BSEP 13-0118, Special Report - Technical Requirements Manual Section 3.4, Accident Monitoring Instrumentation

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Special Report - Technical Requirements Manual Section 3.4, Accident Monitoring Instrumentation
ML13324A534
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 11/07/2013
From: Hamrick G
Duke Energy Progress
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
BSEP 13-0118
Download: ML13324A534 (3)


Text

George T. Hamrick Vice President ENERIGY, Brunswick Nuclear Plant P.O. Box 10429 Southport, NC 28461 o: 910.457.3698 NOV 0 7 2013 Serial: BSEP 13-0118 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555

Subject:

Brunswick Steam Electric Plant, Unit No. 2 Renewed Facility Operating License No. DPR-62 Docket No. 50-324 Special Report - Technical Requirements Manual Section 3.4, Accident Monitoring Instrumentation In accordance with Technical Requirements Manual Section 3.4, "Accident Monitoring Instrumentation," for the Brunswick Steam Electric Plant (BSEP), Unit No. 2, Duke Energy Progress, Inc., is submitting the enclosed Special Report associated with the Unit 2 drywell radiation monitors, TRM Table 3.4-1, Item 2.

This document contains no regulatory commitments.

Please refer any questions regarding this submittal to Mr. Lee Grzeck, Manager - Regulatory Affairs, at (910) 457-2487.

Sincerely, George T. Hamrick GTH/swr

Enclosure:

Special Report - Unit 2 Drywell Radiation Monitoring M~K

U.S. Nuclear Regulatory Commission Page 2 of 2 cc (with enclosure):

U. S. Nuclear Regulatory Commission, Region II ATTN: Mr. Victor M. McCree, Regional Administrator 245 Peachtree Center Ave, NE, Suite 1200 Atlanta, GA 30303-1257 U. S. Nuclear Regulatory Commission ATTN: Ms. Michelle P. Catts, NRC Senior Resident Inspector 8470 River Road Southport, NC 28461-8869 U. S. Nuclear Regulatory Commission ATTN: Mrs. Farideh E. Saba (Mail Stop OWFN 8G9A) 11555 Rockville Pike Rockville, MD 20852-2738 Chair - North Carolina Utilities Commission P.O. Box 29510 Raleigh, NC 27626-0510

BSEP 13-0118 Enclosure Page 1 of 1 Special Report - Unit 2 Drywell Radiation Monitoring

Background

On September 23, 2013, one channel of the Brunswick Steam Electric Plant (BSEP), Unit No. 2 post-accident drywell radiation monitoring 2-CAC-AT-1 262 (i.e., Function 2 of Technical Requirements Manual (TRM) Table 3.4-1, "Accident Monitoring Instrumentation") was removed from service, isolated, and declared inoperable. Operations personnel took this action because of concern that leakage from the monitor sample pump was causing drywell atmosphere pressure to decrease. As a result, Condition A of TRM Section 3.4, "Accident Monitoring Instrumentation," was entered, which requires the affected radiation monitoring channel to be returned to operable status within 31 days. On October 24, 2013, the monitoring instrumentation had not been restored to operable status within the required 31 days. As a result, Condition C of TRM Section 3.4 was entered. This Special Report is submitted in accordance with Condition C of TRM Section 3.4.

Cause of Inoperability On September 23, 2013, Operations personnel noted that drywell atmospheric pressure was slowly declining. Based on a prior history with minor leakage from the sample pump for the drywell radiation monitor, Operations personnel elected to remove the radiation monitoring system from service and close its associated isolation valves to arrest the decline in drywell atmospheric pressure. Since the monitor was isolated and its associated annunciator was disabled, it was declared inoperable.

Preplanned Alternate Monitoring Method During the time period that the drywell radiation monitoring system has been inoperable, redundant radiation monitoring system 2-CAC-AT-1260 has remained operable and in operation.

Plans for Restorinq the Instrumentation Site Engineering has determined that the total gas leakage from the sample pump is within the limits of normal, design parameters. Therefore, the system was returned to operable status on 05 November 2013.