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MONTHYEAR05000499/LER-2010-005, Regarding Startup Feed Pump 24 Breaker Failure and Unit 2 Reactor Trip2011-01-0303 January 2011 Regarding Startup Feed Pump 24 Breaker Failure and Unit 2 Reactor Trip Project stage: Request ML11165A0952011-06-0808 June 2011 Day Response to NRC Bulletin 2011-01, Mitigating Strategies Project stage: Request ASLBP 11-909-02-LR-BD01, Notice of Appearance of Richard S. Harper on Behalf of the U.S. Nuclear Regulatory Commission2011-06-0808 June 2011 Notice of Appearance of Richard S. Harper on Behalf of the U.S. Nuclear Regulatory Commission Project stage: Request ML11195A2092011-07-0707 July 2011 Day Response to NRC Bulletin 2011-01, Mitigating Strategies Project stage: Request 05000499/LER-2010-005-02, Regarding Startup Feed Pump 24 Breaker Failure and Unit 2 Reactor Trip2011-07-0707 July 2011 Regarding Startup Feed Pump 24 Breaker Failure and Unit 2 Reactor Trip Project stage: Request RS-11-137, Supplemental Information Supporting Request for License Amendment Regarding Measurement Uncertainty Recapture Power Uprate2011-08-25025 August 2011 Supplemental Information Supporting Request for License Amendment Regarding Measurement Uncertainty Recapture Power Uprate Project stage: Supplement ML1131101492011-11-28028 November 2011 Request for Additional Information, Regarding 60-Day Response to NRC Bulletin 2011-01, Mitigating Strategies Project stage: RAI NOC-AE-11002770, Response to Request for Additional Information Regarding NRC Bulletin 2011-01, Mitigating Strategies (TAC Nos. ME6486 and Me 6487)2011-12-20020 December 2011 Response to Request for Additional Information Regarding NRC Bulletin 2011-01, Mitigating Strategies (TAC Nos. ME6486 and Me 6487) Project stage: Response to RAI ML12003A2402011-12-20020 December 2011 Response to Request for Additional Information Regarding NRC Bulletin 2011-01, Mitigating Strategies (TAC Nos. ME6486 and Me 6487) Project stage: Response to RAI ML12173A3212012-06-26026 June 2012 Closeout of NRC Bulletin 2011-01, Mitigating Strategies Project stage: Other 2011-06-08
[Table View] |
LER-2010-005, Regarding Startup Feed Pump 24 Breaker Failure and Unit 2 Reactor Trip |
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| Report date: |
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| Reporting criterion: |
10 CFR 50.73(a)(2)(iv)(A), System Actuation
10 CFR 50.73(a)(2)(i)
10 CFR 50.73(a)(2)(vii), Common Cause Inoperability
10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded
10 CFR 50.73(a)(2)(viii)(A)
10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition
10 CFR 50.73(a)(2)(viii)(B)
10 CFR 50.73(a)(2)(iii)
10 CFR 50.73(a)(2)(ix)(A)
10 CFR 50.73(a)(2)(x)
10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown
10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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| 4992010005R00 - NRC Website |
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Nuclear Operating Company South Texas Project Electric Generating Station PO. Box 289 Wadsworth Tcs 77483 January 3, 2011 NOC-AE-1 0002630 File No.: G25 10 CFR 50.73 STI: 32805150 U. S. Nuclear Regulatory Commission Attention: Document Control Desk One White Flint North 11555 Rockville Pike Rockville, MD 20852-2738 South Texas Project Unit 2 Docket No. STN 50-499 Licensee Event Report 2010-005 Startup Feed Pump 24 Breaker Failure and Unit 2 Reactor Trip Pursuant to 10 CFR 50.73, STP Nuclear Operating Company (STPNOC) submits the attached Unit 2 Licensee Event Report (LER) 2010-005 to address the Unit 2 Reactor trip that occurred on November 3, 2010.
This condition is considered reportable under 10 CFR 50.73(a)(2)(iv)(A), any event or condition that resulted in manual or automatic actuation of any of the systems listed in paragraph (a)(2)(iv)(B) of this section, This event did not have an adverse effect on the health and safety of the public.
This is this initial LER submittal. A planned supplement will be submitted no later than April 4, 2011.
There are no commitments contained in this LER.
If there are any questions on this submittal, please contact either J. A. Loya at (361) 972-8005 or me at (361) 972-7158.
L. W. Peter Plant General Manager JAL
Attachment:
LER 2010-005: Startup Feed Pump 24 Breaker Failure and Unit 2 Reactor Trip
NOC-AE-10002630 Page 2 of 2 cc:
(paper copy)
(electronic copy)
Regional Administrator, Region IV U. S. Nuclear Regulatory Commission 612 East Lamar Blvd, Suite 400 Arlington, Texas 76011-4125 Mohan C. Thadani Senior Project Manager U.S. Nuclear Regulatory Commission One White Flint North (MS 8 G14) 11555 Rockville Pike Rockville, MD 20852 Senior Resident Inspector U. S. Nuclear Regulatory Commission P. 0. Box 289, Mail Code: MN1 16 Wadsworth, TX 77483 C. M. Canady City of Austin Electric Utility Department 721 Barton Springs Road Austin, TX 78704 A. H. Gutterman, Esquire Morgan, Lewis & Bockius LLP Mohan C. Thadani U. S. Nuclear Regulatory Commission John Ragan Catherine Callaway Jim von Suskil NRG South Texas LP Ed Alarcon Kevin Polio Richard Pena City Public Service Peter Nemeth Crain Caton & James, P.C.
C. Mele City of Austin Richard A. Ratliff Texas Department of State Health Services Alice Rogers Texas Department of State Health Services
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 08/31/2010 (9-2007)
, the NRC may digits/characters for each block) not conduct or sponsor, and a person is not required to respond to, the information collection.
- 3. PAGE South Texas Unit 2 05000499 1 OF 4
- 4. TITLE
__StartuD Feed Pump 24 Breaker Failure and Unit 2 Reactor Trip
- 5. EVENT DATE
- 6. LER NUMBER
- 7. REPORT DATE
- 8. OTHER FACILITIES INVOLVED MONTH DAY YEAR YEAR SEQUENTIAL REV FACILITY NAME DOCKET NUMBER NUMBER NO.
MONTH DAY YEAR N/A N/A FACILITY NAME DOCKET NUMBER 11 03 2010 2010 - 005 -
0 01 03 2011 N/A N/A
- 9. OPERATING MODE
- 11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR§: (Check all that apply)
El 20.2201(b)
El 20.2203(a)(3)(i)
E-50.73(a)(2)(i)(C)
El 50.73(a)(2)(vii) 1E 20.2201(d)
El 20.2203(a)(3)(ii)
El 50.73(a)(2)(ii)(A)
El 50.73(a)(2)(viii)(A)
[I 20.2203(a)(1)
El 20.2203(a)(4)
El 50.73(a)(2)(ii)(B)
El 50.73(a)(2)(viii)(B)
E] 20.2203(a)(2)(i)
El 50.36(c)(1)(i)(A)
El 50.73(a)(2)(iii)
El 50.73(a)(2)(ix)(A)
- 10. POWER LEVEL [E 20.2203(a)(2)(ii)
El 50.36(c)(1)(ii)(A) 0 50.73(a)(2)(iv)(A)
El 50.73(a)(2)(x)
El 20.2203(a)(2)(iii)
El 50.36(c)(2)
C3 50.73(a)(2)(v)(A)
[I 73.71(a)(4)
El 20.2203(a)(2)(iv)
El 50.46(a)(3)(ii)
[I 50.73(a)(2)(v)(B)
El 73.71(a)(5) 100%
El 20.2203(a)(2)(v)
El 50.73(a)(2)(i)(A)
El 50.73(a)(2)(v)(C)
[: OTHER E3 20.2203(a)(2)(vi)
El 50.73(a)(2)(i)(B)
El 50.73(a)(2)(v)(D)
Specify in Abstract below or in SUMMARY OF THE EVENT On November 3, 2010, the Startup Feed Pump (SUFP) 24 was being started to support a scheduled Partial Discharge Analysis as a preventive maintenance activity. Following the pre-job brief, a Licensed Operator Training (LOT) Trainee made a plant announcement and then placed the hand switch to Start at 1021 hours0.0118 days <br />0.284 hours <br />0.00169 weeks <br />3.884905e-4 months <br />. The SUFP started but then after approximately 4 seconds the pump breaker tripped open. Computer data shows that approximately 8 seconds after the pump breaker tripped the voltage on Standby Bus 2H (which supplies power to the SUFP) spiked low to near zero volts and the Unit 2 reactor tripped on Reactor Coolant Pump (RCP) Undervoltage (the 2C RCP is also powered by Standby Bus 2H).
Standby Diesel Generator (SDG) 23 started and began supplying Engineered Safety Features (ESF) Bus E2C due to Loss of Offsite Power (LOOP) to the ESF bus. Standby Bus 2F experienced a momentary voltage drop of approximately 1 second duration (Standby Buses 2F and 2H are both fed by the X winding of the Unit 2 Auxiliary Transformer) resulting in some A train loads being secured, however the low voltage condition cleared on Bus 2F prior to the point at which associated time delay relays would have started Standby Diesel Generator 21 (ESF Train A). Following the reactor trip, the plant was stabilized in MODE 3 at Normal Operating Pressure and Temperature.
At 1038 hours0.012 days <br />0.288 hours <br />0.00172 weeks <br />3.94959e-4 months <br /> an Unusual Event was declared for Unit 2 due to the breaker cubicle explosion associated with the SUFP breaker failure (ENS Event Number 46387). The breaker malfunction did not result in a fire. The Unusual Event was terminated at 1240 hours0.0144 days <br />0.344 hours <br />0.00205 weeks <br />4.7182e-4 months <br /> when the plant was stabilized in MODE 3.
An Operator in the Turbine Generator Building (TGB) reported substantial damage had occurred to the SUFP Breaker. The front door and access panels for Cubicle 1A in 13.8 KV Standby Bus 2H had been blown open or deformed.
(If more space is required, use additional copies of (If more space is required, use additional copies of NRC Form 366A) (17)
C.
SAFETY CONSEQUENCES AND IMPLICATIONS OF THE EVENT There was no impact to radiological safety, safety of the public, or safety of station personnel during this event.
The Incremental Conditional Core Damage Probability (ICCDP) for the Reactor Trip in Unit 2 on November 3, 2010 is 2.82E-07. The resulting Incremental Conditional Large Early Release Probability (LERP) given a turbine trip is 7.21 E-09.
III. CAUSE OF THE EVENT
The Root Cause of the breaker failure is under investigation and will be submitted in the planned LER supplement.
IV. CORRECTIVE ACTIONS
The Root Cause of the event, including the resulting corrective actions, is under investigation and will be submitted in the planned LER supplement.
V. PREVIOUS SIMILAR EVENTS
There have been no similar events within the last three years.
VI. ADDITIONAL INFORMATION
A supplement to this Licensee Event Report will be submitted by April 4, 2011.
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| 05000499/LER-2010-001-01, Essential Cooling Water System Leak | Essential Cooling Water System Leak | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000498/LER-2010-001, Unit Shutdown Required by Technical Specifications | Unit Shutdown Required by Technical Specifications | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000499/LER-2010-002, Regarding Unanalyzed Condition Regarding the Fire Protection System | Regarding Unanalyzed Condition Regarding the Fire Protection System | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000498/LER-2010-003, Regarding Unit 1 Reactor Trip During Surveillance Testing | Regarding Unit 1 Reactor Trip During Surveillance Testing | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000499/LER-2010-003, Regarding Containment Purge in Operation When Not Permitted by Technical Specifications | Regarding Containment Purge in Operation When Not Permitted by Technical Specifications | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000499/LER-2010-004, Loss of the Train a Essential Cooling Water (Ecw) System Due to a Loss of the Ecw Intake Structure Ventilation Fan 21A | Loss of the Train a Essential Cooling Water (Ecw) System Due to a Loss of the Ecw Intake Structure Ventilation Fan 21A | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000499/LER-2010-005-02, Regarding Startup Feed Pump 24 Breaker Failure and Unit 2 Reactor Trip | Regarding Startup Feed Pump 24 Breaker Failure and Unit 2 Reactor Trip | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2) | | 05000499/LER-2010-005-01, For South Texas Project Unit 2, Regarding Startup Feed Pump 24 Breaker Failure and Unit 2 Reactor Trip | For South Texas Project Unit 2, Regarding Startup Feed Pump 24 Breaker Failure and Unit 2 Reactor Trip | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2) | | 05000499/LER-2010-005, Regarding Startup Feed Pump 24 Breaker Failure and Unit 2 Reactor Trip | Regarding Startup Feed Pump 24 Breaker Failure and Unit 2 Reactor Trip | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000499/LER-2010-006, Regarding Technical Specifications Not Met for Reactor Coolant System Unidentified Leakage | Regarding Technical Specifications Not Met for Reactor Coolant System Unidentified Leakage | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) |
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