ENS 46661
ENS Event | |
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07:40 Mar 7, 2011 | |
Title | Inadvertant Auto-Start Signal to the 1B Diesel Generator During Testing |
Event Description | Farley Unit One was conducting FNP-1-STP-80.8, [test procedure for] 1B DG [Diesel Generator] 1000 KW load rejection. After successfully completing the load rejection portion of the procedure, the control room staff was restoring the 1B diesel to a normal auto start alignment. With the 1B diesel running, the plant operator was required to reset the 1B DG loading sequencer. He incorrectly pressed the Emergency Start reset push-button instead of the Sequencer reset push-button. As a result, the Emergency Diesel generator stop light illuminated for a brief few seconds and then extinguished. Subsequently due to the test configuration, the 1B diesel received an auto-start signal and returned to the running condition prior to the Emergency Start reset. Although further investigation is continuing, this report is being made due to an apparent valid actuation of ESF equipment.
This event had no impact on other equipment or the plant electrical alignment. The Sequencer reset push-button and the Emergency Start reset push-button are not in close proximity to each other. The plant operator was assessed for fatigue and it was determined that fatigue was not a factor. The plant operator was removed from duties pending remedial training and assessment. The licensee has notified the NRC Resident Inspector.
The 8-hour non-emergency report (EN#46661) per 10CFR50.72(b)(3)(iv)(A) was conservatively reported based on the potential for a valid actuation of an Emergency Diesel Generator (EDG) during a 1000 KW load rejection surveillance test. During the restoration phase of the load rejection test to align the 1B EDG to a normal shutdown configuration, a plant operator incorrectly pressed the Emergency Start Reset (ESR) push-button instead of the Sequencer Reset push-button. As a result, the 1B EDG stop light illuminated momentarily and then extinguished. The 1B EDG received a momentary shutdown signal, but remained in a running condition. Upon completion of the 1B EDG circuit analysis, It was determined that the 1B EDG did not receive a valid actuation of the EDG safety function. Depressing the ESR push-button caused the emergency start relays to deenergize and remain de-energized. The emergency start relays energize on receipt of valid signals in response to actual plant conditions or parameters satisfying the requirements for the initiation of the safety function of the EDG. Therefore per section 3.2.6 of NUREG-1022, the 1B EDG did not receive a valid actuation signal. The NRC Resident Inspector has been notified. Notified R2DO(Musser) |
Where | |
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Farley Alabama (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+2.85 h0.119 days <br />0.017 weeks <br />0.0039 months <br />) | |
Opened: | Alton Deweese 10:31 Mar 7, 2011 |
NRC Officer: | John Shoemaker |
Last Updated: | Mar 9, 2011 |
46661 - NRC Website
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Unit 1 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
WEEKMONTHYEARENS 569712024-02-16T11:34:00016 February 2024 11:34:00
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