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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000498/LER-1999-008, :on 990912,unit Tripped During Performance of Main Turbine Emergency Trip Test Procedures.Caused by Failure in Turbine Trip Test Circuitry.Main Control Boards Were Cleaned & Other Panels Were Inspected1999-10-12012 October 1999
- on 990912,unit Tripped During Performance of Main Turbine Emergency Trip Test Procedures.Caused by Failure in Turbine Trip Test Circuitry.Main Control Boards Were Cleaned & Other Panels Were Inspected
05000499/LER-1999-006-01, :on 990901,TS 3.0.3 Entered.Caused by Insufficient Procedural Guidance for Use of TS 3.0.6.SG 2D low-level Channel 2 Input Relay to ESF Actuation Logic Circuitry Replaced on 9909011999-09-30030 September 1999
- on 990901,TS 3.0.3 Entered.Caused by Insufficient Procedural Guidance for Use of TS 3.0.6.SG 2D low-level Channel 2 Input Relay to ESF Actuation Logic Circuitry Replaced on 990901
05000499/LER-1999-005-01, :on 990824,ESFA Following Loss of Power to Standby Transformer 2 Was Noted.Internal Fault Caused C Phase Arrester Failure.Replaced All Surge Arresters for Standby Transformer 21999-09-20020 September 1999
- on 990824,ESFA Following Loss of Power to Standby Transformer 2 Was Noted.Internal Fault Caused C Phase Arrester Failure.Replaced All Surge Arresters for Standby Transformer 2
05000498/LER-1999-007, :on 990812,plant Train B CR Makeup & Cleanup Filtration Sys Was Declared Inoperable for Greater than Aot. Caused by Degradation of Makeup Filter & Filter Charcoal Due to Aging.Subject Filter Was Replaced on 9908051999-09-13013 September 1999
- on 990812,plant Train B CR Makeup & Cleanup Filtration Sys Was Declared Inoperable for Greater than Aot. Caused by Degradation of Makeup Filter & Filter Charcoal Due to Aging.Subject Filter Was Replaced on 990805
NOC-AE-000583, LER 99-S03-00:on 990619,failure to Revitalize Sdg Number 11 Was Noted.Caused by Failure to Communicate Status of Sdg. Subject Sdg Revitalized on 990619 & Licensee Will Develop Security Force Instruction Re Sdgs.With1999-07-15015 July 1999 LER 99-S03-00:on 990619,failure to Revitalize Sdg Number 11 Was Noted.Caused by Failure to Communicate Status of Sdg. Subject Sdg Revitalized on 990619 & Licensee Will Develop Security Force Instruction Re Sdgs.With NOC-AE-000570, LER 99-S01-00:on 990527,discovered That Unescorted Access Had Been Inappropriately Granted.Caused by Failure to Follow Procedure.Util Verified That Individual Did Not Have Current Unescorted Access at STP or Any Other Util.With1999-06-28028 June 1999 LER 99-S01-00:on 990527,discovered That Unescorted Access Had Been Inappropriately Granted.Caused by Failure to Follow Procedure.Util Verified That Individual Did Not Have Current Unescorted Access at STP or Any Other Util.With ML20196G5821999-06-23023 June 1999 LER 99-S02-00:on 990601,failure to Maintain Positive Control of Vital Area Security Key Was Noted.Caused by Lack of Attention to Detail.Discussed Event with Operator Involved IAW Constructive Discipline Program 05000498/LER-1999-004-01, :on 990516,Unit 1 Experienced Automatic Reactor Trip.Caused by Equipment Failure.Stp Will Evaluate Potential Transformer Testing Procedure for Incorporation of Fuse Resistance Measurements by 990715.With1999-06-15015 June 1999
- on 990516,Unit 1 Experienced Automatic Reactor Trip.Caused by Equipment Failure.Stp Will Evaluate Potential Transformer Testing Procedure for Incorporation of Fuse Resistance Measurements by 990715.With
05000498/LER-1999-003-01, :on 990329,CR HVAC Was Placed in Recirculation Mode of Operation Instead of Recirculation Mu Filtered Mode. Caused by Inadequate Verbal Communications.Briefed Crews on Attention to Detail During three-way Communications1999-04-29029 April 1999
- on 990329,CR HVAC Was Placed in Recirculation Mode of Operation Instead of Recirculation Mu Filtered Mode. Caused by Inadequate Verbal Communications.Briefed Crews on Attention to Detail During three-way Communications
05000498/LER-1999-002-01, :on 990327,inadequate Performance of TS Surveillance When Evaluating Source Range Nuclear Instrument Discriminator Bias Curve Results,Was Discovered.Caused by Lack of Process to Incorporate Info.Compared Bias Curves1999-04-26026 April 1999
- on 990327,inadequate Performance of TS Surveillance When Evaluating Source Range Nuclear Instrument Discriminator Bias Curve Results,Was Discovered.Caused by Lack of Process to Incorporate Info.Compared Bias Curves
05000498/LER-1999-001-01, :on 990311,RHR Sys Was Found in Condition Outside Design Basis.Caused by Inadequate Implementation of Design Basis Requirements.Condition Remedied by Opening Disconnect Switches Per Rev to Plant Procedures1999-04-12012 April 1999
- on 990311,RHR Sys Was Found in Condition Outside Design Basis.Caused by Inadequate Implementation of Design Basis Requirements.Condition Remedied by Opening Disconnect Switches Per Rev to Plant Procedures
05000499/LER-1998-004-01, :on 981228,plant Was Shutdown Required by TS 3.3.2.Caused by Failure in Ssps Test Circuitry.Testing Circuit Card Was Replaced1999-01-26026 January 1999
- on 981228,plant Was Shutdown Required by TS 3.3.2.Caused by Failure in Ssps Test Circuitry.Testing Circuit Card Was Replaced
05000498/LER-1998-010, :on 981021,FHB Exhaust Booster Fan 11A Was Declared Inoperable When Ground Indication Was Discovered During Sp.Caused by Fan Motor That Needed to Be Replaced. Preventive Maint Was Performed on Motors.With1998-11-19019 November 1998
- on 981021,FHB Exhaust Booster Fan 11A Was Declared Inoperable When Ground Indication Was Discovered During Sp.Caused by Fan Motor That Needed to Be Replaced. Preventive Maint Was Performed on Motors.With
05000499/LER-1998-003-01, :on 981016,discovered Missed Tube Insp in SG 2B,per TS Surveillance 4.4.5.2.Caused by Lack of Addl Controls to Prevent Re SG Tube Insp Data.Licensee Revised 2FE05 Insp Records & SG Insp Database.With1998-11-12012 November 1998
- on 981016,discovered Missed Tube Insp in SG 2B,per TS Surveillance 4.4.5.2.Caused by Lack of Addl Controls to Prevent Re SG Tube Insp Data.Licensee Revised 2FE05 Insp Records & SG Insp Database.With
05000499/LER-1998-002-01, :on 980922,automatic RT Occurred Due to low-low Level in SG 2A.Caused by Failure to Adequately Verify Technical Accuracy of Changes Made to Original Work Instructions.Reviewed Other Similar Work in Progress1998-10-15015 October 1998
- on 980922,automatic RT Occurred Due to low-low Level in SG 2A.Caused by Failure to Adequately Verify Technical Accuracy of Changes Made to Original Work Instructions.Reviewed Other Similar Work in Progress
ML20237A1201998-08-0505 August 1998 LER 98-S01-00:on 980707,loss of Power Supply to Security Sys Occurred.Caused by Inverter Switching to Alternate Power Source Due to Intermittent Failure of Static Switch Board. Static Switch Board Replaced,Per 10CFR73.71 05000498/LER-1997-013, :on 971111,supplementary CPS Isolation Valve Failed to Meet TS Leak Rate Requirements.Caused by Inadequate Process for Developing Measuring & Test Equipment Calibration Spec.Revised Plants Procedures1998-04-16016 April 1998
- on 971111,supplementary CPS Isolation Valve Failed to Meet TS Leak Rate Requirements.Caused by Inadequate Process for Developing Measuring & Test Equipment Calibration Spec.Revised Plants Procedures
05000498/LER-1997-006, :on 970507,inappropriate Surveillance Procedure Monitoring Parameters Were Noted.Caused by Inadequate Review of Changes Made to TS & Bases.Evaluated Review Processes for TS Changes W/Focus on Changes to Bases1998-04-0909 April 1998
- on 970507,inappropriate Surveillance Procedure Monitoring Parameters Were Noted.Caused by Inadequate Review of Changes Made to TS & Bases.Evaluated Review Processes for TS Changes W/Focus on Changes to Bases
05000498/LER-1998-002, :on 980203,SG Narrow Range Level EOP just-in narrow-range Setpoint Was Noted Different than Setpoint for Current Sgs.Caused by Incorrectly Assuming Height in Calculation to Determine Eop.Revised EOP for SGs1998-03-0505 March 1998
- on 980203,SG Narrow Range Level EOP just-in narrow-range Setpoint Was Noted Different than Setpoint for Current Sgs.Caused by Incorrectly Assuming Height in Calculation to Determine Eop.Revised EOP for SGs
05000498/LER-1998-001-01, :on 980122,failure to Perform an Adequate TS Surveillance Re Containment Structural Integrity.Caused by Ineffective Performance.Training on New Calculation Procedure Has Been Provided1998-02-23023 February 1998
- on 980122,failure to Perform an Adequate TS Surveillance Re Containment Structural Integrity.Caused by Ineffective Performance.Training on New Calculation Procedure Has Been Provided
05000499/LER-1997-007-01, :on 971121,manual Reactor Trip Occurred.Caused by Two Separate Failure Mechanisms That Combined to Result in Loss of Power to Cabinet.Failed Voltage to Pulse Converter Circuit Card Was Replaced1997-12-18018 December 1997
- on 971121,manual Reactor Trip Occurred.Caused by Two Separate Failure Mechanisms That Combined to Result in Loss of Power to Cabinet.Failed Voltage to Pulse Converter Circuit Card Was Replaced
05000498/LER-1997-013, :on 971111,failure to Meet Tech Spec Leak Rate Requirements for Suppl Containment Purge Supply Isolation Valve Occurred.Caused by Inadequate Process for Developing Measuring & Test Equipment.Procedures Revised1997-12-11011 December 1997
- on 971111,failure to Meet Tech Spec Leak Rate Requirements for Suppl Containment Purge Supply Isolation Valve Occurred.Caused by Inadequate Process for Developing Measuring & Test Equipment.Procedures Revised
05000498/LER-1997-010, :on 970920,discovered That MSSVs 7430A & 7430B Failed to Meet Required Relief Capacity.Caused by Inadequate Resolution Issues.Revised Procedures & Corrected Lift Setting Adjustment1997-10-16016 October 1997
- on 970920,discovered That MSSVs 7430A & 7430B Failed to Meet Required Relief Capacity.Caused by Inadequate Resolution Issues.Revised Procedures & Corrected Lift Setting Adjustment
ST-HL-AE-5762, LER 97-S03-00:on 970904,doors to Two Vital Areas Were Not Posted to Compensate for Partial Sys Failure.Caused by Supervisor Failing to Follow Procedure.Searched Affected Vital Areas for Unauthorized Matls & Personnel1997-10-0303 October 1997 LER 97-S03-00:on 970904,doors to Two Vital Areas Were Not Posted to Compensate for Partial Sys Failure.Caused by Supervisor Failing to Follow Procedure.Searched Affected Vital Areas for Unauthorized Matls & Personnel 05000498/LER-1997-009, :on 970902,MSSV Setpoints Were Found Outside Required Tolerance.Caused by Alteration of Nozzle & Disc Oxide Layers.Adjusted Lift Settings of Valves & Refurbished Valves1997-10-0202 October 1997
- on 970902,MSSV Setpoints Were Found Outside Required Tolerance.Caused by Alteration of Nozzle & Disc Oxide Layers.Adjusted Lift Settings of Valves & Refurbished Valves
05000498/LER-1997-008, :on 970811,ESF Containment Spray Actuation Relays Slave Relay Test Were Not Fully Tested by Surveillance.Caused by Failure to Understand Expectations Re Documentation.Spray Pumps Verified Operable1997-09-10010 September 1997
- on 970811,ESF Containment Spray Actuation Relays Slave Relay Test Were Not Fully Tested by Surveillance.Caused by Failure to Understand Expectations Re Documentation.Spray Pumps Verified Operable
ST-HL-AE-5721, LER 97-S02-00:on 970721,all Power Lost to Security Sys at Completion of Lighting DG Performance Test.Caused by Security Personnel Did Not Recognize Nature or Significance of Bypass Trouble Alarm.Training Conducted1997-08-20020 August 1997 LER 97-S02-00:on 970721,all Power Lost to Security Sys at Completion of Lighting DG Performance Test.Caused by Security Personnel Did Not Recognize Nature or Significance of Bypass Trouble Alarm.Training Conducted 05000498/LER-1997-007, :on 970619,ESFAS Pressurizer Pressure Sys Interlock Was Not Fully Tested by Surveillance Procedures. Caused by Failure to Recognize That Circuitry Did Not Include Required Provisions.Revised Sps1997-07-21021 July 1997
- on 970619,ESFAS Pressurizer Pressure Sys Interlock Was Not Fully Tested by Surveillance Procedures. Caused by Failure to Recognize That Circuitry Did Not Include Required Provisions.Revised Sps
05000498/LER-1997-006-01, :on 970508,inappropriate Surveillance Procedure Monitoring Parameters Found,Due to Less than Adequate Review of Vantage 5H License Amend.Limits Established in Operator Log Surveillance Procedure1997-06-10010 June 1997
- on 970508,inappropriate Surveillance Procedure Monitoring Parameters Found,Due to Less than Adequate Review of Vantage 5H License Amend.Limits Established in Operator Log Surveillance Procedure
05000499/LER-1997-006, :on 970430,manual Reactor Trip Occurred.Caused by Malfunctioning Main Feedwater Regulating Valve.Main 2D Feedwater Regulating Valve controller-driver Card Replaced & Control Circuit Tested Satisfactorily1997-05-29029 May 1997
- on 970430,manual Reactor Trip Occurred.Caused by Malfunctioning Main Feedwater Regulating Valve.Main 2D Feedwater Regulating Valve controller-driver Card Replaced & Control Circuit Tested Satisfactorily
05000498/LER-1997-005-01, :on 970402,main Steam Safety Valve Setpoints Were Discovered Outside Required Tolerance Due to Alteration of Nozzle Seat & Disc Seat Oxide Layers.Lift Settings Were Adjusted to Required Allowable Tolerances1997-05-0101 May 1997
- on 970402,main Steam Safety Valve Setpoints Were Discovered Outside Required Tolerance Due to Alteration of Nozzle Seat & Disc Seat Oxide Layers.Lift Settings Were Adjusted to Required Allowable Tolerances
05000499/LER-1997-005, :on 970326,manual Unit Trip Occurred Due to Lowering SG Level.Failed seal-in Relay Was Replaced & Verified That Other seal-in Relays Affecting MFRVs in Both Units 1 & 2 Had Proper Coil Resistances1997-04-24024 April 1997
- on 970326,manual Unit Trip Occurred Due to Lowering SG Level.Failed seal-in Relay Was Replaced & Verified That Other seal-in Relays Affecting MFRVs in Both Units 1 & 2 Had Proper Coil Resistances
05000499/LER-1997-004-01, :on 970319,unit Trip Occurred While Performing Main Turbine Testing Due to Intermittent Failure of Inverter Power Supply for Channel Two Automatic Stop Trip Valve. Inverter Power Supply Was Replaced1997-04-17017 April 1997
- on 970319,unit Trip Occurred While Performing Main Turbine Testing Due to Intermittent Failure of Inverter Power Supply for Channel Two Automatic Stop Trip Valve. Inverter Power Supply Was Replaced
05000498/LER-1997-004, :on 970319,failed to Fully Test 4160 Volt Bus Undervoltage Logic Circuitry by Surveillance Procedures. Caused by Not Recognizing That Failure in One Actuation Scheme.Affected Logic Circuitry Was Tested1997-04-17017 April 1997
- on 970319,failed to Fully Test 4160 Volt Bus Undervoltage Logic Circuitry by Surveillance Procedures. Caused by Not Recognizing That Failure in One Actuation Scheme.Affected Logic Circuitry Was Tested
05000499/LER-1997-002-01, :on 970215,Steam Generators 2A Eddy Current Insp Results Fell Into Category C-3.Caused by Stress Corrosion Cracking at tube-to-tube Support Plate.Sg Tubes Were Plugged in Four Unit 2 Steam Generators1997-03-13013 March 1997
- on 970215,Steam Generators 2A Eddy Current Insp Results Fell Into Category C-3.Caused by Stress Corrosion Cracking at tube-to-tube Support Plate.Sg Tubes Were Plugged in Four Unit 2 Steam Generators
05000499/LER-1997-001-01, :on 970205,main Steam Safety Valve Setpoints Discovered Outside Required Tolerance Occurred.Caused by MSSV Above & Beyond Previously Documented Setpoint Drift. Lift Setting of Five MSSV Were Adjusted1997-03-0606 March 1997
- on 970205,main Steam Safety Valve Setpoints Discovered Outside Required Tolerance Occurred.Caused by MSSV Above & Beyond Previously Documented Setpoint Drift. Lift Setting of Five MSSV Were Adjusted
ST-HL-AE-5591, LER 97-S01-00:on 970130,security Door Intrusion Alarm Was Disabled.Caused Because Risk Assessment for Testing Plan Did Not Ensure Adequate Compensatory Actions Were in Place to Prevent Error.Modified Startup & Testing Plan1997-02-27027 February 1997 LER 97-S01-00:on 970130,security Door Intrusion Alarm Was Disabled.Caused Because Risk Assessment for Testing Plan Did Not Ensure Adequate Compensatory Actions Were in Place to Prevent Error.Modified Startup & Testing Plan 05000498/LER-1997-003, :on 970123,potential for Overpressurization of Piping Identified.Caused by Deficiency in Original Design. Thermal Insulation Installed on Lines 3WL-1009 & 3WL-2009 & Lines Have Been Returned to Service1997-02-24024 February 1997
- on 970123,potential for Overpressurization of Piping Identified.Caused by Deficiency in Original Design. Thermal Insulation Installed on Lines 3WL-1009 & 3WL-2009 & Lines Have Been Returned to Service
05000498/LER-1997-001, :on 970116,failure to Meet Requirements of TS Surveillance Requirement 4.7.13 Identified.Caused by Incorrect Repeatability Value Provided by Supplier of Temp Switch.Switches Evaluated1997-02-13013 February 1997
- on 970116,failure to Meet Requirements of TS Surveillance Requirement 4.7.13 Identified.Caused by Incorrect Repeatability Value Provided by Supplier of Temp Switch.Switches Evaluated
05000498/LER-1997-002, :on 970115,safety Injection Sys Logic Circuitry Not Fully Tested by Surveillance Procedures.Caused by Unusual Logic Arrangement.Containment Sump Isolation Valves Have Been Tested1997-02-13013 February 1997
- on 970115,safety Injection Sys Logic Circuitry Not Fully Tested by Surveillance Procedures.Caused by Unusual Logic Arrangement.Containment Sump Isolation Valves Have Been Tested
05000498/LER-1996-005, :on 961213,reactor Containment Building Personnel Airlock Incorrectly Declared Operable Occurred. Caused by Pertinent Information Re Status of Seal Replacement.Occurrence Has Been Reviewed1997-01-13013 January 1997
- on 961213,reactor Containment Building Personnel Airlock Incorrectly Declared Operable Occurred. Caused by Pertinent Information Re Status of Seal Replacement.Occurrence Has Been Reviewed
05000498/LER-1996-004, :on 961120,unanalyzed Conditions Were Noted Due to Discovery of Two Spare SR Circuit Breakers Not in Seismically Qualified Position.Caused by Failure to Follow Established Procedures.Revised Procedures1996-12-18018 December 1996
- on 961120,unanalyzed Conditions Were Noted Due to Discovery of Two Spare SR Circuit Breakers Not in Seismically Qualified Position.Caused by Failure to Follow Established Procedures.Revised Procedures
05000498/LER-1995-013, :on 951218,turbine Trip & Reactor Trip Occurred,Due to Main Transformer Lockout.Caused by Improper Maint Performance.Grounded Connection Repaired,Mgt Expectations Reinforced & Procedures Revised1996-10-0303 October 1996
- on 951218,turbine Trip & Reactor Trip Occurred,Due to Main Transformer Lockout.Caused by Improper Maint Performance.Grounded Connection Repaired,Mgt Expectations Reinforced & Procedures Revised
05000499/LER-1996-003, :on 960828,failure to Fully Meet Requirements of TS Occurred,Due to Discovery of Improperly Installed Jumper on Main Steam Line Pressure Lead/Lag Circuit Card. Personnel Issues Have Been Addressed1996-09-25025 September 1996
- on 960828,failure to Fully Meet Requirements of TS Occurred,Due to Discovery of Improperly Installed Jumper on Main Steam Line Pressure Lead/Lag Circuit Card. Personnel Issues Have Been Addressed
05000498/LER-1996-009, :on 960620,containment Closeout Insp Failed to Recognize Unauthorized Material Left in Containment.Caused by Inadequate Requirement Review.Removed Bagged Equipment & Completed Containment Closeout Insp1996-07-17017 July 1996
- on 960620,containment Closeout Insp Failed to Recognize Unauthorized Material Left in Containment.Caused by Inadequate Requirement Review.Removed Bagged Equipment & Completed Containment Closeout Insp
05000498/LER-1996-002-01, :on 960507,failure to Meet Requirements of Tech Specs Occurred.Caused by Inattention to Detail During Documentation & Review of Testing Results.Feedback from Event Given to Individuals Involved1996-06-0606 June 1996
- on 960507,failure to Meet Requirements of Tech Specs Occurred.Caused by Inattention to Detail During Documentation & Review of Testing Results.Feedback from Event Given to Individuals Involved
05000498/LER-1996-001-01, :on 960328,Standby Diesel Generator Declared Inoperable.Caused by Barriers for Preparation & Planning Not Being Fully Implemented.Personnel Involved Counseled Re Event & Revised Preventive Maint Documents1996-06-0303 June 1996
- on 960328,Standby Diesel Generator Declared Inoperable.Caused by Barriers for Preparation & Planning Not Being Fully Implemented.Personnel Involved Counseled Re Event & Revised Preventive Maint Documents
05000499/LER-1996-002, :on 960314,fuel Handling Bldg Exhaust Air Damper Inoperable Due to Inappropriate Design Implementation.Made Mods to Fuel Handling Bldg Emergency Exhaust Dampers to Resolve Issue1996-04-24024 April 1996
- on 960314,fuel Handling Bldg Exhaust Air Damper Inoperable Due to Inappropriate Design Implementation.Made Mods to Fuel Handling Bldg Emergency Exhaust Dampers to Resolve Issue
05000499/LER-1996-001, :on 960119,TS 3.0.3 Entry Occurred Due to Two MFW Isolation Valves Being Inoperable at Same Time.Discussed Enhanced Mgt Expectations W/Emphasis on Clear & Concise Communications1996-02-19019 February 1996
- on 960119,TS 3.0.3 Entry Occurred Due to Two MFW Isolation Valves Being Inoperable at Same Time.Discussed Enhanced Mgt Expectations W/Emphasis on Clear & Concise Communications
05000498/LER-1995-012, :on 950926,RHR Pump Impeller Cracks Occurred. Caused by Improper Mfg of Impeller.Rhr Pump Impeller Replaced1996-01-0909 January 1996
- on 950926,RHR Pump Impeller Cracks Occurred. Caused by Improper Mfg of Impeller.Rhr Pump Impeller Replaced
1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K9441999-10-15015 October 1999 SER Accepting Util Alternative Proposed Relief Request RR-ENG-2-4 for Second 10-year ISI Interval at Stp,Units 1 & 2 Pursuant to 10CFR50.55a(a)(3)(i) ML20217K9151999-10-15015 October 1999 SER Authorizing Util Relief Request RR-ENG-2-3 for Second 10-year ISI Interval of Stp,Units 1 & 2 Pursuant to 10CFR50.55a(a)(3)(i) 05000498/LER-1999-008, :on 990912,unit Tripped During Performance of Main Turbine Emergency Trip Test Procedures.Caused by Failure in Turbine Trip Test Circuitry.Main Control Boards Were Cleaned & Other Panels Were Inspected1999-10-12012 October 1999
- on 990912,unit Tripped During Performance of Main Turbine Emergency Trip Test Procedures.Caused by Failure in Turbine Trip Test Circuitry.Main Control Boards Were Cleaned & Other Panels Were Inspected
ML20217D0531999-09-30030 September 1999 Rev 1 to STP Electric Generating Station Unit 2 Cycle 7 Colr NOC-AE-000676, Monthly Operating Repts for Sept 1999 for South Texas Project,Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for South Texas Project,Units 1 & 2.With ML20217D0481999-09-30030 September 1999 Rev 1 to STP Electric Generating Station Unit 1 Cycle 9 Colr 05000499/LER-1999-006-01, :on 990901,TS 3.0.3 Entered.Caused by Insufficient Procedural Guidance for Use of TS 3.0.6.SG 2D low-level Channel 2 Input Relay to ESF Actuation Logic Circuitry Replaced on 9909011999-09-30030 September 1999
- on 990901,TS 3.0.3 Entered.Caused by Insufficient Procedural Guidance for Use of TS 3.0.6.SG 2D low-level Channel 2 Input Relay to ESF Actuation Logic Circuitry Replaced on 990901
05000499/LER-1999-005-01, :on 990824,ESFA Following Loss of Power to Standby Transformer 2 Was Noted.Internal Fault Caused C Phase Arrester Failure.Replaced All Surge Arresters for Standby Transformer 21999-09-20020 September 1999
- on 990824,ESFA Following Loss of Power to Standby Transformer 2 Was Noted.Internal Fault Caused C Phase Arrester Failure.Replaced All Surge Arresters for Standby Transformer 2
ML20212C2811999-09-13013 September 1999 Safety Evaluation Supporting Amends 116 & 104 to Licenses NPF-76 & NPF-80,respectively 05000498/LER-1999-007, :on 990812,plant Train B CR Makeup & Cleanup Filtration Sys Was Declared Inoperable for Greater than Aot. Caused by Degradation of Makeup Filter & Filter Charcoal Due to Aging.Subject Filter Was Replaced on 9908051999-09-13013 September 1999
- on 990812,plant Train B CR Makeup & Cleanup Filtration Sys Was Declared Inoperable for Greater than Aot. Caused by Degradation of Makeup Filter & Filter Charcoal Due to Aging.Subject Filter Was Replaced on 990805
ML20211Q6731999-09-0909 September 1999 Safety Evaluation Accepting First 10-yr Interval ISI Program Plan Request for Relief from ASME Code Case N-498 ML20211P8411999-09-0909 September 1999 Safety Evaluation Supporting Alternative Proposed by Licensee to Surface Exam to Perform Boroscopic VT-1 Visual Exam of Pump Casing Welds within Pump Pits for Welds Covered by Relief Request RR-ENG-24 ML20211P7811999-09-0909 September 1999 SER Approving Second 10-year Interval Inservice Insp Program Plan Relief Request RR-ENG-2-8 (to Use Code Case N-491-2) for South Texas Project,Units 1 & 2 ML20211P9001999-09-0202 September 1999 Safety Evaluation Supporting Amends 115 & 103 to Licenses NPF-76 & NPF-80,respectively ML20212E5191999-08-31031 August 1999 Rev 3 to SG-99-04-005, STP 1RE08 Outage Condition Monitoring Rept & Final Operational Assessment NOC-AE-000643, Monthly Operating Repts for Aug 1999 for South Texas Project,Units 1 & 2.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for South Texas Project,Units 1 & 2.With ML20211F4531999-08-24024 August 1999 Safety Evaluation Supporting Licensee Proposed Alternative to Defer Partial First Period Exams of flange-to-shell Weld to Third Period & Perform Required Ultrasonic Exams,Both Manual & Automated,During Third Period ML20211F5111999-08-23023 August 1999 Safety Evaluation Supporting Licensee Proposed Alternative Contained in Request for Relief RR-ENG-30 ML20211F3651999-08-19019 August 1999 Safety Evaluation Supporting Amends 114 & 102 to Licenses NPF-76 & NPF-80,respectively ML20210K4881999-08-0303 August 1999 Safety Evaluation Supporting Amends 113 & 101 to Licenses NPF-76 & NPF-80,respectively ML20210R3631999-07-31031 July 1999 Monthly Operating Repts for July 1999 for South Tx Project, Units 1 & 2.With ML20210C9411999-07-31031 July 1999 Rev 1 to SG-99-07-002, South Tx,Unit 1 Cycle 9 Voltage- Based Repair Criteria 90-Day Rept, Jul 1999 ML20210D9161999-07-23023 July 1999 Safety Evaluation Accepting Inservice Testing Relief Request RR-56 Re Component Cooling Water & Safety Injection Sys Containment Isolation Check Valve Closure Test Frequency ML20210D4491999-07-21021 July 1999 Revised Chapters to Operations QA Plan, Including Rev 9 to Chapter 1.0, Organization & Rev 6 to Chapter 16.0, Independent Technical Review ML20210D4821999-07-21021 July 1999 1RE08 ISI Summary Rept for Steam Generator Tubing of South Texas Project Electric Generating Station Unit 1 NOC-AE-000583, LER 99-S03-00:on 990619,failure to Revitalize Sdg Number 11 Was Noted.Caused by Failure to Communicate Status of Sdg. Subject Sdg Revitalized on 990619 & Licensee Will Develop Security Force Instruction Re Sdgs.With1999-07-15015 July 1999 LER 99-S03-00:on 990619,failure to Revitalize Sdg Number 11 Was Noted.Caused by Failure to Communicate Status of Sdg. Subject Sdg Revitalized on 990619 & Licensee Will Develop Security Force Instruction Re Sdgs.With ML20207H6361999-07-0808 July 1999 Safety Evaluation Approving 2nd 10 Yr Interval ISI Program Plan Request to Use ASME Section XI Code Case N-546 for Licenses NPF-76 & NPF-80,respectively ML20216D7481999-07-0707 July 1999 1RE08 ISI Summary Rept for Welds & Component Supports of STP Electric Generating Station,Unit 1 ML20196K7091999-07-0202 July 1999 Safety Evaluation Supporting Amend 100 to License NPF-80 NOC-AE-000593, Monthly Operating Repts for June 1999 for Stp,Units 1 & 2. with1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Stp,Units 1 & 2. with NOC-AE-000570, LER 99-S01-00:on 990527,discovered That Unescorted Access Had Been Inappropriately Granted.Caused by Failure to Follow Procedure.Util Verified That Individual Did Not Have Current Unescorted Access at STP or Any Other Util.With1999-06-28028 June 1999 LER 99-S01-00:on 990527,discovered That Unescorted Access Had Been Inappropriately Granted.Caused by Failure to Follow Procedure.Util Verified That Individual Did Not Have Current Unescorted Access at STP or Any Other Util.With ML20212J0031999-06-23023 June 1999 Safety Evaluation Supporting Amends 112 & 99 to Licenses NPF-76 & NPF-80,respectively ML20196G5821999-06-23023 June 1999 LER 99-S02-00:on 990601,failure to Maintain Positive Control of Vital Area Security Key Was Noted.Caused by Lack of Attention to Detail.Discussed Event with Operator Involved IAW Constructive Discipline Program ML20195J6871999-06-17017 June 1999 Safety Evaluation Supporting Proposed Alternative Contained in RR-ENG-2-5.Proposed Alternative Authorized Per 10CFR50.55a(a)(3)(i) for 2nd ISI Interval 05000498/LER-1999-004-01, :on 990516,Unit 1 Experienced Automatic Reactor Trip.Caused by Equipment Failure.Stp Will Evaluate Potential Transformer Testing Procedure for Incorporation of Fuse Resistance Measurements by 990715.With1999-06-15015 June 1999
- on 990516,Unit 1 Experienced Automatic Reactor Trip.Caused by Equipment Failure.Stp Will Evaluate Potential Transformer Testing Procedure for Incorporation of Fuse Resistance Measurements by 990715.With
ML20196A2391999-06-15015 June 1999 Change QA-042 to Rev 13 of Operations QAP, Reflecting Current Organizational Alignment for South Texas Project & Culminating Organizational Realigment That Has Been Taking Place During Past Several Months NOC-AE-000563, Monthly Operating Repts for May 1999 for Stp,Units 1 & 2. with1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Stp,Units 1 & 2. with ML20206U7731999-05-20020 May 1999 Safety Evaluation Supporting Amends 110 & 97 to Licenses NPF-76 & NPF-80,respectively ML20206U5411999-05-18018 May 1999 Non-proprietary Errata Pages for Rev 2,Addendum 1 to WCAP-13699, Laser Welded Sleeves for 3/4 Inch Diamete Tube Feedring Type & W Preheater SGs Generic Sleeving Rept ML20207A1101999-05-17017 May 1999 Safety Evaluation Supporting Amends 109 & 96 to Licenses NPF-76 & NPF-80,respectively NOC-AE-000543, Monthly Operating Repts for Apr 1999 for Stp,Units 1 & 2. with1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Stp,Units 1 & 2. with ML20206A7721999-04-30030 April 1999 STP Electric Generating Station Unit 1 Cycle 9 Colr 05000498/LER-1999-003-01, :on 990329,CR HVAC Was Placed in Recirculation Mode of Operation Instead of Recirculation Mu Filtered Mode. Caused by Inadequate Verbal Communications.Briefed Crews on Attention to Detail During three-way Communications1999-04-29029 April 1999
- on 990329,CR HVAC Was Placed in Recirculation Mode of Operation Instead of Recirculation Mu Filtered Mode. Caused by Inadequate Verbal Communications.Briefed Crews on Attention to Detail During three-way Communications
05000498/LER-1999-002-01, :on 990327,inadequate Performance of TS Surveillance When Evaluating Source Range Nuclear Instrument Discriminator Bias Curve Results,Was Discovered.Caused by Lack of Process to Incorporate Info.Compared Bias Curves1999-04-26026 April 1999
- on 990327,inadequate Performance of TS Surveillance When Evaluating Source Range Nuclear Instrument Discriminator Bias Curve Results,Was Discovered.Caused by Lack of Process to Incorporate Info.Compared Bias Curves
ML20206A1411999-04-19019 April 1999 Safety Evaluation Supporting Amends 107 & 94 to Licenses NPF-76 & NPF-80,respectively ML20206A3611999-04-19019 April 1999 Safety Evaluation Supporting Amends 108 & 95 to Licenses NPF-76 & NPF-80,respectively ML20205Q6771999-04-16016 April 1999 Safety Evaluation Supporting Amends 105 & 92 to Licenses NPF-76 & NPF-80,respectively ML20205Q7321999-04-16016 April 1999 Safety Evaluation Supporting Amends 106 & 93 to Licenses NPF-76 & NPF-80,respectively 05000498/LER-1999-001-01, :on 990311,RHR Sys Was Found in Condition Outside Design Basis.Caused by Inadequate Implementation of Design Basis Requirements.Condition Remedied by Opening Disconnect Switches Per Rev to Plant Procedures1999-04-12012 April 1999
- on 990311,RHR Sys Was Found in Condition Outside Design Basis.Caused by Inadequate Implementation of Design Basis Requirements.Condition Remedied by Opening Disconnect Switches Per Rev to Plant Procedures
ML20205H0321999-03-31031 March 1999 Change QA-040 to Rev 13 of Operations QA Plan 1999-09-09
[Table view] |
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'I NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY GMB NO. 3150-0104 i
(s ea EXPIRES 5/31/95 I
ESTiMMED BURDEN PE R RESPONSE TO COMPLY WITH TH:S a
INFORMATION COLLECTON REOJEET: 53.0 NRS.
FORWARD LICENSEE EVENT REPORT (LER)
COMuacS REGARDus BsRDEN ESnucE TO TsE wOnMucN AND RECORDS MANAGEMENT BMNOH PANDB M14), U.S. NUOLEAR REGULATORY COMMISSON. WASHfNGTON, DC 20$WOOO1. AND TO THE PAPERWORK REDUCTON PRalECT (31WO104), OFFCE OF (See reverse for required number of digits / characters for each bicck)
MANAGEMENT AND BUDGET, WASHNSTON. DC 2D503.
3 F AC8UTY hAME {1; DOCKET NUMBER (2)
PAGE (3)
South Texas, Unit 2 05000 499 1OF05 I
" 5 19 Reactor Trip Due to Failure of a Main Turbine j
Electro-Hydraulic Control Line EVENT DATE (5)
LER NUMBER (6l 3EPORT NUMBER (7)
OTHER FACILITIES INVOLVED (B)
F AQUT Y NAME DOC C NUMBLH ggggg g gg,jggy D^'
M N AY YEAR NuueER NuusER 05000 F ACIUTV NAME DOCKET NUMBER OO 1' O 1 04 2 1 9 3 05000 0 1 2 3 93 93
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OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR 6: (Check one or more) (11)
MODE (9) 1 20 402;b) 20.405(c)
X 50.73(a)(2)(w) 73.71(b)
POWER 20 405(a)(1)(i) 50 36(c)(1) 50 73(a)(2)(v) 73.71(c)
LEVEL (10) 100 20 405(a)(1)(n) 50.36(C)(2) 50.73(a)(2)(vii)
OTHER 20.405fa)(1)(in) 50,73(a)(2)(9 50.73(a)(2)(viii)tA)
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20 405(a)(1)(v) 50.73(aH2)(m) 50.73(a)(2)(x) i LICENSEE CONTACT FOR THIS LER (12) j NwE TREPHONE NUMBLH pouce Ares Gooey l
Jairo Pinzon - Senior Engineer (5 1 2) 972-8 027 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) l
cAUSE
$ V 5TE U COVPONENT MANUFACTURER
CAUSE
SYSTE V COMDONENT MANUFACh)RER g
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SUPPLEMENTAL REPORT EXPECTED (14)
EXPECTED MONTH DAY YEAR 1
SUBMtSSION l
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DATE (15)
ABSTRACT (Limit to 1400 spaces, i e., approximately 15 single-spaced typewritten hnes) (16) j On January 23, 1993, Unit 2 was in Mode 1 at 100% power.
At 2324 hours0.0269 days <br />0.646 hours <br />0.00384 weeks <br />8.84282e-4 months <br />, j
Unit 2 automatically tripped from full power due to a turbine trip above l
the P-9 (50% power) setpoint as the result of a depressurization of the Electro-Hydraulic Control (EHC) supply header.
The low EHC System pressure was due to a leak on the low pressure governor valve line of the Steam Generator Feedwater Pump (SGFP) #22.
The failure initiated on the
]
outside surface with no defect present.
Towards the latter part of the l
l failure, secondary fatigue initiated from the inside as well.
Rapid changes in the valve position created excessive movement within the valve 3
and low pressure line.
The excessive movement was apparently the result I
of an exposed wire on the Linear Variable Differential Transformer
]
(LVDT).
Corrective actions include replacing the failed EHC line and the I
]
LVDT.
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2 FOR REVISION NUMBER l
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7 REPORT DATE 2PRBO UP TO 18 - FACILITY NAME 8
8 TOTAL - DOCKET NUMBER 3 IN ADDITION TO 05000 9
1 OPERATING MODE 10 3
POWER LEVEL i
REQUIREMENTS OF 10 CFR CHECK BOX THAT APPUES UP TO 50 FOR NAME 12 UCENSEE CONTACT 14 FOR TELEPHONE CAUSE VARIES 2 FOR SYSTEM 13 4 FOR COMPONENT EACH COMPONENT FAILURE 4 FOR MANUFACTURER NPRDS VARtES
'4 CHECK BOXTHAT APPUES
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,5 ExeeCTED SUBMISSION DATE
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AN MCD*CS M ANA EMN BMNU WBB W S. NMAA TEXT CONTINUATION AE3J#0RY COMM;S5'ON. EtsSMNG'ON. DO PD*SS D00% AND 70 THE 5'A8'ERwoR< REDUCTON 8'RCJECT (3' soc % OrrCE C5 MANA3E MENT AND BUDGE'f. WAS"W3 TON, DO P3503 f
F ACILITY NAME m DOCPIT NJMBE R (2)
Lf R NUMBER Me
$> AGE (3) smNw rosoN NJVBER NUV95R OF South Texas, Unit 2 05000 499 02 05 9
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DESCRIPTION OF EVENT
On January 23, 1993, Unit 2 was in Mode 1 at 100% power.
At 2324 hours0.0269 days <br />0.646 hours <br />0.00384 weeks <br />8.84282e-4 months <br />, Unit 2 automatically tripped due to a turbine trip above the P-9 (50% power) setpoint.
The Main Turbine tripped due to a low Electro-Hydraulic Control (EHC) pressure below the 1350 psig setpoint.
The depressurization was caused by a failure on the EHC supply line to the low pressure governor valve for Steam Generator Feedwater Pump (SGFP) #22.
The section of fractured tube / fitting assembly has been analyzed.
The failure of the EHC Line was due to fatigue.
The striation spacing appears to indicate low cycle fatigue which occurs typically due to high alternating stresses, possibly accentuated by local stress concentration of a socket weld. The failure initiated on the outside surface with no defect present.
Towards the latter part of the failure, secondary fatigue cracking initiated from inside as well.
The fact that the failure initiation was not i
associated with a weld defect indicates that the fatigue failure was due to vibration rather than due to poor weld quality.
Following repairs on January 28, 1993, excessive motion of SGFP #22 was observed on the high pressure supply line to the low pressure governor valve and in the governor valve itself.
Chart recordings revealed intermittent spiking.
The Linear Variable Differential Transformer (LVDT) which provides the feedback signal to the electronic controller to confirm valve position was replaced.
SGFP startup was initiated and no abnormal line vibrations or valve motions were found.
Visual inspection of the replaced LVDT identified a section of bare wiring.
The LVDT has been sent to the t
l original manufacturer for failure mode analysis.
I During this event, AFW pump #24 started and provided flow to the Steam Generator as required. While manually tripping the Auxiliary Feedwater (AFW) Pump #24 from the Control Room, a mechanical overspeed trip condition was indicated,
- however, no actual j
overspeed condition existed.
An assessment of the AFW overspeed t
trip linkage revealed that when the machine was tripped l
electrically from the Control Room, the trip / throttle valve would i
go shut as designed, but the latch mechanism on the overspeed trip indication device was becoming unlatched.
The uniatching occurred when the pump was electrically tripped from the Control Room, uw-mm j
l l
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!U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 is sa EXPIRES 5/31/95 ES7MA'E3 BJRDEN PE'R FtESPONSE TO COMPLv w7m T its MOAul2ON C AE GJST. 50 0 MRS F OIT6 AEC LICENSEE EVENT REPORT (LER) couvEN,s nEL. met.'ON am BJnot~ EsvuA t To T,E wonunON TEXT CONTINUATION AND,FfCORDS WANt.GEMENT BRANCH fMNBD 7714), U.S NJ,O nE3 any coMuse,,, useyy3s 3: mo:,c,,,m3 TmE F A8'ERWOM REDJCTON PROJECT (3'50@:,4,, 08'F CE OF WANAGEMEN'T AND BJDGEi.
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DOCF f T huMBE R (7)
LER NUMBER (4) f.' AGE (3) hi.QJEN W RE v!W./N NJUBE A NJYBE R OF South Texas, Unit 2 05000 499 03 05
- - 0 0 1-01 pmen ua,a,w.ma..m-m-aw m n v7) i
DESCRIPTION OF EVENT
(Con't)
Additionally, a conflict was noted between the Vendor Manual and s
HL&P procedures with regards to the methods used for tripping the 3
AFW Turbine.
During this event, an additional problem was identified with the Startup eedwater Pump recirculation valve which failed to open, causing feedwater flow oscillations between O to 4000 gpm.
The Startup Feedwater Pump was subsequently secured 1
and the recirc valve was opened.
The Startup Feedwater Pump was
]
restarted and feedwater to the steam generators was established.
CAUSE OF EVENT
j The cause of the reactor / turbine trip was the failure of an j
Electro-Hydraulic Control line of the SGFP #22 causing a low EHC 2
)
system pressure trip.
The f ailure initiated on the outside surface l
with no defect present.
Towards the latter part of the failure, secondary fatigue cracking initiated from inside as well. The fact that the failure initiation was not associated with a weld defect i
indicates that the fatigue failure was due to vibration rather than due to poor weld quality.
It is hypothesized that an exposed wire on the LVDT caused intermittent electrical signals producing rapid changes in the low pressure governor valve position, thus, creating
{
excessive movement within the valve and the low pressure line.
l The cause of the mechanical overspeed indication of the AFW #24 1
pump was a misudjustment in the trip linkage which, when securing the pump electrically, caused the latch mechanism to become unlatched.
t The cause of the Startup Feedwater Pump recirculation valve failure l
to open was valve leakage which caused the valve to become l
j unbalanced and close, or remain closed, with upstream pressure.
Valve leakage was attributed to scoring of the valve plug and body.
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INF CAMATON COLLEC'ON RE3JE ST. 510 HR$
F osrwAt LICENSEE EVENT REPORT (LER)
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TEXT CONTINUATION AND AEO,ORDS MANAGEMEN'T BRAN;N IVNEiB 77tah U $ NJOLEAR
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ANALYSIS OF EVENT
This event is reportable pursuant to 10CFR50.73(a)(2)(iv).
There were no adverse radiological or safety consequences as a result of this event.
All Engineered Safety Systems functioned as designed, with the exception of the problems that were encountered while j
manually tripping the AFW pump #24 which resulted in a mechanical overspeed trip indication.
CORRECTIVE ACTIONS
The following corrective actions have been cr will be taken as the result of the reactor trip:
1.
The failed EHC line was replaced.
l j
i 2.
The failed section of EHC line was sent offsite for failure i
f analysis.
The failure of the EHC Line was due to fatigue.
The I
striation spacing appears to indicate low cycle fatigue which i
I occurs typically due to high alternating stresses, possibly i
accentuated by local stress concentration of a socket weld. The failure initiated on the outside surface with no defect present.
I Towards the latter part of the failure, secondary fatigue l
cracking initiated from inside as well.
The fact that the failure initiation was not associated with a weld defect i
indicates that the fatigue failure was due to vibration rather than due to poor weld quality.
3.
Additional non-destructive examinations were performed on
]
similar welds within the EHC system.
No generic problems were i
identified.
l 4.
The Linear Variable Differential Transformer has been replaced l
and the original LVDT was sent offsite for f ailure analysis.
3 Conversations with the vendor indicates that no problems were identified with the LVDT.
A second failure analysis will be performed using additional information provided by HL&P.
If l-results of the second failure analysis indicate a cause of failure, HL&P will supplement this report.
4 f
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Nac s ouv mA !S sa
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l IU.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104
[
EXPIRES $/31/95 l
m en ESTiMPED BJ4 DEN PER RESDONSE TO COM%y W9 Tws INT ORMATION COii1CTION RE QUEST. 50 0 MRS F onA AR; LICENSEE EVENT REPORT (LER)
Couutes ntaAnam sanotN EswE To T c arDaucos i
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f ACILITY hAME tt)
DOCtIT NUMBEM (7)
LER NUMBE H tSi PAfaE (3) bt OJE%hAL hE chlisN NJVBEA NJUBER OF South Texas, Unit 2 05000 499 05 05 9 3
- - 00 1 -
01 l
s - ~...;. -.... _. - - - -
CORRECTIVE ACTIONS
(Con't)
The following corrective actions have been or will be taken as the i
result of the AFW pump overspeed indication:
l 1.
Adjustments were made to the mechanical overspeed linkage
}
clearance and the pull force on the spring.
2.
HL&P has revised the applicable AFW procedures to ensure these procedures adequately address securing the AFW pump.
j The following corrective action has been taken on the Startup Feedwater Pump recirculation valve
+
1.
The Startup Feedwater Pump recirculation valve was disassembled, inspected, cleaned and reworked. Additionally, the plug seal and plug were replaced.
Upon completion of these troubleshooting i
activities, the valve was satisfactorily stroked.
i
ADDITIONAL INFORMATION
i There have been three previous events involving reactor trips associated with the Electro-Hydraulic Control System. The LERs are as follows:
Unit 1 LER 89-001 regarding a reactor trip due to a failure in e
the Electro-Hydraulic Control circuit which caused the Main i
Turbine throttle valve to close.
The cause of this failure was a poorly crimped lug on a vendor supplied circuit card.
l Unit 2 LER 90-005 regarding a reactor trip due to a loss of EHC l
e fluid caused by a weld failure which was caused by governor l
valve induced vibration.
The cause of the governor valve
[
vibration was determined to be valve plug rotation.
s i
Unit 1 LER 90-015 regarding a reactor trip due to a loss of EHC j
e pressure caused by oscillation in the Main Turbine governor t
valve.
Oscillations were caused by a loose connection in the f
control circuit.
s UMwwt.Ln Na; rDev :t:6A s n, i
u I
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05000498/LER-1993-001, :on 930105,discovered That RCS Loop 3 Outside TS 2.2.1 Range & Loop Declared Inoperable.Caused by Two RCS delta-T Channels Being Inoperable Simultaneously.Loop Restored & Startup Testing Procedure Revised |
- on 930105,discovered That RCS Loop 3 Outside TS 2.2.1 Range & Loop Declared Inoperable.Caused by Two RCS delta-T Channels Being Inoperable Simultaneously.Loop Restored & Startup Testing Procedure Revised
| 10 CFR 50.73(a)(2)(1) | 05000499/LER-1993-001-01, Forwards LER 93-001-01 Re Reactor Trip Due to Failure of Main Turbine electro-hydraulic Control Line.Rev Includes Results of Failure Analyses Performed on Failed Control Line & Linear Variable Differential Transformer | Forwards LER 93-001-01 Re Reactor Trip Due to Failure of Main Turbine electro-hydraulic Control Line.Rev Includes Results of Failure Analyses Performed on Failed Control Line & Linear Variable Differential Transformer | | 05000499/LER-1993-001, :on 930123,unit Automatically Tripped from Full Power Due to Turbine Trip Above P-9 Setpoint as Result of Depressurization of electro-hydraulic Control Supply Header. Failed Line & Differential Transformer Replaced |
- on 930123,unit Automatically Tripped from Full Power Due to Turbine Trip Above P-9 Setpoint as Result of Depressurization of electro-hydraulic Control Supply Header. Failed Line & Differential Transformer Replaced
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) | 05000498/LER-1993-002, :on 930109,TS 3.0.3 Condition Declared When Two Channels of power-range Instrumentation Inoperable.Caused by Inadequate Procedural Guidance in Calibr Procedure.Channel Calorimetrics Procedure Revised |
- on 930109,TS 3.0.3 Condition Declared When Two Channels of power-range Instrumentation Inoperable.Caused by Inadequate Procedural Guidance in Calibr Procedure.Channel Calorimetrics Procedure Revised
| 10 CFR 50.73(a)(2)(1) | 05000499/LER-1993-002-01, :on 930128,unplanned ESF Actuation of Ecw Screen Wash Booster Pump Occurred.Caused by PM Instruction Not Specifically Stating Correct Equipment to Use for Application.Pm Instructions Will Be Revised |
- on 930128,unplanned ESF Actuation of Ecw Screen Wash Booster Pump Occurred.Caused by PM Instruction Not Specifically Stating Correct Equipment to Use for Application.Pm Instructions Will Be Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | 05000498/LER-1993-003, :on 930112,TS 3.0.3 Entered Due to Inoperable Steam Line Pressure Channels.Caused by Lack of Understanding by Procedure Writers Re Calibr Time Constants.Affected Time Constants Calibr |
- on 930112,TS 3.0.3 Entered Due to Inoperable Steam Line Pressure Channels.Caused by Lack of Understanding by Procedure Writers Re Calibr Time Constants.Affected Time Constants Calibr
| 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(1) | 05000499/LER-1993-003-01, :on 930203,unit Entered TS 3.0.3 Due to Loss of Drpi Sys.Caused by Malfunction of Transfer Switch.Design Change Will Be Implemented to Remove Load Associated W/ RT-8010A by 930405 |
- on 930203,unit Entered TS 3.0.3 Due to Loss of Drpi Sys.Caused by Malfunction of Transfer Switch.Design Change Will Be Implemented to Remove Load Associated W/ RT-8010A by 930405
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) | 05000498/LER-1993-004, :on 930112,TS Violated When ASME Section XI Code Surveillance Test Exceeded Grace Period for Outside Containment Isolation Suppl Purge Valve.Desk Top Instruction for Surveillance Coordinator Changed |
- on 930112,TS Violated When ASME Section XI Code Surveillance Test Exceeded Grace Period for Outside Containment Isolation Suppl Purge Valve.Desk Top Instruction for Surveillance Coordinator Changed
| | 05000499/LER-1993-004-01, :on 930203,Unit 2 Experienced Automatic Reactor Trip Due to Low SG Water Level.Caused by Ineffective Action to Correct Failures of Startup SG Feedwater Pumps.Startup Feedwater Pump Seals Will Be Modified |
- on 930203,Unit 2 Experienced Automatic Reactor Trip Due to Low SG Water Level.Caused by Ineffective Action to Correct Failures of Startup SG Feedwater Pumps.Startup Feedwater Pump Seals Will Be Modified
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) | 05000498/LER-1993-005-01, :on 930120,discovered Sdg 13 Failure to Start During Monthly Surveillance Due to Lack of Application of Proper Work Process Controls.Cleaned & Lubricated Affected Fuel Metering Rods |
- on 930120,discovered Sdg 13 Failure to Start During Monthly Surveillance Due to Lack of Application of Proper Work Process Controls.Cleaned & Lubricated Affected Fuel Metering Rods
| 10 CFR 50.73(a)(2)(i) | 05000498/LER-1993-005, Forwards Rev 1 to LER 93-005,in Which Sdg 13 Failed to Start Due to Lack of Application of Proper Work Process Controls Painting Procedures | Forwards Rev 1 to LER 93-005,in Which Sdg 13 Failed to Start Due to Lack of Application of Proper Work Process Controls Painting Procedures | | 05000499/LER-1993-005, :on 930214,control Room Operator Left CR Unmanned During Mode 4 Operation for 41 S.Caused by Inappropriate Action by Unit Supervisor.Event Will Be Included in Licensed Operator Requalification Training |
- on 930214,control Room Operator Left CR Unmanned During Mode 4 Operation for 41 S.Caused by Inappropriate Action by Unit Supervisor.Event Will Be Included in Licensed Operator Requalification Training
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) | 05000499/LER-1993-005-01, Forwards LER 93-005-01 Re CR Unmanned by Senior Licensed Operator During Mode 4 Operation.Original Due Date of 930501 to Complete Command & Control Discussions Not Met. Discussions W/Remaining Personnel to Be Complete by 930 | Forwards LER 93-005-01 Re CR Unmanned by Senior Licensed Operator During Mode 4 Operation.Original Due Date of 930501 to Complete Command & Control Discussions Not Met. Discussions W/Remaining Personnel to Be Complete by 930611 | | 05000498/LER-1993-006, Forwards LER 93-006-00 Re TS Violation Due to RCS Delta Temp/Average Temp Loop Found out-of Tolerance | Forwards LER 93-006-00 Re TS Violation Due to RCS Delta Temp/Average Temp Loop Found out-of Tolerance | | 05000499/LER-1993-006, :on 930217,determined That TS Violation Occurred When MOV-0031A Inoperable from 890409-901108 Due to Misinterpretation of Requirement for Hot Leg Recirculation Operability.Mov Changed to Limit Closed |
- on 930217,determined That TS Violation Occurred When MOV-0031A Inoperable from 890409-901108 Due to Misinterpretation of Requirement for Hot Leg Recirculation Operability.Mov Changed to Limit Closed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) | 05000499/LER-1993-007-01, :on 930310,determined That Control Room Envelope HVAC Sys Was Not in Mode of Operation Required by TS 3.7.7a & 3.3.3.7b.Caused by Implementation & Use of Computer Program.Review Will Be Performed |
- on 930310,determined That Control Room Envelope HVAC Sys Was Not in Mode of Operation Required by TS 3.7.7a & 3.3.3.7b.Caused by Implementation & Use of Computer Program.Review Will Be Performed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) | 05000498/LER-1993-007, :on 930204,TS Required Shutdown Commenced Due to Inoperability of turbine-driven AFW Pump.On 930203,Unit 2 Experienced Reactor Trip.Caused by Water Instrusion Into Pump.Extensive Testing & Analysis Performed |
- on 930204,TS Required Shutdown Commenced Due to Inoperability of turbine-driven AFW Pump.On 930203,Unit 2 Experienced Reactor Trip.Caused by Water Instrusion Into Pump.Extensive Testing & Analysis Performed
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | 05000499/LER-1993-007, Reactor Trip Due to Low SG Water Level.Corrective Actions Will Be Addressed in LER 93-007 | Reactor Trip Due to Low SG Water Level.Corrective Actions Will Be Addressed in LER 93-007 | | 05000499/LER-1993-008, :on 930505,discovered That RHR Pump Suction MOV Had Not Been Environ Qualified Since 901129 Because Replacement of Drain T Not Completed.Drain T Missing from RH-0060B Replaced & Bulletin Issued to Maint Dept |
- on 930505,discovered That RHR Pump Suction MOV Had Not Been Environ Qualified Since 901129 Because Replacement of Drain T Not Completed.Drain T Missing from RH-0060B Replaced & Bulletin Issued to Maint Dept
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | 05000498/LER-1993-008, :on 930206,observed That Requirement of TS 3.3.2 for Containment Pressure High-1 Had Not Been Recorded in Log as Required.Caused by Undetected Error in Control Room Logs.Operator Log Corrected |
- on 930206,observed That Requirement of TS 3.3.2 for Containment Pressure High-1 Had Not Been Recorded in Log as Required.Caused by Undetected Error in Control Room Logs.Operator Log Corrected
| 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) | 05000499/LER-1993-008-01, :on 930505,heat Removal Motor Operated Valve Inoperable in Excess of Allowable Outage Time.Caused by Failure to Recognize Condition.Condition Corrected by Replacing T Drain |
- on 930505,heat Removal Motor Operated Valve Inoperable in Excess of Allowable Outage Time.Caused by Failure to Recognize Condition.Condition Corrected by Replacing T Drain
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | 05000499/LER-1993-009-01, :on 930426,Tech Spec Violation Occurred Due to Use of Inappropriate Ref Value Data for RHR Pump Inservice Test.Surveillance Procedures Revised to Include Appropriate Ref Values |
- on 930426,Tech Spec Violation Occurred Due to Use of Inappropriate Ref Value Data for RHR Pump Inservice Test.Surveillance Procedures Revised to Include Appropriate Ref Values
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | 05000498/LER-1993-009, :on 930217,TS 3.0.3 Entered Due to Potentially Undersized Fuses in Ssps.Caused by Random Age Related Failure of Ssps Fuse.Fuses in Selected Equipment Replaced During Fuse & Breaker Field Verification Effort |
- on 930217,TS 3.0.3 Entered Due to Potentially Undersized Fuses in Ssps.Caused by Random Age Related Failure of Ssps Fuse.Fuses in Selected Equipment Replaced During Fuse & Breaker Field Verification Effort
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) | 05000498/LER-1993-010, :on 930224,halon Actuation Occurred in Plant Computer Room,Associated Distribution Room & Battery Room. Caused by Electrical Load Test on Fps.Licensee Will Revise Fire Harzards Evaluations Procedure |
- on 930224,halon Actuation Occurred in Plant Computer Room,Associated Distribution Room & Battery Room. Caused by Electrical Load Test on Fps.Licensee Will Revise Fire Harzards Evaluations Procedure
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000499/LER-1993-010-01, :on 930526,discovered That Screen Drive Coupling on Essential Cooling Water Traveling Screen 2A Damaged.Caused by Aging of Elastomeric Element.Couplings Replaced & Preventive Maint Initiated |
- on 930526,discovered That Screen Drive Coupling on Essential Cooling Water Traveling Screen 2A Damaged.Caused by Aging of Elastomeric Element.Couplings Replaced & Preventive Maint Initiated
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | 05000498/LER-1993-011, :on 930317,discovered That Monthly Surveillance for Fuel Handling Bldg HVAC Exhaust Sys Did Not Verify That Outside Air Supply Relief Dampers Opened.Caused by Inadequate Procedures.Procedures Revised |
- on 930317,discovered That Monthly Surveillance for Fuel Handling Bldg HVAC Exhaust Sys Did Not Verify That Outside Air Supply Relief Dampers Opened.Caused by Inadequate Procedures.Procedures Revised
| 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) | 05000499/LER-1993-011, Forwards LER 93-011-00 Re Pressurizer Safety Valve Setpoints Outside Required Tolerance | Forwards LER 93-011-00 Re Pressurizer Safety Valve Setpoints Outside Required Tolerance | | 05000499/LER-1993-011-01, :on 930401,pressurizer Safety Valve Setpoints Found Outside Required TS Tolerance.Caused by Setpoint Drift Due to Inherent Valve Characteristics.Mod of Test Procedures Underway |
- on 930401,pressurizer Safety Valve Setpoints Found Outside Required TS Tolerance.Caused by Setpoint Drift Due to Inherent Valve Characteristics.Mod of Test Procedures Underway
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2)(viii)(B) | 05000498/LER-1993-012, :on 930405,TS Violation Occurred Due to Incorrect Settings of Several Molded Case Circuit Breakers. Reset Affected Unit 1 Breakers to Correct Settings |
- on 930405,TS Violation Occurred Due to Incorrect Settings of Several Molded Case Circuit Breakers. Reset Affected Unit 1 Breakers to Correct Settings
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) | 05000499/LER-1993-012-01, :on 930614,lost Spent Fuel Pool Cooling for Approx 13 Hours Due to Insufficient Control Board Awareness. Design Change to Install Annunciator in Control Room to Inform of Loss of Spent Fuel Cooling |
- on 930614,lost Spent Fuel Pool Cooling for Approx 13 Hours Due to Insufficient Control Board Awareness. Design Change to Install Annunciator in Control Room to Inform of Loss of Spent Fuel Cooling
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | 05000498/LER-1993-013, :on 930408,TS 3.1.2.1 & 3.1.2.3 Violated. Caused by Use of Less than Effective Sys for Tracking Inoperable TS Equipment & Actions During Outage.Temporary Labels Placed on Control Board |
- on 930408,TS 3.1.2.1 & 3.1.2.3 Violated. Caused by Use of Less than Effective Sys for Tracking Inoperable TS Equipment & Actions During Outage.Temporary Labels Placed on Control Board
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) | 05000499/LER-1993-013-01, :on 930719,Train B CCW Pump 2B Received Automatic Actuation Signal from non-nuclear Supply Header Low Pressure Signal Due to Less than Adequate Plant Impact review.M0V-0236 Repaired |
- on 930719,Train B CCW Pump 2B Received Automatic Actuation Signal from non-nuclear Supply Header Low Pressure Signal Due to Less than Adequate Plant Impact review.M0V-0236 Repaired
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(e)(2) | 05000498/LER-1993-014, :on 900511,12,14,22 & 23,CR Envelope HVAC Sys Not Operated in Correct Mode.Caused by Increased Administrative Burden & Inadequate Tracking of Lcos. Temporary Labels Placed on Main Control Board |
- on 900511,12,14,22 & 23,CR Envelope HVAC Sys Not Operated in Correct Mode.Caused by Increased Administrative Burden & Inadequate Tracking of Lcos. Temporary Labels Placed on Main Control Board
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) 10 CFR 50.73(a)(2)(viii)(8) | 05000499/LER-1993-015-02, :on 931019,inadvertent Start of Standby Diesel Generator 22 Occurred Due to Spurious Operation of Transistor.Ventilation Fans Installed in All Standby DG Control Cabinets |
- on 931019,inadvertent Start of Standby Diesel Generator 22 Occurred Due to Spurious Operation of Transistor.Ventilation Fans Installed in All Standby DG Control Cabinets
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000498/LER-1993-015-01, :on 930423,Tech Spec Violation Occurred Due to non-conservative Determination of Equipment Svc Time.Caused by Failure to Develop Run Hour Tracking Method.Run Times for Cleanup & Makeup Fans Monitored Individually |
- on 930423,Tech Spec Violation Occurred Due to non-conservative Determination of Equipment Svc Time.Caused by Failure to Develop Run Hour Tracking Method.Run Times for Cleanup & Makeup Fans Monitored Individually
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(8) | 05000498/LER-1993-015, :on 930423,plant Personnel Determined That May 1990 Control Room Makeup & Cleanup Filtration Sys Svc Time Exceeded.Caused by Failure to Develop Run H Tracking Method. Run Times for Cleanup & Makeup Fans Monitored |
- on 930423,plant Personnel Determined That May 1990 Control Room Makeup & Cleanup Filtration Sys Svc Time Exceeded.Caused by Failure to Develop Run H Tracking Method. Run Times for Cleanup & Makeup Fans Monitored
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) 10 CFR 50.73(e)(2)(vii) | 05000498/LER-1993-016, :on 930503,TS Violations Occurred Due to Circuitry for SG Power Operated Relief Valves & Post Accident Monitoring Instruments Being Inoperable.Replaced Missing Screws from Unit 1 Qdps |
- on 930503,TS Violations Occurred Due to Circuitry for SG Power Operated Relief Valves & Post Accident Monitoring Instruments Being Inoperable.Replaced Missing Screws from Unit 1 Qdps
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | 05000499/LER-1993-016-01, :on 931031,train a CCW Pump Received Start Signal When Ccw/Ecw Train a Mode Selector Switch Inadvertently Switched to Run Position Due to Personnel Error.Personnel Involved in Incident Counseled |
- on 931031,train a CCW Pump Received Start Signal When Ccw/Ecw Train a Mode Selector Switch Inadvertently Switched to Run Position Due to Personnel Error.Personnel Involved in Incident Counseled
| 10 CFR 50.73(a)(2)(iv), System Actuation | 05000498/LER-1993-017, :on 930527,concluded That,Based on 930521 Determination,That Feedwater Isolation Bypass Valves Inoperable Since Pneumatic Positioners & Solenoids Remained in Svc Beyond Qualified Life.Control Scheme Modified |
- on 930527,concluded That,Based on 930521 Determination,That Feedwater Isolation Bypass Valves Inoperable Since Pneumatic Positioners & Solenoids Remained in Svc Beyond Qualified Life.Control Scheme Modified
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | 05000498/LER-1993-017-01, Forwards LER 93-017-01 Re Extension of Feedwater Isolation Bypass Positioner & Solenoid Beyond Equipment Qualification Life | Forwards LER 93-017-01 Re Extension of Feedwater Isolation Bypass Positioner & Solenoid Beyond Equipment Qualification Life | | 05000498/LER-1993-018, :on 930707,discovered Remote Position Indication Verification Test for SI Sys Accumulator Vent & Header Valves Had Not Been Performed in 2 Yrs Due to Change to IST Plan |
- on 930707,discovered Remote Position Indication Verification Test for SI Sys Accumulator Vent & Header Valves Had Not Been Performed in 2 Yrs Due to Change to IST Plan
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | 05000498/LER-1993-019, :on 930709,determined That TS Requirement of MSIV Was Not Met Due to Inadequate Design of Field Change to Testing Function of Solid State Protection Sys.Corrected Missing Jumpers & Overlap Testing Discrepancy |
- on 930709,determined That TS Requirement of MSIV Was Not Met Due to Inadequate Design of Field Change to Testing Function of Solid State Protection Sys.Corrected Missing Jumpers & Overlap Testing Discrepancy
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) | 05000498/LER-1993-021, :on 930929,determined That Penetration Backup Fuse 15A Not Wired in Circuit as Required Due to Improper Rewiring of Circuits.Svc Request Disposition to Rework Wiring Per Applicable Design Documents |
- on 930929,determined That Penetration Backup Fuse 15A Not Wired in Circuit as Required Due to Improper Rewiring of Circuits.Svc Request Disposition to Rework Wiring Per Applicable Design Documents
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000498/LER-1993-022, :on 930418,deviation from Method for Contamination Sampling of Fuel Oil Sys Discovered.Caused by Use of Wrong Std to Develop Diesel Fuel Oil Sampling Procedure.Ts Change Will Be Submitted |
- on 930418,deviation from Method for Contamination Sampling of Fuel Oil Sys Discovered.Caused by Use of Wrong Std to Develop Diesel Fuel Oil Sampling Procedure.Ts Change Will Be Submitted
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | 05000498/LER-1993-023-01, :on 931231,non-emergency ESF Actuation of Sdg 12 Occurred.Caused by Electrical Arcing Between Sdg Panel & Test Equipment.Test Equipment & Diesel Circuitry Checked for Malfunction & Degradation |
- on 931231,non-emergency ESF Actuation of Sdg 12 Occurred.Caused by Electrical Arcing Between Sdg Panel & Test Equipment.Test Equipment & Diesel Circuitry Checked for Malfunction & Degradation
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) |
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