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'I NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY GMB NO. 3150-0104 i
(s ea EXPIRES 5/31/95 I
ESTiMMED BURDEN PE R RESPONSE TO COMPLY WITH TH:S a
INFORMATION COLLECTON REOJEET: 53.0 NRS.
FORWARD LICENSEE EVENT REPORT (LER)
COMuacS REGARDus BsRDEN ESnucE TO TsE wOnMucN AND RECORDS MANAGEMENT BMNOH PANDB M14), U.S. NUOLEAR REGULATORY COMMISSON. WASHfNGTON, DC 20$WOOO1. AND TO THE PAPERWORK REDUCTON PRalECT (31WO104), OFFCE OF (See reverse for required number of digits / characters for each bicck)
MANAGEMENT AND BUDGET, WASHNSTON. DC 2D503.
3 F AC8UTY hAME {1; DOCKET NUMBER (2)
PAGE (3)
South Texas, Unit 2 05000 499 1OF05 I
" 5 19 Reactor Trip Due to Failure of a Main Turbine j
Electro-Hydraulic Control Line EVENT DATE (5)
LER NUMBER (6l 3EPORT NUMBER (7)
OTHER FACILITIES INVOLVED (B)
F AQUT Y NAME DOC C NUMBLH ggggg g gg,jggy D^'
M N AY YEAR NuueER NuusER 05000 F ACIUTV NAME DOCKET NUMBER OO 1' O 1 04 2 1 9 3 05000 0 1 2 3 93 93
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OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR 6: (Check one or more) (11)
MODE (9) 1 20 402;b) 20.405(c)
X 50.73(a)(2)(w) 73.71(b)
POWER 20 405(a)(1)(i) 50 36(c)(1) 50 73(a)(2)(v) 73.71(c)
LEVEL (10) 100 20 405(a)(1)(n) 50.36(C)(2) 50.73(a)(2)(vii)
OTHER 20.405fa)(1)(in) 50,73(a)(2)(9 50.73(a)(2)(viii)tA)
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20 405(a)(1)(v) 50.73(aH2)(m) 50.73(a)(2)(x) i LICENSEE CONTACT FOR THIS LER (12) j NwE TREPHONE NUMBLH pouce Ares Gooey l
Jairo Pinzon - Senior Engineer (5 1 2) 972-8 027 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) l
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CAUSE
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SUPPLEMENTAL REPORT EXPECTED (14)
EXPECTED MONTH DAY YEAR 1
SUBMtSSION l
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DATE (15)
ABSTRACT (Limit to 1400 spaces, i e., approximately 15 single-spaced typewritten hnes) (16) j On January 23, 1993, Unit 2 was in Mode 1 at 100% power.
At 2324 hours0.0269 days <br />0.646 hours <br />0.00384 weeks <br />8.84282e-4 months <br />, j
Unit 2 automatically tripped from full power due to a turbine trip above l
the P-9 (50% power) setpoint as the result of a depressurization of the Electro-Hydraulic Control (EHC) supply header.
The low EHC System pressure was due to a leak on the low pressure governor valve line of the Steam Generator Feedwater Pump (SGFP) #22.
The failure initiated on the
]
outside surface with no defect present.
Towards the latter part of the l
l failure, secondary fatigue initiated from the inside as well.
Rapid changes in the valve position created excessive movement within the valve 3
and low pressure line.
The excessive movement was apparently the result I
of an exposed wire on the Linear Variable Differential Transformer
]
(LVDT).
Corrective actions include replacing the failed EHC line and the I
]
LVDT.
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FOR E.ACH BLLCK BLOCK NUMBER OF t
NUMBER DIGITS / CHARACTERS 1
UP TO 40 FAClUTY NAME 1
2 DOCKET NUMBER 3 IN ADDril 0 05000 I
3 VARIES PAGE NUMBER f
4 UP TO 76 1?TLE 5
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2 PER BL CK 7 TOT AL 6
LER NUMBER 3 FOR SEQUENTIAL NUMBER l
2 FOR REVISION NUMBER l
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7 REPORT DATE 2PRBO UP TO 18 - FACILITY NAME 8
8 TOTAL - DOCKET NUMBER 3 IN ADDITION TO 05000 9
1 OPERATING MODE 10 3
POWER LEVEL i
REQUIREMENTS OF 10 CFR CHECK BOX THAT APPUES UP TO 50 FOR NAME 12 UCENSEE CONTACT 14 FOR TELEPHONE CAUSE VARIES 2 FOR SYSTEM 13 4 FOR COMPONENT EACH COMPONENT FAILURE 4 FOR MANUFACTURER NPRDS VARtES
'4 CHECK BOXTHAT APPUES
,lys 1^o'cx
,5 ExeeCTED SUBMISSION DATE
e NRC FORM 306A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 EXPlRES 5/31/95 to sa EST! MAND BJRDEN PER RESPONSE TO COMPiY W'M %'s tnt oRuATON CoalC'ON RE OJt KT $3 0 hrs FOnnAsc LICENSEE EVENT REPORT (LER) coMMms REsmNa sJRoEN EsnMan TO mE wCR,uTo.
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F ACILITY NAME m DOCPIT NJMBE R (2)
Lf R NUMBER Me
$> AGE (3) smNw rosoN NJVBER NUV95R OF South Texas, Unit 2 05000 499 02 05 9
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DESCRIPTION OF EVENT
On January 23, 1993, Unit 2 was in Mode 1 at 100% power.
At 2324 hours0.0269 days <br />0.646 hours <br />0.00384 weeks <br />8.84282e-4 months <br />, Unit 2 automatically tripped due to a turbine trip above the P-9 (50% power) setpoint.
The Main Turbine tripped due to a low Electro-Hydraulic Control (EHC) pressure below the 1350 psig setpoint.
The depressurization was caused by a failure on the EHC supply line to the low pressure governor valve for Steam Generator Feedwater Pump (SGFP) #22.
The section of fractured tube / fitting assembly has been analyzed.
The failure of the EHC Line was due to fatigue.
The striation spacing appears to indicate low cycle fatigue which occurs typically due to high alternating stresses, possibly accentuated by local stress concentration of a socket weld. The failure initiated on the outside surface with no defect present.
Towards the latter part of the failure, secondary fatigue cracking initiated from inside as well.
The fact that the failure initiation was not i
associated with a weld defect indicates that the fatigue failure was due to vibration rather than due to poor weld quality.
Following repairs on January 28, 1993, excessive motion of SGFP #22 was observed on the high pressure supply line to the low pressure governor valve and in the governor valve itself.
Chart recordings revealed intermittent spiking.
The Linear Variable Differential Transformer (LVDT) which provides the feedback signal to the electronic controller to confirm valve position was replaced.
SGFP startup was initiated and no abnormal line vibrations or valve motions were found.
Visual inspection of the replaced LVDT identified a section of bare wiring.
The LVDT has been sent to the t
l original manufacturer for failure mode analysis.
I During this event, AFW pump #24 started and provided flow to the Steam Generator as required. While manually tripping the Auxiliary Feedwater (AFW) Pump #24 from the Control Room, a mechanical overspeed trip condition was indicated,
- however, no actual j
overspeed condition existed.
An assessment of the AFW overspeed t
trip linkage revealed that when the machine was tripped l
electrically from the Control Room, the trip / throttle valve would i
go shut as designed, but the latch mechanism on the overspeed trip indication device was becoming unlatched.
The uniatching occurred when the pump was electrically tripped from the Control Room, uw-mm j
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!U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 is sa EXPIRES 5/31/95 ES7MA'E3 BJRDEN PE'R FtESPONSE TO COMPLv w7m T its MOAul2ON C AE GJST. 50 0 MRS F OIT6 AEC LICENSEE EVENT REPORT (LER) couvEN,s nEL. met.'ON am BJnot~ EsvuA t To T,E wonunON TEXT CONTINUATION AND,FfCORDS WANt.GEMENT BRANCH fMNBD 7714), U.S NJ,O nE3 any coMuse,,, useyy3s 3: mo:,c,,,m3 TmE F A8'ERWOM REDJCTON PROJECT (3'50@:,4,, 08'F CE OF WANAGEMEN'T AND BJDGEi.
- ASH!N3'ON. DC M503 f ACILfTV hAME (t)
DOCF f T huMBE R (7)
LER NUMBER (4) f.' AGE (3) hi.QJEN W RE v!W./N NJUBE A NJYBE R OF South Texas, Unit 2 05000 499 03 05
- - 0 0 1-01 pmen ua,a,w.ma..m-m-aw m n v7) i
DESCRIPTION OF EVENT
(Con't)
Additionally, a conflict was noted between the Vendor Manual and s
HL&P procedures with regards to the methods used for tripping the 3
AFW Turbine.
During this event, an additional problem was identified with the Startup eedwater Pump recirculation valve which failed to open, causing feedwater flow oscillations between O to 4000 gpm.
The Startup Feedwater Pump was subsequently secured 1
and the recirc valve was opened.
The Startup Feedwater Pump was
]
restarted and feedwater to the steam generators was established.
CAUSE OF EVENT
j The cause of the reactor / turbine trip was the failure of an j
Electro-Hydraulic Control line of the SGFP #22 causing a low EHC 2
)
system pressure trip.
The f ailure initiated on the outside surface l
with no defect present.
Towards the latter part of the failure, secondary fatigue cracking initiated from inside as well. The fact that the failure initiation was not associated with a weld defect i
indicates that the fatigue failure was due to vibration rather than due to poor weld quality.
It is hypothesized that an exposed wire on the LVDT caused intermittent electrical signals producing rapid changes in the low pressure governor valve position, thus, creating
{
excessive movement within the valve and the low pressure line.
l The cause of the mechanical overspeed indication of the AFW #24 1
pump was a misudjustment in the trip linkage which, when securing the pump electrically, caused the latch mechanism to become unlatched.
t The cause of the Startup Feedwater Pump recirculation valve failure l
to open was valve leakage which caused the valve to become l
j unbalanced and close, or remain closed, with upstream pressure.
Valve leakage was attributed to scoring of the valve plug and body.
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INF CAMATON COLLEC'ON RE3JE ST. 510 HR$
F osrwAt LICENSEE EVENT REPORT (LER)
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ANALYSIS OF EVENT
This event is reportable pursuant to 10CFR50.73(a)(2)(iv).
There were no adverse radiological or safety consequences as a result of this event.
All Engineered Safety Systems functioned as designed, with the exception of the problems that were encountered while j
manually tripping the AFW pump #24 which resulted in a mechanical overspeed trip indication.
CORRECTIVE ACTIONS
The following corrective actions have been cr will be taken as the result of the reactor trip:
1.
The failed EHC line was replaced.
l j
i 2.
The failed section of EHC line was sent offsite for failure i
f analysis.
The failure of the EHC Line was due to fatigue.
The I
striation spacing appears to indicate low cycle fatigue which i
I occurs typically due to high alternating stresses, possibly i
accentuated by local stress concentration of a socket weld. The failure initiated on the outside surface with no defect present.
I Towards the latter part of the failure, secondary fatigue l
cracking initiated from inside as well.
The fact that the failure initiation was not associated with a weld defect i
indicates that the fatigue failure was due to vibration rather than due to poor weld quality.
3.
Additional non-destructive examinations were performed on
]
similar welds within the EHC system.
No generic problems were i
identified.
l 4.
The Linear Variable Differential Transformer has been replaced l
and the original LVDT was sent offsite for f ailure analysis.
3 Conversations with the vendor indicates that no problems were identified with the LVDT.
A second failure analysis will be performed using additional information provided by HL&P.
If l-results of the second failure analysis indicate a cause of failure, HL&P will supplement this report.
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EXPIRES $/31/95 l
m en ESTiMPED BJ4 DEN PER RESDONSE TO COM%y W9 Tws INT ORMATION COii1CTION RE QUEST. 50 0 MRS F onA AR; LICENSEE EVENT REPORT (LER)
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DOCtIT NUMBEM (7)
LER NUMBE H tSi PAfaE (3) bt OJE%hAL hE chlisN NJVBEA NJUBER OF South Texas, Unit 2 05000 499 05 05 9 3
- - 00 1 -
01 l
s - ~...;. -.... _. - - - -
CORRECTIVE ACTIONS
(Con't)
The following corrective actions have been or will be taken as the i
result of the AFW pump overspeed indication:
l 1.
Adjustments were made to the mechanical overspeed linkage
}
clearance and the pull force on the spring.
2.
HL&P has revised the applicable AFW procedures to ensure these procedures adequately address securing the AFW pump.
j The following corrective action has been taken on the Startup Feedwater Pump recirculation valve
+
1.
The Startup Feedwater Pump recirculation valve was disassembled, inspected, cleaned and reworked. Additionally, the plug seal and plug were replaced.
Upon completion of these troubleshooting i
activities, the valve was satisfactorily stroked.
i
ADDITIONAL INFORMATION
i There have been three previous events involving reactor trips associated with the Electro-Hydraulic Control System. The LERs are as follows:
Unit 1 LER 89-001 regarding a reactor trip due to a failure in e
the Electro-Hydraulic Control circuit which caused the Main i
Turbine throttle valve to close.
The cause of this failure was a poorly crimped lug on a vendor supplied circuit card.
l Unit 2 LER 90-005 regarding a reactor trip due to a loss of EHC l
e fluid caused by a weld failure which was caused by governor l
valve induced vibration.
The cause of the governor valve
[
vibration was determined to be valve plug rotation.
s i
Unit 1 LER 90-015 regarding a reactor trip due to a loss of EHC j
e pressure caused by oscillation in the Main Turbine governor t
valve.
Oscillations were caused by a loose connection in the f
control circuit.
s UMwwt.Ln Na; rDev :t:6A s n, i
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| | | Reporting criterion |
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| 05000498/LER-1993-001, :on 930105,discovered That RCS Loop 3 Outside TS 2.2.1 Range & Loop Declared Inoperable.Caused by Two RCS delta-T Channels Being Inoperable Simultaneously.Loop Restored & Startup Testing Procedure Revised |
- on 930105,discovered That RCS Loop 3 Outside TS 2.2.1 Range & Loop Declared Inoperable.Caused by Two RCS delta-T Channels Being Inoperable Simultaneously.Loop Restored & Startup Testing Procedure Revised
| 10 CFR 50.73(a)(2)(1) | | 05000499/LER-1993-001-01, Forwards LER 93-001-01 Re Reactor Trip Due to Failure of Main Turbine electro-hydraulic Control Line.Rev Includes Results of Failure Analyses Performed on Failed Control Line & Linear Variable Differential Transformer | Forwards LER 93-001-01 Re Reactor Trip Due to Failure of Main Turbine electro-hydraulic Control Line.Rev Includes Results of Failure Analyses Performed on Failed Control Line & Linear Variable Differential Transformer | | | 05000499/LER-1993-001, :on 930123,unit Automatically Tripped from Full Power Due to Turbine Trip Above P-9 Setpoint as Result of Depressurization of electro-hydraulic Control Supply Header. Failed Line & Differential Transformer Replaced |
- on 930123,unit Automatically Tripped from Full Power Due to Turbine Trip Above P-9 Setpoint as Result of Depressurization of electro-hydraulic Control Supply Header. Failed Line & Differential Transformer Replaced
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) | | 05000498/LER-1993-002, :on 930109,TS 3.0.3 Condition Declared When Two Channels of power-range Instrumentation Inoperable.Caused by Inadequate Procedural Guidance in Calibr Procedure.Channel Calorimetrics Procedure Revised |
- on 930109,TS 3.0.3 Condition Declared When Two Channels of power-range Instrumentation Inoperable.Caused by Inadequate Procedural Guidance in Calibr Procedure.Channel Calorimetrics Procedure Revised
| 10 CFR 50.73(a)(2)(1) | | 05000499/LER-1993-002-01, :on 930128,unplanned ESF Actuation of Ecw Screen Wash Booster Pump Occurred.Caused by PM Instruction Not Specifically Stating Correct Equipment to Use for Application.Pm Instructions Will Be Revised |
- on 930128,unplanned ESF Actuation of Ecw Screen Wash Booster Pump Occurred.Caused by PM Instruction Not Specifically Stating Correct Equipment to Use for Application.Pm Instructions Will Be Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | | 05000499/LER-1993-003-01, :on 930203,unit Entered TS 3.0.3 Due to Loss of Drpi Sys.Caused by Malfunction of Transfer Switch.Design Change Will Be Implemented to Remove Load Associated W/ RT-8010A by 930405 |
- on 930203,unit Entered TS 3.0.3 Due to Loss of Drpi Sys.Caused by Malfunction of Transfer Switch.Design Change Will Be Implemented to Remove Load Associated W/ RT-8010A by 930405
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) | | 05000498/LER-1993-003, :on 930112,TS 3.0.3 Entered Due to Inoperable Steam Line Pressure Channels.Caused by Lack of Understanding by Procedure Writers Re Calibr Time Constants.Affected Time Constants Calibr |
- on 930112,TS 3.0.3 Entered Due to Inoperable Steam Line Pressure Channels.Caused by Lack of Understanding by Procedure Writers Re Calibr Time Constants.Affected Time Constants Calibr
| 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(1) | | 05000498/LER-1993-004, :on 930112,TS Violated When ASME Section XI Code Surveillance Test Exceeded Grace Period for Outside Containment Isolation Suppl Purge Valve.Desk Top Instruction for Surveillance Coordinator Changed |
- on 930112,TS Violated When ASME Section XI Code Surveillance Test Exceeded Grace Period for Outside Containment Isolation Suppl Purge Valve.Desk Top Instruction for Surveillance Coordinator Changed
| | | 05000499/LER-1993-004-01, :on 930203,Unit 2 Experienced Automatic Reactor Trip Due to Low SG Water Level.Caused by Ineffective Action to Correct Failures of Startup SG Feedwater Pumps.Startup Feedwater Pump Seals Will Be Modified |
- on 930203,Unit 2 Experienced Automatic Reactor Trip Due to Low SG Water Level.Caused by Ineffective Action to Correct Failures of Startup SG Feedwater Pumps.Startup Feedwater Pump Seals Will Be Modified
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) | | 05000499/LER-1993-005-01, Forwards LER 93-005-01 Re CR Unmanned by Senior Licensed Operator During Mode 4 Operation.Original Due Date of 930501 to Complete Command & Control Discussions Not Met. Discussions W/Remaining Personnel to Be Complete by 930 | Forwards LER 93-005-01 Re CR Unmanned by Senior Licensed Operator During Mode 4 Operation.Original Due Date of 930501 to Complete Command & Control Discussions Not Met. Discussions W/Remaining Personnel to Be Complete by 930611 | | | 05000499/LER-1993-005, :on 930214,control Room Operator Left CR Unmanned During Mode 4 Operation for 41 S.Caused by Inappropriate Action by Unit Supervisor.Event Will Be Included in Licensed Operator Requalification Training |
- on 930214,control Room Operator Left CR Unmanned During Mode 4 Operation for 41 S.Caused by Inappropriate Action by Unit Supervisor.Event Will Be Included in Licensed Operator Requalification Training
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) | | 05000498/LER-1993-005-01, :on 930120,discovered Sdg 13 Failure to Start During Monthly Surveillance Due to Lack of Application of Proper Work Process Controls.Cleaned & Lubricated Affected Fuel Metering Rods |
- on 930120,discovered Sdg 13 Failure to Start During Monthly Surveillance Due to Lack of Application of Proper Work Process Controls.Cleaned & Lubricated Affected Fuel Metering Rods
| 10 CFR 50.73(a)(2)(i) | | 05000499/LER-1993-006, :on 930217,TS Violated Due to Train a Cold Leg Injection MOV Being Inoperable for Greaterthan 72 H.Adequacy of Programmatic Controls Re Operability Determination Evaluated & Enhancements Made |
- on 930217,TS Violated Due to Train a Cold Leg Injection MOV Being Inoperable for Greaterthan 72 H.Adequacy of Programmatic Controls Re Operability Determination Evaluated & Enhancements Made
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | | 05000498/LER-1993-006, Forwards LER 93-006-00 Re TS Violation Due to RCS Delta Temp/Average Temp Loop Found out-of Tolerance | Forwards LER 93-006-00 Re TS Violation Due to RCS Delta Temp/Average Temp Loop Found out-of Tolerance | | | 05000499/LER-1993-007-01, :on 930310,determined That Control Room Envelope HVAC Sys Was Not in Mode of Operation Required by TS 3.7.7a & 3.3.3.7b.Caused by Implementation & Use of Computer Program.Review Will Be Performed |
- on 930310,determined That Control Room Envelope HVAC Sys Was Not in Mode of Operation Required by TS 3.7.7a & 3.3.3.7b.Caused by Implementation & Use of Computer Program.Review Will Be Performed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) | | 05000499/LER-1993-007, Reactor Trip Due to Low SG Water Level.Corrective Actions Will Be Addressed in LER 93-007 | Reactor Trip Due to Low SG Water Level.Corrective Actions Will Be Addressed in LER 93-007 | | | 05000498/LER-1993-007, :on 930204,TS Required Shutdown Commenced Due to Inoperability of turbine-driven AFW Pump.On 930203,Unit 2 Experienced Reactor Trip.Caused by Water Instrusion Into Pump.Extensive Testing & Analysis Performed |
- on 930204,TS Required Shutdown Commenced Due to Inoperability of turbine-driven AFW Pump.On 930203,Unit 2 Experienced Reactor Trip.Caused by Water Instrusion Into Pump.Extensive Testing & Analysis Performed
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | | 05000499/LER-1993-008, On 930505,discovered Failure to Maintain Enviromental Qualifications of a RHR Motor Operated Valve.Caused by Lack of Knowledge Regarding Requirements to Maintain Environ Qualifications | On 930505,discovered Failure to Maintain Enviromental Qualifications of a RHR Motor Operated Valve.Caused by Lack of Knowledge Regarding Requirements to Maintain Environ Qualifications | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(s)(2) | | 05000498/LER-1993-008, :on 930206,observed That Requirement of TS 3.3.2 for Containment Pressure High-1 Had Not Been Recorded in Log as Required.Caused by Undetected Error in Control Room Logs.Operator Log Corrected |
- on 930206,observed That Requirement of TS 3.3.2 for Containment Pressure High-1 Had Not Been Recorded in Log as Required.Caused by Undetected Error in Control Room Logs.Operator Log Corrected
| 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) | | 05000499/LER-1993-008-01, :on 930505,heat Removal Motor Operated Valve Inoperable in Excess of Allowable Outage Time.Caused by Failure to Recognize Condition.Condition Corrected by Replacing T Drain |
- on 930505,heat Removal Motor Operated Valve Inoperable in Excess of Allowable Outage Time.Caused by Failure to Recognize Condition.Condition Corrected by Replacing T Drain
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000499/LER-1993-009-01, :on 930426,Tech Spec Violation Occurred Due to Use of Inappropriate Ref Value Data for RHR Pump Inservice Test.Surveillance Procedures Revised to Include Appropriate Ref Values |
- on 930426,Tech Spec Violation Occurred Due to Use of Inappropriate Ref Value Data for RHR Pump Inservice Test.Surveillance Procedures Revised to Include Appropriate Ref Values
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | | 05000498/LER-1993-009, :on 930217,TS 3.0.3 Entered Due to Potentially Undersized Fuses in Ssps.Caused by Random Age Related Failure of Ssps Fuse.Fuses in Selected Equipment Replaced During Fuse & Breaker Field Verification Effort |
- on 930217,TS 3.0.3 Entered Due to Potentially Undersized Fuses in Ssps.Caused by Random Age Related Failure of Ssps Fuse.Fuses in Selected Equipment Replaced During Fuse & Breaker Field Verification Effort
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) | | 05000499/LER-1993-010-01, :on 930526,discovered That Screen Drive Coupling on Essential Cooling Water Traveling Screen 2A Damaged.Caused by Aging of Elastomeric Element.Couplings Replaced & Preventive Maint Initiated |
- on 930526,discovered That Screen Drive Coupling on Essential Cooling Water Traveling Screen 2A Damaged.Caused by Aging of Elastomeric Element.Couplings Replaced & Preventive Maint Initiated
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000498/LER-1993-010, :on 930224,halon Actuation Occurred in Plant Computer Room,Associated Distribution Room & Battery Room. Caused by Electrical Load Test on Fps.Licensee Will Revise Fire Harzards Evaluations Procedure |
- on 930224,halon Actuation Occurred in Plant Computer Room,Associated Distribution Room & Battery Room. Caused by Electrical Load Test on Fps.Licensee Will Revise Fire Harzards Evaluations Procedure
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000499/LER-1993-011, :on 930401,pressure Safety Valve (Psv) & MSSV Setpoints Found Outside Required Tolerance Due to Industry Known Problem Re Setpoint Drift.Test Procedure to Test Psv Lift Setpoint on Saturated Steam Modified |
- on 930401,pressure Safety Valve (Psv) & MSSV Setpoints Found Outside Required Tolerance Due to Industry Known Problem Re Setpoint Drift.Test Procedure to Test Psv Lift Setpoint on Saturated Steam Modified
| | | 05000499/LER-1993-011-01, :on 930401,pressurizer Safety Valve Setpoints Found Outside Required TS Tolerance.Caused by Setpoint Drift Due to Inherent Valve Characteristics.Mod of Test Procedures Underway |
- on 930401,pressurizer Safety Valve Setpoints Found Outside Required TS Tolerance.Caused by Setpoint Drift Due to Inherent Valve Characteristics.Mod of Test Procedures Underway
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2)(viii)(B) | | 05000498/LER-1993-011, :on 930317,discovered That Monthly Surveillance for Fuel Handling Bldg HVAC Exhaust Sys Did Not Verify That Outside Air Supply Relief Dampers Opened.Caused by Inadequate Procedures.Procedures Revised |
- on 930317,discovered That Monthly Surveillance for Fuel Handling Bldg HVAC Exhaust Sys Did Not Verify That Outside Air Supply Relief Dampers Opened.Caused by Inadequate Procedures.Procedures Revised
| 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) | | 05000498/LER-1993-012, :on 930405,TS Violation Occurred Due to Incorrect Settings of Several Molded Case Circuit Breakers. Reset Affected Unit 1 Breakers to Correct Settings |
- on 930405,TS Violation Occurred Due to Incorrect Settings of Several Molded Case Circuit Breakers. Reset Affected Unit 1 Breakers to Correct Settings
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) | | 05000499/LER-1993-012-01, :on 930614,lost Spent Fuel Pool Cooling for Approx 13 Hours Due to Insufficient Control Board Awareness. Design Change to Install Annunciator in Control Room to Inform of Loss of Spent Fuel Cooling |
- on 930614,lost Spent Fuel Pool Cooling for Approx 13 Hours Due to Insufficient Control Board Awareness. Design Change to Install Annunciator in Control Room to Inform of Loss of Spent Fuel Cooling
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000499/LER-1993-013-01, :on 930719,Train B CCW Pump 2B Received Automatic Actuation Signal from non-nuclear Supply Header Low Pressure Signal Due to Less than Adequate Plant Impact review.M0V-0236 Repaired |
- on 930719,Train B CCW Pump 2B Received Automatic Actuation Signal from non-nuclear Supply Header Low Pressure Signal Due to Less than Adequate Plant Impact review.M0V-0236 Repaired
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(e)(2) | | 05000499/LER-1993-013, :on 930719,inadvertent ESF Actuation Occurred Due to Component Cooling Water Pump Start During Maint Work Activity.Caused by Inadequate Plant Inpact Review.Time Delay Placed in CCW Pump |
- on 930719,inadvertent ESF Actuation Occurred Due to Component Cooling Water Pump Start During Maint Work Activity.Caused by Inadequate Plant Inpact Review.Time Delay Placed in CCW Pump
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) | | 05000498/LER-1993-013, :on 930408,TS 3.1.2.1 & 3.1.2.3 Violated. Caused by Use of Less than Effective Sys for Tracking Inoperable TS Equipment & Actions During Outage.Temporary Labels Placed on Control Board |
- on 930408,TS 3.1.2.1 & 3.1.2.3 Violated. Caused by Use of Less than Effective Sys for Tracking Inoperable TS Equipment & Actions During Outage.Temporary Labels Placed on Control Board
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) | | 05000498/LER-1993-014, :on 900511,12,14,22 & 23,CR Envelope HVAC Sys Not Operated in Correct Mode.Caused by Increased Administrative Burden & Inadequate Tracking of Lcos. Temporary Labels Placed on Main Control Board |
- on 900511,12,14,22 & 23,CR Envelope HVAC Sys Not Operated in Correct Mode.Caused by Increased Administrative Burden & Inadequate Tracking of Lcos. Temporary Labels Placed on Main Control Board
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) 10 CFR 50.73(a)(2)(viii)(8) | | 05000498/LER-1993-015-01, :on 930423,Tech Spec Violation Occurred Due to non-conservative Determination of Equipment Svc Time.Caused by Failure to Develop Run Hour Tracking Method.Run Times for Cleanup & Makeup Fans Monitored Individually |
- on 930423,Tech Spec Violation Occurred Due to non-conservative Determination of Equipment Svc Time.Caused by Failure to Develop Run Hour Tracking Method.Run Times for Cleanup & Makeup Fans Monitored Individually
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(8) | | 05000499/LER-1993-015-02, :on 931019,inadvertent Start of Standby Diesel Generator 22 Occurred Due to Spurious Operation of Transistor.Ventilation Fans Installed in All Standby DG Control Cabinets |
- on 931019,inadvertent Start of Standby Diesel Generator 22 Occurred Due to Spurious Operation of Transistor.Ventilation Fans Installed in All Standby DG Control Cabinets
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000498/LER-1993-015, :on 930423,plant Personnel Determined That May 1990 Control Room Makeup & Cleanup Filtration Sys Svc Time Exceeded.Caused by Failure to Develop Run H Tracking Method. Run Times for Cleanup & Makeup Fans Monitored |
- on 930423,plant Personnel Determined That May 1990 Control Room Makeup & Cleanup Filtration Sys Svc Time Exceeded.Caused by Failure to Develop Run H Tracking Method. Run Times for Cleanup & Makeup Fans Monitored
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) 10 CFR 50.73(e)(2)(vii) | | 05000499/LER-1993-016-01, :on 931031,train a CCW Pump Received Start Signal When Ccw/Ecw Train a Mode Selector Switch Inadvertently Switched to Run Position Due to Personnel Error.Personnel Involved in Incident Counseled |
- on 931031,train a CCW Pump Received Start Signal When Ccw/Ecw Train a Mode Selector Switch Inadvertently Switched to Run Position Due to Personnel Error.Personnel Involved in Incident Counseled
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000498/LER-1993-016, :on 930503,TS Violations Occurred Due to Circuitry for SG Power Operated Relief Valves & Post Accident Monitoring Instruments Being Inoperable.Replaced Missing Screws from Unit 1 Qdps |
- on 930503,TS Violations Occurred Due to Circuitry for SG Power Operated Relief Valves & Post Accident Monitoring Instruments Being Inoperable.Replaced Missing Screws from Unit 1 Qdps
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | | 05000498/LER-1993-017-01, Forwards LER 93-017-01 Re Extension of Feedwater Isolation Bypass Positioner & Solenoid Beyond Equipment Qualification Life | Forwards LER 93-017-01 Re Extension of Feedwater Isolation Bypass Positioner & Solenoid Beyond Equipment Qualification Life | | | 05000498/LER-1993-017, :on 930527,concluded That,Based on 930521 Determination,That Feedwater Isolation Bypass Valves Inoperable Since Pneumatic Positioners & Solenoids Remained in Svc Beyond Qualified Life.Control Scheme Modified |
- on 930527,concluded That,Based on 930521 Determination,That Feedwater Isolation Bypass Valves Inoperable Since Pneumatic Positioners & Solenoids Remained in Svc Beyond Qualified Life.Control Scheme Modified
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000498/LER-1993-018, :on 930707,discovered Remote Position Indication Verification Test for SI Sys Accumulator Vent & Header Valves Had Not Been Performed in 2 Yrs Due to Change to IST Plan |
- on 930707,discovered Remote Position Indication Verification Test for SI Sys Accumulator Vent & Header Valves Had Not Been Performed in 2 Yrs Due to Change to IST Plan
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | | 05000498/LER-1993-019, :on 930709,determined That TS Requirement of MSIV Was Not Met Due to Inadequate Design of Field Change to Testing Function of Solid State Protection Sys.Corrected Missing Jumpers & Overlap Testing Discrepancy |
- on 930709,determined That TS Requirement of MSIV Was Not Met Due to Inadequate Design of Field Change to Testing Function of Solid State Protection Sys.Corrected Missing Jumpers & Overlap Testing Discrepancy
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) | | 05000498/LER-1993-021, :on 930929,determined That Penetration Backup Fuse 15A Not Wired in Circuit as Required Due to Improper Rewiring of Circuits.Svc Request Disposition to Rework Wiring Per Applicable Design Documents |
- on 930929,determined That Penetration Backup Fuse 15A Not Wired in Circuit as Required Due to Improper Rewiring of Circuits.Svc Request Disposition to Rework Wiring Per Applicable Design Documents
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000498/LER-1993-022, :on 930418,deviation from Method for Contamination Sampling of Fuel Oil Sys Discovered.Caused by Use of Wrong Std to Develop Diesel Fuel Oil Sampling Procedure.Ts Change Will Be Submitted |
- on 930418,deviation from Method for Contamination Sampling of Fuel Oil Sys Discovered.Caused by Use of Wrong Std to Develop Diesel Fuel Oil Sampling Procedure.Ts Change Will Be Submitted
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | | 05000498/LER-1993-023-01, :on 931231,non-emergency ESF Actuation of Sdg 12 Occurred.Caused by Electrical Arcing Between Sdg Panel & Test Equipment.Test Equipment & Diesel Circuitry Checked for Malfunction & Degradation |
- on 931231,non-emergency ESF Actuation of Sdg 12 Occurred.Caused by Electrical Arcing Between Sdg Panel & Test Equipment.Test Equipment & Diesel Circuitry Checked for Malfunction & Degradation
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) | | 05000498/LER-1993-023, :on 931231,inadvertent ESF Actuation of Sdg 12 Occurred During Testing.Sdg Will Be Placed in Pull-to-Stop Whenever Maint Activities Performed Involving Connecting Measuring or Test Equipment to Sdg Electrical Circuits |
- on 931231,inadvertent ESF Actuation of Sdg 12 Occurred During Testing.Sdg Will Be Placed in Pull-to-Stop Whenever Maint Activities Performed Involving Connecting Measuring or Test Equipment to Sdg Electrical Circuits
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii)(B) |
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