IR 05000508/1982011
| ML20055A088 | |
| Person / Time | |
|---|---|
| Site: | Satsop |
| Issue date: | 06/16/1982 |
| From: | Albert W, Dodds R NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V) |
| To: | |
| Shared Package | |
| ML20055A077 | List: |
| References | |
| 50-508-82-11, 50-509-82-05, 50-509-82-5, NUDOCS 8207150464 | |
| Download: ML20055A088 (5) | |
Text
U.S. NUCLEAR REGULATORY COMMISSION
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REGION V
50-508/82-11 Report No.
50-5_0X 82-05 Decket No.
50-508/509 License No. CPPR-154, 155 Safeguards Group Licensee:
Washington Public Power Supply System P
O.
Box 1223 Elma, Washington 98541
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Facility Name:
WhP-3, WNP-5 Inspection at:
Construction site Inspection conducted:
,May 1 - 31, 1982 Inspectors:
[- (M N M//W/d/f47 W.
G.
hert[/ Senior Resident Inspector
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Date Signed Date Signed Date Signed Approved By:
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Fate Signed R. T.
Dodds, Chief, Reactor Projects Section 2 Reactor Construction Projects Branch Stsnma ry:
Inspection during the period of May 1 - 31, 1982 (Report Nos. 50-508/
82-11 and 50-509/82-05)
Areas Inspected: Routine unannounced inspection by the resident Inspector of construction activities.
Principal areas inspected included: (1) Open items from previous inspections, (2) weld material controls, (3) installation of control room instrumenta-tion panels (4) primary loop welding and (5) structural welding.
The inspection involved 35 inspection hours by one NRC inspector.
Results: ho items of noncompliance were identified.
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8207150464 820617 PDR ADOCK 05000508 G
PDR RV Form 219 (2)
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DETAILS 1.
Persons Contacted:
The inspector interviewed various engineering, management, inspection, and construction personnel of the organizations listed below.
Key personnel, including those who attended the exit interview, are specifically identified below:
Washington Public Power Supply System (Licensee or Supply a.
System)
R. S. Leddick, Program Director, WNP-3/5 N. F. Blais, Senior Project Quality Engineer D. R. Coody, Proj ect Quality Engineer J. A. Puzauskas, Quality Assurance Engineering Supervisor
- E.
L. Ste phens, Senior Proj ect Quality Engineer C. H. Tewisbury, Quality Assurance Surveillance Supervisor
- 0. E. Trapp, Project Quality Assurance Manager J. A. Vanni, Senior Project Quality Engineer J. M. Walker, Senior Quality Assurance Engineer (Corporate Office)
b.
Ebasco Services, Inc. (Ebasco)
L. A. Bast, Quality Assurance Engineering Supervisor B. H.
Bray, Resident Engineer A. M. Cutrona, Quality Program Site Manager
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R. Harris, Project Quality Engineer W. J. Lear, Nondestructive Examination Specialist c.
Combustion Engineering (CE)
W. B. Douglass, Nuclear Site Manager W. Pratt, Site Representative L. Lehman, Quality Assurance Site Representative d.
Peter Kiewit & Sons, Inc. (PKS)
P. Langille, Welding Engineering Supervisor S. Scott, Quality Control Manager F. Wisner, Project Quality Assurance Manager e.
Morrison-Knudsen (MK)
D. Summers, Quality Assurance / Quality Control Manager f.
Morrison-Knudsen/ESI/ Lord (Joint Venture)
T. Abbotello, Welding Engineer L. Bieronski, Proj ect Welding Engineering Manager
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W. Holcombe, Project Quality Assurance Manager S. Renner, Welding Engineer J. Sowers, Project Quality Director i
A. Walcutt, Project Quality Engineering Supervisor g.
Fishback & Moore (FM)
D. Dishaw, Foreman
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- Designates those attending exit interview on May 14, 1982.
2.
Independent Inspection and Tours Daily tours of some portions of the Unit 3 construction site were normally conducted by the resident inspector during each i
on-site work day.
Tours of Unit 5 were limited to verification of inert atmosphere
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for heavy equipment in the storage area near the Unit 3 cooling
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tower.
No items of noncompliance were identified.
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Proj ect Construction Status - Unit 3 i
At the end of the report period, project site construction had
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reached 54 percent completion.
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4.
Weld Material Controls
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Weld material control for the Morrison-Knudsen (263) structural i
steel contract was further examined during this report period.
The examination included practices and records at one weld rod issue station not previously covered.
Morrison-Knudsen procedure A.I. 07 " Welding Material Control" was examined against AWS D 1.1 requirements and used as the criteria for this examination.
No items of noncompliance were identified.
5.
Welder Qualification Practices of PKS and Joint Venture were examined for controls which assure that the welder qualification process is not com-promised.
One previous question of the resident inspector with regard to the marking of qualification samples had been resolved by the Joint-Venture by changing their system to metal stamp (rather than paint) markings.
PKS routinely uses metal stamps I
but their procedure permits paint if necessary.
The inspector l
believed that the systems of these.two contractors could not be compromised without the deliberate collusion of individuals responsible for conducting.the tests or evaluating the test results.
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6.
Instrumentation and Control Panel Installation
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Control room 7anel installation was1 examined against drawings
I controlling tiis activity.
Questions of the NRC inspector were resolved except for one condition concerning some apparent ex-
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cessive grinding of the shop welds, which was documented as a
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nonconforming condition in order to facilitate engineering
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j evaluation, i
No items of noncompliance were identified.
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7.
C.
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E. Avery Quality Program i
The initial organization and procedure system to be utilized by this Combustion Engineering organization to control the i
quality of pump internals and core internals work was discussed
with CE site personnel.
Quality assurance and control manuals j
for in-office review by the NRC were requested of the Licensee for this activity.
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No items of noncompliance were found.
Follow-up inspection will be conducted as part of the routine NRC inspection program.
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Primary Loop Welding
The preparations for post weld heat treatment of primary loop I
weldments were examined against procedures and ASME Section III l
and IX requirements.
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No items of noncompliance were identified.
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9.
Shutdown Cooling Heat Exchangers A visual inspection of these units by the resident inspector raised certain questions which have not been satisfactorily answered.
a.
The north nozzle of the North Unit contains markings indicating unsatisfactory PT examinations.
Why had the weldment of the safe-end been accepted?
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The north nozzle of the North Unit indicates that the safe j
end weld is excessively close to the heavier nozzle section.
l How could satisfactory radiographs be obtained?
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c.
Is the peeling of metal on the safe end related to a shipping i
nut attachment or base material flaws?
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I d.
Why is the south nozzle of the South Unit configured differently
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from the others?
Is minimum wall maintained?
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-4-These and corollary guestion remain open.
This will be identified as a follow-up item Resolution of SDCHX Safe-end Concerns". (50-508/
82-11-01)
10. Primary Loop Welding Material Control The Joint Venture initiated an investigation of an incident which resulted in the inability to positively confirm whether E-308 or E-309 weld material was deposited in a 6" section of a single pass on primary loop weld No. 214.
The follow-up of this contractor-identified deficiency was examined by the resident inspector.
No items of noncompliance were found and it was determined that the Joint Venture had satisfactorily dispositioned the condition and taken the necessary corrective action.
11. Structural Steel Welding Welding procedure of the Morrison-Knudsen Company (263 contractor)
for welding of the galvanized missile shields was examined.
The procedure, WP-73-WPPSS, and the supporting PQR were examined without finding any deviations from the applicable AWS Code (D 1.1).
However, the procedure was forwarded to the regional office for specialist review.
12. Exit Interview The resident inspector conducted two weekly meetings with the site QA Manager and other Ebasco and WPPSS personnel prior to taking annual leave in the latter half of the report period.
The items of this report were discussed in these meetings.