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Category:Letter type:L
MONTHYEARL-PI-23-034, Response to Request for Additional Information Regarding License Amendment Request to Revise Technical Specification 3.7.8, Cooling Water (Cl) System,2024-01-0202 January 2024 Response to Request for Additional Information Regarding License Amendment Request to Revise Technical Specification 3.7.8, Cooling Water (Cl) System, L-PI-23-035, Response to Request for Additional Information Regarding License Amendment Request to Revise Technical Specifications Section 5.6.6, Reactor Coolant System (RCS) Pressure and Temperature Limits Report2023-12-20020 December 2023 Response to Request for Additional Information Regarding License Amendment Request to Revise Technical Specifications Section 5.6.6, Reactor Coolant System (RCS) Pressure and Temperature Limits Report L-PI-23-033, Supplement to License Amendment Request to Revise Technical Specification 3.8.1, Surveillance Requirement 3.8.1.2, Note 32023-12-0505 December 2023 Supplement to License Amendment Request to Revise Technical Specification 3.8.1, Surveillance Requirement 3.8.1.2, Note 3 L-PI-23-025, License Amendment Request to Revise Technical Specification 3.8.1, Surveillance Requirement 3.8.1.2, Note 32023-09-28028 September 2023 License Amendment Request to Revise Technical Specification 3.8.1, Surveillance Requirement 3.8.1.2, Note 3 L-PI-23-023, Baffle Former Bolts Alternate Aging Management Strategy2023-09-11011 September 2023 Baffle Former Bolts Alternate Aging Management Strategy L-PI-23-018, License Amendment Request to Revise ISFSI Technical Specification 4.4 to Allow Use of a Code Alternative to ASME Code, NB-5130, Examination of Weld Edge Preparation Surfaces, for the TN-40HT2023-07-14014 July 2023 License Amendment Request to Revise ISFSI Technical Specification 4.4 to Allow Use of a Code Alternative to ASME Code, NB-5130, Examination of Weld Edge Preparation Surfaces, for the TN-40HT L-PI-23-006, License Amendment Request to Revise Technical Specification 3.7.8 Required Actions2023-06-22022 June 2023 License Amendment Request to Revise Technical Specification 3.7.8 Required Actions L-PI-23-016, 2022 10 CFR 50.46 LOCA Annual Report2023-06-14014 June 2023 2022 10 CFR 50.46 LOCA Annual Report L-PI-23-010, Annual Report of Individual Monitoring2023-04-27027 April 2023 Annual Report of Individual Monitoring L-PI-23-007, Supplement to Application to Revise Technical Specification Section 5.6.6, Reactor Coolant System (RCS) Pressure and Temperature Limits Report (PTLR)2023-03-28028 March 2023 Supplement to Application to Revise Technical Specification Section 5.6.6, Reactor Coolant System (RCS) Pressure and Temperature Limits Report (PTLR) L-PI-23-005, CFR 50.55a Requests Nos. 1-RR-5-15 and 2-RR-5-15, Proposed Use of Subsequent ASME Code Edition and Addenda in Accordance with 10 CFR 50.55a(g)(4)(iv)2023-03-0303 March 2023 CFR 50.55a Requests Nos. 1-RR-5-15 and 2-RR-5-15, Proposed Use of Subsequent ASME Code Edition and Addenda in Accordance with 10 CFR 50.55a(g)(4)(iv) L-PI-23-001, Day Steam Generator Tube Inspection Report2023-01-30030 January 2023 Day Steam Generator Tube Inspection Report L-PI-22-047, Resubmittal of Prairie Island Nuclear Generating Plant (PINGP) 2018 Unit 1 180-Day Steam Generator Tube Inspection Report2022-12-21021 December 2022 Resubmittal of Prairie Island Nuclear Generating Plant (PINGP) 2018 Unit 1 180-Day Steam Generator Tube Inspection Report L-PI-22-020, Application to Revise Technical Specification Section 5.6.6, Reactor Coolant System (RCS) Pressure and Temperature Limits Report (PTLR)2022-12-0202 December 2022 Application to Revise Technical Specification Section 5.6.6, Reactor Coolant System (RCS) Pressure and Temperature Limits Report (PTLR) L-PI-22-040, Supplement to Application to Revise Technical Specifications to Adopt TSTF-577, Revised Frequencies for Steam Generator Tube Inspections2022-10-0606 October 2022 Supplement to Application to Revise Technical Specifications to Adopt TSTF-577, Revised Frequencies for Steam Generator Tube Inspections L-PI-22-037, Updated Approach for Prairie Island Unit 1 and Unit 2 Baffle Former Bolts2022-09-20020 September 2022 Updated Approach for Prairie Island Unit 1 and Unit 2 Baffle Former Bolts L-PI-22-032, CFR 50.46 LOCA Annual Report2022-06-16016 June 2022 CFR 50.46 LOCA Annual Report L-PI-22-033, Response to Request for Additional Information Prairie Island Nuclear Generating Plant, Units 1 and 2, Amendment to Adopt 24-Month Operating Cycles2022-06-10010 June 2022 Response to Request for Additional Information Prairie Island Nuclear Generating Plant, Units 1 and 2, Amendment to Adopt 24-Month Operating Cycles L-PI-22-003, Application to Revise Technical Specifications to Adopt TSTF-577, Revised Frequencies for Steam Generator Tube Inspections2022-06-0707 June 2022 Application to Revise Technical Specifications to Adopt TSTF-577, Revised Frequencies for Steam Generator Tube Inspections L-PI-22-024, Supplement to Application for License Amendment to Implement 24-Month Operating Cycle2022-03-0707 March 2022 Supplement to Application for License Amendment to Implement 24-Month Operating Cycle L-PI-21-047, Response to Request for Additional Information 24-Month Cycle Amendment Prairie Island Nuclear Generating Plant, Units 1 and 22021-12-0707 December 2021 Response to Request for Additional Information 24-Month Cycle Amendment Prairie Island Nuclear Generating Plant, Units 1 and 2 L-PI-21-045, Response to Request for Additional Information Cooling Water System License Amendment Request2021-11-0404 November 2021 Response to Request for Additional Information Cooling Water System License Amendment Request L-PI-21-029, Exigent License Amendment Request to Revise Technical Specification 3.7.8 to Allow a One-Time Extension of the Completion Time of Required Action B.12021-10-0707 October 2021 Exigent License Amendment Request to Revise Technical Specification 3.7.8 to Allow a One-Time Extension of the Completion Time of Required Action B.1 L-PI-21-006, License Amendment Request to Revise Technical Specification 3.3.1, Reactor Trip System (RTS) Instrumentation, to Incorporate Installed Bypass Test Capability for the Power Range RTS Functions2021-10-0202 October 2021 License Amendment Request to Revise Technical Specification 3.3.1, Reactor Trip System (RTS) Instrumentation, to Incorporate Installed Bypass Test Capability for the Power Range RTS Functions L-PI-21-032, Response to Request for Additional Information Amendment Request to Adopt TSTF-471 and 571-T for Prairie Island2021-09-30030 September 2021 Response to Request for Additional Information Amendment Request to Adopt TSTF-471 and 571-T for Prairie Island L-PI-21-016, Application for License Amendment to Implement 24-Month Operating Cycle2021-08-0606 August 2021 Application for License Amendment to Implement 24-Month Operating Cycle L-PI-21-027, 2020 10 CFR 50.46 LOCA Annual Report2021-06-28028 June 2021 2020 10 CFR 50.46 LOCA Annual Report L-PI-21-023, Independent Spent Fuel Storage Installation - 2020 Annual Radiological Environmental Monitoring Program Report2021-05-14014 May 2021 Independent Spent Fuel Storage Installation - 2020 Annual Radiological Environmental Monitoring Program Report L-PI-21-007, Application to Revise Technical Specifications to Adopt TSTF-471, Eliminate Use of the Term Core Alterations in Actions and Notes2021-04-19019 April 2021 Application to Revise Technical Specifications to Adopt TSTF-471, Eliminate Use of the Term Core Alterations in Actions and Notes L-PI-20-050, Request for a One-Time Exemption from 10 CFR 50, Appendix E, Biennial Emergency Preparedness Exercise Requirements, Due to COVID-19 Pandemic2020-10-0707 October 2020 Request for a One-Time Exemption from 10 CFR 50, Appendix E, Biennial Emergency Preparedness Exercise Requirements, Due to COVID-19 Pandemic L-PI-20-051, Supplement to Application to Revise Technical Specifications to Adopt TSTF-547, Clarification of Rod Position Requirements2020-09-28028 September 2020 Supplement to Application to Revise Technical Specifications to Adopt TSTF-547, Clarification of Rod Position Requirements L-PI-20-026, Response to Request for Additional Information: License Amendment Request to Revise Technical Specifications to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times - RITSTF Initiativ2020-09-0101 September 2020 Response to Request for Additional Information: License Amendment Request to Revise Technical Specifications to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times - RITSTF Initiative 4 L-PI-20-035, = Request for Revision to Reactor Vessel Material Surveillance Capsule Removal Schedule2020-07-28028 July 2020 = Request for Revision to Reactor Vessel Material Surveillance Capsule Removal Schedule L-PI-20-023, Independent Spent Fuel Storage Installation, Response to Request for Additional Information: License Amendment Request to Expand the Storage Capacity of the Independent Spent Fuel Storage Installation (ISFSI)2020-06-10010 June 2020 Independent Spent Fuel Storage Installation, Response to Request for Additional Information: License Amendment Request to Expand the Storage Capacity of the Independent Spent Fuel Storage Installation (ISFSI) L-PI-20-014, Supplement to License Amendment Request: Expand the Storage Capacity of the Independent Spent Fuel Storage Installation (ISFSI2020-04-29029 April 2020 Supplement to License Amendment Request: Expand the Storage Capacity of the Independent Spent Fuel Storage Installation (ISFSI L-PI-20-004, License Amendment Request to Revise Technical Specifications (TS) to Remove Note I from Limiting Condition for Operating (LCO) 3.4.12 and LCO 3.4.132020-03-30030 March 2020 License Amendment Request to Revise Technical Specifications (TS) to Remove Note I from Limiting Condition for Operating (LCO) 3.4.12 and LCO 3.4.13 L-PI-20-001, License Amendment Request to Address Issues Identified in Westinghouse Nuclear Safety Advisory Letter NSAL-09-5, Revision 1, and NSAL-15-12020-01-29029 January 2020 License Amendment Request to Address Issues Identified in Westinghouse Nuclear Safety Advisory Letter NSAL-09-5, Revision 1, and NSAL-15-1 L-PI-19-041, Application to Revise Technical Specifications to Adopt TSTF-547, Clarification of Rod Position Requirements2019-12-23023 December 2019 Application to Revise Technical Specifications to Adopt TSTF-547, Clarification of Rod Position Requirements L-PI-19-031, License Amendment Request: Revise Technical Specifications to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times - RITSTF Initiative 4b2019-12-16016 December 2019 License Amendment Request: Revise Technical Specifications to Adopt Risk Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times - RITSTF Initiative 4b L-PI-19-040, License Amendment Request: Revise Technical Specification 5.5.14 to Permanently Extend Containment Leakage Rate Test Frequency2019-10-0707 October 2019 License Amendment Request: Revise Technical Specification 5.5.14 to Permanently Extend Containment Leakage Rate Test Frequency L-PI-19-038, Submittal of Revised Pressure and Temperature Limits Report2019-09-19019 September 2019 Submittal of Revised Pressure and Temperature Limits Report L-PI-19-037, Response to Request for Additional Information: 10 CFR 50.55a Requests Nos. 1-RR-5-10 and 2-RR-5-10, Proposed Alternative to Reactor Vessel Inservice Inspection (ISI) Intervals2019-09-16016 September 2019 Response to Request for Additional Information: 10 CFR 50.55a Requests Nos. 1-RR-5-10 and 2-RR-5-10, Proposed Alternative to Reactor Vessel Inservice Inspection (ISI) Intervals L-PI-19-025, Request to Approve Site-Specific Probabilistic Risk Assessment (PRA) Model for Flowserve N-Seal Abeyance Seal and Dynamic Testing for the Prairie Island Nuclear Generating Plant (PINGP)2019-08-27027 August 2019 Request to Approve Site-Specific Probabilistic Risk Assessment (PRA) Model for Flowserve N-Seal Abeyance Seal and Dynamic Testing for the Prairie Island Nuclear Generating Plant (PINGP) L-PI-19-029, Supplement to Response to Request for Additional Information: Application to Adopt 10 CFR 50.69, Risk-Informed Categorization and Treatment of Structures, Systems and Components For...2019-08-0505 August 2019 Supplement to Response to Request for Additional Information: Application to Adopt 10 CFR 50.69, Risk-Informed Categorization and Treatment of Structures, Systems and Components For... L-PI-19-002, 10 CFR 50.55a Requests Nos. 1-RR-5-10 and 2-RR-5-10, Proposed Alternative to Reactor Vessel Inservice Inspection (ISI) Intervals for Prairie Island, Unit 1 and Unit 22019-06-13013 June 2019 10 CFR 50.55a Requests Nos. 1-RR-5-10 and 2-RR-5-10, Proposed Alternative to Reactor Vessel Inservice Inspection (ISI) Intervals for Prairie Island, Unit 1 and Unit 2 L-PI-19-014, Response to Request for Additional Information: Application to Adopt 10 CFR 50.69, Risk-Informed Categorization and Treatment of Structures, Systems and Components for Nuclear Power Reactors2019-04-29029 April 2019 Response to Request for Additional Information: Application to Adopt 10 CFR 50.69, Risk-Informed Categorization and Treatment of Structures, Systems and Components for Nuclear Power Reactors L-PI-19-003, Request for Revision to Reactor Vessel Material Surveillance Capsule Removal Schedule for Prairie Island Nuclear Generating Plant (PINGP)2019-02-0404 February 2019 Request for Revision to Reactor Vessel Material Surveillance Capsule Removal Schedule for Prairie Island Nuclear Generating Plant (PINGP) L-PI-19-006, Emergency License Amendment Request Regarding One-Time Extension for Technical Specification Completion Time Requirements2019-01-29029 January 2019 Emergency License Amendment Request Regarding One-Time Extension for Technical Specification Completion Time Requirements L-PI-19-005, Online Reference Portal for NRC Review of License Amendment Request to Implement 10 CFR 50.692019-01-15015 January 2019 Online Reference Portal for NRC Review of License Amendment Request to Implement 10 CFR 50.69 L-PI-18-063, Response to Request for Additional Information: Revise License Condition Associated with Implementation of NFPA 8052018-12-0606 December 2018 Response to Request for Additional Information: Revise License Condition Associated with Implementation of NFPA 805 2024-01-02
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Prairie Island Nuclear Generating Plant Operated by Nuclear Management Company, LLC L-PI-08-028 10 CFR 50.54(f)
U S Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-0001 Prairie Island Nuclear Generating Plant Units 1 and 2 Dockets 50-282 and 50-306 License Nos. DPR-42 and DPR-60 Three Month Response to NRC Generic Letter 2008-01, "Managing Gas Accumulation in Emergencv Core Cooling, Decav Heat Removal, and Containment Sprav Svstems"
Reference:
- 1) NRC Generic Letter 2008-01, "Managing Gas Accumulation in Emergency Core Cooling, Decay Heat Removal, and Containment Spray Systems" dated January 11, 2008.
The Nuclear Regulatory Commission (NRC) issued Generic Letter (GL) 2008-01 (Reference 1) to request that each licensee evaluate the licensing basis, design, testing, and corrective action program for the Emergency Core Cooling System (ECCS),
Residual Heat Removal (RHR) system, and Containment Spray system, to ensure that gas accumulation is maintained less than the amount that challenges operability of these systems, and that appropriate action is taken when conditions adverse to quality are identified. The NRC, in GL 2008-01, requested each licensee to submit a written response in accordance with 10 CFR 50.54(f) within 9 months.
Additionally, the NRC requested that if a licensee cannot meet the requested response date, the licensee "shall provide a response within 3 months of the date of this GL". In the 3 month response, the licensee was requested to describe the alternative course of action that it proposes to take, including the basis for the acceptability of the proposed alternative course of action.
The 2008 Prairie Island Unit 1 refueling outage (1R25) occurred earlier this year. In response to and using the guidance of GL 2008-01, NMC staff conducted walkdowns in Unit 1 containment during 1R25 and identified one vulnerability that has been entered into the corrective action program for resolution. Subsequent to the NMC walkdowns, the Nuclear Energy Institute (NEI) provided detailed guidance for responding to GL 2008-01. Subsequent to receiving the NEI guidance, NMC also received some operating experience from a similarly-designed plant that during ultrasonic examination 1717 Wakonade Drive East Welch, Minnesota 55089-9642 Telephone: 651.388.1121
Document Control Desk Page 2 (UT) conducted as part of their walkdown, a void in a horizontal stretch of RHR line was identified. The walkdown at Prairie Island did not include UT. Based on new NEI guidance and new operating experience from a similar plant, NMC believes it will be necessary to conduct additional Unit 1 walkdowns to fully respond to GL 2008-01.
Since these walkdowns will require the unit to be shutdown, NMC will require additional time to fully respond to GL 2008-01. As an alternative to the nine-month response, NMC proposes to complete detailed Unit 1 walkdowns during the next Unit 1 refueling outage (1R26) and completing GL 2008-01 evaluations within 90 days of completing 1R26.
This alternative course of action is considered acceptable based on current operating experience. Surveillance testing performed on the subject systems has confirmed that there are no currently identified gas voiding issues. In-service testing of the systems are routinely performed and has demonstrated acceptable performance. Also, the vulnerability that has been identified has been entered into the corrective action program for resolution.
Summaw of Commitments This letter contains two new commitments and no revisions to existing commitments:
1 Complete the detailed walkdowns of inaccessible sections of the Generic Letter 2008-01 subject systems prior to startup from the 2009 Unit 1 Refueling Outage.
- 2. Evaluations of the Generic Letter 2008-01 subject systems will be completed within 90 days following the completion of the Unit 1 2009 Refueling Outage.
I declare under penalty of perjury that the foregoing is true and correct. Executed on Michael D. Wadley Site Vice President, Prairie Isl Nuclear Generating Plant Nuclear Management cc: Administrator, Region Ill, USNRC Project Manager, Prairie Island, USNRC Resident Inspector, Prairie Island, USNRC
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Prairie Island Nuclear Generating Plant Operated by Nuclear Management Company, LLC L-PI-08-028 10 CFR 50.54(f)
U S Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-0001 Prairie Island Nuclear Generating Plant Units 1 and 2 Dockets 50-282 and 50-306 License Nos. DPR-42 and DPR-60 Three Month Response to NRC Generic Letter 2008-01, "Managing Gas Accumulation in Emergencv Core Cooling, Decav Heat Removal, and Containment Sprav Svstems"
Reference:
- 1) NRC Generic Letter 2008-01, "Managing Gas Accumulation in Emergency Core Cooling, Decay Heat Removal, and Containment Spray Systems" dated January 11, 2008.
The Nuclear Regulatory Commission (NRC) issued Generic Letter (GL) 2008-01 (Reference 1) to request that each licensee evaluate the licensing basis, design, testing, and corrective action program for the Emergency Core Cooling System (ECCS),
Residual Heat Removal (RHR) system, and Containment Spray system, to ensure that gas accumulation is maintained less than the amount that challenges operability of these systems, and that appropriate action is taken when conditions adverse to quality are identified. The NRC, in GL 2008-01, requested each licensee to submit a written response in accordance with 10 CFR 50.54(f) within 9 months.
Additionally, the NRC requested that if a licensee cannot meet the requested response date, the licensee "shall provide a response within 3 months of the date of this GL". In the 3 month response, the licensee was requested to describe the alternative course of action that it proposes to take, including the basis for the acceptability of the proposed alternative course of action.
The 2008 Prairie Island Unit 1 refueling outage (1R25) occurred earlier this year. In response to and using the guidance of GL 2008-01, NMC staff conducted walkdowns in Unit 1 containment during 1R25 and identified one vulnerability that has been entered into the corrective action program for resolution. Subsequent to the NMC walkdowns, the Nuclear Energy Institute (NEI) provided detailed guidance for responding to GL 2008-01. Subsequent to receiving the NEI guidance, NMC also received some operating experience from a similarly-designed plant that during ultrasonic examination 1717 Wakonade Drive East Welch, Minnesota 55089-9642 Telephone: 651.388.1121
Document Control Desk Page 2 (UT) conducted as part of their walkdown, a void in a horizontal stretch of RHR line was identified. The walkdown at Prairie Island did not include UT. Based on new NEI guidance and new operating experience from a similar plant, NMC believes it will be necessary to conduct additional Unit 1 walkdowns to fully respond to GL 2008-01.
Since these walkdowns will require the unit to be shutdown, NMC will require additional time to fully respond to GL 2008-01. As an alternative to the nine-month response, NMC proposes to complete detailed Unit 1 walkdowns during the next Unit 1 refueling outage (1R26) and completing GL 2008-01 evaluations within 90 days of completing 1R26.
This alternative course of action is considered acceptable based on current operating experience. Surveillance testing performed on the subject systems has confirmed that there are no currently identified gas voiding issues. In-service testing of the systems are routinely performed and has demonstrated acceptable performance. Also, the vulnerability that has been identified has been entered into the corrective action program for resolution.
Summaw of Commitments This letter contains two new commitments and no revisions to existing commitments:
1 Complete the detailed walkdowns of inaccessible sections of the Generic Letter 2008-01 subject systems prior to startup from the 2009 Unit 1 Refueling Outage.
- 2. Evaluations of the Generic Letter 2008-01 subject systems will be completed within 90 days following the completion of the Unit 1 2009 Refueling Outage.
I declare under penalty of perjury that the foregoing is true and correct. Executed on Michael D. Wadley Site Vice President, Prairie Isl Nuclear Generating Plant Nuclear Management cc: Administrator, Region Ill, USNRC Project Manager, Prairie Island, USNRC Resident Inspector, Prairie Island, USNRC