05000498/FIN-2011002-03
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Finding | |
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| Title | Untimely Corrective Action to Correct Nonconforming Steam Generator Power Operated Relief Valve Condition |
| Description | The inspectors reviewed a self-revealing noncited violation of 10 CFR Part 50, Appendix B, Criteria XVI, Corrective Action, for the failure to assure that conditions adverse to quality were corrected in a timely manner, or that an evaluation to justify a longer completion time beyond the first available opportunity was performed. On June 2, 2008, steam generator power operated relief valve 1A failed to stroke full closed as part of surveillance testing. The operability determination concluded that the steam generator power operated relief valves were operable but nonconforming. On August 25, 2010, steam generator power operated relief valve 1D failed to stroke closed as part of surveillance testing. This new prompt operability determined that the previous operability was flawed. It did not consider all functions associated with the valves, in particular, the dose mitigation function. It was also determined that the licensee failed to adequately track an operable but nonconforming condition to ensure resolution in a timely manner. The licensee has since updated the design modification timeline to install the failed closed circuitry in both units during the respective 2011 refueling outages. This finding was more than minor because it affected the Mitigating Systems Cornerstone attributes of Design Control and Equipment Performance and affected the cornerstone objective to ensure that availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The deficiency resulted in the Updated Final Safety Analysis Report Chapter 15 Accident Analysis dose calculations being nonconservative if the relief valves would fail to go closed on loss of power. The inspectors performed the significance determination using NRC Inspection Manual Chapter 0609, Attachment 0609.04, Phase 1 Initial Screening and Characterization of Findings, dated January 10, 2008, because it affected the Mitigating Systems Cornerstone while the plant was at power. The finding was determined to be of very low safety significance because it was a design or qualification deficiency confirmed not to result in loss of operability or functionality. In addition, this finding had problem identification and resolution cross-cutting aspects associated with the corrective action program in that the licensee did not thoroughly evaluate the problem such that the resolutions address causes, and did not properly evaluate for operability conditions adverse to quality. |
| Site: | South Texas |
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| Report | IR 05000498/2011002 Section 1R22 |
| Date counted | Mar 31, 2011 (2011Q1) |
| Type: | NCV: Green |
| cornerstone | Mitigating Systems |
| Identified by: | Self-revealing |
| Inspection Procedure: | IP 71111.22 |
| Inspectors (proximate) | P Goldberg J Dixon K Clayton G Guerra B Tharakan L Carson M Phalen W Walker R Latta B Rice N Greene |
| CCA | P.2, Evaluation |
| INPO aspect | PI.2 |
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Finding - South Texas - IR 05000498/2011002 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (South Texas) @ 2011Q1
Self-Identified List (South Texas)
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