IR 05000155/1986001

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Errata to SALP Rept 50-155/86-01,consisting of App & Corrected Pages 11.12,13,22 & 25
ML20211G473
Person / Time
Site: Big Rock Point File:Consumers Energy icon.png
Issue date: 02/17/1987
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20211G425 List:
References
50-155-86-01, 50-155-86-1, NUDOCS 8702250397
Download: ML20211G473 (13)


Text

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SALP 6

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APPENDIX

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SALP BOARD REPORT.

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U.S. NUCLEAR REGULATORY COPWISSION

REGION III

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SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

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,

50-155/86001 l

Inspection Report

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Consumers Power Company

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Name of Licensee

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Bic Rock Point Plant

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Fame of Facility

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November 1, 1984 through March 31, 1986

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Assessment Period

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8702250397 870217

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PDR

ADOCK 05000155

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Big Rock Point Plant

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Meeting Summary

The findings and conclusions of the SALP Board are documented in Inspection

Report No. 50-155/86001.

They were discussed with the licensee on July 21,

1986, at the Region III office in Glen Ellyn, Illinois.

The licensee's

regulatory performance was presented in each functional area.

Overall

performance and performance in each functional area was found to be acceptable.

The performance rating improved in the area of Licensing Activities.

Performance in the areas of Plant Operations and Surveillance and Inservice

Testing declined based on increased frequency of personnel error and problems

encountered in implementing administrative controls for the Plant Operations

area, and missed surveillances for the Surveillance and Inservice Testing area.

While the performance rating in the new area of Outages was given a Category 3

based on the Severity Level III violation received during the middle of the

SALP period, there has been no opportunity to evaluate the effectiveness of

your corrective measures.

The Emergency Preparedness and Security areas

continued to have a high level of performance.

While this meeting was primarily a discussion between the licensee and the

NRC, it was open to members of the public as observers.

The following licensee and NRC personnel were in attendance on July 21, 1986.

Consumers Power

J. Reynolds, Executive Vice President

F. W. Buckman, Vice President, Nuclear Operations

G. B. Slade, Executive Director, Nuclear Assurance

K. W. Berry, Director, Nuclear Licensing

D. Hoffman, Plant Superintendent

R. R. Frisch, Senior Licensing Analyst

T. C. Bordine, Staff Engineer

B. Alexander, Technical Engineer

U.S. Nuclear Regulatory Commission

A. B. Davis, Deputy Regional Administratcr

E. G. Greenman, Deputy Director, Division of Reactor Projects

D. C. Boyd, Chief, Reactor Projects Section 20

S. Guthrie, Senior Resident Inspector, Big Rock Point

R. B. Landsman, Project Manager, Section 2D

J. Bauer, Technical Staff

NRC Headquarters

T. S. Rotella, NRR Project Manager

J. A. Zwolinski, Director, BWR Project Directorate No.1

.

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ERRATA SHEET

.

Facility: Big Rock Point

SALP Report No.

50-155/86001

Page

Line

Now Reads

Should Read

39-43

The licensee... to

Delete

shutdown.

Basis for Change: Additional information provided by licensee subsequent to

SALP issuance.

45

no training was provided with the exception of

until February 1986,

some I&C classes and

certain skill training,

no training was provided

during this SALP period

until February 1986

Basis for C(a ge:

The phrase incorrectly implied that training was never

provided and should have stated only that during most of

the SALP it wasn't.

26-27

As of this date only

Delete

'

15 have been checked

Basis for Change: Additional information provided by licensee subsequent to

SALP issuance.

38-39

Forced retirement of

Untimely retirement of

i

several older key

several older key members

members of the licensee

of the licensee staff,

staff

which was honored by

licensee management

Basis for Change: The phrase was not meant to mean that the employees were

forced out, only that they were encouraged.

,

I

26

It is noted however that


,

some relief in the form

-

of additional QA personnel

i

from the Palisades plant

'

.

was provided in September

'

.

1985.

t

B4 sis for Change: Additianal information provided by licensee subsequent to

,

i

SALP issuance.

.

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C.

Maintenance / Modifications

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1.

Analysis

Portions of eight routine inspections by the Resident In ector

reviewed maintenance activities. One violation discuss d in

Section IV.H Outages, reflects on the licensee's abi ty to

conduct maintenance work during outages.

In additio, two

Regionally based inspections were performed.

The i spections

included reviews of normal maintenance and modiff

tion activities

j

to ensure that approvals were obtained prior to

itiating work,

activities were accomplished using approved to edures, post

maintenance testing was completed prior t

e rning components

or systems to service, and parts and ma

were properly

certified.

In addition, work plannin

cheduling was

reviewed as well as the effectiveness

ministrative controls

toensureproperpriorityisassigneg

violations or

daviations noted.

During the evaluation period the 44,

see interrupted plant

!

operations for nine unscheduled

tenance outage periods

ranging from one to 11 days,

outages were required to

repair Reactor Depressurizat

stem (RDS) valves due to the

!

degraded condition of the

preventing successful performance

of quarterly surveillances.

ese included one forced shutdown

..

i

required by Technical

ecif cations unidentified leak rate

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limitations. Two ou

(p iods of one day each were required

to successfully repa

K DB, seal leakage to heat exchanger

for Reactor Recir 1

Pump No. 2.

Also, two outages of three

.

and four days eac

required to diagnose and correct steam

leakage from the reac r vessel head o-rings. One outage period

of four days was us

to replace a recirculation pump seal, and

a one day outage w

required to correct steam leaks associated

i

with the plant sc m un December 7,1985.

Proper plannin and outage control was generally evident for the

.

nine unschedu ed outages. Although unplanned, the licensee in

the case of he RDS and recirculation pump outages had sufficient

'

warning to lan activities, prepare parts and procedures, and

perform o er maintenance work that fell within the scope and

time li tations of the forced outage.

Repair to RDS valve top

!

assemb es have become commonplace to the point that the licensee

'

routi ely overhauls spare top assemblies.

The licensee did not

ove aul the spare recirculation pump seal in advance of the

l

ou ge and was still rebuilding the seal as the plant was being

.

utdown to perform the replacement, even though the pump had been

died for two weeks prior to shutdown.

The licensee made

extensive use of vendor consultants and pump experts from the

<

4

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- _ -. - - - -

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... - -

.

. - -

.

,

C.

Maintenance / Modifications

'

1.

Analysis

Portions of eight routine inspections by the Resident Inspector

reviewed maintenance activities. One violation discussed in

Section IV.H. Outages, reflects on the licensee's ability to

conduct maintenance work during outages.

In additional, two

Regionally based inspections were performed. The inspections

included reviews of normal maintenance and modification

activities to ensure that approvals were obtained prior to

initiating work, activities were accomplished using approved

procedures, post maintenance testing was completed prior to

returning components or systems to service, and parts and

materials were properly certified.

In addition, work planning

and scheduling was reviewed as well as the effectiveness of

administrative controls to ensure proper priority is assigned.

No violations or deviations noted.

During the evaluation period, the licensee interrupted plant

operations for nine unscheduled maintenance outage periods

ranging from one to 11 days. Three outages were required to

repair Reactor Depressurization System (RDS) valves due to the

degraded condition of the system preventing successful

performance of quarterly surveillances. These included one

forced shutdown required by Technical Specifications

unidentified leak rate limitations. Two outage period of one

day each were required to successfully repair IA-60B, seal

leakage to heat exchanger for Reactor Recirculation Pump

No. 2.

Also, two outages of three and four days each were

required to diagnose the correct steam leakage from the reactor

vessel head o-rings. One outage period of four days was used

to replace a recirculation pump seal, and a one day outage was

required to correct steam leaks associated with the plant scram

on December 7, 1985.

Proper planning and outage control was generally evident for

the nine unscheduled outages. Although unplanned, the licensee

in the case of the RDS and recirculation pump outages had

sufficient warning to plan activities, prepare parts and

procedures, and perform other maintenance work that fell within

the scope and time limitations of the forced outage.

Repair to

RDS valve top assemblies have become commonplace to the point

that the licensee routinely overhauls spare top assemblies.

The licensee made extensive use of vendor consultants and pump

experts from the General Office for the seal replacement,

resulting in a refined and useful procedure for rebuilding and

installation. Outages for RDS and recirculation pump repairs

were well planned and executed. Outages to repair IA-60B

represented an operational situation that offered little

warning and first attempts at repairs were unsuccessful. The

.

General Office for the seal replacement, resulting in a refined

and useful procedure for rebuilding and installation. Outages

for RDS and recirculation pump repairs were well planned and

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executed. Outages to repair IA-60B represented an operationa

situation that offered little warning and first attempts at

repairs were unsuccessful. The reactor vessel o-ring offer d

no warning prior to failure, but successful repairs were. layed

when the problem was misdiagnosed. Once the decision wa made

to perform the vessel head removal and ring replacemen the

physically demanding job was successfully completed w' h

conservative consideration to ALARA and personne sa ety.

Maintenance work (including mechanical, electr

, and

<

instrument / control) at Big Rock Point is per

by generally

.

competent repairmen who exhibit craftsmans

d a general

familiarity with the facility and the equip

The amount

.

of unsuccessful repair attempts resulting W ework is generally

small.

Repairmen generally are cognizant o procedural require-

ments associated with their assigned

, communicate effec-

tively with operators and health ph

echnicians, and reflect

concern for ALARA considerations.

the input repairmen

provide to machinery history is o

with co-workers and supervisors ' g.arginal, communication

N

tes genuine interest in

continued safe and successful

on of the reactor. The

mechanic who performs the work jo example, often participates

in post maintenance testin. W

e the retirement of older,

experienced maintenance de

tm t personnel during the period

had a negative impact on

,ance as documented further

in Section IV.H, Outage

e naintenance staff demonstrated

flexibility and dedica i

roughout the evaluation period.

The size of the maintenon

staff is generally adequate for all

periods other than major

> fueling outages. A gradually

increasing backlog of ma ntenance orders over the period is

explained in part by i

reased emphasis on skills training which

over the short term r uces staff size availability.

Like the Operations Department the loss of older experienced

l

personnel due to etirement or other duties has altered composi-

l

tion of the main enance staff. While the I & C group remained

unchanged, in

e mechanical maintenance group of 12 men, five

'

were added dur ng the assessment period. Because hiring and

promotion is eavily influenced by Labor Relations agreements

that emphas'ze seniority, newly added staff members generally

l

have litt

or no experience with nuclear powered generating

plants i general or Big Rock Point specifically. Although the

I

license has long recognized the need for maintenance staff

l

traini g, no training was provided until February 1986, when a

i

regu'

r program of skills training offsite was initiated. The

skiy s training is general in nature and is not nuclear plant

splcific. No nuclear plant system or concepts training is

provided.

!

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reactor vessel o-ring offered no warning prior to failure, but

successful repairs were delayed when the problem was misdiagnosed.

Once the decision was made to perform the vessel head removal and

-

'

ring replacement the physically demanding job was successfully

completed with conservative consideration to ALARA and

personnel safety.

Maintenance work (including mechanical, electrical, and

instrument / control) at Big Rock Point is performed by generally

competent repairmen who exhibit craftsmanship and a general

familiarity with the facility and the equipment.

The amount

of unsuccessful repair attempts resulting in rework is generally

small.

Repairmen generally are cognizant of procedural require-

ments associated with their assigned task, communicate effec-

tively with operators and health physics technicians, and reflect

concern for ALARA considerations. While the input repairmen

provide to machinery history is often marginal, communication

with co-workers and supervisors indicates genuine interest in

continued safe and successful operation of the reactor. The

mechanic who performs the work, for example, often participates

in post maintenance tasting. While the retirement of older,

experienced maintenance department personnel during the period

had a negative impact on performance as documented further

in Section IV.H, Outages, the maintenance staff demonstrated

flexibility and dedication throughout the evaluation period.

The size of the maintenance staff is generally adequate for all

periods other than major refueling outages. A gradually

increasing backlog of maintenance orders over the period is

explained in part by increased emphasis on skills training which

over the short term reduces staff size availability.

Like the Operations Department the loss of older experienced

personnel due to retirement or other duties has altered composi-

tion of the maintenance staff. While the I & C group remained

unchanced, in the mechanical maintenance group of 12 men, five

were added during the assessment period. Because hiring and

promotion is heavily influenced by Labor Relations agreements

that emphasize seniority, newly added staff members generally

have little or no experience with nuclear powered generating

plants in general or Big Rock Point specifically. Although the

licensee has long recognized the need for maintenance staff

training, with the exception of some I&C classes and certain

skill training, no training was provided during this SALP

period until February 1986, when a regular program of skills

training offsite was initiated. The skills training is general

in nature and is not nuclear plant specific.

No nuclear plant

system or concepts training is provided.

.

First line supervision in the maintenance department reflects

adequate technical skills and managerial competence. During the

1985 outage, the maintenance department overcame the loss of

staff experience, inadequate outage planning, and parts proc

e-

ment to accomplish a relatively large number of modificati

s,

repairs, and preventive maintenance tasks.

Throughout the evaluation period several recurring pro ems were

not successfully repaired or adequately addressed. V ve M0-7067,

Turbine Bypass Isolation Valve, was not declare op able for

much of the evaluation period, based on diffic ti s with the

valve operator. Reactor Depressurization Sy

m RDS) valves

exhibit inherent design deficiencies that

sulted in three

forced shutdowns during the assessment p

1d a long history

of problems dating back to their instal

Management,

.

however, has not placed a high priority

comprehensive

solution and as a result the RDS system w

not improved over

the period.

Problems with the Emer M y iesel Generator (EDG)

fuel pump were allowed to continue nu

design change to the

pump mounting bracket scheduled

pletion during the 1985

refueling outage was deleted i

fort to return the plant to

an operable status. Shortly

ter the pump failed again,

placing the EDG in an actio

ment for the generator's

Limiting Condition for Oped]

Finally, the licensee made a

.

commitment to verify, prior

startup from the 1985 outage,

Limitorque Switch sett

so 18 Limitorque Valves the licensee

considered important

ty. As of this date only 15 have

been checked. The t

.ettings for valve M0-7067 have been

reset on three di

occasions, indicating a lack of decisive

direction on probl

th Limitorques Operators that goes back

to September, 1984, a was addressed in SALP 5.

SALP 5 expressed c cern that the Prevention Maintenance (PM)

program may be in dequate to address aging equipment. At the end

of this assessm t period the PM program continues to be reactive

in nature, rel

ng heavily on visual inspections that do not

involve disa embly or physical measurements, and on the obser-

vations of

erators monitoring noticeable changes in component

operating

aracteristics. There continues to be no program to

analyze

r trends in failures or any other measurable parameter

other

an pump capacity on certain pumps. The licensee has not

respo ed to NRC initiatives to upgrade the PM program to incor-

pora e vendor recommendations and industry experience. The plant

co

inues to rely on surveillance tests to identify problems that

m

be in some advanced stage of development due to aging

quipment. At the close of the assessment period the licensee

assigned an engineer to develop a program of predictive analysis

focusing on vibration and lubricating oil analysis.

Evidence of

problems associated with aging of plant equipment during the

assessment period included:

a.

Several examples of end of service life for solenoid valves

on the turbine stop valve, diesel fire pump (DFP), and the

exhaust ventilation downstream isolation valve.

.

First line supervision in the maintenance department reflects

adequate technical skills and managerial competence. During the

1985 outage, the maintenance department overcame the loss of

staff experience, inadequate outage planning, and parts procure-

ment to accomplish a relatively large number of modifications,

repairs, and preventive maintenance tasks.

Throughout the evaluation period several recurring problems were

not successfully repaired or adequately addressed. Valve M0-7067,

Turbine Bypass Isolation Valve, was not declared operable for

much of the evaluation period, based on difficulties with the

valve operator. Reactor Depressurization System (RDS) valves

exhibit inherent design deficiencies that have resulted in three

forced shutdowns during the assessment period and a long history

of problems dating back to their installation. Management,

however, has not placed a high priority on a comprehensive

solution and as a result the RDS system was not improved over

the period. Problems with the Emergency Diesel Generator (EDG)

fuel pump were allowed to continue and a design change to the

pump mounting bracket scheduled for completion during the 1985

refueling outage was, deleted in an effort to return the plant to

an operable status.

Shortly thereafter the pump failed again,

placing the EDG in an action statement for the generator's

Limiting Condition for Operation.

Finally, the licensee made a

commitment to verify, prior to startup from the 1985 outage,

Limitorque Switch settings on 18 Limitorque Valves the licensee

considered important to safety. The torque settings for valve

M0-7067 have been reset on three different occasions, indicating

a lack of decisive direction on problems with Limitorques

Operators that goes back to September,1984, as was addressed

in SALP 5.

SALP 5 expressed concern that the Prevention Maintenance (PM)

program may be inadequate to address aging equipment. At the end

of this assessment period the PM program continues to be reactive

in nature, relying heavily on visual inspections that do not

involve disassembly or physical measurements, and on the obser-

vations of operators monitoring noticeable changes in component

operating characteristics. There continues to be no program to

analyze for trends in failures or any other measurable parameter

other than pump capacity on certain pumps. The licensee has not

responded to NRC initiatives to upgrade the PM program to incor-

porate vendor recomendations and industry experience. The plant

continues to rely on surveillance tests to identify problems that

may be in some advanced stage of development due to aging

equipment. At the close of the assessment period the licensee

assigned an engineer to develop a program of predictive analysis

focusing on vibration and lubricating oil analysis. Evidence of

problems associated with aging of plant equipment during the

assessment period included:

a.

Several examples of end of service life for solenoid valves

on the turbine stop valve, diesel fire pump (DFP), and the

exhaust ventilation downstream isolation valve.

.

Operations Department personnel performed fuel handling

operations for the 1985 refueling outage.

Fuel handling was

safely conducted by adequately trained individuals in accordance

-

with approved procedural requirements.

Staffing on both the

reactor deck and in the control room was adequate, and communi-

cation between the two areas was effective.

Management involve-

ment in refueling activities was evident.

Tool control and

status board mainteaance was adequate.

Licensee responsive ss

to NRC initiative was evident by their prompt action to co rect

procedural deficiencies in data recording and in relocat' n of

bagged equipment that had obstructed access to the refu

ling

deck status board.

During the 1935 refueling outage several incid

s ccurred

which demonstrated inadequate management con

er the outage

process.

The incidents involved:

Repeated examples of contractors and

see travel crew

personnel, not normally assigned to B

Rock Point,

performing work on the wrong com nen or system, pointing

to inadequate control over the

ties of travel crews

and contractors.

Repeated examples of superv

, maintenance, operations,

and engineering personnel p@a19d ravel crew personnel,

circumventing or failing

t

ere to administrative

~

requirements, particula)

ose related to component

tagging and isolation.

Repeated examples b

'n ividuals, throughout the

organization, o

ntion to detail and failure to

exercise suffic

re in performance of outage related

work to ensure p

safety.

Several factors contr' uted to the breakdown in the outage

management process:

Throughout

e facility, components, valves, and systems

identifica on was generally inadequate, with many compo-

nents un1

eled.

The licensee had not acted upon earlier

request from the Resident Inspector to improve component

identi ication and discounted warnings on the potential for

mish-s.

F ced retirement of several older key members of the

icensee staff, including the Operations Superintendent,

the coordinator of the ISI program, an experienced Shift

Supervisor, and a Maintenance Supervisor who in the past

had acted as a coordinator and single contact point for

control of travel crew personnel.

The impact of the loss

of these individuals two months prior to commencement of

[

.

Operations Department personnel performed fuel handling

operations for the 1985 refueling outage.

Fuel handling was

'

safely conducted by adequately trained individuals in accordance

with approved procedural requirements. Staffing on both the

reactor deck and in the control room was adequate, and communi-

cation between the two areas was effective. Management involve-

ment in refueling activities was evident. Tool control and

status board maintenance was adequate. Licensee responsiveness

to NRC initiative was evident by their prompt action to correct

procedural deficiencies in data recording and in relocation of

bagged equipment that had obstructed access to the refueling

deck status board.

During the 1985 refueling outage several incidents occurred

which demonstrated inadequate management control over the outage

process. The incidents involved:

Repeated examples of contractors and licensee travel crew

personnel, not normally assigned to Big Rock Point,

performing work on the wrong component or system, pointing

to inadequate control over the activities of travel crews

and contractors.

Repeated examples of supervisors, maintenance, operations,

and engineering personnel, and travel crew personnel,

circumventing or failing to adhere to administrative

requirements, particularly those related to component

tagging and isolation.

Repeated examples by individuals, throughout the

organization, of inattention to detail and failure to

exercise sufficient care in performance of outage related

work to ensure plant safety.

Several factors contributed to the breakdown in the outage

management process:

'

Throughout the facility, components, valves, and systems

identification was generally inadequate, with many compo-

nents unlabeled. The licensee had not acted upon earlier

requests from the Resident Inspector to improve component

identification and discounted warnings on the potential for

mishaps.

Untimely retirement of several older key members of the

licensee staff, which was honored by licensee management,

including the Operations Superintendent, the coordinator

of the ISI program, an experienced Shift Supervisor, and

a Maintenance Supervisor who in the past had acted as

a coordinator and single contact point for control of

travel crew personnel. The impact of the loss of these

individuals two months prior to commencement of

F

.

During the evaluation period there was evidence that the site

staff was in danger of becoming overburdened by assignment of

-

several functions formerly performed by the corporate QA grc p.

Those added duties were subsequently completed or reassigned

elsewhere and the site staff appears adequate for the rem (ning

workload.

The site QA staff communicates effectively wi

i plant

management and is persistent in pressing for managemen action

,

to resolve audit findings. The Plant Review Committe (PRC)

'

considers the quality aspects of technical and safet issues.

In turn, plant management generally demonstrate th r regard

for the significance of findings and comments

the QA staff.

Site QC inspectors are generally thorougt, and

cientious and

draw heavily on their plant experience. Botgj

QA and QC site

staff are responsive to NRC initiatives a W iries.

Licensee corporate management detracted

the effectiveness of

Programs and Administrative controls affe

ng quality. Examples

include:

a.

Licensee corporate management,

ransferring to the site

staff several significant Qu

Assurance functions with-

out a corresponding increas

vailable site resources,

placed a burden on the sta

ch resulted in QA reviews

thatwerelesscomprehensQa.,

ithdrawal of commitments to

..

support audit activitie

ff site, and a virtual elimination

of time available to au

s to review and observe activi-

ties in the plant.

Some

functions were performed by QC

inspectors.

The rel ta e of corporate management to

respond to the co

of the site QA Superintendent in

this regard and t

oor response to NRC initiatives to

address the iss

noted.

b.

Licensee Corporate anagement deleted entirely fifteen NODS,

the document in w ich the licensee staff can theoretically

be assured of fi ding all applicable code and regulatory

requirements c piled in one location.

The NODS are the

means by whic the licensee's Quality Assurance Program

Description or Operational Nuclear Power Plants (Topical

Report CPC-A) is implemented, and results from a commitment

l

made in t

licensee's Regulatory Performance Improvement

Program

bmitted in response to a March 9, 1981 Confirmatory

Order.

holesale deletion of the NODS without a review to

insur all of the quality requirements contained therein

'

were 1 ready addressed in existing administrative procedures

,

j

res ted in a period when the quality requirements were not

av lable to the NODS user.

Inspectors identified at least

o examples of cancelled NODS being referenced in other

,

rocedures.

.

.

.

..

e

.

During the evaluation period there was evidence that the site

QA staff was in danger in becoming overburden by assignment of

several functions formerly performed by the corporate QA group.

Those added duties were subsequently completed or reassigned

elsewhere and the site staff appears adequate for the remaining

workload. The site QA staff communicates effectively with plant

management and is persistent in pressing for management action

to resolve audit findings. The Plant Review Committee (PRC)

considers the quality aspects of technical and safety issues.

In turn, plant management generally demonstrates their regard

.

for significance of findings and coninents from the QA staff.

Site QC inspecto s are generally thorough and conscientious and

draw heavily on their plant experience. Both the QA and QC site

staff are respontible to NRC initiatives and inquiries.

Licensee corporate management detracted from the effectiveness

of Programs and Administrative controls affecting quality.

Examples include:

a.

Licensee corporate management, by transferring to the

site staff several significant Quality Assurance functions

without a correspor. ding increase in available site resources,

placed a burden on the staff which resulted in QA reviews

that were less comprehensive, withdrawal of commitments to

support audit activities off site, and a virtual elimination

of time available to auditors to review and observe

activities in the plant. Some QA functions were performed

by QC inspectors.

It is noted however that some relief in

the form of additional QA personnel from the Palisades

plant was provided in September 1985. The reluctance of

corporate management to respond to the concerns of the

site QA Superintendent in this regard and their poor

response to NRC initiatives to address the issue was noted,

b.

Licensee Corporate management deleted entirely fifteen N0DS,

the document in which the licensee staff can theoretically

be assured of finding all applicable code and regulatory

requirements complied in one location.

The N0DS are the

means by which the licensee's Quality Assurance Program

Description for Operational Nuclear Power Plants (Topical

Report CPC-2A) is implemented, and results from a commitment

made in the licensee's Regulatory Performance Improvement

Prograa submitted in response to a March 9, 1981

Confirmatory Order. Wholesale deletion of the N0DS without

a review to insure all of the quality requirements contained

therein were already addressed in existing administrative

procedures resulted in a period when the quality

requirements were not available to the N0DS user.

Inspectors identified at least two examples of

cancelled N0DS referenced in other procedures.

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