05000499/LER-1993-001, :on 930123,unit Automatically Tripped from Full Power Due to Turbine Trip Above P-9 Setpoint as Result of Depressurization of electro-hydraulic Control Supply Header. Failed Line & Differential Transformer Replaced

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:on 930123,unit Automatically Tripped from Full Power Due to Turbine Trip Above P-9 Setpoint as Result of Depressurization of electro-hydraulic Control Supply Header. Failed Line & Differential Transformer Replaced
ML20035G122
Person / Time
Site: South Texas STP Nuclear Operating Company icon.png
Issue date: 04/21/1993
From: Pinzon J
HOUSTON LIGHTING & POWER CO.
To:
Shared Package
ML20035G120 List:
References
LER-93-001, LER-93-1, NUDOCS 9304260188
Download: ML20035G122 (5)


LER-1993-001, on 930123,unit Automatically Tripped from Full Power Due to Turbine Trip Above P-9 Setpoint as Result of Depressurization of electro-hydraulic Control Supply Header. Failed Line & Differential Transformer Replaced
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)

10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

10 CFR 50.73(a)(2)(viii)

10 CFR 50.73(a)(2)(x)

10 CFR 50.73(a)(2)(iv), System Actuation
4991993001R00 - NRC Website

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ESTiMMED BURDEN PE R RESPONSE TO COMPLY WITH TH:S a

INFORMATION COLLECTON REOJEET: 53.0 NRS.

FORWARD LICENSEE EVENT REPORT (LER)

COMuacS REGARDus BsRDEN ESnucE TO TsE wOnMucN AND RECORDS MANAGEMENT BMNOH PANDB M14), U.S. NUOLEAR REGULATORY COMMISSON. WASHfNGTON, DC 20$WOOO1. AND TO THE PAPERWORK REDUCTON PRalECT (31WO104), OFFCE OF (See reverse for required number of digits / characters for each bicck)

MANAGEMENT AND BUDGET, WASHNSTON. DC 2D503.

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South Texas, Unit 2 05000 499 1OF05 I

" 5 19 Reactor Trip Due to Failure of a Main Turbine j

Electro-Hydraulic Control Line EVENT DATE (5)

LER NUMBER (6l 3EPORT NUMBER (7)

OTHER FACILITIES INVOLVED (B)

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OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR 6: (Check one or more) (11)

MODE (9) 1 20 402;b) 20.405(c)

X 50.73(a)(2)(w) 73.71(b)

POWER 20 405(a)(1)(i) 50 36(c)(1) 50 73(a)(2)(v) 73.71(c)

LEVEL (10) 100 20 405(a)(1)(n) 50.36(C)(2) 50.73(a)(2)(vii)

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Jairo Pinzon - Senior Engineer (5 1 2) 972-8 027 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) l

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ABSTRACT (Limit to 1400 spaces, i e., approximately 15 single-spaced typewritten hnes) (16) j On January 23, 1993, Unit 2 was in Mode 1 at 100% power.

At 2324 hours0.0269 days <br />0.646 hours <br />0.00384 weeks <br />8.84282e-4 months <br />, j

Unit 2 automatically tripped from full power due to a turbine trip above l

the P-9 (50% power) setpoint as the result of a depressurization of the Electro-Hydraulic Control (EHC) supply header.

The low EHC System pressure was due to a leak on the low pressure governor valve line of the Steam Generator Feedwater Pump (SGFP) #22.

The failure initiated on the

]

outside surface with no defect present.

Towards the latter part of the l

l failure, secondary fatigue initiated from the inside as well.

Rapid changes in the valve position created excessive movement within the valve 3

and low pressure line.

The excessive movement was apparently the result I

of an exposed wire on the Linear Variable Differential Transformer

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(LVDT).

Corrective actions include replacing the failed EHC line and the I

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LVDT.

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REQUIREMENTS OF 10 CFR CHECK BOX THAT APPUES UP TO 50 FOR NAME 12 UCENSEE CONTACT 14 FOR TELEPHONE CAUSE VARIES 2 FOR SYSTEM 13 4 FOR COMPONENT EACH COMPONENT FAILURE 4 FOR MANUFACTURER NPRDS VARtES

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DESCRIPTION OF EVENT

On January 23, 1993, Unit 2 was in Mode 1 at 100% power.

At 2324 hours0.0269 days <br />0.646 hours <br />0.00384 weeks <br />8.84282e-4 months <br />, Unit 2 automatically tripped due to a turbine trip above the P-9 (50% power) setpoint.

The Main Turbine tripped due to a low Electro-Hydraulic Control (EHC) pressure below the 1350 psig setpoint.

The depressurization was caused by a failure on the EHC supply line to the low pressure governor valve for Steam Generator Feedwater Pump (SGFP) #22.

The section of fractured tube / fitting assembly has been analyzed.

The failure of the EHC Line was due to fatigue.

The striation spacing appears to indicate low cycle fatigue which occurs typically due to high alternating stresses, possibly accentuated by local stress concentration of a socket weld. The failure initiated on the outside surface with no defect present.

Towards the latter part of the failure, secondary fatigue cracking initiated from inside as well.

The fact that the failure initiation was not i

associated with a weld defect indicates that the fatigue failure was due to vibration rather than due to poor weld quality.

Following repairs on January 28, 1993, excessive motion of SGFP #22 was observed on the high pressure supply line to the low pressure governor valve and in the governor valve itself.

Chart recordings revealed intermittent spiking.

The Linear Variable Differential Transformer (LVDT) which provides the feedback signal to the electronic controller to confirm valve position was replaced.

SGFP startup was initiated and no abnormal line vibrations or valve motions were found.

Visual inspection of the replaced LVDT identified a section of bare wiring.

The LVDT has been sent to the t

l original manufacturer for failure mode analysis.

I During this event, AFW pump #24 started and provided flow to the Steam Generator as required. While manually tripping the Auxiliary Feedwater (AFW) Pump #24 from the Control Room, a mechanical overspeed trip condition was indicated,

however, no actual j

overspeed condition existed.

An assessment of the AFW overspeed t

trip linkage revealed that when the machine was tripped l

electrically from the Control Room, the trip / throttle valve would i

go shut as designed, but the latch mechanism on the overspeed trip indication device was becoming unlatched.

The uniatching occurred when the pump was electrically tripped from the Control Room, uw-mm j

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DESCRIPTION OF EVENT

(Con't)

Additionally, a conflict was noted between the Vendor Manual and s

HL&P procedures with regards to the methods used for tripping the 3

AFW Turbine.

During this event, an additional problem was identified with the Startup eedwater Pump recirculation valve which failed to open, causing feedwater flow oscillations between O to 4000 gpm.

The Startup Feedwater Pump was subsequently secured 1

and the recirc valve was opened.

The Startup Feedwater Pump was

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restarted and feedwater to the steam generators was established.

CAUSE OF EVENT

j The cause of the reactor / turbine trip was the failure of an j

Electro-Hydraulic Control line of the SGFP #22 causing a low EHC 2

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system pressure trip.

The f ailure initiated on the outside surface l

with no defect present.

Towards the latter part of the failure, secondary fatigue cracking initiated from inside as well. The fact that the failure initiation was not associated with a weld defect i

indicates that the fatigue failure was due to vibration rather than due to poor weld quality.

It is hypothesized that an exposed wire on the LVDT caused intermittent electrical signals producing rapid changes in the low pressure governor valve position, thus, creating

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excessive movement within the valve and the low pressure line.

l The cause of the mechanical overspeed indication of the AFW #24 1

pump was a misudjustment in the trip linkage which, when securing the pump electrically, caused the latch mechanism to become unlatched.

t The cause of the Startup Feedwater Pump recirculation valve failure l

to open was valve leakage which caused the valve to become l

j unbalanced and close, or remain closed, with upstream pressure.

Valve leakage was attributed to scoring of the valve plug and body.

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ANALYSIS OF EVENT

This event is reportable pursuant to 10CFR50.73(a)(2)(iv).

There were no adverse radiological or safety consequences as a result of this event.

All Engineered Safety Systems functioned as designed, with the exception of the problems that were encountered while j

manually tripping the AFW pump #24 which resulted in a mechanical overspeed trip indication.

CORRECTIVE ACTIONS

The following corrective actions have been cr will be taken as the result of the reactor trip:

1.

The failed EHC line was replaced.

l j

i 2.

The failed section of EHC line was sent offsite for failure i

f analysis.

The failure of the EHC Line was due to fatigue.

The I

striation spacing appears to indicate low cycle fatigue which i

I occurs typically due to high alternating stresses, possibly i

accentuated by local stress concentration of a socket weld. The failure initiated on the outside surface with no defect present.

I Towards the latter part of the failure, secondary fatigue l

cracking initiated from inside as well.

The fact that the failure initiation was not associated with a weld defect i

indicates that the fatigue failure was due to vibration rather than due to poor weld quality.

3.

Additional non-destructive examinations were performed on

]

similar welds within the EHC system.

No generic problems were i

identified.

l 4.

The Linear Variable Differential Transformer has been replaced l

and the original LVDT was sent offsite for f ailure analysis.

3 Conversations with the vendor indicates that no problems were identified with the LVDT.

A second failure analysis will be performed using additional information provided by HL&P.

If l-results of the second failure analysis indicate a cause of failure, HL&P will supplement this report.

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DOCtIT NUMBEM (7)

LER NUMBE H tSi PAfaE (3) bt OJE%hAL hE chlisN NJVBEA NJUBER OF South Texas, Unit 2 05000 499 05 05 9 3

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CORRECTIVE ACTIONS

(Con't)

The following corrective actions have been or will be taken as the i

result of the AFW pump overspeed indication:

l 1.

Adjustments were made to the mechanical overspeed linkage

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clearance and the pull force on the spring.

2.

HL&P has revised the applicable AFW procedures to ensure these procedures adequately address securing the AFW pump.

j The following corrective action has been taken on the Startup Feedwater Pump recirculation valve

+

1.

The Startup Feedwater Pump recirculation valve was disassembled, inspected, cleaned and reworked. Additionally, the plug seal and plug were replaced.

Upon completion of these troubleshooting i

activities, the valve was satisfactorily stroked.

i

ADDITIONAL INFORMATION

i There have been three previous events involving reactor trips associated with the Electro-Hydraulic Control System. The LERs are as follows:

Unit 1 LER 89-001 regarding a reactor trip due to a failure in e

the Electro-Hydraulic Control circuit which caused the Main i

Turbine throttle valve to close.

The cause of this failure was a poorly crimped lug on a vendor supplied circuit card.

l Unit 2 LER 90-005 regarding a reactor trip due to a loss of EHC l

e fluid caused by a weld failure which was caused by governor l

valve induced vibration.

The cause of the governor valve

[

vibration was determined to be valve plug rotation.

s i

Unit 1 LER 90-015 regarding a reactor trip due to a loss of EHC j

e pressure caused by oscillation in the Main Turbine governor t

valve.

Oscillations were caused by a loose connection in the f

control circuit.

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