IR 05000269/2008005

From kanterella
Jump to navigation Jump to search
IR 05000269-08-005, 05000270-08-005, 05000287-08-005; on 10/01/2008 - 12/31/2008; Oconee Nuclear Station, Units 1, 2, and 3; Routine Integrated Inspection Report
ML090280315
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 01/27/2009
From: Bartley J
Division Reactor Projects II
To: Baxter D
Duke Energy Carolinas, Duke Power Co
References
IR-08-005
Download: ML090280315 (31)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION ary 27, 2009

SUBJECT:

OCONEE NUCLEAR STATION - INTEGRATED INSPECTION REPORT 05000269/2008005, 05000270/2008005, AND 05000287/2008005

Dear Mr. Baxter:

On December 31, 2008, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Oconee Nuclear Station. The enclosed report documents the inspection results which were discussed on January 12, 2008, with Mr. Rich Freudenberger, Safety Assurance Manager, and other members of your staff.

The inspection examined activities conducted under your licenses as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your licenses. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. Based on the results of the inspection, no findings of significance were identified.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Jonathan H. Bartley, Chief Reactor Projects Branch 1 Division of Reactor Projects Docket Nos.: 50-269, 50-270, 50-287 License Nos.: DPR-38, DPR-47, DPR-55

Enclosure:

NRC Integrated Inspection Report 05000269/2008005, 05000270/2008005, 05000287/2008005 w/Attachment: Supplemental Information

REGION II==

Docket Nos: 50-269, 50-270, 50-287 License Nos: DPR-38, DPR-47, DPR-55 Report Nos: 05000269/2008005, 05000270/2008005, 05000287/2008005 Licensee: Duke Power Company, LLC Facility: Oconee Nuclear Station, Units 1, 2 and 3 Location: 7800 Rochester Highway Seneca, SC 29672 Dates: October 1, 2008 - December 31, 2008 Inspectors: A. Hutto, Senior Resident Inspector E. Riggs, Resident Inspector G.Ottenberg, Resident Inspector R. Chou, Reactor Inspector (Sections 1R08, 4OA5.3)

Approved by: Jonathan H. Bartley, Chief Reactor Projects Branch 1 Division of Reactor Projects Enclosure

SUMMARY OF FINDINGS

IR 05000269/2008005, 05000270/2008005, 05000287/2008005; 10/01/2008 -

12/31/2008; Oconee Nuclear Station, Units 1, 2, and 3; Routine Integrated Inspection Report.

The report covered a three-month period of inspection by the onsite resident inspectors and one region based reactor inspector. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.

NRC Identified and Self-Revealing Findings

None.

Licensee-Identified Violations

None.

REPORT DETAILS

Summary of Plant Status

Unit 1 began the report period at 100 percent rated thermal power (RTP). On November 23, 2008, the unit was reduced to 88 percent RTP for turbine valve movement testing. It was returned to 100 percent RTP later the same day, where it remained through the end of the inspection period.

Unit 2 began the report period at 100 percent RTP. On October 25, 2008, the unit was shutdown from 100 percent RTP for the End-of-Cycle (EOC)-23 refueling outage. On December 11, 2008, the unit was taken critical following outage activities. It achieved 100 percent RTP on December 15, 2008, where it remained through the end of the inspection period.

Unit 3 began the report period at 100 percent RTP. On November 7, 2008, the unit experienced an automatic shutdown due to a fault in the digital Control Rod Drive (CRD) system. The unit entered a forced outage in order to identify and correct the cause of the trip. On November 9, 2008, the unit was taken critical. It achieved 100 percent RTP on November 10, 2008, where it remained through the end of the inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

1R01 Adverse Weather Protection

Cold Weather Preparations

a. Inspection Scope

The inspectors reviewed the licensees preparations for adverse weather associated with cold ambient temperatures for the three risk significant systems listed below. This included field walkdowns to assess the material condition and operation of freeze protection equipment (e.g., heat tracing, instrument box heaters, area space heaters, etc.), as well as other preparations made to protect plant equipment from freeze conditions. In addition, the inspectors conducted discussions with operations, engineering, and maintenance personnel responsible for implementing the licensees cold weather protection program in order to assess the licensees ability to identify and resolve deficient conditions associated with cold weather protection equipment prior to cold weather events. Documents reviewed during this inspection are listed in the to this report.

  • Essential Siphon Vacuum System
  • Unit 1, 2, and 3 Borated Water Storage Tank Level Instrumentation
  • Elevated Water Storage Tank Level Instrumentati

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment

.1 Partial Walkdown

a. Inspection Scope

The inspectors conducted three partial equipment alignment walkdowns to evaluate the operability of selected redundant trains or backup systems while the other train or system was inoperable or out-of-service (OOS). The walkdowns included, as appropriate, reviews of plant procedures and other documents to determine correct system lineups, and verification of critical components to identify any discrepancies which could affect operability of the redundant train or backup system. Documents reviewed are listed in the Attachment to this report. The following systems were included in this review:

  • 2B Reactor Building Spray (RBS) train and 2A, B, and C Reactor Building Cooling Units with the 2A RBS pump OOS for pump modifications
  • Unit 1 and 3 Emergency Feedwater Water (EFW) systems with the Station Auxiliary Service Water (ASW) and Standby Shutdown Facility (SSF) ASW systems OOS during Unit 2 Condenser Circulating Water (CCW) maintenance and SSF maintenance outage
  • CT-2, Keowee Hydro-electric Units (KHUs), and Underground Power Path during SSF maintenance outage

b. Findings

No findings of significance were identified.

.2 Complete Walkdown of KHU-1

a. Inspection Scope

The inspectors performed a system walkdown on accessible portions of KHU 1. The inspectors focused on verifying proper breaker positioning, proper tap changer settings on the associated transformers, support system alignment and availability, and material condition.

A review of Problem Investigation Process reports (PIPs) and preventive maintenance work orders was performed to assess whether material condition deficiencies significantly affected the KHUs ability to perform its design functions and determine if appropriate corrective action was being taken by the licensee.

The inspectors conducted a review of the system engineers trending data and system health reports to determine if appropriate trending parameters were being monitored and that no adverse trends were noted. Documents reviewed for this semiannual inspection sample are listed in the Attachment to this report.

b. Findings

No findings of significance were identified.

1R05 Fire Protection

Fire Area Walkdowns

a. Inspection Scope

The inspectors conducted tours in four areas of the plant to assess whether combustibles and ignition sources were properly controlled, and that fire detection and suppression capabilities were intact. The inspectors selected the areas based on a review of the licensees safe shutdown analysis and the probabilistic risk assessment based sensitivity studies for fire-related core damage sequences. Documents reviewed are listed in the Attachment to this report. The following areas were inspected during this inspection period:

  • Unit 2 Reactor Building (RB) (1)
  • Unit 1 Turbine Building Basement (1)
  • Unit 3 Control Room (1)
  • Unit 1 & 2 Cable Spreading Room (1)

b. Findings

No findings of significance were identified.

1R08 In-service Inspection (ISI) Activities (71111.08P, Unit 2)

.1 In-service Inspection Activities Other Than Steam Generator Tube Inspections, PWR

Vessel Upper Head Penetration Inspections, and Boric Acid Corrosion Control Program

a. Inspection Scope

The inspectors reviewed the implementation of the licensees ISI program for monitoring degradation of the reactor coolant system (RCS) boundary and risk significant piping boundaries during the Unit 2 Fall 2008 refueling outage (2EOC23). The inspectors activities consisted of an on-site review of non-destructive examination (NDE) and welding activities to evaluate compliance with the applicable edition of the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code (BPVC),

Sections XI (Code of record for the Fourth 10-year ISI interval was 1998 Edition through 2000 Addenda), and to verify that indications and defects (if present) were appropriately evaluated and dispositioned in accordance with the requirements of the ASME Code,Section XI acceptance standards. Documents reviewed are listed in the Attachment to this report.

The inspectors reviewed NDE activities including examination procedures, NDE reports, equipment and consumable certification records, personnel qualification records, calibration reports, and calibration block fabrication drawings (as applicable) for the following examinations:

Ultrasonic Testing (UT):

  • Weld 2RC-279-90V, Pipe to Elbow on Suction Pipe 33.5 Diameter from SG A to Cooling Pump A2
  • Weld 2-01A-4-29, Pipe to Elbow on Main Steam Pipe 36 Diameter in Turbine Building
  • Weld 2RC-279-89V, Elbow to Elbow on Hot Leg Pipe 36 Diameter to SG A Magnetic Particle Testing (MT):
  • Weld 2RC-279-91V, Pipe to Elbow on Suction Pipe 33.5 Diameter from SG A to Cooling Pump A1
  • Weld 2RC-279-90V, Pipe to Elbow on Suction Pipe 33.5 Diameter from SG A to Cooling Pump A2 Radiographic Testing (RT):
  • Weld 2-SGA-W250-4 on SG A Emergency Feed Water Pipe 3 Diameter
  • Weld 2-SGA-W335 on SG A Emergency Feed Water Pipe 3 Diameter
  • Weld 2-SGA-W251-4 on SG A Emergency Feed Water Pipe 3 Diameter The inspectors reviewed In-service Examination Evaluations from Refueling Outage 2EOC22 (the previous outage) for relevant indications that were accepted by the licensee for the continued service. Four recordable indications were reviewed:
  • Report UT-07-050, UT Vessel Examination on the Weld between Pressurizer Sampling Nozzle and Shell
  • Report PT-07-029, Liquid Penetrant Examination on the Weld between Plate and Shell on 2-LS-Tank (Letdown Storage Tank)
  • Report VT-07-152, Visual Examination (VT-3) on 2-LS-Tank Supports
  • Report VT-07-156, Visual Examination (VT-3) on Steam Generator 2-SGB Lateral Support The inspectors reviewed welding activities including an in-process welding activity for ASME Class 1 piping to evaluate compliance with procedures and the ASME Code.

The inspectors directly observed part of the welding process and verified welding machine settings for the welding activity described below.

The inspectors also reviewed weld process control reports, welding procedures, procedure qualification records, certified material test reports for filler material, and welder qualification records.

b. Findings

No findings of significance were identified.

.2 PWR Vessel Upper Head Penetration (VUHP) Inspection Activities

a. Inspection Scope

The bare metal visual examination required by Order EA 03-009 for the surface of the reactor vessel upper head, including 360 degrees around each reactor pressure vessel head penetration nozzle, was performed during this refueling outage. The inspectors reviewed Problem Investigation Process report (PIP) O-08-06882, which documented the results of the examination. The examination also included the insulation and other service structures above the head for identifying potential boric acid leaks from pressure-retaining components above the reactor pressure vessel head, as required by Order EA 03-009. The inspectors also reviewed the effective degradation years (EDY) calculation performed by the licensee. Documents reviewed are listed in the Attachment to this report.

b. Findings

No findings of significance were identified.

.3 Boric Acid Corrosion Control (BACC) Inspection Activities

a. Inspection Scope

The inspectors reviewed the licensees BACC program activities to ensure implementation of commitments made in response to NRC Generic Letter 88-05, Boric Acid Corrosion of Carbon Steel Reactor Pressure Boundary, and applicable industry guidance documents. Specifically, the inspectors performed a record review of procedures and the results of the licensees Mode 3 containment walkdown inspections performed during the fall 2008 outage, including generated PIPs and their subsequent engineering evaluations.

The inspectors conducted an independent walkdown of the reactor building to evaluate compliance with licensees BACC program requirements and verify that degraded or non-conforming conditions, such as boric acid leaks identified during the Mode 3 or 4 containment walkdown, were properly identified and corrected in accordance with the licensees BACC and Corrective Action programs. Documents reviewed are listed in the to this report.

b. Findings

No findings of significance were identified.

.4 SG Tube Inspection Activities

a. Inspection Scope

The inspectors reviewed activities, plans, condition monitoring and operational assessments, the pre-outage degradation assessment, and procedures for the inspection and evaluation of the SG Inconel Alloy 690TT tubing for Unit 2 SGs A and B to determine if the activities were being conducted in accordance with Technical Specifications (TS) and applicable industry standards. Data gathering, analysis, and evaluation activities were reviewed. Documents reviewed are listed in the Attachment to this report.

The inspectors reviewed data results to verify the adequacy of the licensee=s primary, secondary, and resolution analyses.

The tube maximum through-wall depth wear from the tube vibration around the tube support plates during the inspection period was 42 percent at SG A tube R137C66. The inspectors reviewed equipment, data operators, and analyst certifications and qualifications, including medical exams.

The inspectors reviewed data for the following tubes:

  • SG A - R6C38, R137C66, R76C130, R141C55, R73C1, R76C2, R86C121, R127C90, R120C95, R115C93, R151C16, R149C32, R147C30, and R145C40
  • SG B - R76C2, R9C13, R15C69, R19C74, R20C76, R60C5, R60C7, R62C5, R65C1, R68C10, R73C1, R74C1, and R78C1

b. Findings

No findings of significance were identified.

.5 Identification and Resolution of Problems

a. Inspection Scope

The inspectors performed a review of ISI-related problems, including welding and BACC that were identified by the licensee and entered into the corrective action program as PIPs. The inspectors reviewed the PIPs to confirm that the licensee had appropriately described the scope of the problem and had initiated corrective actions. The review also included the licensees consideration and assessment of operating experience events applicable to the plant. The inspectors performed this review to ensure compliance with 10CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requirements. The corrective action documents reviewed by the inspectors are listed in the Attachment to this report.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification

Simulator Training

a. Inspection Scope

The inspectors observed licensed operator simulator training on December 5, 2008. The simulator scenarios involved Just-In-Time (JIT) training for Zero Power Physics Testing and for unit start-up following the Unit 2EOC23 refueling outage. The scenarios involved the initial approach to criticality, the development of 1/M plots, the temperature coefficient measurement, and the differential boron and rod worth measurement. The following procedures were utilized during the JIT training:

  • PT/0/A/0711/001, Zero Power Physics Test
  • OP/2/A/1102/001, Controlling Procedure for Unit Startup The inspectors observed crew performance in terms of communications between the operators and reactor engineering; ability to take timely and proper actions; prioritizing, interpreting, and verifying alarms; correct use and implementation of procedures, including the alarm response procedures; timely control board operation and manipulation, including high-risk operator actions; and, oversight and direction provided by the shift supervisor.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors reviewed the licensees effectiveness in performing routine maintenance activities. This review included an assessment of the licensees practices pertaining to the identification, scoping, and handling of degraded equipment conditions, as well as common cause failure evaluations. For each item selected, the inspectors performed a detailed review of the problem history and surrounding circumstances, evaluated the extent of condition reviews as required, and reviewed the generic implications of the equipment and/or work practice problem. For those structures, systems, and components (SSCs) scoped in the Maintenance Rule per 10 CFR 50.65, the inspectors verified that reliability and unavailability were properly monitored and that 10 CFR 50.65 (a)(1) and (a)(2) classifications were justified in light of the reviewed degraded equipment condition. The inspectors reviewed the following items:

  • PIP O-08-7681, Documentation for lessons learned for SSF Major Outages and PIP O-08-8311, 2EOC23 SSF Outage Critique Items
  • PIPs associated with Instrument Air (IA) deficiencies. The PIPs reviewed included the following: PIP O-08-7391, Spare Diesel Service Air Compressor auto started for unknown reason; PIP O-08-6720, Instrument Air leak discovered on IA-3101 flange when "A" Primary, IA Dryer was returned to service; PIP O-08-6584, AP/22 "Loss of Instrument Air" was entered due to low IA header pressure; PIP O-08-6560, AP/22 "Loss of Instrument Air" was entered due to low IA header pressure; PIP O-08-6436, Primary Instrument Air Compressor Discharge Pressure Lower than Expected when restored by OP/0/A/1106/027 (Compressed Air System); PIP O-08-4897, Request revisions to AP/22 (Loss of Instrument Air) - lessons learned from 8/7/08

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessment and Emergent Work Evaluations

a. Inspection Scope

The inspectors evaluated the following attributes for the seven SSCs and activities listed below:

(1) the effectiveness of the risk assessments performed before maintenance activities were conducted;
(2) the management of risk;
(3) that, upon identification of an unforeseen situation, necessary steps were taken to plan and control the resulting emergent work activities; and
(4) that maintenance risk assessments and emergent work problems were adequately identified and resolved. Documents reviewed are listed in the to this report.
  • Critical Activity Plan for SSF outage and CCW activities during 2EOC23, Revision 0
  • PIP O-08-7023, Select Licensee Commitment (SLC) Not Met During Mod Install with Proper Communications to Operations, PIP O-08-7024, SLC 16.9.11.a Entry Required for Low Pressure Service Water (LPSW) piping removal in 2EOC23 RFO
  • Critical Activity Plan for OD200934, Unit 2 CCW Protected Service Water Pump Minimum Flow Mod
  • Critical Activity Plan for SSF outage and CCW activities during 2EOC23, Revision 1
  • Critical Activity Plan for Low Pressure Injection (LPI) and RBS Cyclone Separator Fill and Testing

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations

a. Inspection Scope

The inspectors reviewed six operability evaluations affecting risk significant systems, to assess, as appropriate:

(1) the technical adequacy of the evaluations;
(2) whether continued system operability was warranted;
(3) whether other existing degraded conditions were considered;
(4) if compensatory measures were involved, whether the compensatory measures were in place, would work as intended, and were appropriately controlled; and
(5) where continued operability was considered unjustified, the impact on TS limiting condition for operations. Documents reviewed are listed in the Attachment to this report. The inspectors reviewed the following operability evaluations:
  • PIP O-08-6125, 2A LPI Pump Vibration in the Alert Range per PT/2/A/0203/006A
  • PIP O-08-6278, Possible Cracked Insulation/Overheating Found on Field End Turns During Inspection of KHU-1 Generator
  • PIP O-08-6727, Documentation of Unit 2 RB Emergency Sump Coating Inspection
  • PIP O-08-7028, FME Found in Unit 2 Fuel Transfer Canal Deep End Drains
  • PIP O-08-6244, Unit 2 SSF Pressurizer Heaters not Functioning
  • PIP O-08-8492, SSF PZR Level Transmitter, 2RC LT0072, Found Out-of-Tolerance While Performing Preventive Maintenance (PM)

b. Findings

No findings of significance were identified.

1R18 Plant Modifications

Permanent Plant Modifications

a. Inspection Scope

The inspectors reviewed documents and observed portions of the installation of two selected temporary modifications. Among the documents reviewed were system design bases, the Updated Finial Safety Analysis Report (UFSAR), TS, system operability/

availability evaluations, and the 10 CFR 50.59 screening. The inspectors observed, as appropriate, that the installation was consistent with the modification documents, was in accordance with the configuration control process, adequate procedures and changes were made, and post installation testing was adequate. Additional documents reviewed are listed in the Attachment to this report. The following items were reviewed under this inspection procedure:

  • OD 300729, Unit 3 North Control Room Wall - Natural Phenomenon Barrier System Installation
  • OD 201964, Replace LPI Pump Cyclone Separator and Seal Orifices

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed six Post-Maintenance Test procedures and/or test activities, as appropriate, for selected risk significant systems to assess whether:

(1) the effect of testing on the plant had been adequately addressed by control room and/or engineering personnel;
(2) testing was adequate for the maintenance performed;
(3) acceptance criteria were clear and adequately demonstrated operational readiness consistent with design and licensing basis documents;
(4) test instrumentation had current calibrations, range, and accuracy consistent with the application;
(5) tests were performed as written with applicable prerequisites satisfied;
(6) jumpers installed or leads lifted were properly controlled;
(7) test equipment was removed following testing; and
(8) equipment was returned to the status required to perform its safety function. Documents reviewed are listed in the Attachment to this report. The inspectors observed testing and/or reviewed the results of the following tests:
  • PT/2/A/0203/006A, LPI pump test following cyclone separator modification installation
  • PT/0/A/0400/011, SSF Diesel Generator Test, and PT/0/A/0600/021, Standby Shutdown Facility Diesel-Generator Operation following jacket water expansion tank repair
  • PT/0/A/0400/005, SSF ASW Pump Test following SSF outage and PMs
  • PT/0/A/0600/021, SSF Diesel Generator Operation following overhaul of diesel engine
  • PT/0/A/0400/011, SSF Diesel Generator Test following overhaul of diesel engine
  • TT/2/A/3117/001, LPSW Waterhammer Prevention System (WPS) Pneumatic Valves Air Accumulator, TT/2/A/3117/002, LPSW WPS System Boundary Leakage Test, TT/2/A/3117/003, LPSW WPS Leakage Accumulator Functional Test following the installation of the Unit 2 LPSW WPS modification

b. Findings

No findings of significance were identified.

1R20 Refueling & Outage Activities

a. Inspection Scope

The inspectors conducted reviews and observations for selected outage activities to ensure that:

(1) the licensee considered risk in developing the outage plan;
(2) the licensee adhered to the outage plan to control plant configuration based on risk;
(3) that mitigation strategies were in place for losses of key safety functions; and
(4) the licensee adhered to operating license and TS requirements.

Documents reviewed are listed in the Attachment to this report. Between October 25, 2008, and December 15, 2008, the following activities related to the Unit 2 refueling outage 2EOC23 were reviewed for conformance to applicable procedures and selected activities associated with each evaluation were witnessed:

  • Outage risk management plan/assessment
  • Clearance activities
  • Plant cooldown
  • Mode changes from Mode 1 (power operation) to No Mode (defueled)
  • Containment closure
  • Refueling activities
  • Plant heatup/mode changes
  • Core physics testing
  • Power Escalation

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors witnessed five surveillance tests and/or reviewed test data of the risk-significant SSCs listed below, to assess, as appropriate, whether the SSCs met TS, UFSAR, and licensee procedure requirements. In addition, the inspectors determined if the testing effectively demonstrated that the SSCs were ready and capable of performing their intended safety functions. Documents reviewed are listed in the to this report.

  • PT/3/A/0600/012, Unit 3 Turbine Driven Emergency Feedwater Pump (TDEFWP)

Test (IST)

  • PT/2/A/0610/028A, Unit 2 Main Feeder Bus 2 Lockout Relay Test
  • PT/2/A/0151/019, Penetration 19 Leak Rate Test (Containment Isolation Valve LRT)
  • PT/0/A/0711/001, Unit 2 Zero Power Physics Test
  • PT/2/A/0600/012, Unit 2 TDEFWP Test (IST)

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator (PI) Verification

.1 Mitigating Systems Cornerstone

a. Inspection Scope

The inspectors reviewed the PI listed in the table below (for all three units), to determine its accuracy and completeness against requirements in Nuclear Energy Institute (NEI)99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5.

Cornerstone: Mitigating Systems

Performance Indicator Verification Period Records Reviewed MSPI

  • Operating Logs, Train

- high pressure injection Unavailability Data

- emergency feedwater 4th Quarter, 2007; 1st, 2nd,

  • Maintenance Records

- emergency AC power and 3rd Quarter, 2008

  • Maintenance Rule Data

- residual heat removal

  • Corrective Action Program

- support cooling water

  • Consolidated Data Entry Derivation Reports
  • System Health Reports

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems

.1 Daily Screening of Corrective Action Reports

In accordance with IP 71152, Identification and Resolution of Problems, and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed daily screening of items entered into the licensees corrective action program. This review was accomplished by reviewing copies of PIPs, attending daily screening meetings, and accessing the licensees computerized database.

.2 Focused Review

a. Inspection Scope

The inspectors performed an in-depth review of one issue entered into the licensees corrective action program, and also performed an in-depth review of existing plant operator workarounds. The sample was within the initiating events cornerstone and involved risk significant systems. The inspectors reviewed the actions taken to determine if the licensee had adequately addressed the following attributes:

  • Complete, accurate and timely identification of the problem
  • Evaluation and disposition of operability and reportability issues
  • Consideration of previous failures, extent of condition, generic or common cause implications
  • Prioritization and resolution of the issue commensurate with safety significance
  • Identification of the root cause and contributing causes of the problem
  • Identification and implementation of corrective actions commensurate with the safety significance of the issue.

The following issues and corrective actions were reviewed:

PIP O-08-7110, Unit 3 Tripped

b. Findings

No findings of significance were identified.

.3 Semi-Annual Trend Review

a. Inspection Scope

As required by IP 71152, Identification and Resolution of Problems, the inspectors performed a review of the licensees Corrective Action Program (CAP) and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors review was focused on repetitive equipment issues, but also considered the results of daily inspector CAP item screenings discussed in Section 4OA2.1 above, licensee trending efforts, and licensee human performance results. The inspectors review nominally considered the six month period of January 2008, through June 2008, although some examples expanded beyond those dates when the scope of the trend warranted. The review also included issues documented outside the normal CAP in major equipment problem lists, plant health team vulnerability lists, focus area reports, system health reports, self-assessment reports, maintenance rule reports, and Safety Review Group Monthly Reports. The inspectors compared and contrasted their results with the results contained in the licensees latest quarterly trend reports listed in the Attachment to this report. Corrective actions associated with a sample of the issues identified in the licensees trend report were reviewed for adequacy.

b. Observations and Findings

No findings of significance were identified. In general, the licensee identified trends and appropriately addressed the trends with their CAP. However, the inspectors identified a trend that the licensee had not previously recognized within their trending program. The trend was associated with issues related to the adequacy and thoroughness of coordination of outage activities. During the fall 2008 Unit 2 outage, the inspectors noted three examples where outage activities were not adequately coordinated or communicated between work groups which resulted in unintended system interactions or incomplete operational awareness of plant configurations. The inspectors also noted three similar examples of outage work coordination or communication issues during the previous two outages. These issues were documented in the licensees corrective action program under PIPs O-08-6643, O-08-7023, O-08-7024, O-08-6998, O-08-2056, O-07-7374, and O-07-7674. The licensee initiated PIP O-09-0150 to fully evaluate their performance in outage work/activity coordination and communication through their trending program. The inspectors will continue to monitor this area and assess the effectiveness of any corrective actions that may come out of the licensees evaluation.

4OA3 Event Follow-up

a. Inspection Scope

The inspectors evaluated the event listed below to assess the overall impact on the plant and mitigating actions. As appropriate, the inspectors:

(1) observed plant parameters and status, including mitigating systems/trains;
(2) determined alarms/conditions preceding or indicating the event;
(3) evaluated performance of mitigating systems and licensee actions; and
(4) confirmed that the licensee properly classified, if applicable, the event in accordance with emergency action level procedures and made timely notifications to NRC and state/county governments as required. Documents reviewed are listed in the Attachment to this report.
  • PIP O-08-7110, Unit 3 Tripped

b. Findings

No findings of significance were identified.

4OA5 Other Activities

.1 Quarterly Resident Inspector Observations of Security Personnel and Activities

a. Inspection Scope

During the inspection period the inspectors conducted observations of security force personnel and activities to ensure that the activities were consistent with licensee security procedures and regulatory requirements relating to nuclear plant security.

These observations took place during both normal and off-normal plant working hours.

These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspectors' normal plant status reviews and inspection activities.

b. Findings

No findings of significance were identified.

.2 (Closed) Unresolved Item (URI) 05000269,270,287/2007008-02, Untimely Corrective

Action to Determine if Steel Plate Laminations Existed in Safety-Related Applications.

This issue involved the licensees discovery of a lamination in a 3/4 inch steel plate slated for use in the fabrication of an LPI pipe hanger in July 2003, and subsequent discovery in September 2006 that additional steel plates of the same heat number had not been segregated and inspected prior to use. The inspectors noted during a corrective action program inspection in 2007 (IR 0500269,270,287/2007008) that corrective actions to inspect safety-related supports in the Unit 2 and 3 containments that were fabricated from the suspect steel had not been performed. This URI was written as it was determined that the results of the licensees inspections of the Unit 2 and 3 supports were required to assess the significance of the issue.

The inspectors reviewed completed work orders (WO) 1765202, 1765203, 1765204, 1765205, 1765212, 1765208, 1765207, 1765209, and 1765210 to verify the licensee completed the inspections on the Unit 3 and Unit 2 supports. No laminations or defects were identified by the inspections. The results of these inspections were documented in PIP O-03-4686. Based on the results of the inspections, the untimely corrective action associated with this issue constitutes a violation of minor significance that is not subject to enforcement action in accordance with Section IV of the Enforcement Policy. This URI is closed.

.3 (Open) NRC Temporary Instruction (TI) 2515/172, Reactor Coolant System Dissimilar

Metal Butt Welds (DMBWs)

a. Inspection Scope

The inspectors reviewed the licensees activities related to the inspection and mitigation of dissimilar metal butt welds in the Reactor Coolant System (RCS) to ensure that the licensee activities were consistent with the industry requirements established in the Materials and Reliability Program (MRP) document MRP-139, Primary System Piping Butt Weld Inspection and Evaluation Guideline, dated July 2005. The inspectors activities took place during this refueling outage and covered the documentation review and direct observation of the full structural weld overlay (FSWOL) process on the reactor cooling system hot leg decay heat removal line nozzle weld 2-53A-10-10A. The inspectors also reviewed the qualifications of the welders, as well as those of the personnel conducting the liquid penetrant testing prior to the application of the FSWOL.

The inspectors only implemented portions of TI-172 that corresponded to the available activities during this outage. Previous TI-172 inspection activities were documented in NRC Inspection Report 05000269,270,287/2008004. Documents reviewed are listed in the Attachment to this report.

b. Findings and Observations

No findings of significance were identified.

TI 2515/172 REPORTING REQUIREMENTS FOR OCONEE UNIT 2 Examinations/Weld Overlays Mitigations Performed - Hot Leg Decay Heat Removal Nozzle Weld 2-53A-10-10A 1) For each weld overlay inspected, was the activity performed in accordance with ASME Code welding requirements and consistent with NRC staff relief request authorizations? Has the licensee submitted a relief request and obtained NRR staff authorization to install weld overlays?

Yes, the licensee performed the FSWOL to reinforce the existing weld during the inspectors direct observation in accordance with the applicable sections of the ASME Boiler and Pressure Vessel Code (ASME Code). The licensee submitted Relief Request (RR)-07-ON-004 for a proposed alternative based on ASME Code Cases N-504-2 and N-638-1 to meet ASME Code requirements.

The licensee obtained NRC approval for the relief request in a safety evaluation report (SER) on January 17, 2008.

The inspectors reviewed welding procedure specifications, procedure qualification records, weld wire certifications, and the in-process welding process control sheets for compliance with ASME Section IX requirements and adherence to the SER.

The licensee performed a liquid penetrant examination on the prepared surface of the pipe and existing weld prior to the application of the FSWOL.

2) For each weld overlay inspected, was the activity performed by qualified personnel?

Yes, welding personnel were qualified in accordance with the requirements identified in ASME Code Section IX. The inspectors reviewed the welder performance qualification test records and compared them with the requirements of QW-300. The in-process welding process control sheets were reviewed for compliance with the proposed alternative and ASME Code Section IX requirements.

3) For each weld overlay inspected, was the activity performed such that deficiencies were identified, dispositioned, and resolved?

Yes, the vendor, Welding Service Inc., had a program in place to identify, disposition, and resolve deficiencies encountered during the FSWOL work. No deficiencies were identified during the preparation and in-process welding.

.4 Institute of Nuclear Power Operations (INPO) Plant Assessment Report Review

a. Inspection Scope

The inspectors reviewed the final report for the INPO plant assessment of Oconee Nuclear Station conducted in July 2008. The inspectors reviewed the report to ensure that issues identified were consistent with the NRC perspectives of licensee performance and to determine if any significant safety issues were identified that required further NRC follow-up.

b. Findings

No findings of significance were identified.

4OA6 Management Meetings (Including Exit Meeting)

Exit Meeting Summary

The inspectors presented the inspection results to Mr. Rich Freudenberger, Safety Assurance Manager, and other members of licensee management at the conclusion of the inspection on January 12, 2009. The licensee acknowledged the findings presented.

The inspectors asked the licensee whether any of the material examined during the inspection should be considered proprietary. No proprietary information was identified.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

E. Anderson, Superintendent of Operations
S. Batson, Engineering Manager
D. Baxter, Site Vice President
D. Brewer, Safety Assessments Manager
R. Brown, Emergency Preparedness Manager
E. Burchfield, Reactor and Electrical Systems Manager
C. Curry, Mechanical/Civil Engineering Manager
P. Culbertson, Maintenance Manager
G. Davenport, Compliance Manager
R. Fruedenberger, Safety Assurance Manager
P. Gillespie, Station Manager
M. Glover, General Manager of Projects
D. Hubbard, Training Manager
J. Kammer, Modification Engineering Manager
T. King, Security Manager
B. Meixell, Regulatory Compliance
M. Stephenson, Shift Operations Manager
J. Smith, Regulatory Compliance
J. Steely, Continuing Training Supervisor
J. Weast, Regulatory Compliance

NRC

J. Stang, Project Manager, NRR

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

None

Discussed

2515/172 TI Reactor Coolant System Dissimilar Metal Butt Welds (Section 40A5.3)

Closed

05000269,270,287/2007008-02 URI Untimely Corrective Action to Determine if Steel Plate Laminations Existed in Safety-Related Applications (Section 4OA5.2)

DOCUMENTS REVIEWED