ENS 52932
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ENS Event | |
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12:37 Aug 28, 2017 | |
Title | |
Event Description | On 8/28/2017 at 0837 [EDT], VC Summer Nuclear Station automatically tripped due to a turbine trip. The turbine trip was caused by the Main Generator Differential Lockout due to a fault on the center phase lightning arrester on the Main Transformer (XTF-001).
There were no complications with the trip. All control rods fully inserted. Balance of Plant (BOP) buses automatically transferred to their alternate power source XTF 31/32. All Emergency Feedwater pumps started as required. All systems responded as required. The plant is stable in Mode 3. Station personnel are investigating the cause of the fault on the main transformer lightning arrester. This event is reportable per 10 CFR 50. 72(b)(2)(iv)(B) and 10 CFR 50. 72(b)(3)(iv)(A). The NRC Resident Inspector has been notified. The unit is currently stable in Mode 3 with decay heat removal via the Main Steam to the Main Condenser. The licensee will inform both State and local authorities. |
Where | |
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Summer South Carolina (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+-1.7 h-0.0708 days <br />-0.0101 weeks <br />-0.00233 months <br />) | |
Opened: | Hank Kirkland 10:55 Aug 28, 2017 |
NRC Officer: | Steve Sandin |
Last Updated: | Aug 28, 2017 |
52932 - NRC Website
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Unit 1 | |
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Reactor critical | Critical |
Scram | A/R |
Before | Power Operation (100 %) |
After | Hot Standby (0 %) |
Summer with 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
WEEKMONTHYEARENS 569782024-02-19T07:36:00019 February 2024 07:36:00
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