ENS 43046
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ENS Event | |
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14:07 Dec 12, 2006 | |
Title | Manual Reactor Trip During Turbine Control System Maintenance |
Event Description | At 0907 Calvert Cliffs Unit 1 experienced a manual reactor trip during turbine control maintenance. Maintenance was being performed on turbine control to replace circuit cards. This system is a two out of three logic system. Only one logic branch was being de-powered at a time. When the first logic branch was de-powered, the control room supervisor noticed a transient on the reactor coolant system and ordered a manual trip.
Decay heat is being removed via normal methods through the Turbine Bypass Valves to the condenser. At the time of the trip, 11 Auxiliary Feedwater (AFW) Pump was being tested but it was not feeding the steam generators. This was an uncomplicated trip. The plant responded normally to the event. All control rods fully inserted. The plant is stable and operators are maintaining the unit in Hot Standby. The licensee notified the NRC Resident Inspector. The trip had no effect on Unit 2, The licensee was in no significant safety system LCO action statement at the time (other than for the AFW 11 surveillance that was in progress at the time of the event.) The steam generators remained on normal feed throughout the event. No Porv's or safeties lifted during the transient. All systems functioned as required. The licensee is investigating how de-powering only one control system logic circuits resulted in the transient. |
Where | |
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Calvert Cliffs Maryland (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation | |
LER: | 05000317/LER-2006-004 |
Time - Person (Reporting Time:+-2.83 h-0.118 days <br />-0.0168 weeks <br />-0.00388 months <br />) | |
Opened: | Brian Hayden 11:17 Dec 12, 2006 |
NRC Officer: | Bill Huffman |
Last Updated: | Dec 12, 2006 |
43046 - NRC Website
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Unit 1 | |
---|---|
Reactor critical | Critical |
Scram | Yes, Manual Scram |
Before | Power Operation (100 %) |
After | Hot Standby (0 %) |
WEEKMONTHYEARENS 573722024-10-10T09:57:00010 October 2024 09:57:00
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