|
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000498/LER-1999-008, :on 990912,unit Tripped During Performance of Main Turbine Emergency Trip Test Procedures.Caused by Failure in Turbine Trip Test Circuitry.Main Control Boards Were Cleaned & Other Panels Were Inspected1999-10-12012 October 1999
- on 990912,unit Tripped During Performance of Main Turbine Emergency Trip Test Procedures.Caused by Failure in Turbine Trip Test Circuitry.Main Control Boards Were Cleaned & Other Panels Were Inspected
05000499/LER-1999-006-01, :on 990901,TS 3.0.3 Entered.Caused by Insufficient Procedural Guidance for Use of TS 3.0.6.SG 2D low-level Channel 2 Input Relay to ESF Actuation Logic Circuitry Replaced on 9909011999-09-30030 September 1999
- on 990901,TS 3.0.3 Entered.Caused by Insufficient Procedural Guidance for Use of TS 3.0.6.SG 2D low-level Channel 2 Input Relay to ESF Actuation Logic Circuitry Replaced on 990901
05000499/LER-1999-005-01, :on 990824,ESFA Following Loss of Power to Standby Transformer 2 Was Noted.Internal Fault Caused C Phase Arrester Failure.Replaced All Surge Arresters for Standby Transformer 21999-09-20020 September 1999
- on 990824,ESFA Following Loss of Power to Standby Transformer 2 Was Noted.Internal Fault Caused C Phase Arrester Failure.Replaced All Surge Arresters for Standby Transformer 2
05000498/LER-1999-007, :on 990812,plant Train B CR Makeup & Cleanup Filtration Sys Was Declared Inoperable for Greater than Aot. Caused by Degradation of Makeup Filter & Filter Charcoal Due to Aging.Subject Filter Was Replaced on 9908051999-09-13013 September 1999
- on 990812,plant Train B CR Makeup & Cleanup Filtration Sys Was Declared Inoperable for Greater than Aot. Caused by Degradation of Makeup Filter & Filter Charcoal Due to Aging.Subject Filter Was Replaced on 990805
NOC-AE-000583, LER 99-S03-00:on 990619,failure to Revitalize Sdg Number 11 Was Noted.Caused by Failure to Communicate Status of Sdg. Subject Sdg Revitalized on 990619 & Licensee Will Develop Security Force Instruction Re Sdgs.With1999-07-15015 July 1999 LER 99-S03-00:on 990619,failure to Revitalize Sdg Number 11 Was Noted.Caused by Failure to Communicate Status of Sdg. Subject Sdg Revitalized on 990619 & Licensee Will Develop Security Force Instruction Re Sdgs.With NOC-AE-000570, LER 99-S01-00:on 990527,discovered That Unescorted Access Had Been Inappropriately Granted.Caused by Failure to Follow Procedure.Util Verified That Individual Did Not Have Current Unescorted Access at STP or Any Other Util.With1999-06-28028 June 1999 LER 99-S01-00:on 990527,discovered That Unescorted Access Had Been Inappropriately Granted.Caused by Failure to Follow Procedure.Util Verified That Individual Did Not Have Current Unescorted Access at STP or Any Other Util.With ML20196G5821999-06-23023 June 1999 LER 99-S02-00:on 990601,failure to Maintain Positive Control of Vital Area Security Key Was Noted.Caused by Lack of Attention to Detail.Discussed Event with Operator Involved IAW Constructive Discipline Program 05000498/LER-1999-004-01, :on 990516,Unit 1 Experienced Automatic Reactor Trip.Caused by Equipment Failure.Stp Will Evaluate Potential Transformer Testing Procedure for Incorporation of Fuse Resistance Measurements by 990715.With1999-06-15015 June 1999
- on 990516,Unit 1 Experienced Automatic Reactor Trip.Caused by Equipment Failure.Stp Will Evaluate Potential Transformer Testing Procedure for Incorporation of Fuse Resistance Measurements by 990715.With
05000498/LER-1999-003-01, :on 990329,CR HVAC Was Placed in Recirculation Mode of Operation Instead of Recirculation Mu Filtered Mode. Caused by Inadequate Verbal Communications.Briefed Crews on Attention to Detail During three-way Communications1999-04-29029 April 1999
- on 990329,CR HVAC Was Placed in Recirculation Mode of Operation Instead of Recirculation Mu Filtered Mode. Caused by Inadequate Verbal Communications.Briefed Crews on Attention to Detail During three-way Communications
05000498/LER-1999-002-01, :on 990327,inadequate Performance of TS Surveillance When Evaluating Source Range Nuclear Instrument Discriminator Bias Curve Results,Was Discovered.Caused by Lack of Process to Incorporate Info.Compared Bias Curves1999-04-26026 April 1999
- on 990327,inadequate Performance of TS Surveillance When Evaluating Source Range Nuclear Instrument Discriminator Bias Curve Results,Was Discovered.Caused by Lack of Process to Incorporate Info.Compared Bias Curves
05000498/LER-1999-001-01, :on 990311,RHR Sys Was Found in Condition Outside Design Basis.Caused by Inadequate Implementation of Design Basis Requirements.Condition Remedied by Opening Disconnect Switches Per Rev to Plant Procedures1999-04-12012 April 1999
- on 990311,RHR Sys Was Found in Condition Outside Design Basis.Caused by Inadequate Implementation of Design Basis Requirements.Condition Remedied by Opening Disconnect Switches Per Rev to Plant Procedures
05000499/LER-1998-004-01, :on 981228,plant Was Shutdown Required by TS 3.3.2.Caused by Failure in Ssps Test Circuitry.Testing Circuit Card Was Replaced1999-01-26026 January 1999
- on 981228,plant Was Shutdown Required by TS 3.3.2.Caused by Failure in Ssps Test Circuitry.Testing Circuit Card Was Replaced
05000498/LER-1998-010, :on 981021,FHB Exhaust Booster Fan 11A Was Declared Inoperable When Ground Indication Was Discovered During Sp.Caused by Fan Motor That Needed to Be Replaced. Preventive Maint Was Performed on Motors.With1998-11-19019 November 1998
- on 981021,FHB Exhaust Booster Fan 11A Was Declared Inoperable When Ground Indication Was Discovered During Sp.Caused by Fan Motor That Needed to Be Replaced. Preventive Maint Was Performed on Motors.With
05000499/LER-1998-003-01, :on 981016,discovered Missed Tube Insp in SG 2B,per TS Surveillance 4.4.5.2.Caused by Lack of Addl Controls to Prevent Re SG Tube Insp Data.Licensee Revised 2FE05 Insp Records & SG Insp Database.With1998-11-12012 November 1998
- on 981016,discovered Missed Tube Insp in SG 2B,per TS Surveillance 4.4.5.2.Caused by Lack of Addl Controls to Prevent Re SG Tube Insp Data.Licensee Revised 2FE05 Insp Records & SG Insp Database.With
05000499/LER-1998-002-01, :on 980922,automatic RT Occurred Due to low-low Level in SG 2A.Caused by Failure to Adequately Verify Technical Accuracy of Changes Made to Original Work Instructions.Reviewed Other Similar Work in Progress1998-10-15015 October 1998
- on 980922,automatic RT Occurred Due to low-low Level in SG 2A.Caused by Failure to Adequately Verify Technical Accuracy of Changes Made to Original Work Instructions.Reviewed Other Similar Work in Progress
ML20237A1201998-08-0505 August 1998 LER 98-S01-00:on 980707,loss of Power Supply to Security Sys Occurred.Caused by Inverter Switching to Alternate Power Source Due to Intermittent Failure of Static Switch Board. Static Switch Board Replaced,Per 10CFR73.71 05000498/LER-1997-013, :on 971111,supplementary CPS Isolation Valve Failed to Meet TS Leak Rate Requirements.Caused by Inadequate Process for Developing Measuring & Test Equipment Calibration Spec.Revised Plants Procedures1998-04-16016 April 1998
- on 971111,supplementary CPS Isolation Valve Failed to Meet TS Leak Rate Requirements.Caused by Inadequate Process for Developing Measuring & Test Equipment Calibration Spec.Revised Plants Procedures
05000498/LER-1997-006, :on 970507,inappropriate Surveillance Procedure Monitoring Parameters Were Noted.Caused by Inadequate Review of Changes Made to TS & Bases.Evaluated Review Processes for TS Changes W/Focus on Changes to Bases1998-04-0909 April 1998
- on 970507,inappropriate Surveillance Procedure Monitoring Parameters Were Noted.Caused by Inadequate Review of Changes Made to TS & Bases.Evaluated Review Processes for TS Changes W/Focus on Changes to Bases
05000498/LER-1998-002, :on 980203,SG Narrow Range Level EOP just-in narrow-range Setpoint Was Noted Different than Setpoint for Current Sgs.Caused by Incorrectly Assuming Height in Calculation to Determine Eop.Revised EOP for SGs1998-03-0505 March 1998
- on 980203,SG Narrow Range Level EOP just-in narrow-range Setpoint Was Noted Different than Setpoint for Current Sgs.Caused by Incorrectly Assuming Height in Calculation to Determine Eop.Revised EOP for SGs
05000498/LER-1998-001-01, :on 980122,failure to Perform an Adequate TS Surveillance Re Containment Structural Integrity.Caused by Ineffective Performance.Training on New Calculation Procedure Has Been Provided1998-02-23023 February 1998
- on 980122,failure to Perform an Adequate TS Surveillance Re Containment Structural Integrity.Caused by Ineffective Performance.Training on New Calculation Procedure Has Been Provided
05000499/LER-1997-007-01, :on 971121,manual Reactor Trip Occurred.Caused by Two Separate Failure Mechanisms That Combined to Result in Loss of Power to Cabinet.Failed Voltage to Pulse Converter Circuit Card Was Replaced1997-12-18018 December 1997
- on 971121,manual Reactor Trip Occurred.Caused by Two Separate Failure Mechanisms That Combined to Result in Loss of Power to Cabinet.Failed Voltage to Pulse Converter Circuit Card Was Replaced
05000498/LER-1997-013, :on 971111,failure to Meet Tech Spec Leak Rate Requirements for Suppl Containment Purge Supply Isolation Valve Occurred.Caused by Inadequate Process for Developing Measuring & Test Equipment.Procedures Revised1997-12-11011 December 1997
- on 971111,failure to Meet Tech Spec Leak Rate Requirements for Suppl Containment Purge Supply Isolation Valve Occurred.Caused by Inadequate Process for Developing Measuring & Test Equipment.Procedures Revised
05000498/LER-1997-010, :on 970920,discovered That MSSVs 7430A & 7430B Failed to Meet Required Relief Capacity.Caused by Inadequate Resolution Issues.Revised Procedures & Corrected Lift Setting Adjustment1997-10-16016 October 1997
- on 970920,discovered That MSSVs 7430A & 7430B Failed to Meet Required Relief Capacity.Caused by Inadequate Resolution Issues.Revised Procedures & Corrected Lift Setting Adjustment
ST-HL-AE-5762, LER 97-S03-00:on 970904,doors to Two Vital Areas Were Not Posted to Compensate for Partial Sys Failure.Caused by Supervisor Failing to Follow Procedure.Searched Affected Vital Areas for Unauthorized Matls & Personnel1997-10-0303 October 1997 LER 97-S03-00:on 970904,doors to Two Vital Areas Were Not Posted to Compensate for Partial Sys Failure.Caused by Supervisor Failing to Follow Procedure.Searched Affected Vital Areas for Unauthorized Matls & Personnel 05000498/LER-1997-009, :on 970902,MSSV Setpoints Were Found Outside Required Tolerance.Caused by Alteration of Nozzle & Disc Oxide Layers.Adjusted Lift Settings of Valves & Refurbished Valves1997-10-0202 October 1997
- on 970902,MSSV Setpoints Were Found Outside Required Tolerance.Caused by Alteration of Nozzle & Disc Oxide Layers.Adjusted Lift Settings of Valves & Refurbished Valves
05000498/LER-1997-008, :on 970811,ESF Containment Spray Actuation Relays Slave Relay Test Were Not Fully Tested by Surveillance.Caused by Failure to Understand Expectations Re Documentation.Spray Pumps Verified Operable1997-09-10010 September 1997
- on 970811,ESF Containment Spray Actuation Relays Slave Relay Test Were Not Fully Tested by Surveillance.Caused by Failure to Understand Expectations Re Documentation.Spray Pumps Verified Operable
ST-HL-AE-5721, LER 97-S02-00:on 970721,all Power Lost to Security Sys at Completion of Lighting DG Performance Test.Caused by Security Personnel Did Not Recognize Nature or Significance of Bypass Trouble Alarm.Training Conducted1997-08-20020 August 1997 LER 97-S02-00:on 970721,all Power Lost to Security Sys at Completion of Lighting DG Performance Test.Caused by Security Personnel Did Not Recognize Nature or Significance of Bypass Trouble Alarm.Training Conducted 05000498/LER-1997-007, :on 970619,ESFAS Pressurizer Pressure Sys Interlock Was Not Fully Tested by Surveillance Procedures. Caused by Failure to Recognize That Circuitry Did Not Include Required Provisions.Revised Sps1997-07-21021 July 1997
- on 970619,ESFAS Pressurizer Pressure Sys Interlock Was Not Fully Tested by Surveillance Procedures. Caused by Failure to Recognize That Circuitry Did Not Include Required Provisions.Revised Sps
05000498/LER-1997-006-01, :on 970508,inappropriate Surveillance Procedure Monitoring Parameters Found,Due to Less than Adequate Review of Vantage 5H License Amend.Limits Established in Operator Log Surveillance Procedure1997-06-10010 June 1997
- on 970508,inappropriate Surveillance Procedure Monitoring Parameters Found,Due to Less than Adequate Review of Vantage 5H License Amend.Limits Established in Operator Log Surveillance Procedure
05000499/LER-1997-006, :on 970430,manual Reactor Trip Occurred.Caused by Malfunctioning Main Feedwater Regulating Valve.Main 2D Feedwater Regulating Valve controller-driver Card Replaced & Control Circuit Tested Satisfactorily1997-05-29029 May 1997
- on 970430,manual Reactor Trip Occurred.Caused by Malfunctioning Main Feedwater Regulating Valve.Main 2D Feedwater Regulating Valve controller-driver Card Replaced & Control Circuit Tested Satisfactorily
05000498/LER-1997-005-01, :on 970402,main Steam Safety Valve Setpoints Were Discovered Outside Required Tolerance Due to Alteration of Nozzle Seat & Disc Seat Oxide Layers.Lift Settings Were Adjusted to Required Allowable Tolerances1997-05-0101 May 1997
- on 970402,main Steam Safety Valve Setpoints Were Discovered Outside Required Tolerance Due to Alteration of Nozzle Seat & Disc Seat Oxide Layers.Lift Settings Were Adjusted to Required Allowable Tolerances
05000499/LER-1997-005, :on 970326,manual Unit Trip Occurred Due to Lowering SG Level.Failed seal-in Relay Was Replaced & Verified That Other seal-in Relays Affecting MFRVs in Both Units 1 & 2 Had Proper Coil Resistances1997-04-24024 April 1997
- on 970326,manual Unit Trip Occurred Due to Lowering SG Level.Failed seal-in Relay Was Replaced & Verified That Other seal-in Relays Affecting MFRVs in Both Units 1 & 2 Had Proper Coil Resistances
05000498/LER-1997-004, :on 970319,failed to Fully Test 4160 Volt Bus Undervoltage Logic Circuitry by Surveillance Procedures. Caused by Not Recognizing That Failure in One Actuation Scheme.Affected Logic Circuitry Was Tested1997-04-17017 April 1997
- on 970319,failed to Fully Test 4160 Volt Bus Undervoltage Logic Circuitry by Surveillance Procedures. Caused by Not Recognizing That Failure in One Actuation Scheme.Affected Logic Circuitry Was Tested
05000499/LER-1997-004-01, :on 970319,unit Trip Occurred While Performing Main Turbine Testing Due to Intermittent Failure of Inverter Power Supply for Channel Two Automatic Stop Trip Valve. Inverter Power Supply Was Replaced1997-04-17017 April 1997
- on 970319,unit Trip Occurred While Performing Main Turbine Testing Due to Intermittent Failure of Inverter Power Supply for Channel Two Automatic Stop Trip Valve. Inverter Power Supply Was Replaced
05000499/LER-1997-002-01, :on 970215,Steam Generators 2A Eddy Current Insp Results Fell Into Category C-3.Caused by Stress Corrosion Cracking at tube-to-tube Support Plate.Sg Tubes Were Plugged in Four Unit 2 Steam Generators1997-03-13013 March 1997
- on 970215,Steam Generators 2A Eddy Current Insp Results Fell Into Category C-3.Caused by Stress Corrosion Cracking at tube-to-tube Support Plate.Sg Tubes Were Plugged in Four Unit 2 Steam Generators
05000499/LER-1997-001-01, :on 970205,main Steam Safety Valve Setpoints Discovered Outside Required Tolerance Occurred.Caused by MSSV Above & Beyond Previously Documented Setpoint Drift. Lift Setting of Five MSSV Were Adjusted1997-03-0606 March 1997
- on 970205,main Steam Safety Valve Setpoints Discovered Outside Required Tolerance Occurred.Caused by MSSV Above & Beyond Previously Documented Setpoint Drift. Lift Setting of Five MSSV Were Adjusted
ST-HL-AE-5591, LER 97-S01-00:on 970130,security Door Intrusion Alarm Was Disabled.Caused Because Risk Assessment for Testing Plan Did Not Ensure Adequate Compensatory Actions Were in Place to Prevent Error.Modified Startup & Testing Plan1997-02-27027 February 1997 LER 97-S01-00:on 970130,security Door Intrusion Alarm Was Disabled.Caused Because Risk Assessment for Testing Plan Did Not Ensure Adequate Compensatory Actions Were in Place to Prevent Error.Modified Startup & Testing Plan 05000498/LER-1997-003, :on 970123,potential for Overpressurization of Piping Identified.Caused by Deficiency in Original Design. Thermal Insulation Installed on Lines 3WL-1009 & 3WL-2009 & Lines Have Been Returned to Service1997-02-24024 February 1997
- on 970123,potential for Overpressurization of Piping Identified.Caused by Deficiency in Original Design. Thermal Insulation Installed on Lines 3WL-1009 & 3WL-2009 & Lines Have Been Returned to Service
05000498/LER-1997-001, :on 970116,failure to Meet Requirements of TS Surveillance Requirement 4.7.13 Identified.Caused by Incorrect Repeatability Value Provided by Supplier of Temp Switch.Switches Evaluated1997-02-13013 February 1997
- on 970116,failure to Meet Requirements of TS Surveillance Requirement 4.7.13 Identified.Caused by Incorrect Repeatability Value Provided by Supplier of Temp Switch.Switches Evaluated
05000498/LER-1997-002, :on 970115,safety Injection Sys Logic Circuitry Not Fully Tested by Surveillance Procedures.Caused by Unusual Logic Arrangement.Containment Sump Isolation Valves Have Been Tested1997-02-13013 February 1997
- on 970115,safety Injection Sys Logic Circuitry Not Fully Tested by Surveillance Procedures.Caused by Unusual Logic Arrangement.Containment Sump Isolation Valves Have Been Tested
05000498/LER-1996-005, :on 961213,reactor Containment Building Personnel Airlock Incorrectly Declared Operable Occurred. Caused by Pertinent Information Re Status of Seal Replacement.Occurrence Has Been Reviewed1997-01-13013 January 1997
- on 961213,reactor Containment Building Personnel Airlock Incorrectly Declared Operable Occurred. Caused by Pertinent Information Re Status of Seal Replacement.Occurrence Has Been Reviewed
05000498/LER-1996-004, :on 961120,unanalyzed Conditions Were Noted Due to Discovery of Two Spare SR Circuit Breakers Not in Seismically Qualified Position.Caused by Failure to Follow Established Procedures.Revised Procedures1996-12-18018 December 1996
- on 961120,unanalyzed Conditions Were Noted Due to Discovery of Two Spare SR Circuit Breakers Not in Seismically Qualified Position.Caused by Failure to Follow Established Procedures.Revised Procedures
05000498/LER-1995-013, :on 951218,turbine Trip & Reactor Trip Occurred,Due to Main Transformer Lockout.Caused by Improper Maint Performance.Grounded Connection Repaired,Mgt Expectations Reinforced & Procedures Revised1996-10-0303 October 1996
- on 951218,turbine Trip & Reactor Trip Occurred,Due to Main Transformer Lockout.Caused by Improper Maint Performance.Grounded Connection Repaired,Mgt Expectations Reinforced & Procedures Revised
05000499/LER-1996-003, :on 960828,failure to Fully Meet Requirements of TS Occurred,Due to Discovery of Improperly Installed Jumper on Main Steam Line Pressure Lead/Lag Circuit Card. Personnel Issues Have Been Addressed1996-09-25025 September 1996
- on 960828,failure to Fully Meet Requirements of TS Occurred,Due to Discovery of Improperly Installed Jumper on Main Steam Line Pressure Lead/Lag Circuit Card. Personnel Issues Have Been Addressed
05000498/LER-1996-009, :on 960620,containment Closeout Insp Failed to Recognize Unauthorized Material Left in Containment.Caused by Inadequate Requirement Review.Removed Bagged Equipment & Completed Containment Closeout Insp1996-07-17017 July 1996
- on 960620,containment Closeout Insp Failed to Recognize Unauthorized Material Left in Containment.Caused by Inadequate Requirement Review.Removed Bagged Equipment & Completed Containment Closeout Insp
05000498/LER-1996-002-01, :on 960507,failure to Meet Requirements of Tech Specs Occurred.Caused by Inattention to Detail During Documentation & Review of Testing Results.Feedback from Event Given to Individuals Involved1996-06-0606 June 1996
- on 960507,failure to Meet Requirements of Tech Specs Occurred.Caused by Inattention to Detail During Documentation & Review of Testing Results.Feedback from Event Given to Individuals Involved
05000498/LER-1996-001-01, :on 960328,Standby Diesel Generator Declared Inoperable.Caused by Barriers for Preparation & Planning Not Being Fully Implemented.Personnel Involved Counseled Re Event & Revised Preventive Maint Documents1996-06-0303 June 1996
- on 960328,Standby Diesel Generator Declared Inoperable.Caused by Barriers for Preparation & Planning Not Being Fully Implemented.Personnel Involved Counseled Re Event & Revised Preventive Maint Documents
05000499/LER-1996-002, :on 960314,fuel Handling Bldg Exhaust Air Damper Inoperable Due to Inappropriate Design Implementation.Made Mods to Fuel Handling Bldg Emergency Exhaust Dampers to Resolve Issue1996-04-24024 April 1996
- on 960314,fuel Handling Bldg Exhaust Air Damper Inoperable Due to Inappropriate Design Implementation.Made Mods to Fuel Handling Bldg Emergency Exhaust Dampers to Resolve Issue
05000499/LER-1996-001, :on 960119,TS 3.0.3 Entry Occurred Due to Two MFW Isolation Valves Being Inoperable at Same Time.Discussed Enhanced Mgt Expectations W/Emphasis on Clear & Concise Communications1996-02-19019 February 1996
- on 960119,TS 3.0.3 Entry Occurred Due to Two MFW Isolation Valves Being Inoperable at Same Time.Discussed Enhanced Mgt Expectations W/Emphasis on Clear & Concise Communications
05000498/LER-1995-012, :on 950926,RHR Pump Impeller Cracks Occurred. Caused by Improper Mfg of Impeller.Rhr Pump Impeller Replaced1996-01-0909 January 1996
- on 950926,RHR Pump Impeller Cracks Occurred. Caused by Improper Mfg of Impeller.Rhr Pump Impeller Replaced
1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K9151999-10-15015 October 1999 SER Authorizing Util Relief Request RR-ENG-2-3 for Second 10-year ISI Interval of Stp,Units 1 & 2 Pursuant to 10CFR50.55a(a)(3)(i) ML20217K9441999-10-15015 October 1999 SER Accepting Util Alternative Proposed Relief Request RR-ENG-2-4 for Second 10-year ISI Interval at Stp,Units 1 & 2 Pursuant to 10CFR50.55a(a)(3)(i) 05000498/LER-1999-008, :on 990912,unit Tripped During Performance of Main Turbine Emergency Trip Test Procedures.Caused by Failure in Turbine Trip Test Circuitry.Main Control Boards Were Cleaned & Other Panels Were Inspected1999-10-12012 October 1999
- on 990912,unit Tripped During Performance of Main Turbine Emergency Trip Test Procedures.Caused by Failure in Turbine Trip Test Circuitry.Main Control Boards Were Cleaned & Other Panels Were Inspected
NOC-AE-000676, Monthly Operating Repts for Sept 1999 for South Texas Project,Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for South Texas Project,Units 1 & 2.With 05000499/LER-1999-006-01, :on 990901,TS 3.0.3 Entered.Caused by Insufficient Procedural Guidance for Use of TS 3.0.6.SG 2D low-level Channel 2 Input Relay to ESF Actuation Logic Circuitry Replaced on 9909011999-09-30030 September 1999
- on 990901,TS 3.0.3 Entered.Caused by Insufficient Procedural Guidance for Use of TS 3.0.6.SG 2D low-level Channel 2 Input Relay to ESF Actuation Logic Circuitry Replaced on 990901
ML20217D0531999-09-30030 September 1999 Rev 1 to STP Electric Generating Station Unit 2 Cycle 7 Colr ML20217D0481999-09-30030 September 1999 Rev 1 to STP Electric Generating Station Unit 1 Cycle 9 Colr 05000499/LER-1999-005-01, :on 990824,ESFA Following Loss of Power to Standby Transformer 2 Was Noted.Internal Fault Caused C Phase Arrester Failure.Replaced All Surge Arresters for Standby Transformer 21999-09-20020 September 1999
- on 990824,ESFA Following Loss of Power to Standby Transformer 2 Was Noted.Internal Fault Caused C Phase Arrester Failure.Replaced All Surge Arresters for Standby Transformer 2
ML20212C2811999-09-13013 September 1999 Safety Evaluation Supporting Amends 116 & 104 to Licenses NPF-76 & NPF-80,respectively 05000498/LER-1999-007, :on 990812,plant Train B CR Makeup & Cleanup Filtration Sys Was Declared Inoperable for Greater than Aot. Caused by Degradation of Makeup Filter & Filter Charcoal Due to Aging.Subject Filter Was Replaced on 9908051999-09-13013 September 1999
- on 990812,plant Train B CR Makeup & Cleanup Filtration Sys Was Declared Inoperable for Greater than Aot. Caused by Degradation of Makeup Filter & Filter Charcoal Due to Aging.Subject Filter Was Replaced on 990805
ML20211P8411999-09-0909 September 1999 Safety Evaluation Supporting Alternative Proposed by Licensee to Surface Exam to Perform Boroscopic VT-1 Visual Exam of Pump Casing Welds within Pump Pits for Welds Covered by Relief Request RR-ENG-24 ML20211Q6731999-09-0909 September 1999 Safety Evaluation Accepting First 10-yr Interval ISI Program Plan Request for Relief from ASME Code Case N-498 ML20211P7811999-09-0909 September 1999 SER Approving Second 10-year Interval Inservice Insp Program Plan Relief Request RR-ENG-2-8 (to Use Code Case N-491-2) for South Texas Project,Units 1 & 2 ML20211P9001999-09-0202 September 1999 Safety Evaluation Supporting Amends 115 & 103 to Licenses NPF-76 & NPF-80,respectively ML20212E5191999-08-31031 August 1999 Rev 3 to SG-99-04-005, STP 1RE08 Outage Condition Monitoring Rept & Final Operational Assessment NOC-AE-000643, Monthly Operating Repts for Aug 1999 for South Texas Project,Units 1 & 2.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for South Texas Project,Units 1 & 2.With ML20211F4531999-08-24024 August 1999 Safety Evaluation Supporting Licensee Proposed Alternative to Defer Partial First Period Exams of flange-to-shell Weld to Third Period & Perform Required Ultrasonic Exams,Both Manual & Automated,During Third Period ML20211F5111999-08-23023 August 1999 Safety Evaluation Supporting Licensee Proposed Alternative Contained in Request for Relief RR-ENG-30 ML20211F3651999-08-19019 August 1999 Safety Evaluation Supporting Amends 114 & 102 to Licenses NPF-76 & NPF-80,respectively ML20210K4881999-08-0303 August 1999 Safety Evaluation Supporting Amends 113 & 101 to Licenses NPF-76 & NPF-80,respectively ML20210R3631999-07-31031 July 1999 Monthly Operating Repts for July 1999 for South Tx Project, Units 1 & 2.With ML20210C9411999-07-31031 July 1999 Rev 1 to SG-99-07-002, South Tx,Unit 1 Cycle 9 Voltage- Based Repair Criteria 90-Day Rept, Jul 1999 ML20210D9161999-07-23023 July 1999 Safety Evaluation Accepting Inservice Testing Relief Request RR-56 Re Component Cooling Water & Safety Injection Sys Containment Isolation Check Valve Closure Test Frequency ML20210D4821999-07-21021 July 1999 1RE08 ISI Summary Rept for Steam Generator Tubing of South Texas Project Electric Generating Station Unit 1 ML20210D4491999-07-21021 July 1999 Revised Chapters to Operations QA Plan, Including Rev 9 to Chapter 1.0, Organization & Rev 6 to Chapter 16.0, Independent Technical Review NOC-AE-000583, LER 99-S03-00:on 990619,failure to Revitalize Sdg Number 11 Was Noted.Caused by Failure to Communicate Status of Sdg. Subject Sdg Revitalized on 990619 & Licensee Will Develop Security Force Instruction Re Sdgs.With1999-07-15015 July 1999 LER 99-S03-00:on 990619,failure to Revitalize Sdg Number 11 Was Noted.Caused by Failure to Communicate Status of Sdg. Subject Sdg Revitalized on 990619 & Licensee Will Develop Security Force Instruction Re Sdgs.With ML20207H6361999-07-0808 July 1999 Safety Evaluation Approving 2nd 10 Yr Interval ISI Program Plan Request to Use ASME Section XI Code Case N-546 for Licenses NPF-76 & NPF-80,respectively ML20216D7481999-07-0707 July 1999 1RE08 ISI Summary Rept for Welds & Component Supports of STP Electric Generating Station,Unit 1 ML20196K7091999-07-0202 July 1999 Safety Evaluation Supporting Amend 100 to License NPF-80 NOC-AE-000593, Monthly Operating Repts for June 1999 for Stp,Units 1 & 2. with1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Stp,Units 1 & 2. with NOC-AE-000570, LER 99-S01-00:on 990527,discovered That Unescorted Access Had Been Inappropriately Granted.Caused by Failure to Follow Procedure.Util Verified That Individual Did Not Have Current Unescorted Access at STP or Any Other Util.With1999-06-28028 June 1999 LER 99-S01-00:on 990527,discovered That Unescorted Access Had Been Inappropriately Granted.Caused by Failure to Follow Procedure.Util Verified That Individual Did Not Have Current Unescorted Access at STP or Any Other Util.With ML20196G5821999-06-23023 June 1999 LER 99-S02-00:on 990601,failure to Maintain Positive Control of Vital Area Security Key Was Noted.Caused by Lack of Attention to Detail.Discussed Event with Operator Involved IAW Constructive Discipline Program ML20212J0031999-06-23023 June 1999 Safety Evaluation Supporting Amends 112 & 99 to Licenses NPF-76 & NPF-80,respectively ML20195J6871999-06-17017 June 1999 Safety Evaluation Supporting Proposed Alternative Contained in RR-ENG-2-5.Proposed Alternative Authorized Per 10CFR50.55a(a)(3)(i) for 2nd ISI Interval ML20195J6531999-06-16016 June 1999 Safety Evaluation Supporting Amends 111 & 76 to Licenses NPF-76 & NPF-80,respectively ML20196A2391999-06-15015 June 1999 Change QA-042 to Rev 13 of Operations QAP, Reflecting Current Organizational Alignment for South Texas Project & Culminating Organizational Realigment That Has Been Taking Place During Past Several Months 05000498/LER-1999-004-01, :on 990516,Unit 1 Experienced Automatic Reactor Trip.Caused by Equipment Failure.Stp Will Evaluate Potential Transformer Testing Procedure for Incorporation of Fuse Resistance Measurements by 990715.With1999-06-15015 June 1999
- on 990516,Unit 1 Experienced Automatic Reactor Trip.Caused by Equipment Failure.Stp Will Evaluate Potential Transformer Testing Procedure for Incorporation of Fuse Resistance Measurements by 990715.With
NOC-AE-000563, Monthly Operating Repts for May 1999 for Stp,Units 1 & 2. with1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Stp,Units 1 & 2. with ML20206U7731999-05-20020 May 1999 Safety Evaluation Supporting Amends 110 & 97 to Licenses NPF-76 & NPF-80,respectively ML20206U5411999-05-18018 May 1999 Non-proprietary Errata Pages for Rev 2,Addendum 1 to WCAP-13699, Laser Welded Sleeves for 3/4 Inch Diamete Tube Feedring Type & W Preheater SGs Generic Sleeving Rept ML20207A1101999-05-17017 May 1999 Safety Evaluation Supporting Amends 109 & 96 to Licenses NPF-76 & NPF-80,respectively NOC-AE-000543, Monthly Operating Repts for Apr 1999 for Stp,Units 1 & 2. with1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Stp,Units 1 & 2. with ML20206A7721999-04-30030 April 1999 STP Electric Generating Station Unit 1 Cycle 9 Colr 05000498/LER-1999-003-01, :on 990329,CR HVAC Was Placed in Recirculation Mode of Operation Instead of Recirculation Mu Filtered Mode. Caused by Inadequate Verbal Communications.Briefed Crews on Attention to Detail During three-way Communications1999-04-29029 April 1999
- on 990329,CR HVAC Was Placed in Recirculation Mode of Operation Instead of Recirculation Mu Filtered Mode. Caused by Inadequate Verbal Communications.Briefed Crews on Attention to Detail During three-way Communications
05000498/LER-1999-002-01, :on 990327,inadequate Performance of TS Surveillance When Evaluating Source Range Nuclear Instrument Discriminator Bias Curve Results,Was Discovered.Caused by Lack of Process to Incorporate Info.Compared Bias Curves1999-04-26026 April 1999
- on 990327,inadequate Performance of TS Surveillance When Evaluating Source Range Nuclear Instrument Discriminator Bias Curve Results,Was Discovered.Caused by Lack of Process to Incorporate Info.Compared Bias Curves
ML20206A1411999-04-19019 April 1999 Safety Evaluation Supporting Amends 107 & 94 to Licenses NPF-76 & NPF-80,respectively ML20206A3611999-04-19019 April 1999 Safety Evaluation Supporting Amends 108 & 95 to Licenses NPF-76 & NPF-80,respectively ML20205Q7321999-04-16016 April 1999 Safety Evaluation Supporting Amends 106 & 93 to Licenses NPF-76 & NPF-80,respectively ML20205Q6771999-04-16016 April 1999 Safety Evaluation Supporting Amends 105 & 92 to Licenses NPF-76 & NPF-80,respectively 05000498/LER-1999-001-01, :on 990311,RHR Sys Was Found in Condition Outside Design Basis.Caused by Inadequate Implementation of Design Basis Requirements.Condition Remedied by Opening Disconnect Switches Per Rev to Plant Procedures1999-04-12012 April 1999
- on 990311,RHR Sys Was Found in Condition Outside Design Basis.Caused by Inadequate Implementation of Design Basis Requirements.Condition Remedied by Opening Disconnect Switches Per Rev to Plant Procedures
1999-09-09
[Table view] |
text
_
r
~
.The Light companth Texas Project Electric Generating Station P.O. Box 289 Wadsworth Howton lighteng & Power February 19, 1996 ST-HL-AE-5294 File No.: G26 10CFR50.73 U. S. Nuclear Regulatory Commission Attention: Document Control Desk Washington, DC 20555 i
South Texas Project i
Unit 2 Docket No. STN 50-499 Licensee Event Report 96-001 I
Technical Specification 3.0.3 Entry Due to Two Main Feedwater Isolation Valves Beine Inonerable at the Same Time i
t Pursuant to 10CFR50.73, South Texas Project submits the attached Unit 2 Licensee Event Report 96-001 regarding Technical Specification 3.0.3 entry due to two main feedwater isolation valves being inoperable at the same time. This event did not have an adverse effect on the health and safety of the pubhc.
If you should have any questions on this matter, please contact Mr. S. M. Head at (512) 972-7136 or me at (512) 972-8664.
1 J. F. Groth Vice President, Nuclear Generation l
KJT/
i i
Attachment: LER 96-001 (South Texas, Unit 2) 9602290076 960219 PDR ADOCK 05000499 S
PDR g/jfff 290016 Project Manager on Behalf of the Participants in the South Texas Project i
E:\\wp\\nl\\nrc wk\\ler-96\\129601.wpw
l
,- Houston. Lighting & Power Company ST-HL-AE-5294 South Texas Project Electric Generating Static" File No.: G26 Page 2 c
c:
l Leonard J. Callan Rufus S. Scott i
Regional Administrator, RegionIV Associate General Counsel l
U. S.' Nuclear Regulatory Commission Houston Lighting & Power Company -
t 611 Ryan Plaza Drive, Suite 400 P. O. Box 61067 Arlington, TX 76011-8064 Houston, TX 77208 Thomas W. Alexion Institute of Nuclear Power Project Manager Operations.- Records Center U. S. Nuclear Regulatory Commission 700 Galleria Parkway Washington, DC 20555-0001 13H15 Atlanta, GA 30339-5957 l
l David P. Loveless Dr. Joseph M. Hendrie Sr. Resident Inspector 50 Bellport Lane l
c/o U. S. Nuclear Regulatory Comm.
Bellport, NY l1713 P. O. Box 910 Bay City, TX 77404-0910 Richard A. Ratliff Bureau of Radiation Control J. R. Newman, Esquire Texas Department of Health Morgan, Lewis & Bockius 1100 West 49th Street 1800 M Street, N.W.
Austin, TX 78756-3189 Washington, DC 20036-5869 U. S. Nuclear Regulatory Comm.
K. J. Fiedler/M. T. Hardt Attn: Document Control Desk l
City Public Service Washington, D. C. 20555-0001 P. O. Box 1771 San Antonio, TX 78296 j
J. C. Lanier/M. B.12e J. R. Egan, Esquire City of Austin Egan & Associates, P.C.
Electric Utility Department 2300 N Street, N.W.
721 Barton Springs Road Washington, D.C. 20037 Austin, TX 78704 Central Power and Light Company J. W. Beck ATTN: G. E. Vaughn/C. A. Johnson Little Harbor Consultants, Inc.
P. O. Box 289, Mail Code: N5012 44 Nichols Road Wadsworth, TX 77483 Cohassett, MA 02025-1166
NRC FORM 386 U.S. NUCLEAR kEAULATouY COMMASION APPR5VE3 SY OMS NO. 3150 0104 (4-96) -
EXPIRES 04/30/98 ESTIMATED EUR MANDATORY IN, DEN PER RESPONSE TO COMTLY WITH THIS i
ORMATION COLLECTION REQUEST: 50.0 HRS.
=== === m= >
052#Muf:Es","#.?C,a8?Na"1#.,'W.=
^
<s r.v.r.. ior r.quir.o nomo., or r,=,gN = reg #o.*MANA0 EMgT,"RANCs W.,,',y.
u"o5"
^'5 digits /charact.rs for.ach block)
U N E
REG TO,RY T9 p pERWOR RE C T
PAC 8LNY NAME p)
DOCKET NUMSta S)
PAGE 9)
South Texas, Unit 2 05000 499 1 OF 4 ne p) l Technical Specification 3.0.3 entry due to two main feedwater isolation valves being inoperable at the same time
[
EVENT DATE (5)
LER NUMBER (6)
REPORT DATE (7)
OTHER FACIUTIES INVOLVED (5)
FACluTY NAME DOCMET NUMBER SE MONTH DAY YEAR YEAR MONTH DAY YEAR NUMBER NU E 05000 FACIUTY NAME DOCKET NUMBER 01 19
% -- 001 00 02 19 g3999 CPERATING THIS REP RT IS SUBMITTED PURSUANT TO THE REOUIREMENTS OF 10 CFR S: (Check one or more) (11) 3 CODE (9) 20.2201(b) 20.2203(a)(2)(v)
X 50.73(a)(2)(i) 50.73(a)(2)(vni)
POWER 0
LEVEL (10) 20.2203(a)(2)(i) 20.2203(a)(3)(n) 50.73(a)(2)(hi) 73.71 20.2203(a)(2)(ii) 20.2203(a)(4) 50.73(a)(2)(iv) oTHER 20.2203(a)(2)(ni) 50.36(c)(1) 50.73(a)(2)(v) gyge below 20.2203(a)(2)(sv) 50.36(c)(2) 50.73(a)(2)(vH)
UCENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER pneude Area Code)
Scott M. Head - Sr. Consulting Engineer (512) 972-7136 COMPLETE ONE UNE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
REPORTABL T^
CAUSE
SYSTEM COMPONENT MANUFACTURER E
CAUSE
SYSTEM COMPONENT MANUFACTURER r NPRD SUPPLEMENTAL REPORT EXPECTED (14)
MONTH DAY YEAR EXPECTED YES SUBMISSION X
NO (if yes, complete EXPECTED SUBMISSION DATE).
DATE (15)
ABSTRACT (umet to 1400 spaces,6.e, approximately 15 single-spaced typewntion knes) (16)
On January 19,19%, Unit 2 was in Mode 3 at 0% power. At 0825 hours0.00955 days <br />0.229 hours <br />0.00136 weeks <br />3.139125e-4 months <br />, Technical Specification 3.0.3 was entered when it was determined that a Limiting Condition for Operation was not met for an existing condition in which two closed main feedwater isolation valves were declared inoperable for maintenance on January 18,1996 at 1750 hours0.0203 days <br />0.486 hours <br />0.00289 weeks <br />6.65875e-4 months <br />. An Usual Event was declared at 0935 hours0.0108 days <br />0.26 hours <br />0.00155 weeks <br />3.557675e-4 months <br /> on January 19,1996. Post maintenance testing on one of the affected main feedwater isolation valves was performed satisfactorily and the valve was declared operable. With one remaining main feedwater isolation valve inoperable and closed, the required action for Technical Specification 3.7.1.7 Limiting Condition for Operation was met. Technical Specification 3.0.3 was exited at 1028 hours0.0119 days <br />0.286 hours <br />0.0017 weeks <br />3.91154e-4 months <br /> and the Unusual Event was exited at 1031 hours0.0119 days <br />0.286 hours <br />0.0017 weeks <br />3.922955e-4 months <br /> on January 19, 1996. Subsequent investigation determined that the declaration of an Unusual Event was inappropriate. The root cause of this event was human error. Corrective actions included a discussion of enhanced management j
expectations with emphasis on clear, concise communications, use of the chain of command, and control of logging entry into Technical Specification Limiting Condition for Operation. Other corrective actions involve Emergency Plan refresher training with emphasis on continued application of conservative decision making and guidance regarding commumcations and work coordination.
i NRC ForN 366 (4-95)
E:\\wp\\nl\\nrc-wk\\ler-96\\129601.wpw
l NRCP0xM 306A U.S. NUCLEAR REJULATORY COMMAS 10N
(&os)
LICENIEE EVENT REPORT (LER)
{
TEXT CONTINUATION FACRJTY NAME (1)
DOCKET LER NUMBER iS)
PAGE (3)
)
"ONP =
=
South Texas, Unit 2 05000 499 2
OF 4 001 -
00 TEKT (if more space ss required, use additional copies of NRC Form 366A) (t7)
\\
l DI?SCRIPTION OF EVENT:
)
L On January 19,1996, Unit 2 was in Mode 3 at 0% power in a planned outage for main electrical generator j
r: pairs. At 0825 hours0.00955 days <br />0.229 hours <br />0.00136 weeks <br />3.139125e-4 months <br />, Technical Specification 3.0.3 was entered and preparations were started for transition
(
to Mode 4 operations. Technical Specification 3.0.3 was entered when it was determined that a Limiting l
Condition for Operation was not met for a existing condition in which two closed main feedwater isolation valves were declared inoperable.
L Work to adjust the packing for main feedwater isolation valves FW-7141 and FW-7143 was planned to be conducted on one main feedwater isolation valve at a time. The intent was to test the first valve after packing adjustment was completed in order to verify operability before packing adjustments were conducted on the second valve. This plan was not effectively communicated to personnel involved in controlling the activity.
Work Start' Authority in the outage work control facility reviewed the effect of planned packing adjustment maintenance on Technical Specifications. After a review of Technical Specification 3.7.1.7 and a supporting Technical Specification Interpretation, it was concluded that the main feedwater isolation valves would remain i
operable and performing their intended safety function as long as the valves remained closed and a positive means was maintained to prevent the valve from inadvertently opening. The review failed to note that the Technical Specification Interpretation only applied to Modes I and 2. As a result, work start authorization was given to perform maintenance on both valves.
On January 18,1996, at 1750 hours0.0203 days <br />0.486 hours <br />0.00289 weeks <br />6.65875e-4 months <br />, main feedwater isolation valves FW-7141 and FW-7143 were logged out of service. The condition of these valves was documented in the Operability Assessment System for tracking work and subsequent testing. In addition, an entry was made in the Control Room log that Technical Specification 3.7.1.7 was applicable for main feedwater isolation valves FW-7141 and FW-7143 being placed out of service. Work Start Authority did not fully discuss the documented condition of these two valves with the Control Room except that the valves were out of service.
During the next two shift changes, main feedwater isolation valves FW-7141 and FW-7143 were turned over as inoperable. Neither shift recognized that Technical Specification 3.7.1.7 Limiting Condition for Operation included no provisions for two inoperable main feedwater isolation valves in Mode 3. At approximately 1800 hours0.0208 days <br />0.5 hours <br />0.00298 weeks <br />6.849e-4 months <br /> and 2300 hours0.0266 days <br />0.639 hours <br />0.0038 weeks <br />8.7515e-4 months <br />, the packing on valves FW-7143 and FW-7141 respectively was adjusted, which i
potentially affected each valve's stroke time and brought into question whether each valve's Technical Specification surveillance stroke requirement could be met.
l On January 19, 1996 shortly after turnover to the day shift, discussions were conducted regarding the operability of main feedwater isolation valves FW-7141 and FW-7143 and entry into Technical Specification 3.7.1.7.
At 0825 hours0.00955 days <br />0.229 hours <br />0.00136 weeks <br />3.139125e-4 months <br />, it was determined that there was no provision in Technical Specification 3.7.1.7 Limiting Condition for Operation for two inoperable closed main feedwater isolation valves while in Mode l
3 c.nd Technical Specification 3.0.3 was entered. After further discussion, an Unusual Event was declared l
at 0935 hours0.0108 days <br />0.26 hours <br />0.00155 weeks <br />3.557675e-4 months <br />.
l l
E \\wp\\nl\\nrc-wk\\ler-96\\129601.wpw
I NRC FORJ 366A U.S. NUCLEAA REA ULATo..Y CoMMmSION (M5)
LICENZEE EVENT REPORT (LER)
TEXT CONTINUATION FACIUTV NAME (1)
DOCKET LER NUMBER (6)
PAGE (3)
YEAR SEQUENTIAL REVlRION South Texas, Unit 2 05000 499 3
OF 4
96 - 001 00 TEXT (if more space is required use additional copies of NRC Form 366A) (17)
DESCRIPTION OF EVENT (CONTINU.ED1 Operability testing on main feedwater isolatie valve FW-7141 was performed satisfactorily and the valve was declared operable. With one remaining main feedwater isolation valve inoperable and closed, the required action for Technical Specification 3.7.1.7 Limiting Condition for Operation in Mode 3 was met. Technical Specification 3.0.3 was exited at 1028 hours0.0119 days <br />0.286 hours <br />0.0017 weeks <br />3.91154e-4 months <br /> and the Unusual Event was exited at 1031 hours0.0119 days <br />0.286 hours <br />0.0017 weeks <br />3.922955e-4 months <br /> on January 19, 1996. The preparations to transition to Mode 4 were stopped. No plant cooldown was conducted.
i Subsequent investigation determined that the declaration of an Unusual Event was inappropriate. The bases used for declaring the Unusual Event states that an immediate declaration of an Unusual Event is required when the plant cannot be brought to the required operating mode within the allowable action statement time in the Technical Specifications, as the plant is outside its safety envelope. For this event, the plant was required to be in Mode 4 within the 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> following initiation of action to transition to Mode 4 as required by the entry into Technical Specification 3.0.3. There was no indication that the required action of Technical Specification 3.0.3 could not be met at the time of the declaration of the Unusual Event. A conservative decision had been made to declare an Unusual Event.
CAUSE OF EVENT
The root cause of this event was human error.
l The misapplication of the interpretation for Technical Specification 3.7.1.7 resulted in allowing the performance l
of maintenance that affected the operability of more components than allowed Sv Technical Specifications.
The failure to recognize that the plant was in a condition not allowed by Technical Specifications for approximately 15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br /> resulted from a lack of a questioning attitude regarding the condition of main feedwater isolation valves FW-7141 and FW-7143.
Contributing to this event was ineffective communications between the work start authority and the control room.
l 1
ANALYSIS OF EVENT
Any operation or condition prohibited by Technical Specifications is reportable pursuant to 10CFR50.73(a)(2)(i)(B). The main feedwater isolation valves were shut and performing their required safety function. However, the maintenance performed on main feedwater i!.olation valves FW-7141 and FW-7143 brought into question the ability of these valves to meet their Technical Specification stroke time surveillance requirement and resulted in declaring these valves inoperable until post maintenance testing could verify valve operability. In the closed position, the potential inability of the valves to meet their stroke time has no safety 4
E:\\wp\\nl\\nrc-wk\\ler-96\\129601.wpw
i iU.S. NUCLEAR RE.ULAToRY COMM SloN j
(4 95)
LICENCEE EVENT REPORT (LER)
]
TEXT CONTINUATION FACluTY NAME (1)
DOCKET LER NUMBER (6)
PAGE (3)
YEAR SEQUENTIAL REVISION South Texas, Unit 2 05000 499 4
OF 4 96 - 001 00 TEXT (if more space is required, use additional copies of NRC Form 366A) (t7)
ANALYSIS OF EVENT (CONTINUEDh significance. Post maintenance testing after packing adjustment confirmed that main feedwater isolation valves FW-7141 and FW-7143 met their Technical Specification surveillance requirements.
M in feedwater isolation valves FW-7141 and FW-7143 have large actuator output force of 202,268 lbs-force.
The total valve stem friction component due to packing makes up approximately 3.2 per cent of the actuator output force. Historically, these valves have passed stroke time testing following packing adjustment.
Therefore,it is unlikely that adjusting the packing of the main feedwater isolation valves would have had any significant effect on the valve stroke time and operability.
There were no adverse safety or radiological consequences of this event.
1
CORRECTIVE ACTIONS
l 1.
The lessons from this event resulted in discussions regarding enhanced management expectations including emphasis on clear, concise communications, use of the chain of command, and control of logging entry into Technical Specification Limiting Condition for Operation. These expectations were discussed with the operating crews of both units.
2.
Emergency Plan refresher training discussing the lessons learned from this event will be conducted for Licensed Operators by November 1996. Continued application of conservative decision making in regard to issuing reports will be emphasized.
3.
Guidance has been issued regarding communications and work coordination between the work start authority and the Control Room.
i
ADDITIONAL INFORMATION
A revision to Technical Specification 3.7.1.7 will be submitted as part of the station's Improved Technical Specification submittal. The implementation of Improved Technical Specifications should eliminate the need for Technical Specification Interpretations and clear up potential confusion surrounding the application of Technical Specification 3.7.1.7.
There have been no previous reports by the South Texas Project to the Nuclear Regulatory Commission within the last three years regarding Technical Specification 3.0.3 entry due to two main feedwater isolation valves being inoperable at the same time.
E \\wp\\nl\\nre-wk\\ler-96\\129601.wpw
|
---|
|
|
| | Reporting criterion |
---|
05000498/LER-1996-001-01, :on 960328,Standby Diesel Generator Declared Inoperable.Caused by Barriers for Preparation & Planning Not Being Fully Implemented.Personnel Involved Counseled Re Event & Revised Preventive Maint Documents |
- on 960328,Standby Diesel Generator Declared Inoperable.Caused by Barriers for Preparation & Planning Not Being Fully Implemented.Personnel Involved Counseled Re Event & Revised Preventive Maint Documents
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) | 05000499/LER-1996-001, :on 960119,TS 3.0.3 Entry Occurred Due to Two MFW Isolation Valves Being Inoperable at Same Time.Discussed Enhanced Mgt Expectations W/Emphasis on Clear & Concise Communications |
- on 960119,TS 3.0.3 Entry Occurred Due to Two MFW Isolation Valves Being Inoperable at Same Time.Discussed Enhanced Mgt Expectations W/Emphasis on Clear & Concise Communications
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2) | 05000498/LER-1996-002-01, :on 960507,failure to Meet Requirements of Tech Specs Occurred.Caused by Inattention to Detail During Documentation & Review of Testing Results.Feedback from Event Given to Individuals Involved |
- on 960507,failure to Meet Requirements of Tech Specs Occurred.Caused by Inattention to Detail During Documentation & Review of Testing Results.Feedback from Event Given to Individuals Involved
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) | 05000499/LER-1996-002, :on 960314,fuel Handling Bldg Exhaust Air Damper Inoperable Due to Inappropriate Design Implementation.Made Mods to Fuel Handling Bldg Emergency Exhaust Dampers to Resolve Issue |
- on 960314,fuel Handling Bldg Exhaust Air Damper Inoperable Due to Inappropriate Design Implementation.Made Mods to Fuel Handling Bldg Emergency Exhaust Dampers to Resolve Issue
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2) | 05000499/LER-1996-003, :on 960828,failure to Fully Meet Requirements of TS Occurred,Due to Discovery of Improperly Installed Jumper on Main Steam Line Pressure Lead/Lag Circuit Card. Personnel Issues Have Been Addressed |
- on 960828,failure to Fully Meet Requirements of TS Occurred,Due to Discovery of Improperly Installed Jumper on Main Steam Line Pressure Lead/Lag Circuit Card. Personnel Issues Have Been Addressed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | 05000498/LER-1996-004, :on 961120,unanalyzed Conditions Were Noted Due to Discovery of Two Spare SR Circuit Breakers Not in Seismically Qualified Position.Caused by Failure to Follow Established Procedures.Revised Procedures |
- on 961120,unanalyzed Conditions Were Noted Due to Discovery of Two Spare SR Circuit Breakers Not in Seismically Qualified Position.Caused by Failure to Follow Established Procedures.Revised Procedures
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | 05000498/LER-1996-005, :on 961213,reactor Containment Building Personnel Airlock Incorrectly Declared Operable Occurred. Caused by Pertinent Information Re Status of Seal Replacement.Occurrence Has Been Reviewed |
- on 961213,reactor Containment Building Personnel Airlock Incorrectly Declared Operable Occurred. Caused by Pertinent Information Re Status of Seal Replacement.Occurrence Has Been Reviewed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) | 05000498/LER-1996-009, :on 960620,containment Closeout Insp Failed to Recognize Unauthorized Material Left in Containment.Caused by Inadequate Requirement Review.Removed Bagged Equipment & Completed Containment Closeout Insp |
- on 960620,containment Closeout Insp Failed to Recognize Unauthorized Material Left in Containment.Caused by Inadequate Requirement Review.Removed Bagged Equipment & Completed Containment Closeout Insp
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) |
|