ENS 40472
ENS Event | |
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20:29 Jan 23, 2004 | |
Title | Manual Reactor Trip with Safety Injection Actuation Signals |
Event Description | At 1529 ET the reactor was manually tripped due to low steam generator level as a result of the loss of the 22 SGFP (Steam Generator Feed Pump). When the reactor was tripped, the turbine bypass and atmospheric dump valves went full open and did not shut. This lead to a SIAS (Safety Injection Actuation Signal) and SGIS (Steam Generator Isolation Signal). At 1718 ET, a second SIAS actuation occurred while reestablishing pressurizer level. The cause of the SGFP trip is unknown. The cause of the over steaming on turbine bypass valves and atmospheric dump valves is unknown.
All control rods fully inserted. Auxiliary Feedwater initiated normally. The licensee stated that there was no actual ECCS injection to the RCS. The plant electrical system responded normally and all emergency diesel generators remain operable. All ECCS systems remain operable. There are no primary to secondary leaks. Decay heat is currently being removed via the steam-driven auxiliary feedwater pump and the atmospheric steam dumps. As of 1830 ET, primary pressure is approximately 2103 psi and pressurizer level is at 242 inches. Plant conditions are being stabilized at normal hot standby values . The licensee notified the NRC Resident Inspector who responded to the Control Room.
The licensee reported that their post trip review determined that the reactor received an automatic trip about 2 seconds before the manual trip. The automatic trip was due to low steam generator water level. The licensee notified the NRC Resident Inspector. Notified NRR (Reis) and R1DO (Meyer)
During post event review of the 1/23/04 Rx Trip event (40472), it was discovered that Unit 2 met the entry criteria for EOP-4, Excess Steam Demand event. This condition required declaration of an Unusual Event. No declaration was made at the time because of the transitory nature of the condition. Transitory conditions such as this, however, still require reporting per NUREG-1022, Rev. 2. Immediate notification to the NRC via the Emergency Notification System is required per 10 CFR 50.72(a)(1)(i). The NRC Resident Inspector will be notified. |
Where | |
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Calvert Cliffs Maryland (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
LER: | 05000318/LER-2004-001 |
Time - Person (Reporting Time:+-2.73 h-0.114 days <br />-0.0162 weeks <br />-0.00374 months <br />) | |
Opened: | David Frye 17:45 Jan 23, 2004 |
NRC Officer: | Mike Ripley |
Last Updated: | Mar 23, 2004 |
40472 - NRC Website
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Unit 2 | |
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Reactor critical | Critical |
Scram | A/R |
Before | Power Operation (100 %) |
After | Hot Standby (0 %) |
Calvert Cliffs with 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
WEEKMONTHYEARENS 573722024-10-10T09:57:00010 October 2024 09:57:00
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Remove Residual Heat, 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Dual Unit Automatic Reactor Trips Due to a Voltage Transient Resulting in Generator Trips ENS 500782014-05-01T14:16:0001 May 2014 14:16:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip ENS 497542014-01-22T02:25:00022 January 2014 02:25:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Dual Unit Trip on the Loss of the "21" 13Kv Bus ENS 490542013-05-21T09:33:00021 May 2013 09:33:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip After a Feed Pump Trip ENS 490122013-05-09T01:47:0009 May 2013 01:47:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip ENS 472082011-08-28T03:02:00028 August 2011 03:02:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event - Transformer Explosion Near Turbine Building ENS 459202010-05-12T17:51:00012 May 2010 17:51:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Rps Actuation - Load Reject ENS 457092010-02-18T13:24:00018 February 2010 13:24:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Dual Unit Automatic Reactor Trips Due to Partial Loss of Offsite Power ENS 430462006-12-12T14:07:00012 December 2006 14:07:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip During Turbine Control System Maintenance ENS 429952006-11-16T05:18:00016 November 2006 05:18:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Turbine Trip and Discovery of After-The-Fact Emergency Condition of an Unsual Event ENS 414522005-03-01T05:43:0001 March 2005 05:43:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Scram from 15% Power Due to High Turbine Vibration ENS 406012004-03-20T18:40:00020 March 2004 18:40:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip at Calvert Cliffs Unit 1 Due to a Loss of Feedwater ENS 404722004-01-23T20:29:00023 January 2004 20:29:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip with Safety Injection Actuation Signals 2024-07-18T19:24:00 | |