IR 05000254/1979002

From kanterella
Jump to navigation Jump to search
IE Insp Repts 50-254/79-02 & 50-265/79-02 on 790103-05,10-11 & 23-25.No Noncompliance Noted.Major Areas Inspected:Qa Program,Review of Plant Operations,Fire Protection Action Followup,Ie Bulletin/Circular & LER Followup
ML19284A652
Person / Time
Site: Quad Cities  Constellation icon.png
Issue date: 02/05/1979
From: Chrissotimas N, Knop R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML19284A646 List:
References
50-254-79-02, 50-254-79-2, 50-265-79-02, 50-265-79-2, NUDOCS 7903150150
Download: ML19284A652 (4)


Text

.

.

U.S. NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT REGION lII Report No. 50-254/79-02; 50-265/79-02 Docket No. 50-254; 50-265 License No. DPR-29; DPR-30 Licensee:

Commonwealth Edison Company Post Office Box 767 Chicago, IL 60690 Facility Name: Quad-Cities Nuclear Power Station, Units 1 and 2 Inspection At: Quad-Cities Site, Cordova, IL Inspection Cond, ted: Jan ry 3-5, 10-11 and 23-25, 1979 V ~..., -

Inspector:

N./ J.!

a,.

e

'

Chrissotimos r-

-

e m*l k

.

,

Approved By:

R. C. Knop, Chief Reactor Projects Section 1 Inspection Summary Inspection on January 3-5, 10-11 and 23-25, 1979 (Recort No. 50-254/79-02; 5C-265/79-02)

Areas Inspected: Routine, unannounced inspection of QA program, review of plant operations, fire protection action followup; IE Bulletin and Circular followup; licensee event report followup.

The inspection involved 52 inspector-hours onsite by one NRC inspector.

Results: Of the six areas inspected no apparent items of noncompliance or deviations were identified.

..

790315 O/fC

'

,

,

DETAILS 1.

Persons Contacted

  • N.

Kalivianakis, Superintendent J. Gudac, Assistant Superintendent T. Tamlyn, Lead Operating Engineer K. Graesser, Administrative Assistant

  • L.

Gerner, Technical Staff Supervisor D. Bax, Operating Engineer, Unit 2 G. Conschack, Operating Engineer, Unit 1 R. Spear, Maintenance Engineer

  • J. Heilman, Quality Assurance, Operations R. Flessner, Assistant Technical Staff Supervisor The inspector also interviewed several other licensee employees, including shift engineers and foremen, reactor operators, tech-nical staff personnel and quality control personnel.
  • Denotes those present at the exit interview.

2.

Plant Operations During the course of this inspection the following plant activities were observed by the inspector; new fuel inspection, LPRM removal and fuel moves.

The inspector confirmed that proper procedures and controls were being implemented during these observations.

Partial tours of the plant were made throughout the inspection.

Primary emphasis was given to observations of cleanliness, radiation control and control room operations.

Control room observation included review of logs, data sheets and out of service procedures.

Activ-ities in the inspected areas appeared adequate considering that Unit 1 is currently involved in a refueling outage.

No items of soncompliance or deviations were identified.

3.

Fire Protection The inspector verified portions of the staff positions as outlined in the * Fire Protection Evaluation Report have been completed.

  • Refer to Headquarters report for details.

-2-

-

,.

_

_

4.

Inspection and Enforcement Bulletin / Circular Followup The inspector reviewed action taken by the licensee with regard to Bulletins and Circulars to verify that responses to IE Bulletins represent the action taken by the licensee and that IE Circulars sent to the licensee were received and reviewed.

(Closed) IE Circular 78-13:

Inoperability of service water pumps.

(Closed) IE Circular 78-15:

Tilting disk check valves fail to close with gravity in vertical position.

(Closed) lE Circular 78-16:

Limitorque valve actuators.

5.

Office Review of Event Reports The inspector reviewed licensee's event reports to ascertain whether corrective actions discussed in the reports appear appropriate and whether.: 'ormation reported to the NRC satisfies reporting require-ments.

The following event reports were reviewed and are considered closed:

Unit 1 RO 75-31 dated November 11, 1978, Pressure switch failed to operate within limits.

RO 78-28 dated November 9, 1978, "A" SJAE off-gas monitor failed downscale.

Unit 2 RO 78-35 dated October 4, 1978, Reactor vent / refuel floor vent monitors spiking.

RO 78-37 dated November 16, 1978, Reactor building to suppression chamber vacuum breaker valve failed to open.

RO 78-38 dated November 25, 1978, Drywell vent valve could not be opened.

6.

Review of Quality Assurance Program The inspector conducted a review of the licensee's Quality Assurance program.

The inspector verified that; independent operations audits-3-

,.

t were being conducted by qualified technical staff personnel; QA audits are performed in accordance with a master plan and the scope of these audits are defined and administrative controls of the program are adequate. The inspector also verified that the licen-see's control of quality assurance manual revisions was adequate.

Quality assurance audits for 1978 were reviewed for overall effec-tiveness and appeared to be adequate.

No items of noncompliance or deviations were identified.

7.

Exit Interview The inspector met with licensee representatives (denoted in Paragraph 1) on January 25, 1978.

The inspector summarized the scope and findings of the inspection. The licensee announced that at the conclusion of the current Unit I refuel outage Mr.

S. I!opewell, Radiation-Chemistry Supervisor will leave the station and be replaced by Mr. R. Flessner.

-4-