air flow representative of the
activity entering the control room. This was a violation of Unit 1 Technical Specification,
Table 3.5.1-1, and Unit 2 Technical Specification, Table 3.3-6. This was also reported
as a condition that could have prevented the fulfillment of the safety function of a system
that is needed to mitigate the consequences of an accident.
The licensee initiated CR ANO-2001-0207 to address the issue and corrective actions.
The licensee reported this condition and its inadequate procedural guidance for
radiation monitor operability in the LER.
The inspectors reviewed the LER and concluded that the licensees root cause
determination was adequate and the completed and proposed corrective actions were
appropriate. This finding was considered to be of very low safety significance because
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the condition existed less than 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> and another control room area radiation monitor
was available to automatically initiate emergency ventilation if a high radiation condition
in the control room existed. This violation of NRC requirements meets the criteria of
Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as a
noncited violation.
4OA5 Other Activities
.1
The inspectors reviewed information only the Accreditation Evaluation Report, issued by
the Institute of Nuclear Power Operations National Academy of Nuclear Training
Nuclear Training Accrediting Board of ANO training programs, performed in May 2002.
4OA6 Meetings, Including Exit
The inspectors presented the results of the ALARA Planning and Controls inspection to
Mr. Craig Anderson, Vice President, Operations, and other members of the licensees
staff at the conclusion of the inspection on January 31, 2003. The licensee
acknowledged the findings presented. The inspectors conducted a followup telephonic
exit meeting with Mr. Glenn Ashley, Licensing Manager, and other members of the
licensees staff on February 20, 2003.
The inspectors presented the inspection results of the emergency plan change review to
Mr. R. Fowler, Acting Supervisor, Emergency Planning, during a telephonic exit
interview conducted on February 20, 2003. The licensee acknowledged the findings
presented.
The resident inspectors presented the inspection results of the resident inspections to
Mr. Craig Anderson, Vice President, Operations, and other members of the licensee's
staff on April 3, 2003. The licensee acknowledged the findings presented.
The inspectors asked the licensee whether any materials examined during the
inspection should be considered proprietary. No proprietary information was identified.
40A7
Licensee-Identified Findings
The following findings of very low significance (Green) were identified by the licensee.
They are violations of NRC requirements which meet the criteria of Section VI of the
NRC Enforcement Policy, NUREG-1600, for being dispositioned as a noncited violation.
.1
On March 19, 2003, the licensee identified that Unit 1 turbine-driven emergency
feedwater pump steam admission bypass Valves SV-2613 and SV-2663 were not
environmentally qualified in accordance with 10 CFR 50.49. The safety significance of
this finding was very low because the valves remained operable. This issue was
entered into the licensee's corrective action program as CR ANO-1-2003-0369.
.2
On April 17, 2001, the licensee identified that the radiation monitors for both trains of the
control room emergency ventilation system were inoperable. This event is discussed in
Section 4OA3.
ATTACHMENT 1
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee
C. Anderson, Vice President, Operations
B. Beaird, Supervisor, Systems Engineering
S. Bennett, Licensing
M. Byram, Senior Lead Engineer
M. Chisum, Manager, Systems Engineering
M. Cooper, Licensing Specialist
S. Cotton, Director, Nuclear Safety Assurance
G. Dobbs, Design Engineer
B. Eichenberger, Manager, Unit 1 Operations
C. Eubanks, General Manager, Plant Operations
D. Fouts, Supervisor, Nuclear Engineering
R. Fowler, Acting Supervisor, Emergency Planning
M. Harris, Manager, Dry Fuel Storage Project
D. Hawkins, Licensing Specialist
A. Heflin, Acting Manager, Planning, Scheduling and Outages
J. Hoffpauir, Plant Manager, Operations
D. James, Manager, Engineering Programs and Components
J. Kowalewski, Director, Engineering
T. Mitchell, Manager, Unit 2 Operations
T. Nickels, Superintendent, Radiation Protection
B. Patrick, Operations Supervisor, Radiation Protection
D. Phillips, Design Supervisor
D. Scheide, Licensing Specialist
L. Schwartz, Manager, Nuclear Engineering
J. Sigle, Shift Assistant Operations Manager
D. Stoltz, Supervisor, Radiation Protection
R. To, Design Engineer
C. Tyrone, Manager, Quality Assurance
D. Williams, Senior Staff Engineer, Nuclear Engineering
C. Zimmerman, Plant Manager, Support
ITEMS OPENED
50-313/0302-02; 50-368/0302-02
Failure to obtain a license amendment for
upgrade of the spent fuel area crane
(Section 1R17)
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ITEMS OPENED AND CLOSED
50-313/0302-01; 50-368/0302-01
Deletion of containment integrity controls for
secondary system containment penetrations
(Section 1R02)
50-313/0302-03
Unauthorized temporary alteration
(Section 1R23)
50-313/0302-04; 50-368/0302-04
Failure to provide adequate justifications for
work activity dose estimate adjustments
(Section 2OS2)
ITEMS CLOSED
50-368/2001-001-00
LER
Crediting a designated operator for manual
action during surveillance tests affected
operability of the emergency feedwater
system if condensate pumps had been lost
during the tests (Section 4OA3)
50-313/2001-003-00
LER
Control room emergency ventilation system
radiation monitors were inoperable due to
an inadequate procedure change caused by
training and system knowledge deficiencies
(Section 4OA3)
LIST OF ACRONYMS
as low as reasonably achievable
CIAS
containment isolation actuation signal
CR
condition report
ER
engineering request
Final Safety Analysis Report
GDC
general design criterion
LCO
limiting condition for operation
LER
licensee event report
MAI
maintenance action item
Office of Nuclear Reactor Regulation
radiation work permit
significance determination process
safety evaluation report
Updated Final Safety Analysis Report
ATTACHMENT 2
ANO PAPER
"Secondary System Pressure Boundary as an Extension of Containment Liner"