ENS 46660
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ENS Event | |
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21:44 Mar 6, 2011 | |
Title | Manual Reactor Trip Due to Secondary Sodium Concentrations Exceeding Chemistry Limits |
Event Description | This is a 4-hr Non-Emergency notification to the NRCOC [Nuclear Regulatory Commission Operations Center] for an event that results in actuation of the Reactor Protection System (RPS) when the reactor is critical in accordance with 10CFR50.72(b)(2)(iv)(B).
On 3/6/11 at approx 16:20 [EST], Steam Generator sodium concentrations started to rise and exceeded 3-ONOP-071.1 (Secondary Chemistry Deviation from limits) Action Level 3 criteria (250 ppb Sodium). The plant power was reduced to 25% per 3-ONOP-100, Fast Load Reduction, and a manual plant trip [was] initiated per procedure at 16:44 [EST]. Unit [3] is stabilized in Mode 3, and [the licensee] is performing secondary clean-up. All rods fully inserted. All safety systems functioned as required. The reactor trip was uncomplicated. Unit 4 was unaffected by this event. The licensee has notified the NRC Resident Inspector. |
Where | |
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Turkey Point Florida (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation | |
LER: | 05000250/LER-2011-001 |
Time - Person (Reporting Time:+-2.1 h-0.0875 days <br />-0.0125 weeks <br />-0.00288 months <br />) | |
Opened: | Paul Reimers 19:38 Mar 6, 2011 |
NRC Officer: | John Knoke |
Last Updated: | Mar 6, 2011 |
46660 - NRC Website
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Unit 3 | |
---|---|
Reactor critical | Critical |
Scram | Yes, Manual Scram |
Before | Power Operation (23 %) |
After | Hot Standby (0 %) |
WEEKMONTHYEARENS 568132023-10-25T01:59:00025 October 2023 01:59:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip ENS 567552023-09-22T22:19:00022 September 2023 22:19:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip ENS 566582023-08-04T17:20:0004 August 2023 17:20:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip ENS 551172021-03-01T16:12:0001 March 2021 16:12:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip Due to Reactor Protection System Actuation ENS 548472020-08-21T03:54:00021 August 2020 03:54:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Steam Generator Water Level Control ENS 548442020-08-19T17:25:00019 August 2020 17:25:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip During Startup ENS 548392020-08-18T01:13:00018 August 2020 01:13:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Rising Steam Generator Level ENS 547622020-07-06T01:09:0006 July 2020 01:09:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Reactor Trip Due to Turbine Trip ENS 540722019-05-18T15:08:00018 May 2019 15:08:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due Grid Disturbance ENS 529602017-09-10T22:55:00010 September 2017 22:55:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip on Lowering Steam Generator Water Level ENS 526232017-03-18T15:07:00018 March 2017 15:07:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Reactor Trip and Loss of Ability for Unit 4 to Supply Power to Unit 3 ENS 521362016-07-30T07:33:00030 July 2016 07:33:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Turkey Point Unit 3 Shutdown Due to Water Hammer ENS 510652015-05-12T08:30:00012 May 2015 08:30:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Main Generator Differential Trip ENS 503542014-08-11T14:20:00011 August 2014 14:20:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip on Loss of Instrument Air Followed by Safety Injection ENS 501402014-05-25T09:36:00025 May 2014 09:36:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip Due to Turbine Trip on Loss of Condenser Vacuum ENS 490212013-05-10T15:08:00010 May 2013 15:08:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Unit 3 Manual Reactor Trip Due to Malfunction of Turbine Valves ENS 489482013-04-19T21:20:00019 April 2013 21:20:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Due to Loss of Offsite Power Greater than 15 Minutes ENS 488172013-03-12T18:31:00012 March 2013 18:31:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip Due to Turbine Inlet Pressure Perturbation ENS 487642013-02-18T06:31:00018 February 2013 06:31:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to High Seal Leakoff on Reactor Coolant Pump 3A ENS 487442013-02-12T03:36:00012 February 2013 03:36:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Turbine Trip on Loss of Condenser Vacuum ENS 466602011-03-06T21:44:0006 March 2011 21:44:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Secondary Sodium Concentrations Exceeding Chemistry Limits ENS 464712010-12-10T03:58:00010 December 2010 03:58:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip After Indications of a Condenser Tube Leak ENS 464192010-11-15T11:03:00015 November 2010 11:03:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Loss of a Circulating Water Pump with Another Pump Out of Service for Maintenance ENS 462742010-09-23T21:14:00023 September 2010 21:14:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Inadvertent Energization Generator Trip ENS 462652010-09-22T00:17:00022 September 2010 00:17:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip ENS 462352010-09-08T17:45:0008 September 2010 17:45:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip During Maintenance on a Reactor Protection System Relay ENS 456192010-01-11T15:55:00011 January 2010 15:55:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Initiated Due to High Steam Generator Level ENS 440162008-02-29T09:51:00029 February 2008 09:51:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to High Steam Generator Water Level ENS 440092008-02-26T18:09:00026 February 2008 18:09:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Units 3 and 4 Tripped Due to Grid Fluctuations ENS 420562005-10-15T11:02:00015 October 2005 11:02:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Auxiliary Feedwater Actuation on a Manual Reactor Trip ENS 418002005-06-27T07:16:00027 June 2005 07:16:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Declaration of an Unusual Event Due Transformer Fire >10 Minutes ENS 415162005-03-24T00:56:00024 March 2005 00:56:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Reactor Manually Tripped from 20% Power During Load Reduction. ENS 415112005-03-22T08:47:00022 March 2005 08:47:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Manually Tripped Following Loss of Main Feed Pump ENS 412982004-12-29T03:46:00029 December 2004 03:46:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Generator Exciter Cooling Water Leak ENS 412922004-12-25T12:36:00025 December 2004 12:36:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Unit4 Manually Tripped Due to Lowering Condenser Vacuum ENS 412572004-12-14T16:45:00014 December 2004 16:45:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Reactor Manually Tripped Due to Fire on Unit 3 Hp Turbine ENS 407522004-05-14T21:29:00014 May 2004 21:29:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Scram Due to Lowering Steam Generator Level 2023-09-22T22:19:00 | |
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