ML021680568

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Plant Performance Update Meeting, McGuire Nuclear Station
ML021680568
Person / Time
Site: McGuire, Mcguire  
Issue date: 06/06/2002
From: Barron H
Duke Energy Corp
To:
Office of Nuclear Reactor Regulation
Shared Package
ML021680561 List:
References
Download: ML021680568 (20)


Text

Plant Performance Update Meeting June 6, 2002

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Agenda

  • Introduction-Brew Barron
  • Operational Performance-Dhiaa Jamil

- Generation Status Trending

- 2EOC14 Refueling Outage

- ALARA Performance

- Correct Component Verification

  • Miscellaneous-Bryan Dolan

- Corrective Action Program

- Special Nuclear Material

- Security 2

Operational Performance 3

McGuire Nuclear Station GENERATION STATUS TRENDING 2001 - 2003 Actual vs. Target o

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Unit 2 (2.8 days)

Main Steam Pressure Trip Unit 2 (0.44 days)

Add Oil to 2B NCP 1EOC14 (38.2 days)

Cond. Boost Pmp Mtrs.

Busline Relay Mod Non-vital Spare Inverter (KXS to KXA)

Vital Inverters Replace.

Rx Vessel 1 0-year ISI CA Tank Tie-in 1 EOC15 (25 days)

Main Gen. Volt Reg.

No S/G Work 10W% Vessel Head Bare Metal Inspection 2EOC15 (30 days)

Rx Vessel 10-year ISI Main Gen. Volt Reg No S/G Work Unit. (3133 days)

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2EOC14 (32.3 days)

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Generation Status Trending 4

2EOC14 Refueling Outage 5

Completed Auxiliary Feedwater Storage Tank Tie In 6

Repaired CRDM K-8 Intermediate Canopy Seal Weld Intermediate Canopy Seal Approx. 6 ft.

Reactor Head 7

Performed 100% Bare Metal Head Inspection -

No Corrosion or Boron Found 8

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Shutdown/Startup Performance Improvements

  • Tuning of process control system
  • Tuning of valve actuators
  • Sequencing of steam dump valves
  • Procedural improvements
  • Simulator and training improvements

ALARA Performance

  • Changes

- Step change in ALARA planning and scheduling

- Radiation Work Permit setpoint adjusted down to more effectively use dosimetry as ALARA tool

- Focused on radiation worker desired behavior prior to and during the outage

- PIP threshold changes 11

ALARA Performance (continued)

  • Results

- Desired worker behavior demonstrated

- Desired increase of PIPs at lower threshold was obtained

- Comprehensive self-assessment of outage radiation practices - complete 12

2 EOC1 4 Refueling Outage

  • Zero
  • Zero
  • Zero
  • 32 dc LERs events injuries jys 13

Correct Component Verification (CCV)

  • Defined specific behaviors associated with CCV
  • Created a CCV flag
  • Conducted classroom and flow loop scenario training
  • Targeted observations with CCV focus
  • 2EOC14 was completed without a CCV event
  • Similar focus on CCV is now underway in operations and chemistry 14

Miscellaneous 15

Corrective Action Program PIP Significance Categories ACA No Cause Analysis 16

Corrective Action Program

  • PIP Action Codes

- Corrective Actions to Prevent Recurrence (CAPR)

  • Directed at the Root Cause of Category I and 2 PIPS

- Corrective Actions (CA)

  • Directed at CAQ

- Elective / Enhancement Actions (ELEC)

- Structure helps focus corrective action effectiveness reviews on highest priority actions (CAPRs) 17

Special Nuclear Materials

  • Completed comprehensive inventory
  • No discrepancies 18

Security

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  • No concerns about schedule for compliance with NRC order.

19

Questions 20