05000499/LER-2014-001, Standby Diesel Generator 23 Essential Cooling Water Leak Through the Wall of Aluminum-Bronze Pipe Nipple

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Standby Diesel Generator 23 Essential Cooling Water Leak Through the Wall of Aluminum-Bronze Pipe Nipple
ML14086A388
Person / Time
Site: South Texas STP Nuclear Operating Company icon.png
Issue date: 03/17/2014
From: Gerry Powell
South Texas
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
NOC-AE-14003102 LER 14-001-00
Download: ML14086A388 (6)


LER-2014-001, Standby Diesel Generator 23 Essential Cooling Water Leak Through the Wall of Aluminum-Bronze Pipe Nipple
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

10 CFR 50.73(a)(2)(v), Loss of Safety Function

10 CFR 50.73(a)(2)(i)

10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded

10 CFR 50.73(a)(2)(viii)(A)

10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

10 CFR 50.73(a)(2)(viii)(B)

10 CFR 50.73(a)(2)(iii)

10 CFR 50.73(a)(2)(ix)(A)

10 CFR 50.73(a)(2)(iv)(A), System Actuation

10 CFR 50.73(a)(2)(x)

10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor

10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat

10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown
4992014001R00 - NRC Website

text

Nuclear Operating Company South Texas Pro/ed Electric Genera/tig Sta2t,,,,

PO Box 289 Wadsworth. Texas 77483 March 17, 2014 NOC-AE-14003102 10 CFR 50.73 U. S. Nuclear Regulatory Commission Attention: Document Control Desk Washington, DC 20555-0001 South Texas Project Unit 2 Docket No. STN 50-499 Licensee Event Report 2014-001-00 LER 2014-001-00: Standby Diesel Generator 23 Essential Cooling Water Leak Throuqh the Wall of Aluminum-Bronze Pipe Nipple Pursuant to 10 CFR 50.73(a)(2)(i)(B) and 10 CFR 50.73(a)(2)(v), South Texas Project Nuclear Operating Company (STPNOC) submits the attached South Texas Project (STP) Unit 2 Licensee Event Report (LER) 2014-001-00 regarding a Standby Diesel Generator 23 Essential Cooling Water leak through the wall of an Aluminum-Bronze pipe nipple.

This event did not have an adverse effect on the health and safety of the public.

There are no commitments in this letter. Corrective actions will be implemented in accordance with the STP Corrective Action Program.

If there are any questions, please contact Wendy Brost at (361) 972-8516, or me at (361) 972-7566.

G. T. Powell Site Vice President web

Attachment:

Unit 2 LER 2014-001-00

/L-XI-4 STI33840342

NOC-AE-14003102 Page 2 of 2 cc:

(paper copy)

Regional Administrator, Region IV U. S. Nuclear Regulatory Commission 1600 East Lamar Boulevard Arlington, TX 76011-4511 Balwant K. Singal Senior Project Manager U.S. Nuclear Regulatory Commission One White Flint North (MS 8 B1) 11555 Rockville Pike Rockville, MD 20852 NRC Resident Inspector U. S. Nuclear Regulatory Commission P. 0. Box 289, Mail Code: MN1 16 Wadsworth, TX 77483 Jim Collins City of Austin Electric Utility Department 721 Barton Springs Road Austin, TX 78704 (electronic copy)

A. H. Gutterman, Esquire Morgan, Lewis & Bockius LLP Balwant K. Singal U. S. Nuclear Regulatory Commission John Ragan Chris O'Hara Jim von Suskil NRG South Texas LP Kevin Polio Richard Pei~a L. D. Blaylock City Public Service Peter Nemeth Crain Caton & James, P.C.

C. Mele City of Austin Richard A. Ratliff Robert Free Texas Department of State Health Services

NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 01131/2017 (02-2014)

Estimated burden per response to comply with this mandatory collection request: 80 hours9.259259e-4 days <br />0.0222 hours <br />1.322751e-4 weeks <br />3.044e-5 months <br />.

Reported lessons learned are incorporated into the licensing process and fed back to industry.

Send comments regarding burden estimate to the FOIA, Privacy and Information Collections SLICENSEE EVENT REPORT (LER)

Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by m

internet e-mail to Infocollects.Resource@nrc.gov, and to the Desk Officer, Office of Information and (See Page 2 for required number of Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB digits/characters for each block) control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

3. PAGE South Texas Unit 2 05000499 1 OF 4 K.

TITLE Standby Diesel Generator 23 Essential Cooling Water Leak through the Wall of Aluminum-Bronze Pipe Nipple

5. EVENT DATE
6. LER NUMBER
7. REPORT DATE
8. OTHER FACILITIES INVOLVED MONTH DAY YEAR YEAR SEQUENTIAL REV MONTH DAY YEAR NA NUMBER NO.

N/A N/A FACILITY NAME DOCKET NUMBER 12 31 2013 2014-001

- 001 03 17 2014 N/A N/A
9. OPERATING MODE
11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check all that apply)

D1 20.2201(b) 0 20.2203(a)(3)(i)

F1 50.73(a)(2)(i)(C)

El 50.73(a)(2)(vii)

D1 20.2201(d)

ED 20.2203(a)(3)(ii)

D1 50.73(a)(2)(ii)(A)

[I 50.73(a)(2)(viii)(A)

D1 20.2203(a)(1)

D 20.2203(a)(4)

[D 50.73(a)(2)(ii)(B)

D1 50.73(a)(2)(viii)(B) 1 R 20.2203(a)(2)(i) 0 50.36(c)(1)(i)(A)

El 50.73(a)(2)(iii)

El 50.73(a)(2)(ix)(A)

10. POWER LEVEL 20.2203(a)(2)(ii)

F1 50.36(c)(1)(ii)(A) 50.73(a)(2)(iv)(A)

LI 50.73(a)(2)(x)

El 20.2203(a)(2)(iii)

F1 50.36(c)(2)

[] 50.73(a)(2)(v)(A)

[] 73.71 (a)(4)

LI 20.2203(a)(2)(iv)

- I 50.46(a)(3)(ii)

EL 50.73(a)(2)(v)(B)

[1 73.71(a)(5) 099 E] 20.2203(a)(2)(v)

LI 50.73(a)(2)(i)(A)

El 50.73(a)(2)(v)(C)

LI OTHER EL 20.2203(a)(2)(vi)

Z 50.73(a)(2)(i)(B)

Z 50.73(a)(2)(v)(D)

Specify in Abstract below or in

12. LICENSEE_

CONTACTFOR_

THIS____

1.

DESCRIPTION OF EVENT

A.

REPORTABLE EVENT CLASSIFICATION

This event is reportable pursuant to 10 CFR 50.73(a)(2)(i)(B), any operation or condition which was prohibited by the plant's Technical Specifications. The event is also reportable pursuant to 10 CFR 50.73(a)(2)(v)(D), any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident.

B.

PLANT OPERATING CONDITIONS PRIOR TO EVENT

Unit 2 was operating in Mode 1 at 99.5% power.

C.

STATUS OF STRUCTURES, SYSTEMS, AND COMPONENTS THAT WERE INOPERABLE AT THE START OF THE EVENT AND THAT CONTRIBUTED TO THE EVENT The event resulted from the inoperability of Standby Diesel Generator (SDG) 23 due to leakage from an aluminum-bronze nipple and tee assembly. There were no other structures, systems, or components that were inoperable at the start of the event that contributed to the event.

D.

NARRATIVE SUMMARY OF THE EVENT

On October 3, 2013, an approximately one gpm leak was identified on SDG 22 due to unsatisfactory thread engagement and only slight erosion was noted. This condition was immediately documented and repaired. Work orders were then scheduled to replace the aluminum-bronze tees and piping nipples on SDG 23 and SDG 11 with stainless steel components using an existing design change package (DCP).

The aluminum-bronze components had already been replaced with stainless steel components for SDGs 13, 21 and 12.

On November 6, 2013, during a monthly surveillance run of SDG 23, a 60 drop per minute (dpm) leak was identified from a half-inch aluminum-bronze threaded tee connecting the intercooler continuous flowing vents to the Essential Cooling Water (ECW) return piping. This condition was evaluated by Operations and the SDG was declared Operable but Degraded.

During a monthly surveillance run of SDG 23 on December 31, 2013 at 13:46 hours, an approximately three gpm ECW leak was discovered on SDG 23 originating from the same location as the smaller leak identified on November 6, 2013. Operations subsequently declared SDG 23 inoperable and non-functional. The leaking nipple and tee assembly was replaced with stainless steel components on December 31, 2013. SDG 23 was declared operable January 1, 2014.

A Reportability Review completed on January 16, 2014 determined this condition was reportable as a condition prohibited by Technical Specifications pursuant to CFR 50.73(a)(2)(i)(B) and as a condition that could have prevented fulfillment of a safety function reportable pursuant to CFR 50.73(a)(2)(v).

E.

METHOD OF DISCOVERY

Both the initial 60 dpm leak on November 6, 2013 and the three gpm leak on December 31, 2013 were discovered during monthly surveillance runs of SDG 23.

Following a reportability review completed on January 16, 2014, the event was determined to be reportable as a condition prohibited by Technical Specifications and a condition that could have prevented the fulfillment of a safety function.

11.

EVENT-DRIVEN INFORMATION A.

SAFETY SYSTEMS THAT RESPONDED The SDG leaks were discovered during surveillance activities. No safety systems were required to respond to this event.

B.

DURATION OF SAFETY SYSTEM INOPERABILITY

SDG 23 was determined to be inoperable from the time of discovery of the initial leak on November 6, 2013 at approximately 1330 hours0.0154 days <br />0.369 hours <br />0.0022 weeks <br />5.06065e-4 months <br /> until the time SDG was declared operable following maintenance and post-maintenance testing on January 1, 2014 at 0157 hours0.00182 days <br />0.0436 hours <br />2.595899e-4 weeks <br />5.97385e-5 months <br />, a time period of approximately 55 days 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and 27 minutes, which exceeded the 14-day allowed outage time allowed by Technical Specification 3.8.1.1. During the time period when SDG 23 was inoperable, there were short periods when one of the other SDGs was also inoperable. Therefore, in addition to being a condition prohibited by Technical Specifications this event is also reportable as a condition that could have prevented the fulfillment of a safety function.

C.

SAFETY CONSEQUENCES AND IMPLICATIONS OF THE EVENT The event did not have an adverse effect on the health and safety of the public.

A risk assessment was performed for this event. The assessment concluded that, given a small leak of three gpm, SDG 23 would fail in 1.5 days due to flooding of the room; however, SDG 23 would still meet the PRA mission time of 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Credit was given for the performance of operator rounds which would give sufficient time to discover the leak and to implement mitigating strategies. In the case of a Loss of Offsite Power (LOOP), the assessment concludes that the LOOP non-recovery probability is low and recovery is likely to occur before the SDG fails. The calculated incremental core damage probability and incremental large early release probability are very small for this event.

II1.

CAUSE OF THE EVENT

The cause of the event is erosion of the aluminum-bronze nipple and tee assembly that led to a through-wall ECW leak.

IV.

CORRECTIVE ACTIONS

The aluminum-bronze tee and piping nipple for SDG 23 were replaced with stainless steel components on December 31, 2013 using a previously approved design change. On January 8, 2014 the aluminum-bronze tee and piping nipple for SDG 11 were also replaced, completing the replacement of the aluminum-bronze tee assemblies with stainless steel components for the six SDGs at STPEGS.

V.

PREVIOUS SIMILAR EVENTS

There have been no similar reportable events at STP related to erosion based degradation within the last three years that have occurred for the same reason as this event.

VI.

ADDITIONAL INFORMATION

None